ML040790507

From kanterella
Jump to navigation Jump to search
Minutes of Internal Meeting of the Davis-Besse Oversight Panel
ML040790507
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 03/18/2004
From: Grobe J
NRC/RGN-III
To:
NRC/RGN-III
References
Download: ML040790507 (14)


Text

March 18, 2004 MEMORANDUM TO: Davis-Besse Oversight Panel FROM: John A. Grobe, Chairman, Davis-Besse Oversight Panel /RA/

SUBJECT:

MINUTES OF INTERNAL MEETING OF THE DAVIS-BESSE OVERSIGHT PANEL The implementation of the IMC 0350 process for the Davis-Besse Nuclear Power Station was announced on April 29, 2002. An internal panel meeting was held on February 24, 2004. Attached for your information are the minutes from the internal meeting of the Davis-Besse Oversight Panel, Inspection Results Memorandum for closure of Restart Checklist Item 4.b, and the Open Action Items List.

Attachments: As stated cc w/att: D. Weaver, OEDO J. Caldwell, RIII G. Grant, RIII S. Reynolds, DRP B. Clayton, EICS G. Wright, DRP DB0350 DOCUMENT NAME: C:\ORPCheckout\FileNET\ML040790507.wpd To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RIII RIII RIII RIII NAME DPassehl/trn CLipa JGrobe DATE 03/12/04 03/17/04 03/18/04 OFFICIAL RECORD COPY

MEETING MINUTES: Internal IMC 0350 Oversight Panel Meeting Davis-Besse Nuclear Power Station DATE: February 24, 2004 TIME: 12:30 p.m. Central ATTENDEES:

J. Grobe B. Ruland J. Hopkins C. Lipa A. Mendiola R. Baker D. Passehl R. Lanksbury K. Riemer J. Rutkowski D. Hills S. Orth Agenda Items:

1. Discuss/Approve Todays Agenda The Panel approved the agenda, but modified the order of presentations. THE APPROVED AGENDA REFLECTS THE ORDER LISTED IN THESE MINUTES.
2. Discuss Plant Status and Inspector Insights and Emergent Issues S. Thomas led a discussion of plant status and inspector insights and emergent issues.

The plant is in Mode 3 (hot standby) at Normal Operating Pressure/Normal Operating Temperature (2155 psig/532OF). The licensee expects to maintain the plant in these conditions until restart. The licensee is currently tracking outstanding activities that need to be completed prior to restart. There are approximately 16 restart items. The licensee is evaluating repairs to a nonisolable steam leak from a normally closed/capped 3/4-inch manual vent valve from the Steam Generator 1.

3. Discuss New/Potential Licensing Issues J. Hopkins led a discussion of new/potential licensing issues. J. Hopkins mentioned that OGC was asked to expedite review of the Licensing Amendment Request regarding steam generator inspections. J. Grobe mentioned that J. Caldwell requested information on the licensee's efforts to resolve Thermo-Lag.

J. Hopkins identified that there was one Confirmatory Order issued to Davis-Besse on Thermo-Lag dated June 22, 1998. On May 4, 1998, NRR sent the draft Confirmatory Order to the licensee asking them to sign for consent to the Order. Following some negotiation of the Order language, consent was signed on June 11, 1998, and Order was issued June 22, 1998. The Order said complete Thermo-Lag corrective actions by December 31, 1998. By letter dated January 25, 1999, the licensee provided written confirmation of a telephone call to the NRC on December 23, 1998, that modifications for Thermo-Lag were completed on December 22, 1998. The staff took action to contact the licensee's staff to determine whether the issue was evaluated as part of the licensee's efforts related to resolution of Restart Checklist Item 3.i, to determine what the licensee had done regarding the January 25, 1999, letter, and provide this information to Jim Caldwell.

4. Discuss Licensed Operator Qualification Status R. Lanksbury briefed the Panel on the status of licensed operator qualifications.

R. Lanksbury stated that the qualifications are current for all except ten people. These 10 people hold inactive licenses and the licensee is closely monitoring them.

R. Lanksbury stated that the operator license requalification program was never suspended during the current extended outage.

