ML040300257

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IR 05000275-03-008, 05000323-03-008; 09/28/03 - 12/31/03; Fire Protection, Maintenance Effectiveness, Postmaintenance Testing, ALARA Planning and Controls, Problem Identification and Resolution
ML040300257
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 01/30/2004
From: William Jones
NRC/RGN-IV/DRP/RPB-E
To: Rueger G
Pacific Gas & Electric Co
References
IR-03-008
Download: ML040300257 (51)


See also: IR 05000275/2003008

Text

January 30, 2004

Gregory M. Rueger, Senior Vice

President, Generation and

Chief Nuclear Officer

Pacific Gas and Electric Company

Diablo Canyon Power Plant

P.O. Box 3

Avila Beach, CA 93424

SUBJECT: DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION

REPORT 05000275/2003008 AND 05000323/2003008

Dear Mr. Rueger:

On December 31, 2003, the U.S. Nuclear Regulatory Commission completed an inspection at

your Diablo Canyon Power Plant, Units 1 and 2, facility. The enclosed integrated report

documents the inspection findings that were discussed on January 8, 2004, with Mr. David H.

Oatley and members of your staff.

This inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

There were five findings of very low safety significance (Green) identified in this report. Four of

the findings were NRC-identified and one was self-revealing. Four of these findings involved

violations of NRC requirements. However, because of their very low safety risk significance

and because they are entered into your corrective action program, the NRC is treating these

four findings as noncited violations (NCVs) consistent with Section VI.A of the NRC

Enforcement Policy. If you contest any NCV in this report, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC

20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission,

Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the Director, Office

of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the

NRC Resident Inspector at the Diablo Canyon Power Plant.

During the period of December 22, 2003, through January 9, 2004, the NRC has been

conducting event followup inspections at the Diablo Canyon Nuclear Plant in direct response to

the December 22, 2003, San Simeon earthquake. These event followup inspections continue.

The results of the inspections conducted through December 31, 2003, (referred to as Phase 1

of the event followup inspections) are documented in the enclosed inspection report (see

Section 1R14). The results of the inspection conducted January 1-9, 2004, (referred to as

Phase 2 of the event followup inspections) and additional onsite inspections planned through

Pacific Gas and Electric Company -2-

Unit 1 refueling outage, scheduled to begin in March 2004, (referred to as Phase 3 of the event

followup inspections) will be documented in NRC Inspection Report 05000275;323/2004002, to

be issued approximately at the end of April 2004.

On January 16, 2004, we provided you with some preliminary results of the NRCs event

followup for the December 22, 2003, San Simeon earthquake. (ADAMS

Accession ML040160653). That letter provided the preliminary results of the inspection

activities (Phases 1 and 2) conducted through January 9, 2004, and provided the scope for

Phase 3 of the NRCs actions that are ongoing. The Phase 3 activities will involve additional

planned inspections, including the visual inspections in Unit 1 containment during the March

2004 refueling outage and further review of your Special Report, submitted to the NRC on

January 5, 2004, and any supplemental report.

We plan to conduct a technical meeting with you on February 4, 2004, regarding your January

5, 2004, Special Report in San Luis Obispo, California. This meeting will be open to public

observation and will provide attending members of the public a period for comments and

questions prior to the conclusion of the meeting.

Pacific Gas and Electric Company operated under voluntary bankruptcy proceedings during this

inspection period. The NRC has monitored plant operations, maintenance, and planning to

better understand the impact of the financial situation and how it relates to your responsibility to

safely operate the Diablo Canyon reactors. NRC inspections, to date, have confirmed that you

are operating these reactors safely and that public health and safety is assured.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records System (PARS) component of NRC's document

system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

William B. Jones, Chief

Project Branch E

Division of Reactor Projects

Dockets: 50-275

50-323

Licenses: DPR-80

DPR-82

Enclosure:

Inspection Report 05000275/2003008

and 05000323/2003008

w/attachment: Supplemental Information

Pacific Gas and Electric Company -3-

cc w/enclosure:

David H. Oatley, Vice President

and General Manager

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424

Lawrence F. Womack, Vice President, Power

Generation & Nuclear Services

Diablo Canyon Power Plant

P.O. Box 56

Avila Beach, CA 93424

James R. Becker, Vice President

Diablo Canyon Operations and

Station Director, Pacific Gas and

Electric Company

Diablo Canyon Power Plant

P.O. Box 3

Avila Beach, CA 93424

Sierra Club California

2650 Maple Avenue

Morro Bay, CA 93442

Nancy Culver

San Luis Obispo Mothers for Peace

P.O. Box 164

Pismo Beach, CA 93448

Chairman

San Luis Obispo County Board of

Supervisors

Room 370

County Government Center

San Luis Obispo, CA 93408

Truman Burns\Robert Kinosian

California Public Utilities Commission

505 Van Ness Ave., Rm. 4102

San Francisco, CA 94102-3298

Diablo Canyon Independent Safety Committee

Robert R. Wellington, Esq.

Legal Counsel

857 Cass Street, Suite D

Monterey, CA 93940

Pacific Gas and Electric Company -4-

Ed Bailey, Radiation Control Program Director

Radiologic Health Branch

State Department of Health Services

P.O. Box 942732 (MS 178)

Sacramento, CA 94234-7320

Richard F. Locke, Esq.

Pacific Gas and Electric Company

P.O. Box 7442

San Francisco, CA 94120

City Editor

The Tribune

3825 South Higuera Street

P.O. Box 112

San Luis Obispo, CA 93406-0112

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Chief, Technological Services Branch

FEMA Region IX

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Pacific Gas and Electric Company -5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

Senior Resident Inspector (DLP)

Branch Chief, DRP/E (WBJ)

Senior Project Engineer, DRP/E (VGG)

Staff Chief, DRP/TSS (PHH)

RITS Coordinator (NBH)

Anne Boland, OEDO RIV Coordinator (ATB)

DC Site Secretary (AWC1)

Dale Thatcher (DFT)

W. A. Maier, RSLO (WAM)

ADAMS: Yes * No Initials: ___WBJ___

Publicly Available * Non-Publicly Available * Sensitive Non-Sensitive

R:\_DC\2003\DC2003-08RP-DLP.wpd

RIV:RI:DRP/E SRI:DRP/E TL:DRS/EMB C:DRS/PSB C:DRP/E

TWJackson DLProulx RLNease TWPruett WBJones

E E /RA/ /RA/ /RA/

1/28/04 1/28/04 1/27/04 1/26/04 1/28/04

D:DRP DRA RA C:DRP/E (for Signature)

ATHowell For TPGwynn BSMallett For WBJones

MASatorius /RA/ TPGwynn /RA/

1/28 /04 1 /30/04 1/30/04 1/30/04

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-275, 50-323

Licenses: DPR-80, DPR-82

Report: 05000275/2003008

05000323/2003008

Licensee: Pacific Gas and Electric Company (PG&E)

Facility: Diablo Canyon Power Plant, Units 1 and 2

Location: 7 1/2 miles NW of Avila Beach

Avila Beach, California

Dates: September 28 through December 31, 2003

Inspectors: D. L. Proulx, Senior Resident Inspector

T. W. Jackson, Resident Inspector

S. M. Wong, Risk Analyst

R. E. Lantz, Senior Emergency Preparedness Inspector

M. P. Shannon, Senior Health Physicist

B. Tharakan, Health Physicist

Approved By: W. B. Jones, Chief, Project Branch E

Division of Reactor Projects

Enclosure

CONTENTS

PAGE

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

REACTOR SAFETY

1R04 Equipment Alignments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R06 Flood Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R11 Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R13 Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . 11

1R14 Operator Performance during Nonroutine Evolutions and Events, Including

Followup Response to Earthquakes Impacting Diablo Canyon Power Plant . . 12

1R16 Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R19 Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

1EP2 Alert Notification System Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

1EP3 Emergency Response Organization Augmentation Testing . . . . . . . . . . . . . . . 22

1EP4 Emergency Action Level and Emergency Plan Changes . . . . . . . . . . . . . . . . . 22

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies . . . . . 23

1EP6 Emergency Preparedness Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

RADIATION SAFETY

2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

OTHER ACTIVITIES

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

40A4 Crosscutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

40A5 Other . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 31

40A6 Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32

ATTACHMENT: SUPPLEMENTAL INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

List of Acronyms . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-5

Enclosure

SUMMARY OF FINDINGS

IR 05000275/2003-008, 05000323/2003-008; 09/28/03 - 12/31/03; Diablo Canyon Power Plant

Units 1 and 2; Fire Protection, Maintenance Effectiveness, Postmaintenance Testing, ALARA

Planning and Controls, Problem Identification and Resolution.

This report covered a 14-week period of inspection by resident inspectors and announced

inspections in emergency preparedness and radiation protection and followup inspections to the

October 18 and December 22, 2003, earthquakes. Specifically, Section 1R14.1 documents the

followup inspections performed in response to earthquakes impacting the Diablo Canyon Power

Plant. The NRC identified four Green noncited violations and one Green finding. The

significance of most findings is indicated by their color (Green, White, Yellow, or Red) using

Inspection Manual Chapter 0609, Significance Determination Process. Findings for which the

Significance Determination Process does not apply may be Green or be assigned a severity

level after NRC management review. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

which requires written procedures be established, implemented, and maintained

covering the Fire Protection Program implementation. Specifically, PG&E failed

to adequately establish and implement procedural changes that provided for

senior control operators, licensed control operators, and nonlicensed, Level 8

nuclear operators to serve in the operator responder position. The inspectors

noted that the applicable attachment to the procedure for conduct of the

operations response position was not established until after training had been

provided on implementing the procedure. Operations responders supporting the

fire brigades exhibited a knowledge weakness in activities such as

communications with the control room, manual actuation of fire suppression

equipment, and providing information to the fire brigade regarding safe shutdown

equipment.

The finding impacted the procedure quality objective under the mitigating

systems cornerstone and was more than minor since there was an adverse

impact to a fire protection defense-in-depth element. Using the Significance

Determination Process (SDP) Phase I Screening Worksheet and the SDP

Phase II Notebook in Appendix F of Inspection Manual Chapter (IMC) 0609, the

inspectors determined that the finding was of very low safety significance.

Specifically, the significance of the finding was evaluated by considering fire

scenarios in the vital 4 kV Bus F switchgear room and auxiliary saltwater

Pump 1-1 vault. These two areas have the highest dependence on fire brigade

response since they have the highest fire ignition frequency for areas that do not

have automatic fire suppression. The inspectors evaluated the risk-significance

using half of the nominal credit for manual fire suppression as a result of the

Enclosure

-2-

finding. Using Tables 5.4, 5.5, and 5.6 of IMC 0609, both fire scenarios

screened as very low safety significance. Since the two fire scenarios were

considered worst-case for the finding, the inspectors determined that the finding

was of very low safety significance (Section 1R05.2).

  • Green. The inspectors identified a noncited violation for the failure to adequately

monitor the performance of the Unit 1 auxiliary feedwater system in accordance

with 10 CFR 50.65(a)(2). Specifically, the unavailability time performance criteria

for the auxiliary feedwater system had been exceeded during its monitoring

period, but the system was not monitored per 10 CFR 50.65(a)(1).

The finding impacted the mitigating systems cornerstone objective to ensure the

availability and reliability of the auxiliary feedwater system to respond to initiating

events. The finding is greater than minor using Example 1.f of Inspection

Manual Chapter 0612, Appendix E. Similar to the example, the inspectors

identified that Pacific Gas and Electric did not consider unavailability time for the

Unit 1 auxiliary feedwater system, although the unavailability time was due to

prior poor maintenance practices on Valve FW-1-FCV-437. If the unavailability

time was considered, the 10 CFR 50.65(a)(2) evaluation would be invalid. Using

the Significance Determination Process Phase I worksheet in Inspection Manual

Chapter 0609, Appendix A, the finding is of very low safety significance, since

there was no loss of an actual safety function, no loss of a safety-related train for

greater than the Technical Specification allowed outage time, and the finding is

not potentially risk significant due to a seismic, fire, flooding, or severe weather

initiating event (Section 1R12).

Appendix B, Criterion III, when Pacific Gas and Electric personnel failed to

adequately evaluate the capability of core exit thermocouples to measure the

radial temperature gradient for Quadrant 1 of the Unit 1 reactor core.

Specifically, maintenance personnel inadvertently swapped core exit

thermocouples at a connection, leaving only three operable thermocouples per

Trains A and B for Quadrant 1. When questioned by the inspectors, engineering

personnel could not provide an adequate technical bases for how measurement

of radial temperature gradient could be accomplished.

The finding impacts the mitigating system cornerstone through degraded overall

availability of the components within a system used to assess and respond to

initiating events to prevent undesirable consequences. The finding was greater

than minor when compared to Example 3.a of Inspection Manual Chapter 0612,

Appendix E. Similar to Example 3.a, Pacific Gas and Electric performed

additional work to verify the ability of the core exit thermocouples to measure

radial temperature gradient within Quadrant 1 of the Unit 1 reactor core. Using

the Significance Determination Process Phase 1 screening worksheet from

Inspection Manual Chapter 0609, Appendix A, the finding was determined to be

of very low safety significance, since the deficiency was confirmed not to result in

loss of function per Generic Letter 91-18, Revision 1 (Section 1R19).

Enclosure

-3-

was identified for failure to promptly identify and correct a condition adverse to

quality. Specifically, in December 2000, Pacific Gas and Electric failed to identify

and correct the population of Rockwell-Edwards valves in safety-related and risk-

significant systems that were susceptible to failure of the packing gland follower

flange from intergranular stress corrosion cracking. Pacific Gas and Electric

received an industry notification in December 2000 that Rockwell-Edwards

valves were vulnerable for this type of failure, but initiated corrective actions on a

very limited population of valves (those involving a trip risk). As a result, on

December 3, 2003, the packing gland follower flange for safety injection

Valve SI-1-8890A (pressure equalization valve) on the hot leg injection line

failed, due to intergranular stress corrosion cracking, resulting in excessive

packing gland leakage.

The finding impacted the mitigating systems cornerstone through degraded

equipment performance for a system train that responds to initiating events to

prevent undesirable consequences. The finding is greater than minor because

the finding would become a more significant safety concern if the valve condition

was left uncorrected. The amount of leakage from the valve would be

significantly greater than a 30 drop per minute leak rate, if the safety injection

pumps were fully running in the hot leg injection mode. The Valve SI-1-8890A

leak rate is bounded by a residual heat removal pump seal failure. Pacific Gas

and Electric concluded the safety injection system was operable but degraded

because both safety injection system trains would be available to provide

adequate flow if a demand occurs. Using the Significance Determination

Process Phase 1 worksheet in Inspection Manual Chapter 0609, Appendix A, the

finding was determined to be of very low safety significance, since there is no

loss of an actual safety function, no loss of a safety-related train for greater than

the Technical Specification allowed outage time, and the finding is not potentially

risk significant due to a seismic, fire flooding, or severe weather initiating event

(Section 4OS2.2)

Cornerstone: Occupational Radiation Safety

  • Green. A finding was identified because Pacific Gas and Electric failed to

maintain collective doses as low as is reasonably achievable. Specifically, work

activities associated with Radiation Work Permit 03-2055, "Reactor Coolant

Pump (RCP) 2-2, 10 year inspection," exceeded 5 person-rem and the dose

estimation by more than 50 percent due to a miscommunication among work

groups.

The failure to maintain collective doses as low as is reasonably achievable is a

performance deficiency. This finding was more than minor because it is

associated with the Occupational Radiation Safety Cornerstone attribute

(program and process) and affected the associated cornerstone objective (to

ensure adequate protection of workers health and safety from exposure to

radiation). This occurrence involved inadequate planning which resulted in

Enclosure

-4-

unplanned, unintended occupational collective dose for the work activity. When

processed through the Occupational Radiation Safety Significance Determination

Process, this finding was found to have no more than very low safety

significance because the finding was an as low as is reasonably achievable

planning issue and Pacific Gas and Electric Companys 3-year rolling average

collective dose was less than 135 person-rem (Section 2OS2).

B. Licensee-Identified Violations

None.

Enclosure

REPORT DETAILS

Summary of Plant Status

Diablo Canyon Unit 1 began this inspection period at 100 percent power. On December 10,

2003, operators reduced power on Unit 1 to approximately 24 percent power in anticipation of

high swells and kelp impacting the traveling screens. On December 11 operators increased

reactor power to 53 percent to support a leak search in the main condenser. Following the

search for the leak, operators increased reactor power and Unit 1 reached 100 percent power

on December 12. Unit 1 remained at 100 percent power for the duration of the inspection

period.

Diablo Canyon Unit 2 began this inspection period at 100 percent power. On December 10,

2003, operators reduced power to approximately 24 percent power in anticipation of high swells

and kelp impacting the traveling screens. Following the high swells, operators increased

reactor power on December 11 and achieved 100 percent power on the same day. Unit 2

remained at 100 percent power for the duration of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignments (71111.04)

The inspectors performed four partial system walkdowns and one complete system

walkdown during this inspection period.

Partial System Walkdowns

.1 Unit 2 Startup Transformer 2-1

a. Inspection Scope

On October 21, 2003, while Diesel Engine Generator (DEG) 2-2 was in a maintenance

outage window, the inspectors performed a partial system walkdown of Startup

Transformer 2-1. The inspectors observed valve alignment, material condition, labeling,

lubrication, and structural support. The inspectors used Procedure OP J-2:II, Startup

Bank Return to Service, Revision 18, for reference during the inspection.

b. Findings

No findings of significance were identified.

Enclosure

-2-

.2 Unit 1 DEG 1-1

a. Inspection Scope

On October 27, 2003, while DEG 1-2 was in a maintenance outage window, the

inspectors performed a partial system walkdown of DEG 1-1. The inspectors reviewed

valve alignment, leakage, electrical power availability, labeling, lubrication, ventilation,

seismic supports, and absence of physical interference. The inspectors used the

following documents as reference during the inspection:

  • Procedure OP J-6B:I, Diesel Generator 1-1 Make Available, Revision 26
  • Drawing 106721, Diesel Engine - Generator

- Sheet 3, Revision 43

- Sheet 4, Revision 37

- Sheet 5, Revision 27

- Sheet 6, Revision 40

b. Findings

No findings of significance were identified.

.3 Unit 2 Residual Heat Removal (RHR) Pump 2-2

a. Inspection Scope

During a plant status walkdown on November 5, 2003, the inspectors noticed a slight

accumulation of bearing oil at the base of RHR Pump 2-2. The inspectors reported the

potential oil leak to operators, who in turn initiated Action Request (AR) A0594205. The

inspectors followed up with Pacific Gas and Electric Companys (PG&Es) actions

regarding the potential oil leak by performing a partial system walkdown of RHR

Pump 2-2 on November 6. The inspectors used the following documents during the

partial system walkdown:

  • A0533113, RHR Pump 2-2 Oil Leak
  • A0594205, RHR PP 2-2 Motor Oil at Base of Pump

b. Findings

No findings of significance were identified.

.4 Unit 2 Radiation Monitors

a. Inspection Scope

On November 5, 2003, while Radiation Monitor Power Supply Transformer TPRM21

was in a maintenance outage window, the inspectors performed a partial system

Enclosure

-3-

walkdown of Unit 2 radiation monitors. The inspectors reviewed valve alignment,

electrical power availability, labeling, operational status, ventilation, seismic supports,

and absence of physical interference. The inspectors used Clearance 76058 and

Technical Specification Sheet T0047944.

b. Findings

No findings of significance were identified.

Complete System Walkdown

Unit 1 Control Room Ventilation System (CRVS)

a. Inspection Scope

The inspectors performed a complete system walkdown of the Unit 1 control room

ventilation system on November 12, 2003. During the walkdown, the inspectors

observed proper system alignment and material condition. The inspectors also

reviewed past and present deficiencies. The inspectors used Drawing 106723,

Ventilation and Air Conditioning, Sheet 16, Revision 82. The inspectors also reviewed

the ARs listed in Attachment 1.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

The inspectors performed four fire protection walkdowns and one fire drill review during

this inspection period.

.1 Routine Observations

a. Inspection Scope

The inspectors performed four fire protection walkdowns to assess the material

condition of plant fire detection and suppression, fire seal operability, and proper control

of transient combustibles. The inspectors used Section 9.5 of the Final Safety Analysis

Report (FSAR) Update as guidance. The inspectors considered whether the

suppression equipment and fire doors complied with regulatory requirements and

conditions specified in Procedures STP M-69A, Monthly Fire Extinguisher Inspection,

Revision 33, STP M-69B, Monthly CO2 Hose Reel and Deluge Valve Inspection,

Revision 14, STP M-70C, Inspection/Maintenance of Doors, Revision 8, and OM8.ID4,

Control of Flammable and Combustible Materials, Revision 10. Specific risk-significant

areas inspected included:

  • Units 1 and 2, 4kV switchgear rooms in the turbine building

Enclosure

-4-

  • Units 1 and 2, switchgear rooms of the auxiliary building

b. Findings

No findings of significance were identified.