5. Discuss EAL Status and Conversation with CI K. Riemer briefed the Panel on the status of Davis-Besse Emergency Action Levels and a conversation with a concerned individual. On February 11, 2004, NRC Headquarters EP staff and Region III inspectors completed an in depth review of the Davis-Besse Emergency Action Levels (EALs) as part of agency actions in advance of plant restart.

The EAL review provided an evaluation of potential areas where a decrease in effectiveness (DIE) could have occurred as a result of historical changes to the original NRC approved NUREG-0654 classification scheme used at Davis-Besse. The result of this review concluded that there are no DIE issues with the Davis-Besse EALs which would affect restart. The Panel accepted the results of the screening contingent upon resolution of three potential discrepancies identified during a Region III inspection of this area. Specifically, these issues involve:

1. An EAL change pertaining to actuation of the Steam/Feed Rupture Control System;
2. An EAL pertaining to a radiological release into the protected area; and
3. A question regarding units (microcuries per cubic centimeter) of an EAL.

The resolutions of these concerns, as well as the results of the Region III EP inspection will be documented in NRC Inspection Report 50-346/04-02.

K. Riemer also led a discussion from a concerned individual regarding a potential emergency preparedness issue at Davis-Besse. The Panel determined that this concern was not needed to be resolved prior to restart and that it should be handled in the normal allegation process.

6. Discuss Allegation Status D. Passehl led a discussion on the status of allegations. The Panel discussed a February 14, 2004, letter to J. Caldwell. The Panel determined that this letter did not contain allegations that needed to be responded to prior to restart based on the Panels established criteria. J. Hopkins stated that the 10 CFR 2.206 Petition Review Board determined that letter is not a 10 CFR 2.206 request.
7. Discuss Safety Culture Paper J. Grobe led a discussion of a safety culture paper. THE PAPER IS A MEMORANDUM TO J. GROBE FROM G. WRIGHT REGARDING RESTART CHECKLIST ITEM 4.b CLOSURE AND IS ATTACHED TO THESE MINUTES.
8. Discuss Action Items The Panel reviewed the following open Action Items with comments as noted:

Item 234 (Closed) - Develop protocol paper for NRC representative on DOJ committee interface with 0350 Panel for updates.

The Panel closed this item based on agency managements decision.

9. Discuss Hot List C. Lipa led a discussion of the Hot List.
10. Discuss/Update Milestones and Commitments The Panel reviewed and discussed upcoming milestones and commitments.

February 24, 2004 DAVIS-BESSE OVERSIGHT PANEL OPEN ACTION ITEM LIST Item No. Action Item Assigned to Comments Due

    • - Post (Date generated) Date Restart 208 Evaluate the need to call D. Passehl 10/14-Investigation is still ongoing; TBD
    • back CI regarding Allegation 12/23-Discussed, awaiting DOJ RIII-2002-A-0177 (D-B) after Investigation; 2/20-Discussed, Panel the OI Investigation is decided this item will be considered complete (08/21) post-restart.

224 Rewrite the proposed IN on D. Hills 12/15-Discussed, D. Hills is working; TBD

    • TSP to be generic and 12/23-Discussed, this issue will be reflect attainable plant discussed internally in RIII and brought conditions and what to Panel on 1/06/03 for a final decision information should be on how to proceed; 1/20-Discussed, disseminated to the industry revised IN is with Panel Chairman for concerning Boric Acid review; 1/30-Discussed, Chairmans Corrosion Control comments were sent to J. Lara; 2/20-Programs. (12/09) Discussed, Panel decided this item will be considered post-restart.

228 Place all Email requests R. Baker 1/06-Discussed, will verify ADAMS 02/24/04 sent throughout Agency, package is in place to support responses received, and collection of emails and responses-issue resolutions in ADAMS email requests will be resent due to package for documentation. small response to date; 1/30-(12/16) Discussed, will verify and update Panel on 2/5/04; 2/3-Discussed, Lead changed, verified ADAMS package in place, coordinate with J. Shea and A.

Mendiola that all emails included in ADAMS package. 2/18-Discussed, contents verified and need to add in additional email; 2/20-Discussed, only remaining item is to scan in one email from NRR Technical staff.