.2 Fire Drill

a. Inspection Scope

The inspectors verified the capability of the fire brigade to effectively prevent and fight

fires at the Diablo Canyon Power Plant. Specifically, the inspectors reviewed the

qualification and training of the operations responder position. The purpose of the

operations responder is to provide a communications link between the control room and

the incident commander (fire brigade leader), provide fire and fire protection system

status information, and support protection of safe shutdown equipment. The inspectors

interviewed PG&E operators and fire protection personnel, and reviewed fire protection

documents as part of the inspection effort.

b. Findings

Introduction. The inspectors identified a violation of Technical Specification 5.4.1.d,

which requires written procedures be established, implemented, and maintained

covering the Fire Protection Program implementation. Specifically, PG&E failed to

adequately establish and implement a procedure that provided for senior control

operators, licensed control operators and nonlicensed, Level 8 nuclear operators to

serve in the operator responder position. The inspectors noted that the applicable

attachment to the procedure for conduct of the operations response position was not

established until after training had been provided on implementing the procedure.

Operations responders supporting the fire brigades exhibited a knowledge weakness in

activities such as communications with the control room, manual actuation of fire

suppression equipment, and providing information to the fire brigade regarding safe

shutdown equipment. The failure to adequately establish the procedure and its

attachment and implement the procedural changes through effective training resulted in

an adverse change in the fire protection program, during the period the violation existed.

Description. Prior to 1998, the fire brigade leader was a senior control operator and the

fire brigade members were licensed and nonlicensed operators. The senior control

operator possessed knowledge of fire protection systems, safe shutdown equipment,

and other plant equipment, and also acted as a liaison to the control room. Following

the change to a professional fire brigade in 1998, senior control operators were

assigned to be the operations responder to a fire event. In this position, they primarily

acted as a liaison between the control room and the fire brigade and provided limited

recommendations for protecting safe shutdown equipment.

On August 29, 2003, PG&E instituted an additional change to the operations responder

position. In addition to using the senior control operators, licensed control operators and

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nonlicensed, Level 8 nuclear operators could be used as operations responders. A

2-hour training session was provided to nuclear operators on the duties of an operations

responder, prior to August 29, 2003. The training session was outlined in Lesson

Number R032C12, Operations Responder Responsibilities. Procedure CP M-6, Fire,

Revision 2, included a checklist for the operations responder duties in Attachment 4.2,

Operations Responder Checklist. However, the procedure and checklist were not

issued until September 12, 2 weeks after licensed control operators and nuclear

operators could serve as operations responders.

The inspectors interviewed various control operators and nuclear operators and

identified the following deficiencies and issues concerning the operations responder

position:

  • Senior control operators and licensed control operators had not received formal

training on the operations responder position.

  • A majority of the operators served on the fire brigade before the professional fire

brigade took over, and they expressed a higher degree of confidence in

performing the duties of the operations responder, as compared to those who did

not have prior fire brigade experience.

  • More than one of the operators did not know the phone number for accessing

the fire conference bridge, and others had learned about the protocol for the fire

conference bridge the day the interview was performed.

  • The operators expressed a desire for more thorough training on the operations

responder position.

  • The operators were not aware that Attachment 4.2 of Procedure CP M-6, titled

Operations Responder Checklist, existed.

  • The operations responder position does not have a qualification card, nor is it

part of requalification training for operators.

  • Action Request A0579928 stated that, as of August 29, 2003, all Level 8 nuclear

operators had received the operations responder training, but the inspectors

interviewed one nuclear operator that had not received the training.

  • The control operators and nuclear operators had not participated in drills with the

fire brigades and identified a lack of interaction with the brigades.

In addition to interviews, the inspectors compared Attachment 4.2 of Procedure CP M-6

to Lesson R032C12, Operations Responder Responsibilities. The inspectors noted

the following items were missing from the lesson plan when compared to

Attachment 4.2. The lesson plan did not discuss:

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  • The need for the operations responder to be on the fire conference call by dialing

onto the associated bridge;

  • The need to pick up the radio, pre-plans, and checklist from the fire equipment

storage locker before reporting to the incident commander;

  • The combination to the fire equipment storage locker although all operators that

were interviewed knew the combination;

  • The need for the operations responders to identify and communicate which fire

doors are propped open; and

  • Manual actions when the automatic fire suppression systems did not operate.

Section 9.5 of the FSAR Update outlines PG&Es compliance with NRC Branch

Technical Position APCSB 9.5-1. Table B-1 of Appendix 9.5B, Regulatory Compliance

Summary, states, in part, the following aspects of Branch Technical

Position APCSB 9.5-1 for which PG&E is committed to comply with:

  • Personnel

. . . the FSAR should discuss the training and the updating provisions such as

fire drills provided for maintaining the competence of the station fire fighting and

operating crew . . .

C Fire Brigade Organization, Training, and Equipment

Basic training is a necessary element in effective fire fighting operation. In

order for a fire brigade to operate effectively, it must operate as a team. All

members must know what their individual duties are.

The inspectors determined that PG&E failed to comply with the above items since all fire

brigade members did not know what their individual duties are. The inspectors

observed that PG&E does not consider the operations responder as part of the fire

brigade; therefore, they provided little or no training to the operations responders. Prior

to the implementation of the professional fire brigade in 1998, the operations responder

duties were performed by the fire team leader who was a senior control operator. When

PG&E implemented the professional fire brigade, the operations knowledge was

separated out from the fire brigade and given to the operations responder. Therefore,

without the presence of a competent operations responder, the fire brigades capability

would be adversely impacted following the 1998 fire brigade change. Since senior

control operators had performed the function of the fire brigade leader prior to the

professional fire brigade implementation, the senior control operators indicated they

were comfortable filling the operations responder position. However, operators who had

no prior experience on the fire brigade indicated they were not comfortable with

performing the operations responder duties.

Enclosure

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Analysis. The performance deficiency associated with this finding is a failure to adequately

establish and maintain Procedure CP M-6. The finding impacted the procedure quality

objective under the mitigating systems cornerstone and was more than minor since there was

an adverse impact to a fire protection defense-in-depth element. Using the Significance

Determination Process (SDP) Phase I Screening Worksheet and the SDP Phase II Notebook in

Appendix F of Inspection Manual Chapter (IMC) 0609, the inspectors determined that the

finding was of very low safety significance. Specifically, the significance of the finding was

evaluated by considering fire scenarios in the vital 4 kV Bus F switchgear room and auxiliary

saltwater Pump 1-1 vault. These two areas have the highest dependence on fire brigade

response since they have the highest fire ignition frequency for areas that do not have

automatic fire suppression. The inspectors evaluated the risk-significance using half of the

nominal credit for manual fire suppression as a result of the finding. Using Tables 5.4, 5.5, and

5.6 of IMC 0609, both fire scenarios screened as very low safety significance. Since the two

fire scenarios were considered worst-case for the finding, the inspectors determined that the

finding was of very low safety significance.

Enforcement. The inspectors identified a violation of Technical Specification 5.4.1.d, which

requires written procedures be established, implemented, and maintained covering the Fire

Protection Program implementation. Specifically, PG&E failed to adequately establish and

implement Procedure CP M-6 for senior control operators, licensed control operators, and non-

licensed operators to serve in the operations responder position. The inspectors noted that

Attachment 4.2 of the procedure was not established until after operators could be assigned the

operations responder position. Because the failure to establish and implement

Procedure CP M-6 was determined to be of very low safety significance and has been entered

into the corrective action program as AR A0597355, this violation is being treated as a non-

cited violation, consistent with Section VI.A of the NRC Enforcement Policy: NCV 50-275;

323/03-08-01, Failure to Establish and Implement Fire Program Procedural Changes for

Operations Responders in Support of the Fire Brigade.

1R06 Flood Protection (71111.06)

The inspectors performed one external and one internal flood protection inspection

during this inspection period.

.1 External Flood Protection

a. Inspection Scope

The inspectors reviewed PG&Es flood protection measures for Units 1 and 2 to ensure

that adequate precautions had been taken to mitigate external flood risks. Specifically,

the inspectors walked down the exterior areas of the intake structure, auxiliary building,

and turbine building for flood water entry paths. The inspectors used Chapter 3 of the

FSAR Update in support of this inspection.

b. Findings

No findings of significance were identified.

Enclosure

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.2 Internal Flood Protection

a. Inspection Scope

The inspectors reviewed PG&Es flood protection measures for Units 1 and 2 to ensure

that adequate precautions had been taken to mitigate internal flood risks. Specifically,

the inspectors reviewed corrective action documents and walked down cable pull-boxes.

The inspectors verified operable sump pumps and drains, settings for level alarms, and

intact condition of cable splices subject to submergence. The inspectors used

Probabilistic Risk Assessment Calculation F.4, PRA Internal Floods Analysis,

Revision 4, in support of this inspection.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

a. Inspection Scope

The inspectors witnessed one operator requalification training session during routine

training in the simulator. The inspectors verified the crews ability to meet the objectives

of the training scenario and attended the post-scenario critique to verify that crew

weaknesses were identified and corrected by PG&E staff. The inspectors witnessed

simulator training involving shutting down and return to power of an operating unit using

the new digital electrohydraulic control system, including startup and connecting the unit

to the electrical grid. In addition, operators performed a surveillance of the reactor

protection system with respect to the turbine control and stop valves. The inspectors

used Procedures L-3, "Secondary Plant Startup," Revision 28; L-4, "Normal Operation at

Power," Revision 44; OP C-3:II, "Main Unit Turbine-Startup," Revision 33; and

OP C-3:III, "Main Unit Turbine-At Power Operations," Revision 12A, to support the

inspection activities.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors performed three inspections of PG&Es Maintenance Rule

implementation for equipment performance problems. The inspectors assessed

whether the equipment was properly placed into the scope of the rule, whether the

failures were properly characterized, and whether goal setting was recommended, if

required. Procedure MA1.ID17, Maintenance Rule Monitoring Program, Revision 11,

was used as guidance. The inspectors reviewed the following ARs:

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  • A0576813, Maintenance Rule Performance Criteria, Goal Setting Review for

Units 1 and 2 Containment Isolation Valves

  • A0574369, Maintenance Rule Performance Criteria, Goal Setting Review for

Unit 1 Auxiliary Feedwater System

  • A0584097, Maintenance Rule Performance Criteria, Goal Setting Review for

Units 1 and 2 Containment Fan Cooler Unit Drain Collection System

b. Findings

Introduction. A Green noncited violation was identified by the inspectors for the failure

to adequately monitor the performance of the Unit 1 auxiliary feedwater (AFW) system

in accordance with 10 CFR 50.65(a)(2).

Description. On October 31, 2003, the inspectors reviewed a 10 CFR 50.65(a)(1)

evaluation in AR A0574369 for the Unit 1 AFW system. The inspectors noted a series

of AFW system water contaminations that were first noted in June 2001. Contaminates

included chlorides and other minerals and elements commonly found in natural water

supplies near the plant. The cause of the AFW system water contaminations was due

to incorrect travel stop settings for Valve FW-1-FCV-437. Valve FW-1-FCV-437 is a

butterfly valve that utilizes a Limitorque HBC gear drive and a handwheel to manually

actuate the valve. The safety function of the valve is to open and allow water from the

raw water reservoir to be used as a backup to the condensate storage tank and the

firewater storage tank. Since the travel stops were not at the proper setting, they

prevented the valve from fully closing, thus allowing water from the raw water reservoir

to enter the AFW system and result in contamination. PG&E staff discovered that the

travel stops were set during preventive maintenance, but moved when the valve was

actuated. The travel stops moved because the cover of the travel stop box on the HBC

drive did not secure the travel stop nuts. PG&E is initiating corrective actions to prevent

the travel stops from moving. Other similar valves in Units 1 and 2 have been evaluated

for travel stop movement. No other valves were found to exhibit the same condition.

Due to the water contamination, operators cleared portions of the Unit 1 AFW system in

order to flush the system. The Unit 1 AFW system incurred additional hours of

unavailability time for the flushing operation. Per AR A0574369, the performance

criteria for the Unit 1 AFW system to remain monitored under 10 CFR 50.65(a)(2) has

an unavailability time less than or equal to 67.17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br />. The total unavailability time for

the Unit 1 AFW system was 69.18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br />. Despite exceeding the unavailability

performance criteria, PG&E continued to monitor the Unit 1 AFW system under

10 CFR 50.65(a)(2) for two reasons. First, they believed the root causes and corrective

actions under Nonconformance Reports (NCR) N0002129 and N0002148 were

sufficient to address the issue and to prevent a similar event from recurring. Second,

the cause of the contamination events was due to improper maintenance practices and

not equipment failures. Therefore, PG&E staff felt that the corrective actions for

contamination events were related to human performance and that the issue was

outside the intentions of 10 CFR 50.65(a)(1).

Enclosure

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The inspectors determined that PG&E did not meet the requirements of

10 CFR 50.65(a)(2) when the Unit 1 AFW system exceeded the unavailability time goals

and was not placed in 10 CFR 50.65(a)(1). The inspectors identified that the corrective

actions under NCRs N0002129 and N0002148 did not fully address the issues with the

Unit 1 AFW system water contamination. PG&E initiated a third NCR, N0002167, to

address the movement of Valve FW-1-FCV-437 travel stops due to the clearance

between the travel stop box cover and the travel stop nuts. NCR N0002167 also

contained actions to address the failure of the two previous NCRs to identify and correct

the cause of the Unit 1 AFW system water contamination. NCR N0002167 was initiated

after AR A0574369 documented that corrective actions under NCRs N0002129

and N0002148 were sufficient to address the cause of the water contamination.

The inspectors determined that PG&Es conclusion regarding human performance and

10 CFR 50.65 was incorrect. Specifically, PG&E did not consider human performance

errors during maintenance activities to be within the scope of 10 CFR 50.65, even if

human performance errors resulted in a maintenance preventable functional failure or

unavailability time. 10 CFR 50.65(a)(2) states, in part, that monitoring under

10 CFR 50.65(a)(1) is not required if it has been demonstrated that the performance or

condition of a structure, system, or component is being effectively controlled through the

performance of appropriate preventive maintenance. The inspectors identified the

human performance errors, regarding preventive maintenance, on Valve FW-1-FCV-437

to be inappropriate, resulting in the Unit 1 AFW system incurring additional unavailability

time for flushing.

Analysis. The inspectors determined that PG&Es failure to adequately monitor the

performance of the Unit 1 AFW system in accordance with 10 CFR 50.65(a)(2) was a

performance deficiency. The finding impacted the mitigating systems cornerstone

objective to ensure the availability and reliability of the AFW system to respond to

initiating events and is greater than minor, using Example 1.f of Inspection Manual

Chapter (IMC) 0612, Appendix E. Similar to the example, the inspectors discovered that

PG&E staff did not consider unavailability time for the Unit 1 AFW system, although the

unavailability time was due to prior poor maintenance practices on

Valve FW-1-FCV-437. With the unavailability time considered, PG&Es

10 CFR 50.65(a)(2) evaluation was invalid. Using the SDP Phase I worksheet in

IMC 0609, Appendix A, the finding is of very low safety significance, since there was no

loss of an actual safety function, no loss of a safety-related train for greater than the

Technical Specification allowed outage time, and the finding is not potentially risk

significant due to a seismic, fire, flooding, or severe weather initiating event.

Enforcement. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in

10 CFR 50.65(a)(1) is not required where it has been demonstrated that the

performance or condition of a structure, system, or component is being effectively

controlled through the performance of appropriate preventive maintenance, such that

the structure, system, or component remains capable of performing its intended

function. However, PG&E did not consider all the unavailability time for the Unit 1 AFW

system when reviewing the systems status in 10 CFR 50.65(a)(2). The performance

criteria for the Unit 1 AFW system to remain monitored under 10 CFR 50.65(a)(2) was

Enclosure

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exceeded, in part, because of the human performance errors such that PG&E did not

demonstrate that the performance of the system was being effectively controlled

through the performance of appropriate preventive maintenance. Because the failure to

adequately monitor performance of the Unit 1 AFW system according to

10 CFR 50.65(a)(2) is of very low safety significance and has been entered into the

corrective action program as AR A0595257, this violation is being treated as a noncited

violation, consistent with Section VI.A of the NRC Enforcement Policy: NCV 50-275/

03-08-02, Failure to Adequately Monitor Auxiliary Feedwater System According to

10 CFR 50.65(a)(2).

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

The inspectors performed five inspection samples of maintenance risk assessments and

emergent work control.

.1 Risk Assessments

a. Inspection Scope

The inspectors reviewed daily work schedules and compensatory measures to confirm

that PG&E had performed proper risk management for routine work. The inspectors

considered whether risk assessments were performed according to their procedures

and PG&E had properly used their risk categories, preservation of key safety functions,

and implementation of work controls. The inspectors used Procedure AD7.DC6,

On-line Maintenance Risk Management, Revision 7, as guidance. The inspectors

specifically observed the following work activities during the inspection period:

  • Unit 1, maintenance outage windows for Component Cooling Water Heat

Exchanger 1-2, Atmospheric Dump Valve MS-1-PCV-19, and Positive

Displacement Pump 1-3 on September 30

  • Unit 2, Eagle 21 Protection Set Rack 13 Nonvolatile Random Access Memory

replacement and Atmospheric Dump Valve MS-2-PCV-20 calibration on

October 23

  • Units 1 and 2, 500 kV breaker replacement work on November 6

b. Findings

No findings of significance were identified.

.2 Emergent Work

a. Inspection Scope

The inspectors observed two emergent work activities to verify that actions were taken

to minimize the probability of initiating events, maintain the functional capability of

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mitigating systems, and maintain barrier integrity. The scope of work activities reviewed

includes troubleshooting, work planning, plant conditions and equipment alignment,

tagging and clearances, and temporary modifications. The following activities were

observed during this inspection period:

  • Unit 2, Valve FCV-495 actuator replacement
  • Unit 1, Valve SI-1-8890 packing leakage

b. Findings

No findings of significance were identified.

1R14 Operator Performance during Nonroutine Evolutions and Events, Including Followup in

Response to Earthquakes Impacting Diablo Canyon Power Plant (71111.14)

a. Inspection Scope

The inspectors reviewed three inspection samples (two earthquakes and high Pacific

Ocean swells) of nonroutine evolutions or events.

.1 Earthquakes In the Vicinity of the Diablo Canyon Power Plant

Background

Diablo Canyon Power Plant is located in a seismically active area along the interface of

the Pacific and North American Plates. Several faults are located within 50 miles of the

plant. PG&E is required by the operating license to maintain a Long-Term Seismic

Program to reevaluate the seismic design bases against insights and knowledge gained

with each seismic event. FSAR Update Section 3.7 describes the seismic design basis

of the facility. The plant was designed for ground motion from a Design Earthquake,

equivalent to an "Operating Basis Earthquake," in which the plant can be expected to

continue to operate. This value is ground motion acceleration at the containment base

of 0.2g. The Double Design Earthquake, equivalent to a Safe Shutdown Earthquake,

is the design basis for most safety-related structures, and has ground motion

acceleration of 0.4. The plant is also evaluated for the maximum ground acceleration

which can result from an earthquake originating in the Hosgri fault. This evaluation

ensures the plant can be safely shut down if the expected maximum ground motion

were to occur.

Technical Specification 3.3.1, "Reactor Trip System," requires instrumentation to initiate

a reactor trip for a nominal ground acceleration of 0.35 g. An earthquake force monitor,

which has three sensors, provides an alarm in the control room at a minimum of 0.01g

of ground acceleration. Procedure CP M-4, Earthquake, Revision 18, addresses the

actions required to be taken in the event of an earthquake of 0.01 g or greater.

Enclosure

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Deer Canyon Earthquakes

Description

At 12:52 a.m., on October 18, 2003, Diablo Canyon Power Plant Units 1 and 2 declared

a Notification of Unusual Event (NOUE) because an earthquake that measured 3.4 was

felt by the control room operators. No damage to plant equipment was observed and

both units remained at 100 power throughout the event.

A preshock occurred at 12:27 a.m. that lasted approximately 3 seconds and was felt by

the control room operators. No alarms or other effects were noted. The primary shock

occurred at 12:39 a.m. and lasted approximately one second. The epicenter of the

seismic event was located 2.8 miles east-southeast of the plant (within the owner

controlled area) and measured 3.4. The primary shock resulted in momentary turbine

bearing high vibration alarms on both units and a high level alarm on the Unit 1 Safety

Injection Accumulator 1-3. The plants seismic monitor recorded a peak acceleration of

0.02 g.

Following declaration of the NOUE, operators entered Procedure CP M-4, which

contained instructions for response to earthquakes detected at the site. The shift

manager initiated a preliminary evacuation of the intake structure (where valve

maintenance was in progress) until the extent of the seismic event was understood.

PG&E performed walkdowns of both containments and all vital areas to ensure no

immediate structural damage was evident. PG&E performed enhanced monitoring of

safety-related tank levels to ensure no ruptures occurred. No damage to any plant

equipment was identified.

Following confirmation that the earthquake resulted in no plant damage, PG&E exited

the NOUE at 3:30 a.m. The inspectors responded to the site to monitor PG&Es actions

and verified that PG&E performed the actions prescribed by Procedure CP M-4. The

inspectors walked down safety-related areas of the plant and noted no evidence of

damage that would affect safety system operability. The inspectors continued to

examine the status of structures following the October 18, 2003, earthquake during

routine plant status walkdowns throughout the inspection period.