234 Develop protocol paper for W. Ruland 10/15/04-Discussed, protocol paper TBD NRC representative on DOJ regarding decision making being committee interface with drafted as a letter from Sam Collins to 0350 Panel for updates. Bruce Boger and includes criteria for (01/06) Immediate Action; 1/20-Discussed, the draft has been sent to B. Boger for DOJ comments; 1/26-Discussed, B.

Boger is reviewing with senior management; 2/3-Discussed, protocol paper in review by OGC; 2 Discussed, J.Grobe working with Craig; 2/20-Discussed, Panel decided this item will be considered post-restart; 2/24-Discussed, The Panel decided this item is Closed.

February 24, 2004 DAVIS-BESSE OVERSIGHT PANEL OPEN ACTION ITEM LIST Item No. Action Item Assigned to Comments Due

    • - Post (Date generated) Date Restart 244 Security (J. Creed) contact D. Passehl 2/19-Spoke with J. Creed on 2/18, and 2/25/04 NSIR to determine if DHS he will update Panel.

needs notification at restart as an applicable Federal Agency. (2/10) 245 NRR contact FEMA to verify W. Ruland 2/19-Additional correspondence with 2/25/04 there are still no objections FEMA is necessary to verify no to restart. (2/10) objections to restart.

246 Verify which remaining C. Lipa 2/19-Verifying schedule for any 2/25/04 meetings of all special remaining interviews.

inspection team leads with the RA exist. (2/10) 249 Ensure Enhanced G. Wright 2/19-Determined not necessary prior to TBD

    • Inspection Plan includes restart decision; 2/20-Discussed, Panel followup M&HP review of decided this item will be considered licensee monthly PIs and 2nd post-restart.

quarter corrective action effectiveness for Nov 03 ECP survey results. (2/18) 250 Ensure Enhanced C. Lipa 2/19-Determined not necessary prior to TBD

    • Inspection Plan includes restart decision; 2/20-Discussed, Panel commitments listed in RAM decided this item will be considered item C-41. (2/18) post-restart.

251 Ensure Enhanced C. Lipa 2/19-Determined not necessary prior to TBD

    • Inspection Plan includes a restart decision; 2/20-Discussed, Panel followup on the UHS SW decided this item will be considered CR resolution. (2/18) post-restart.

February 24, 2004 February 25, 2004 MEMORANDUM TO: John A. Grobe, Chairman Davis-Besse Oversight Panel FROM: Geoffrey C. Wright, Leader, Davis-Besse Management /RA/

and Human Performance Inspection Team

SUBJECT:

RESTART CHECKLIST ITEM 4.b CLOSURE RECOMMENDATION The Management and Human Performance inspection was designed to evaluate the licensees actions in response to the degraded reactor vessel head issue. Specifically, the inspection was to evaluate the following areas: the licensees root cause assessments, the licensees corrective actions and their implementation, and the licensees tools for monitoring the effectiveness of the corrective actions.

Because of concerns which developed following the root cause analyses, the inspection also included an evaluation of the licensees actions regarding safety conscious work environment (SCWE) and the employee concerns program (ECP). The inspection report for the Follow Up Management and Human Performance inspection, Report 50-346/04-03, will not be issued prior to the restart decision by the Oversight Panel. This memorandum serves to document the Teams overall conclusion with respect to Restart Checklist Item 4.b. Attachment 1 provides additional detail on the results of the Management and Human Performance inspections three phases and the Follow Up inspection into the November 2003 SCWE survey results.