The inspectors reviewed Special Report 50-275;323/03-03-00, "Seismic Event of

October 18, 2003," which discussed the Deer Canyon earthquakes of October 18 and

provided analysis of the effects of the earthquakes on plant structures, systems, and

components. The inspectors found the report properly analyzed the seismic data and

the impact that the ground motion had on structures, systems, and components.

San Simeon Earthquake 35 Miles Northwest of the Site

Description

At approximately 10:30 a.m. PST on December 22, 2003, the resident inspectors heard

a noise on the roof of the Diablo Canyon administrative building. The inspectors

Enclosure

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responded to the control room to report this information to the shift manager. The shift

manager received similar reports from personnel in the warehouse and the training

building outside the protected area. The inspectors and the operators verified that no

alarms were received in the control room and that the seismic monitor did not register

this event. The shift manager and the inspectors reviewed Procedure CP M-4 and

verified that no action was required.

At 11:16 a.m. PST a magnitude 6.5 earthquake struck 35 miles north-northwest of

Diablo Canyon. Both resident inspectors were at the site. The shaking lasted

22 seconds. The senior resident inspector (SRI) immediately contacted the Region IV

branch chief and informed the branch chief that an earthquake had been felt.

While the SRI was briefing Region IV, the resident inspector (RI) responded to the

control room at 11:18 a.m. to observe the operators. The RI walked down the panels,

reviewed the status of safety systems, and verified that PG&E was implementing the

emergency plan. The RI noted that the seismic monitor recorded a seismic event of

0.04g. The RI established the NRCs reactor safety counterpart link and advised the

NRC headquarters operations officer that PG&E would soon be declaring a NOUE.

The SRI reported to the control room to observe PG&E actions. The inspectors verified

that the requirements of Procedure CP M-4 were followed. The procedure required

verification of the tank levels of all of the major safety-related tanks to ensure that no

catastrophic failures of the important tanks had occurred. The inspectors verified the

applicable tank levels. The procedure also required a complete walkdown of plant

areas. PG&E received annunciators for the Unit 1 spent fuel pool level and safety

injection accumulator high and low levels for both units during the seismic event

because of sloshing of the water. Operators received temporary alarms that included

high vibration for the Unit 1 turbine. The operating electrohydraulic control pump tripped

and was immediately restarted. Operators cleared the alarms following the shaking.

PG&E declared a NOUE at 11:22 a.m. The inspectors verified that PG&E made the

required calls to the state and local officials. PG&E sent personnel to the Emergency

Operating Facility (EOF), which is co-located with the San Luis Obispo County Office of

Emergency Services to assist in monitoring the community and the emergency services

response. PG&E established a video conference between the EOF and the shift

manager's office for the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. One of the inspectors was present in the shift

managers office during each of the updates between the EOF and the control room.

The EOF advised the control room of damage to Highway 46 and fallen rocks on

Highway 41, which is an emergency evacuation route. The inspectors communicated

the status of local roadways to Region IV. Highways 46 and 41 had debris on the road,

and Highway 46 experienced some buckling, but the highways were passable for

emergency response purposes. In addition, personnel in the EOF communicated the

status of several emergency sirens that were inoperable because of the power outages

in San Luis Obispo county.

Fifty-six of the 131 emergency sirens were inoperable because of power outages.

Alternate means of notifying people within the affected areas were available. As of

Enclosure

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3:40 p.m., on December 22, 2003, 35 sirens were without power, and at 6 p.m.

26 sirens were still without power. At 1:30 a.m., on December 23, 2003, four sirens

were without power. The remaining four were restored in the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The inspectors monitored reports of PG&E walkdowns of the plant. At approximately

3 p.m., the RIs began independent inspections of plant equipment, for Phase I of the

NRC inspection plan following the earthquake. One RI remained in the control room to

monitor operator actions and maintain communications within the agency, while the

other inspector walked down plant areas.

The inspectors walked down the turbine building first. The emergency diesel

generators, the component cooling water heat exchangers, and high voltage switchgear

are in this building. The inspectors verified that no leaks existed in the safety-related

systems and that no cracks were evident in structural members.

The inspectors then walked down the switchgear areas of the auxiliary building. The

inspectors verified that no damage occurred in the ac and dc switchgear rooms, the

cable spreading room, and the battery rooms.

The inspectors entered the radiologically controlled area of the auxiliary building and

performed complete inspections of the emergency core cooling pumps and systems,

component cooling water pumps, auxiliary feedwater pumps, and RHR system heat

exchangers.

The inspectors entered the fuel building and verified the level in the spent fuel pools. All

structural elements in the spent fuel pool were unaffected. Spent fuel pool water clarity

was good. No cracks were evident in the fuel building ventilation system or structural

members.

The inspectors walked down the outside areas of the plant. The inspectors verified that

the applicable security barriers were still intact. The inspectors verified that the major

outside tanks (condensate storage tanks, refueling water storage tanks, primary water

storage tanks, and fire water storage tank) had no cracks or obvious damage. The

inspectors toured the intake structure and verified that no damage occurred to the

traveling screens and auxiliary saltwater pumps, pipes, and valves.

The RIs provided continuous site coverage until PG&E exited the NOUE. Because the

area continued to experience aftershocks, PG&E elected to remain in a NOUE for

approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The RIs continued to inspect the facility and monitor control

room actions for the duration of the NOUE. During the evening, the inspectors walked

down the offsite power sources (startup transformers) and continued to monitor

communications with the emergency facilities. The inspectors examined the auxiliary

and startup transformers for damage. PG&E personnel reported that two switches were

damaged in the 230 kV system at the offsite Morro Bay switchyard. The Morro Bay

switchyard is one source of offsite power to the startup transformers. PG&E declared

the startup transformers inoperable to provide safe electrical isolation and cleared the

230 kV lines to support replacement of the damaged switches. The startup

Enclosure

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transformers were returned to operable status within the 72-hour limiting condition for

operation action statement. The RIs remained at the site, continuing to inspect and

monitor PG&E actions until 2 p.m. PST on December 23. PG&E exited the NOUE at

approximately 12:15 p.m., PST on December 23, 2003.

In the days following the event, the inspectors continued to review PG&Es response to

aftershocks and the adequacy of the PG&E procedures and the Emergency Plan. The

inspectors attended PG&E's Event Review Team meetings throughout the remainder of

the inspection period.

a. Findings

During the inspections, no system or structural damage or evidence of differential

deflections were detected, and no site ground effects were noted during exterior visual

inspections. In addition, no damage was noted to the administration building, which is

designed to the Uniform Building Code. The licensees immediate response to the

earthquake was effective in ensuring continued safe operation, and their implementation

of the NRCs prompt notification requirements was timely and correct.

All seismic instrumentation functioned correctly. The NRC inspectors conducted a

review of the required surveillances on seismic monitoring instruments. All instruments

were correctly calibrated. The inspectors noted that the licensee is in the process of

upgrading the current Earthquake Force Monitor to a digital distributed system that will

provide better information (e.g., wider frequency response and more monitoring

locations).

Casualty Procedure M-4 was used in responding to the earthquake. Although overall

response to the earthquake was adequate, several lessons were learned by PG&E from

a subsequent review of the implementation of the procedure. PG&E has begun a

general revision to improve its quality based on this experience.

The inspectors reviewed PG&Es reportability procedure for loss of the early warning

system sirens. During the review, the inspectors noted that the procedure for

notification of the NRC for a loss of the early warning system sirens only addressed

sirens within a 10-mile radius and not the entire Diablo Canyon Emergency Planning

Zone, as defined in the Emergency Plan. In this case, the licensee did inform the NRC

of the loss at the time the Unusual Event notification was made.

.2 Units 1 and 2 Downpowers because of High Pacific Ocean Swells

a. Inspection Scope

On December 9, 2003, PG&E received warning of impending high Pacific Ocean swells.

Upon notification of the high swells, PG&E management determined that the units would

be ramped down to approximately 25 percent power to prevent the traveling screens,

from being clogged with kelp, which could necessitate tripping the circulating water

pumps and a reactor trip of the affected unit. At 1:30 a.m., on December 10, operators

Enclosure

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slowly decreased power on both units. The inspectors responded to the site and

monitored the operator performance during the downpower and operator response to

any high differential pressure across the traveling screens.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds

a. Inspection Scope (71111.16)

The inspectors reviewed three samples of operator workarounds.

The inspectors reviewed PG&Es documented actions in which degraded conditions or

changes to accident analyses required additional operator action beyond that credited in

the design basis to compensate for these conditions. PG&E tracked two types of these

conditions: operator burdens and operator workarounds.

PG&E defined an operator burden as a manual action taken to compensate for

degraded equipment that affected normal operation of a unit. PG&E had 17 operator

burdens.

PG&E defined an operator workaround as a manual action taken to compensate for a

degraded condition required for response to abnormal or emergency operating

procedures. PG&E had 17 active operator workarounds. The inspectors assessed the

cumulative affect of the operator workarounds to determine if operators would be overly

taxed with working around numerous degraded conditions that would complicate an

abnormal or emergency condition.

The NRC inspectors reviewed PG&Es program for tracking the operator workarounds

and restoring the applicable systems to full qualification to determine if PG&E

appropriately managed these items. None of the operator workarounds involved

risk-significant actions.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed eight postmaintenance tests for selected risk-significant

systems to verify their operability and functional capability. As part of the inspection

process, the inspectors witnessed and/or reviewed the postmaintenance test

acceptance criteria and results. The test acceptance criteria was compared to the

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Technical Specifications and the FSAR Update. Additionally, the inspectors verified that

the tests were adequate for the scope of work and were performed as prescribed,

jumpers and test equipment were properly removed after testing, and test equipment

range, accuracy, and calibration were consistent for the application. The following

selected corrective maintenance activities were reviewed by the inspectors:

  • Unit 1, Thermocouple Monitoring System Trains A and B reconnection following

open thermocouple detection circuit on April 13 and 26, 2002 (Work

Orders C0176158 and C0176579)

  • Unit 1, RHR Pump 1-2 inspection for water intrusion into terminal box on

January 14 (Work Orders C0178108 and C0178123)

  • Unit 2, Diesel Engine Generator 2-1 routine maintenance outage window on

September 30 (Work Orders R0240283, R0231007, and R0231009)

  • Unit 2, Diesel Engine Generator 2-3 high pressure fuel line leak repair on

October 9 (AR A0592470 and Work Order C0184992)

  • Unit 1, Atmospheric Dump Valve MS-1-PCV-21 calibration on October 21-22

(Work Orders R0245981 and R0245983)

  • Unit 1, Diesel Engine Generator 1-2 air start motor preventive maintenance on

October 27 (Work Order C0182839)

  • Unit 1, Auxiliary Building Ventilation System Exhaust Fan E-1 preventive

maintenance on December 2 (Work Order R0228685)

  • Unit 1, Pressure Balancing Valve SI-1-8890A packing replacement and repair

tool installation on December 3 (Work Order C0185920)

b. Findings

Introduction. A Green noncited violation was identified by the inspectors for failure to

adequately evaluate the capability of core exit thermocouples to measure radial

temperature gradient for Quadrant 1 of the Unit 1 reactor core, as required by 10 CFR

Part 50, Appendix B, Criterion III.

Description. During Refueling Outage 1R11, maintenance personnel disconnected the

core exit thermocouple connections on top of the Unit 1 reactor vessel head for reactor

vessel head removal for refueling operations. On April 26-27, 2002, maintenance

personnel concluded reconnection of the core exit thermocouples on top of the Unit 1

reactor vessel head. On September 10, 2003, reactor engineers identified a

discrepancy among several of the core exit thermocouple temperature readings while

performing an in-core flux map. The reactor engineers noticed that some of the

thermocouples were reading lower than expected temperatures and others were reading

higher than expected temperatures. A troubleshooting team evaluated the

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discrepancies and concluded that maintenance personnel had incorrectly swapped the

Trains A and B thermocouple connectors at Port 79 on the reactor vessel head.

Maintenance personnel and operators did not identify the incorrect connection prior to

reactor startup, since the temperature readings were uniform for all thermocouples. The

discrepancy in thermocouple readings becomes noticeable at full reactor power when

the thermocouples near the center of the reactor core read higher than those towards

the outside of the core. However, operators did not notice the discrepancy at full power

operation since they checked to see if the thermocouple readings were in a valid range

rather than checking to see if the readings were an expected value.

The inspectors reviewed the Technical Specification bases documents for core exit

thermocouples and identified the following design aspects:

  • At least two channels of valid core exit thermocouples per quadrant are required,

with a channel consisting of two thermocouples.

  • In a channel, one thermocouple must be near the core center and the other must

be near the core periphery in order to measure radial temperature gradient.

  • The two channels must ensure that a single failure will not disable the ability to

determine radial temperature gradient.

The inspectors observed that PG&E did not take credit for the swapped thermocouples,

leaving only 6 operable thermocouples in Quadrant 1 of the reactor core. The

inspectors questioned whether the possible core exit thermocouple pairs for each train

could meet the requirement for measuring radial temperature gradient. Specifically,

Train A relied on a combination of Thermocouple 15 with Thermocouples 1 or 11.

Thermocouple 15 had three assemblies from the outside of the core, while

Thermocouples 1 and 11 had one and two assemblies from the outside of the core,

respectively. Similarly, Train B relied on a combination of Thermocouple 5 with

Thermocouples 14 or 36. Thermocouple 5 had three assemblies from the outside of the

core, while Thermocouples 14 and 36 had one and two assemblies from the outside of

the core, respectively. When the inspectors requested design bases information for the

selection of thermocouple pairs for each quadrant, PG&E was not able to provide the

design documents or an adequate technical basis for the selection.

The inspectors reviewed AR A0528665, which was initiated in April 4, 2001. The AR

requested a clarification of the core exit thermocouple surveillance procedure with the

design bases. However, the AR failed to adequately address the technical basis for the

location of thermocouples for measuring radial temperature gradient within the reactor

core. The inspectors determined that both core exit thermocouple channels for

Quadrant 1 of the Unit 1 reactor could be considered operable if appropriate

compensatory actions/modifications were taken. Specifically, the swapped

thermocouples continued to provide reliable temperature information, but in the wrong

locations. The inspectors observed that PG&E posted a sign on the Unit 1

thermocouple monitoring system, indicating the swapped thermocouples and what

locations of the core they were actually measuring temperature.

Enclosure

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Analysis. The inspectors determined that, following the swapping of core exit

thermocouples, PG&Es failure to adequately evaluate the technical bases for

measuring radial temperature gradient within the reactor core was a performance

deficiency. The finding impacts the mitigating system cornerstone through degraded

overall availability of the components within a system used to assess and respond to

initiating events to prevent undesirable consequences and was greater than minor when

compared to Example 3.a of IMC 0612, Appendix E. Similar to Example 3.a, PG&E

staff performed additional work to verify the ability of the core exit thermocouples to

measure radial temperature gradient within Quadrant 1 of the Unit 1 reactor core. Using

the SDP Phase 1 screening worksheet from IMC 0609, Appendix A, the finding was

determined to be of very low safety significance, since the deficiency was confirmed not

to result in loss of function per Generic Letter 91-18, Revision 1.

Enforcement. 10 CFR Part 50, Appendix B, Criterion III, states, in part, that measures

shall be established for the selection and review for suitability of application of materials,

parts, equipment, and processes that are essential to the safety-related functions of

structures, systems, and components. Contrary to the above, PG&E failed to

adequately address the suitability of the remaining operable Quadrant 1 core exit

thermocouples for measuring core radial temperature gradient. Because this failure to

provide adequate technical basis for core exit thermocouple operability is of very low

safety significance and has been entered into the corrective action program as

AR A0597575, this violation is being treated as a noncited violation, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 50-275/03-08-03, Failure to Provide

Adequate Technical Bases for Core Exit Thermocouple Radial Temperature

Measurement.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors performed three inspection samples of surveillance testing.

The inspectors evaluated several routine surveillance tests to determine if PG&E

complied with the applicable Technical Specification requirements to demonstrate that

equipment was capable of performing its intended safety functions and operational

readiness. The inspectors performed a technical review of the procedure, witnessed

portions of the surveillance test, and reviewed the completed test data. The inspectors

also considered whether proper test equipment was utilized, preconditioning occurred,

test acceptance criteria agreed with the equipment design basis, and equipment was

returned to normal alignment following the test. The following tests were evaluated

during the inspection period:

  • Procedure STP I-1C, Routine Weekly Checks Required By Licenses (Unit 1),

Revision 77 on October 9

  • Procedure STP P-AFW-21, "Routine Surveillance Test of Turbine Driven

Auxiliary Feedwater Pump 2-1," Revision 16, on October 16

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  • Procedure STP I-2D, Nuclear Power Range Incore/Excore Calibration,

Revision 48 on November 18

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed two inspection samples of temporary plant modifications.

The inspectors reviewed a sample of two temporary plant modifications that could

potentially impact the mission of important safety systems. Temporary plant

modifications include jumpers, lifted leads, temporary systems, repairs, design

modifications, and procedure changes which can introduce changes to plant design or

operations. There were 30 active temporary modifications during this inspection period.

Inspection activities included a review of the temporary modification impact on:

(1) operability of equipment, (2) energy requirements, (3) material compatibility,

(4) structural integrity, (5) environmental qualification, (6) response time, and (7) logic

and control integration. The inspectors also verified the design and alignment of safety

systems when the temporary modifications were no longer needed. The following

temporary modification was reviewed during this inspection period:

  • Unit 1, Measuring and test equipment added to battery Charger 1-2 float

feedback circuit for troubleshooting per Work Order C0185038 and

AR A0592302

  • Unit 1, Add second off-globe valve to 1-04L-41, per Work Order C0184388 and

AR A0588971

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert Notification System Testing (71114.02)

a. Inspection Scope

The inspector performed one inspection sample. The inspector discussed the status of

offsite siren and tone alert radio systems with the PG&E staff to determine if significant

changes had been made to those systems or methods of maintenance and testing of

the systems. The inspector reviewed the documents and correspondence associated

Enclosure

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with the November 2000 Early Warning System Operating System Project Proposal.

The inspector compared the current testing and maintenance methods described in

EP MT-43, Early Warning System Testing and Maintenance, with requirements in

10 CFR Part 50, Appendix E. PG&Es alert and notification system testing program was

compared with criteria in NUREG-0654, Criteria for Preparation and Evaluation of

Radiological Emergency Response Plans and Preparedness in Support of Nuclear

Power Plants; Federal Emergency Management Agency (FEMA) Report REP-10,

Guide for the Evaluation of Alert and Notification Systems for Nuclear Power Plants;

and the PG&Es FEMA-approved alert and notification system design report.

b. Findings

No findings of significance were identified.

1EP3 Emergency Response Organization Augmentation Testing (71114.03)

a. Inspection Scope

One inspection sample was performed. The inspector discussed with PG&E the status

of primary and backup systems for mobilizing the emergency response organization

during an emergency to determine PG&Es ability to staff emergency response facilities

in accordance with PG&Es emergency plan and the requirements of 10 CFR Part 50,

Appendix E. The inspector reviewed correspondence associated with contracting out

the emergency response organization call out function. The inspector reviewed the

results of three rapid-response drills conducted following activation of the new call out

process. The inspector also reviewed the following documents related to the

emergency response organization augmentation system:

  • EP G-2, Interim Emergency Response Organization
  • EP G-3, Emergency Notification of Off-Site Agencies

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

One inspection sample was performed. The inspector performed an on-site review of

the following Emergency Plan revisions. The revisions were compared to the previous

revisions; the criteria of NUREG-0654, Criteria for Preparation and Evaluation of

Radiological Emergency Response Plans and Preparedness in Support of Nuclear

Power Plants; and the requirements of 10 CFR 50.47(b) and 50.54(q) to determine if

the revisions decreased the effectiveness of the emergency plan.

Enclosure

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  • Revision 4, Change 4 to Tab 5, Organizational Control of Emergencies, and

Revision 4, Change 3 to Tab 7, Emergency Facilities and Equipment, submitted

on November 4, 2003. These revisions replaced the on-site health physics

communication phone line with a satellite phone system.

  • Revision 4, Change 3 to Tab 4, Emergency Classification, and Revision 33 to

EP G-1, Attachment 7.1, Emergency Action Level Classification Chart,

submitted November 4, 2003. This revision replaced the control room main

annunciator printer with a computer and touch screen monitor to provide the

same functions.

b. Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a. Inspection Scope

One inspection sample was performed. The inspector reviewed the following

documents related to PG&Es corrective action program to determine PG&Es ability to

identify and correct problems in accordance with 10 CFR 50.47(b)(14) and 10 CFR Part

50, Appendix E:

department between September 2001 and October 2003

  • Detailed review of 27 action requests
  • Annual exercise and quarterly drill self-assessments from October 23, 2002;

May 28, 2003; and July 17, 2003

  • 50.54(t) Review, May 11, 2002; and April 4, 2003
  • Quality Performance Assessment Report, Third Period 2003, July 1 to

September 30, 2003

b. Findings

No findings of significance were identified.