The Management and Human Performance inspection was divided into three phases to look at the three areas. Phase 1 evaluated the licensees root cause analyses. Phase 1 concluded that while the initial analyses that the licensee had performed were acceptable, they had missed a number of areas and as such, the licensee needed to perform additional analyses to appropriately cover all potential areas of concern. Phase 1 results were documented in Inspection Report 50-346/2002015. Phase 2 reviewed the corrective actions associated with the root or contributing causes. The review looked at whether the actions would address the causes and the schedule for implementing the actions. Phase 2 concluded that the proposed corrective actions if properly implemented and monitored should preclude recurrence of the causes for the head degradation. Phase 2 results were documented in Inspection Report 50-346/2002018. Phase 3 evaluated the licensees tools for monitoring the effectiveness of the management and human performance corrective actions. Phase 3 also evaluated the licensees activities to improve the sites SCWE, the activities of the safety conscious work environment review team (SCWERT), and the current status of the employee concern program. Phase 3 concluded that the tools the licensee was using to monitor safety culture and SCWE were appropriate and provided valuable information in these areas. Further, Phase 3 concluded that the current ECP was appropriate and was functioning as designed. Phase 3 results were documented in Inspection Report 50-346/20003012.

Notwithstanding the generally positive characterizations above, the Teams review of the licensees November SCWE survey, one monitoring tool that included safety culture attributes,

February 24, 2004 DOCUMENT NAME: C:\ORPCheckout\FileNET\ML040790507.wpd To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RES NRR OE NRR NAME GWright for (email) GWright for GWright for (email) GWright for (email)

JPersensky/trn (email) LJarriel DDesaulniers CGoodman DATE 02/24/04 02/24/04 02/24/04 02/24/04 OFFICE RI RIII RES NRR NAME GWright for (email) GWright for GWright for (email) GWright for (email)

HEichenholz (email) MKeefe JCai JHeller DATE 02/24/04 02/25/04 02/24/04 02/24/04 OFFICE RIII RIII RIII RIII NAME GWright for (email) MBrothers GWright JBeck unavailable DATE 02/23/04 02/ /04 02/25/04 OFFICIAL RECORD COPY

February 24, 2004 J. Grobe identified that a number of key organizations had provided more negative responses to some questions then in March 2003. Specifically operations, plant engineering, quality assurance, and to a lesser extent maintenance provided more negative responses to questions dealing with production over safety/quality, SCWE, corrective action program, and management involvement then in May 2003. For example, operations went from 6% to 23.4% negative responses to the question Management cares more about safety than cost and schedule, Plant Engineering went from 6.6% to 12% negative responses to the question I can raise nuclear safety or quality concern without fear of retaliation, and Quality Assurance went from 0% to 8.7% negative responses to the question I am aware of others who have been subjected to HIRD within the last 6 months. Additional details are provided in . Because the responses raised questions regarding the continuing effectiveness of the licensees actions to improve safety culture, the Team determined that additional inspection was necessary to understand the cause(s) of the additional negative responses.

The Team developed a detailed inspection methodology to evaluate and independently validate the licensees assessment of the increases in negative responses. The inspection methodology included document reviews and interviews with approximately 120 individuals, in the departments of concern, to gain insights into why there was an increase in negative responses.

The Team validated, through independent inspection, that the licensees assessment of the causes for the increase in negative responses was appropriate. The licensee had used an appropriate approach to determine the causes of the decline and interviewed an acceptable sample of staff from the affected departments. Throughout the NRC interview process, the Team noted a less positive tone by the licensees staff when responding to questions dealing with the behavior and effectiveness of their management than the NRC Team noted during interviews in May 2003. The staffs responses related in large part to work hours, schedule credibility, and management comments that appeared to be inconsistent with the licensees Leadership In Action training. The Team also noted that interviewees personally exhibited a high focus on safety and indicated that their management placed the highest priority on addressing safety concerns. While the licensee is developing additional corrective actions in response to their assessment, the Team concluded that the licensees immediate corrective actions were adequate for restart and that there were no outstanding issues that would preclude restart.

In summary, through the three phases and Follow Up inspections, the Management and Human Performance Team concluded that the licensees root cause analyses and associated corrective actions for the safety culture issues which resulted in the reactor head degradation, were appropriate.

The Team also concluded that the corrective actions with the associated monitoring activities, have been sufficiently effective to provide reasonable assurance to preclude recurrence of the conditions which led to the degradation of Davis-Besses reactor vessel head. While additional actions are planned for continued improvement in the safety culture at Davis-Besse, no issues were identified that would preclude unit restart. Therefore, the Team recommended closure of restart checklist item 4.b.