Enclosure

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1EP6 Emergency Preparedness Evaluation (71114.06)

a. Inspection Scope

The inspectors witnessed one emergency preparedness drill that included emergency

plan implementation conducted on October 29, 2003. The scenario simulated a large

break loss-of-coolant accident, coupled with clogging of the containment recirculation

sump. The scenario continued with damage to fission product barriers, core damage,

and a radiological release to the environment to demonstrate PG&Es capabilities to

implement the emergency plan. The inspectors witnessed PG&E performance in the

control room (i.e., simulator), the Technical Support Center, and the Emergency Offsite

Facility. The inspectors also attended PG&Es self-critique of the scenario. The

following procedures were used to evaluate the performance:

  • Procedure EOP E-1, Loss of Reactor or Secondary Coolant, Revision 18
  • Procedure EOP FR-C.1, Response to Inadequate Core Cooling, Revision 15

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS2 As Low as is Reasonable Achievable (ALARA) Planning and Controls (71121.02)

a. Inspection Scope

The inspector completed eight samples of ALARA planning and controls.

The inspector assessed PG&Es performance in implementing physical and

administrative controls for airborne radioactivity areas, radiation areas, and high

radiation areas, radiation worker practices, and work activity dose results against

procedural and regulatory requirements. No high exposure work activities in high

radiation or airborne areas were performed during the inspection. Therefore, this aspect

could not be evaluated.

The inspector interviewed radiation protection staff and other radiation workers to

determine the level of planning, communication, ALARA practices, and supervisory

oversight integrated into work planning and work activities. The inspector reviewed

initial and emergent work scopes and estimated man-hours provided to the radiation

protection group for accuracy. In addition, the following items were reviewed and

compared with procedural and regulatory requirements to assess PG&Es program to

maintain occupational exposures ALARA:

Enclosure

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  • Plant collective exposure history for the past 3 years, current exposure trends,

source term measurements, and 3-year rolling average dose information

  • Processes, methodology, and bases used to estimate, justify, adjust, track, and

evaluate exposures

  • Three ALARA prejob, in-progress, and postjob reviews and associated radiation

work permit (RWP) packages from Unit 2 Refueling Outage 11 activities which

resulted in some of the highest personnel collective exposures (RWPs 03-2002,

03-2044, and 03-2005)

  • Temporary shielding program and implementation
  • Hot spot tracking and reduction program
  • Quality Verification Audit 031700023, Quality Verification Assessment Report for

the Third Period 2003, Quality Verification Assessment Report 030410010, and

the 2002 Annual Review of the DCPP Radiation Protection Program

  • Three ALARA Review Committee meeting minutes (February 6, June 19, and

October 14, 2003)

  • Declared pregnant worker and embryo/fetus dose evaluation, monitoring, and

controls

  • Summary of corrective action documents written since the last inspection and

selected documents relating to exposure tracking, higher than planned exposure

levels, radiation worker practices, and repetitive and significant individual

deficiencies.

b. Findings

Introduction. The inspector identified collective doses for reactor coolant pump (RCP)

work activities performed during Unit 2 Refueling Outage 11 were not maintained

ALARA. Specifically, the inspector determined that the work activity associated with

RWP 03-2055, "Reactor Coolant Pump (RCP) 2-2, 10 year inspection," exceeded

5 person-rem and the dose estimation by more than 50 percent.

Description. During a review of RWP packages and accumulated dose for Unit 2

Refueling Outage 11 work, the inspector identified that work associated with RCP 2-2

was originally estimated on January 10, 2003, to be completed for 1.5 person-rem. Due

to concerns identified during the inspection of RCP 2-2, the work scope was expanded

to include similar work on RCP 2-1. On February 15, 2003, the job dose was properly

re-estimated and justified, for the known work scope, to be 2.9 person-rem. However,

due to the failure to communicate the full work scope and radiological conditions among

Enclosure

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the predictive maintenance personnel, the RCP component engineer, and the ALARA

staff, the 2.9 person-rem estimate was exceeded. Specifically, the ALARA staff and the

RCP component engineer were not informed by the predictive maintenance staff that

the maintenance task included numerous motor stator balance efforts that would be

performed during the time the steam generators were drained. The job was completed

for 5.4 person-rem (86 percent greater than the justified estimate).

Analysis. The failure to maintain collective doses ALARA is a performance deficiency.

This finding was more than minor because it is associated with the Occupational

Radiation Safety Cornerstone attribute (program and process) and affected the

associated cornerstone objective (to ensure adequate protection of worker health and

safety from exposure to radiation). This occurrence involved inadequate planning,

which resulted in unplanned, unintended occupational collective dose for a work activity.

When processed through the Occupational Radiation Safety SDP, this finding was

found to have no more than very low safety significance because the finding was an

ALARA planning issue and the PG&Es 3-year rolling average collective dose was less

than 135 person-rem. PG&E entered this finding into their corrective action program as

AR A0595776 (FIN 50-323/2003-08-04, Failure to maintain job dose ALARA).

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

a. Inspection Scope

Three inspection samples were performed. The inspector sampled PG&E submittals for

the performance indicators listed below for the period from October 31, 2002, through

September 30, 2003. The definitions and guidance of NEI (Nuclear Energy

Institute 99-02, Regulatory Assessment Indicator Guideline, were used to verify

PG&Es basis for reporting each data element in order to verify the accuracy of

performance indicator data reported during the assessment period. PG&Es

performance indicator data were reviewed against the requirements of Procedure

AWP EP-001, Emergency Preparedness Performance Indicators.

Emergency Preparedness Cornerstone:

  • Drill and Exercise Performance (DEP)
  • Emergency Response Organization Participation (ERO)
  • Alert and Notification System Reliability

The inspector reviewed a sample of drill and exercise scenarios and licensed operator

simulator training sessions, notification forms, and attendance and critique records

associated with training sessions, drills, and exercises conducted during the verification

period. PG&Es performance was reviewed against the requirements of the PG&Es

Emergency Plan and EP G-3, Emergency Notification of Off-Site Agencies. The

inspector reviewed a sample of 8 emergency responder qualification and training

Enclosure

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records and a sample of 10 drill participation records. The inspector reviewed alert and

notification system testing procedures, maintenance records, and a 100 percent sample

of siren test records.

b. Findings

The inspector observed one instance where a DEP performance indicator opportunity

for notification accuracy and timeliness was incorrectly judged as a successful

opportunity. During an operator continuing training simulator session, the scenario

conditions required an Alert declaration and changed approximately 3 minutes later to

require a Site Area Emergency declaration. The first emergency declaration was made

as a Site Area Emergency approximately 17 minutes after conditions required the Alert

declaration. This performance was critiqued thoroughly by the PG&E operations and

emergency preparedness staff, and it was concluded to be acceptable performance due

to the rapidly changing plant conditions. The DEP performance indicator for event

classification was also evaluated as successful. The inspectors discussed this

evaluation with the emergency preparedness staff and concluded that the classification

opportunity should have been evaluated as a missed opportunity. NEI 99-02 requires

that the classification opportunity be evaluated as unsuccessful if the declaration of the

emergency classification is not made within 15 minutes of the time that conditions that

require the declaration are available to the decision maker. Based on that criteria in this

case, the performance indicator would be successful if an Alert or Site Area Emergency

had been declared within 15 minutes of the time that conditions for an Alert were

available. This change would not have affected the reported performance indicator

color.

The inspector also noted that Procedures EP G-2 and EP G-3 discussed the role of the

unaffected unit shift foreman as the control room communicator with responsibilities

including gathering information and completing the offsite notification form and

performing the communications to the offsite agencies. This would require that the unit

shift foremen be tracked in the ERO performance indicator as control room

communicators, in addition to the Shift Manager, who also performs those functions.

PG&E only tracks the shift manager for the ERO performance indicator, since, in

practice, the shift manager is the only individual who completes the notification form.

PG&E entered the procedure inconsistency in the corrective action process as

AR A0594284 to change Procedures EP G-2 and EP G-3 to reflect the site practice that

only the shift manager performs the communicator functions of filling out the notification

forms.

4OA2 Problem Identification and Resolution (71152)

.1 Emergency Planning Annual Sample Review

a. Inspection Scope

The inspector selected 27 action requests for detailed review. The entries were

reviewed to ensure that the full extent of the issues was identified, an appropriate

Enclosure

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evaluation was performed, and appropriate corrective actions were specified and

prioritized. The inspector reviewed seven assessment reports and corrective actions

resulting from those assessments. The inspector evaluated corrective actions against

the requirements of Procedure OM7.ID1, Problem Identification and Resolution-Action

Requests, and Emergency Planning Guide EPG01, Problem Identification.

b. Findings

No findings of significance were identified.

.2 Packing Gland Follower Failure (Unit 1)

a. Inspection Scope

The inspectors reviewed the licensee response and actions that led to a packing gland

follower failure and leak from Valve SI-1-8890. The inspectors reviewed operator

actions on December 3, 2003, upon discovery of a significant leak from the packing

gland of Valve SI-1-8890 (as discussed in AR A0595692). The inspectors also

evaluated PG&E operating experience reviews dating to December 2000 that discussed

the potential for packing gland follower failures in Rockwell-Edwards valves

(AR A0522770).

b. Findings

Introduction. A self-revealing Green noncited violation was identified for the failure to

adequately evaluate operating experience related to failed packing gland followers for

Rockwell-Edwards valves. This was a violation of 10 CFR Part 50, Appendix B,

Criterion XVI, for failure to identify and correct a condition adverse to quality.

Description. On December 3, 2003, at 10:24 a.m., inservice inspection engineers

identified that Unit 1 Valve SI-1-8890A (the hot leg injection equalizing valve) had a

30 drop per minute leak rate from the packing gland. The inservice inspection engineer

initiated AR A0595692 to enter this item into the corrective action program. This

information was reported to the control room but not immediately acted upon. The

engineers reported this information to the system and component engineers, who

inspected the valve. The system engineer found that the packing gland follower flange

for Valve SI-1-8890 had split in two and that the valve leakage was excessive for the low

pressure condition with no pumps running. The system engineer reported this additional

information to the control room and stated that the packing would be rejected from the

valve and an excessive amount of leakage (on the order of several gallons per minute)

would result if the safety injection pumps were running.

The shift foreman evaluated this condition and, due to the cross-connected alignment of

the safety injection system, declared both trains of safety injection inoperable at

1:10 p.m. This entry into Technical Specification 3.0.3 required PG&E to take action to

shut down Unit 1 within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and go to Hot Standby within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. At

1:18 p.m., operators closed Valve SI-1-8821A, the cross-connect valve between the two

Enclosure

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safety injection trains. Thus, safety injection Pump 1-2 was isolated from the leak and

failed packing follower of Valve SI-1-8890A, and the shift foreman exited Technical Specification 3.0.3. The shift foreman entered the 72-hour limiting condition for

operation for inoperable safety injection Pump 1-2. On December 4, 2003, the

mechanics repaired and retested Valve SI-1-8890A and declared safety injection

Pump 1-2 operable.