Attachments: 1. Safety Culture Issues at the Davis-Besse Nuclear Power Station

2. Davis-Besse March and November 2003 SC/SCWE Survey Department Data -

FENOC and Contract Employees

February 24, 2004 ATTACHMENT 1 SAFETY CULTURE ISSUES AT THE DAVIS-BESSE NUCLEAR POWER STATION DEFINITION OF THE PROBLEM On August 21, 2002, the licensee submitted its root cause analysis for the reactor pressure vessel head degradation. The licensee concluded that there was a lack of sensitivity to nuclear safety and the focus was on justifying conditions, that there was less than adequate nuclear safety focus, and that there was less than adequate implementation of the corrective action program as indicated by addressing symptoms rather than causes. To address these cultural deficiencies in its past performance, the licensee created the Management and Human Performance building block in its Return to Service Plan. The building block was designed to further identify organizational performance and cultural causal factors, and to identify and track corrective action implementation.

NRC INSPECTION AND ASSESSMENT The NRC structured its inspection in this area in three phases; (1) inspection of the root cause evaluations; (2) inspection of the corrective action development, prioritization and implementation; and (3) evaluation of the effectiveness of the corrective actions at improving organizational effectiveness and cultural.

Phase 1 - Inspection of the Root Cause Evaluations The inspections first phase was the assessment of the adequacy of the licensees root cause evaluations. This inspection was conducted by Region III, NRR and contract staff experts in inspection and assessment, root cause evaluation techniques, and human and organizational performance. The licensee used the Management Oversight and Risk Tree (MORT) analysis technique to perform their overall root cause assessment. The inspection team found that the principles of MORT were properly applied; however, the scope of the assessment was not sufficient to reveal all potential causal factors.

The licensee performed additional assessments in multiple areas including engineering, operations, and corporate support, among others. Review by the team revealed that the combined assessments resulted in sufficient breadth and depth to be confident that the causal factors were identified. During the course of these assessments, many contributors were identified, including deficiencies in the licensees safety conscious work environment, the ombudsman program, and safety culture at the facility.

Phase 2 - Inspection of the Corrective Action Development, Prioritization and Implementation The same team returned to evaluate corrective action development and implementation to ensure those actions addressed all the causal factors. The licensee developed over 125 specific corrective actions. The team concluded that each of the causal factors was addressed in the corrective actions.

In addition, the team concluded that the corrective actions were properly prioritized and sampled implementation of the corrective actions concluding that the actions would be implemented properly.

Corrective actions ranged from corporate governance issues and executive pay structures, policy and 1

February 24, 2004 procedural alignment in safety culture areas, replacing the ombudsman program with a structured employee concerns program, establishing a formal safety conscious work environment program and addressing a multitude of organizational and communication issues.

Phase 3 - Evaluating the Effectiveness of Corrective Actions at Improving Safety Cultural Recognizing the key role safety culture deficiencies played in the root cause of the head degradation event, the Panel determined that it was necessary to evaluate the effectiveness of the improvement in safety culture at the facility. Because the NRC has only broadly stated expectations in cultural areas, the approach the Panel employed was not to specifically assess organizational safety culture, but to ensure that the licensee had adequate tools to self-assess in the safety culture areas, that the assessments were appropriately performed and provided meaningful insights into organizational weaknesses, and that the licensee was responding to those assessment results by taking actions to ensure a continuing trend of improvement.

The Panel brought together a team of experts from Region III, NRR, RES, OE and contractors who were highly capable and credible in performing this type of assessment. The team utilized national and international guidance and standards as a foundation for its assessment. The team concluded that the combination of licensee internal management assessments, surveys, and independent assessments provided a solid foundation for understanding organizational safety performance strengths and weaknesses. The team also found that the licensee, with some exceptions, was using their corrective action program to address safety culture deficiencies. The team noted steady improvement in overall organizational performance in this area.

Recent Results of the SC/SCWE Survey In November 2003, the licensee performed their third safety culture/safety conscious work environment survey of all staff. The results of all the surveys have been presented and discussed publicly. The first survey, conducted in August 2002, revealed significant cultural problems in many areas of the organization, including a significant lack of confidence in facility managements focus on safety. The second survey, conducted in March 2003, revealed double digit percentage improvements in many areas of the organization. The November 2003 survey showed steady or slightly improving overall organizational performance; however, several critical departments including operations, system engineering and quality assurance exhibited declines in some areas.

The NRC inspection team performed surveys of plant staff in May 2003 following the March 2003 survey to validate the veracity of the survey technique and implementation. Following the November 2003 survey results, an expanded team, including an individual from Region I, performed a follow-up inspection, to evaluate the licensees assessment of the declines. The team performed detailed document reviews and conducted a survey of selected licensee staff in January 2004. The team found that in all cases, staff understood and would fulfill their responsibility for identifying safety concerns and had confidence that management would place the proper priority on addressing safety concerns.

However, when the team contrasted its interview results from May 2003 with January 2004, the team identified a less positive perspective of some staff in their confidence in managements behaviors and effectiveness in other areas. The team concluded that the licensee had identified the contributing factors to this decline, including excessive work hours, inadequate work scheduling resulting in schedule adherence problems, and poor or inappropriate communication vertically in the organization on critical management decisions. The team found that licensee management had identified and implemented short term actions to address these issues. The team concluded that the short term actions were adequate for the identified issues and, while some of the actions had not been in place 2

February 24, 2004 long enough to obtain feedback on their effectiveness, other actions had received positive response from the licensees staff. The licensee has committed to perform a follow up effectiveness evaluation, patterned after the initial evaluation, toward the end of the 2nd quarter 2004. The team considered this appropriate.

Conclusions Overall, the three phases of the inspection and the Follow Up inspection revealed adequate cause assessments, sufficient corrective actions, and effective assessment techniques for measuring organizational improvement.

3

February 24, 2004 Attachment 2 Davis-Besse March and November 2003 SC/SCWE Survey Department Data - FENOC and Contract Employees All Ops Plant Maint QA Blank Engr Mar Nov Mar Nov Mar Nov Mar Nov Mar Nov Mar Nov Number of surveys 1139 780 100 77 107 75 285 167 24 23 87 14 Management care mor about safety than 15.2% 17.1% 6% 23.4% 18.7% 24.0% 21.4% 25.0% 0.0% 21.7% 18.6% 35.7%

cost & schedule Management expectations on safety and 9.9% 12.5% 9.0% 11.7% 8.8% 16.0% 12.4% 16.2% 4.3% 13.0% 9.3% 8.3%

quality are reflected in appraisals, reward, and discipline Resolution of nuclear safety and quality 10.2% 9.8% 6.0% 11.0% 16.9% 16.7% 11.2% 7.8% 4.2% 23.9% 11.2% 18.5%

issues, including Root Cause is effective in our organization CR issues are properly prioritized, evaluated 13.2% 10.9% 6.0% 15.6% 16.8% 21.3% 14.4% 9.6% 4.2% 17.4% 12.8% 21.4%

and resolved in timely manner CR process is effectively utilized by DB to 12.1% 11.4% 7.0% 14.3% 18.9% 18.7% 13.7% 7.2% 8.3% 26.1% 14.1% 21.4%

resolve quality issues in timely manner I can raise nuclear safety or quality concern 7.1% 6.5% 3.0% 5.2% 6.6% 12.0% 9.5% 11.4% 0.0% 0.0% 15.1% 7.1%

without fear of retaliation ECP will keep my identity confidential at my 6.4% 9.3% 8.0% 11.8% 3.8% 12.0% 9.1% 7.2% 0.0% 13.0% 13.1% 14.3%

request I am aware of SCWERT and its purpose 6.2% 8.5% 4.0% 11.7% 11.2% 14.7% 6.4% 10.2% 0.0% 13.0% 8.3% 14.3%

I have been subjected to HIRD within the 8.1% 3.7% 5.0% 2.6% 8.5% 8.0% 9.5% 4.2% 0.0% 4.3% 21.2% 0.0%

last 6 months I am aware of others who have been 15.3% 7.3% 8.0% 13.0% 15.1% 18.7% 22.8% 4.3% 0.0% 8.7% 28.6% 7.7%

subjected to HIRD within the last 6 months 1