Valve SI-1-8890A was a one-inch manual globe valve purchased from the

Rockwell-Edwards company. Operating experience Letter OE11685 issued in

December 2000 discussed a failure of a Rockwell-Edwards 1-inch manual globe valve at

another facility that resulted in a reactor trip. The valve failure at the other facility also

resulted from the splitting in two of the packing gland follower flange, ejecting the

packing gland follower, causing excessive packing leakage. The other licensee analyzed

this failure and determined that the packing gland follower flange was made from 410

stainless steel, a material with a very high hardness that was very susceptible to

intergranular stress corrosion cracking.

PG&E analyzed operating experience Letter OE11685 and determined that this

operating experience was applicable to Diablo Canyon. PG&E initiated AR A0522770 to

evaluate the impact of this industry experience on Diablo Canyon and take corrective

actions as deemed necessary. The engineers noted that Diablo Canyon had

225 Rockwell-Edwards valves installed, 113 for Unit 1 and 112 for Unit 2. PG&E staff

determined that, since the operating experience letter described an event in which the

packing gland follower flange failure resulted in a reactor trip, the evaluation for Diablo

Canyon need only encompass valves whose failure could cause a reactor trip. The

engineers did not consider taking action for valves in emergency core cooling systems

or valves that served as containment isolation valves, nor did the evaluation examine the

impact on plant risk. Thus, PG&E identified that only 12 valves at Diablo Canyon

needed to be repaired or back seated to meet the intent of operating experience

Letter OE11685.

The inspectors evaluated PG&Es review in AR A0522770 and determined that this

review of industry experience was insufficient, lacked thoroughness, and did not meet

the intent of determining the impact of the operating experience on plant safety. The

inspectors determined that this was a missed opportunity to identify and correct this

condition at Diablo Canyon, a violation of 10 CFR Part 50, Appendix B, Criterion XVI.

PG&E initiated AR A0595762 to enter this item into the corrective action program and

reevaluate operating experience OE 11685. PG&E then prioritized and took action to

either backseat, repair, or use a strongback on risk important valves.

Analysis. The inspectors determined that PG&Es failure to promptly identify and correct

a condition adverse to quality, which resulted in a packing gland follower failure and leak

from Valve SI-1-8890, was a performance deficiency. The finding impacts the mitigating

system cornerstone through degraded overall availability of the components within a

system used to assess and respond to initiating events to prevent undesirable

consequences and is greater than minor because the finding would become a more

significant safety concern if the leaky valve condition was left uncorrected. The amount

Enclosure

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of leakage from the valve would be significantly greater than a 30 drop per minute leak

rate, if the safety injection pumps were fully running in the hot leg injection mode. The

Valve SI-1-8890A leak rate is bounded by a RHR pump seal failure. Although PG&E

declared both trains of the safety injection system to be inoperable and entered

Technical Specification 3.0.3 upon discovery of the condition, the safety injection system

was considered to be operable but degraded because both safety injection system

trains would be available to provide adequate flow when a demand occurs. Using the

SDP Phase 1 worksheet in IMC 0609, Appendix A, the finding was determined to be of

very low safety significance, since there is no loss of an actual safety function, no loss of

a safety-related train for greater than the Technical Specification allowed outage time,

and the finding is not potentially risk significant due to a seismic, fire flooding, or severe

weather initiating event.

Enforcement. 10 CFR Part 50, Appendix B, Criterion XVI, states, in part, that measures

shall be established to assure that conditions adverse to quality are promptly identified

and corrected. Contrary to the above, in December 2000, PG&E failed to identify and

correct the population of Rockwell-Edwards valves in safety-related and risk-significant

systems that were susceptible to intergranular stress corrosion cracking and failure of

the packing gland follower flange. As a result, on December 3, 2003, the packing gland

follower flange for Valve SI-1-8890A on the hot leg injection line failed, due to

intergranular stress corrosion cracking. Because the failure to promptly identify and

correct Rockwell-Edwards valves that were susceptible to the hardened packing gland

follower flanges is of very low safety significance and has been entered into the

corrective action program as AR A0595762, this violation is being treated as a noncited

violation, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 50-275/03-08-05, Failure to promptly identify and correct Rockwell-Edwards valves

susceptible to packing gland follower flange failures.

.3 Cross-References to Problem Identification and Resolution Findings Documented

Elsewhere

Section 1RO5.2 of this report describes a PI&R crosscutting aspect for corrective

actions not being promptly implemented, related to the Fire Protection Program,

following concerns with implementation of the operations responder position.

4OA3 Event Followup (71153)

.1 (Closed) Licensee Event Report 50-275/03-001-00: Technical Specification 3.8.1,

Action B.1, Not Met Due to Personnel Error.

On October 9, 2003, a unit shift foreman recognized that operators failed to perform an

offsite power circuit check when an emergency diesel generator was declared

inoperable for exhaust stack slide bearing replacement. Technical Specification 3.8.1,

AC Sources - Operating, Action B.1, requires that an offsite power circuit check be

performed within one hour upon declaring an emergency diesel generator inoperable.

PG&E determined that the cause of Technical Specification violation was a failure of the

Unit 1 shift foreman to recognize the need to perform the offsite power circuit check.

Enclosure

-31-

The operators subsequently determined that two independent circuits between the off-

site transmission network and the on-site distribution system were operable. Corrective

actions include briefing all operating crews on effective control room communication and

modifying the Technical Specification tracking module to require a sign-off that any

required conditional surveillances are being implemented upon declaring equipment

inoperable. No new findings were identified in the inspectors review. The finding

constitutes a violation of minor significance that is not subject to enforcement action in

accordance with Section IV of the NRCs Enforcement Policy. PG&E documented the

problem in Nonconformance Report N0002172. This licensee event report is closed.

40A4 Crosscutting Aspects of Findings

Section 1R12 of the report describes a human performance crosscutting issue where

maintenance personnel performed improper maintenance practices on Valve FW-1-

FCV-437.

Section 1R19 of the report describes a human performance crosscutting issue where

personnel inappropriately assembled the core exit thermocouples and subsequently

failed to recognize for an extended period the thermocouple readings were not

consistent with the core design.

40A5 Other

Evaluation of Diablo Canyon Safety Condition in Light of Financial Conditions

a. Inspection Scope

Due to PG&Es financial condition, Region IV initiated special review processes for

Diablo Canyon. The RIs continued to evaluate the following factors to determine

whether the financial condition and power needs of the station impacted plant safety.

The factors reviewed included: (1) impact on staffing, (2) corrective maintenance

backlog, (3) corrective action system backlogs, (4) changes to the planned maintenance

schedule, (5) reduction in outage scope, (6) availability of emergency facilities and

operability of emergency sirens, and (7) grid stability (i.e., availability of offsite power to

the switchyard, status of the operating reserves, and main generator Volt-Ampere

reactive loading).

b. Findings

No findings of significance were identified.

Enclosure

-32-

40A6 Management Meetings

Exit Meeting Summary

The resident inspection results were presented on January 8, 2004, to Mr. David H.

Oatley, Vice President and General Manager, and other members of PG&E

management. PG&E acknowledged the findings presented.

The inspectors asked PG&E whether any materials examined during the inspection

should be considered proprietary. Proprietary information was reviewed by the

inspectors and left with PG&E at the end of the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

PG&E personnel

J. Becker, Vice President - Diablo Canyon Operations and Station Director

C. Belmont, Director, Nuclear Quality, Analysis, and Licensing

S. Chesnut, Director, Engineering Services

J. Hays, Director, Maintenance Services

S. Ketelsen, Manager, Regulatory Services

T. King, Manager, Learning Services

M. Lemke, Manager, Emergency Preparedness

D. Oatley, Vice President and General Manager, Diablo Canyon

P. Roller, Director, Operations Services

J. Tompkins, Director, Site Services

L. Womack, Vice President Nuclear Services

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Opened and Closed

50-275; 323/03-08-01 NCV Failure to Establish and Implement Fire Program

Procedural Changes for Operations Responders in Support

of the Fire Brigade (Section 1R05.2)

50-275/03-08-02 NCV Failure to Adequately Monitor Auxiliary Feedwater System

According to 10 CFR 50.65(a)(2) (Section 1R12)

50-275/03-08-03 NCV Failure to Provide Adequate Technical Bases for Core Exit

Thermocouple Radial Temperature Measurement

(Section 1R19)

50-323/03-08-04 FIN Failure to Maintain Job Dose ALARA (Section 2OS2)

50-275;323/03-08-05 NCV Failure to promptly identify and correct Rockwell-Edwards

valves susceptible to packing gland follower flange failures

(Section 4OA2.2)

Closed

50-275/03-001-00 LER Technical Specification 3.8.1, Action B.1, Not Met Due to

Personnel Error (Section 4OA3.1)

-2-

A-1 Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R04: Complete System Walkdown

Action Requests

A0546025 A0565358 A0575523 A0585572

A0546040 A0565369 A0575525 A0586410

A0547457 A0566251 A0575726 A0586489

A0549020 A0566911 A0577029 A0588816

A0549960 A0569438 A0577556 A0589346

A0552544 A0570386 A0577805 A0589783

A0553380 A0571874 A0579085 A0593236

A0558563 A0572253 A0583139 A0593493

A0560487 A0573626 A0584455 A0593495

A0560628 A0574099 A0584487

A0564139 A0575499 A0584685

A0564837 A0575511 A0584839

Section 1R05: Fire Protection

Licensing Basis Impact Evaluation Screen 1998-146, FSAR Section 9.5H - Revision 12"

Licensing Basis Impact Evaluation Screen 2003-004, FSAR Section 9.5H - Revision 14"

Section 1R06: Flood Protection

Action Requests

A0565300 A0568332 A0572819 A0581849

A0566672 A0571777 A0573248 A0592884

A0566894 A0572772 A0573508

Work Orders

R0239570

A-2 Attachment

Section 1R19: Post-Maintenance Testing

Action Requests

A0528665

A0538684

A0590156

Work Orders

C0176158

C0176579

Other Documents

Diablo Canyon Units 1 & 2, Technical Specification Bases, B3.3.3, PAM Instrumentation,

Revision 2

Procedure STP R-27A, Monthly Incore Thermocouple Evaluation, Revisions 6 & 8

Troubleshooting Log for A0590156

NRC Safety Evaluation Report SSER 31, Diablo Canyon - SSER 31: Staff Evaluation of

Miscellaneous Matters for Unit 2 (Board Notification No.85-051), May 2, 1985

Section 1EP2: Alert Notification System Testing

DCPP EWS Operating System - Project Proposal, November 2000

FEMA Region IX letters to PG&E, February 22 and May 11, 2001

PGE letter to FEMA Region IX, April 24, 2001

FEMA Early Warning System Design Report, December 1984

Section 1EP3: Emergency Response Organization Augmentation Testing

Rapid response drill reports from January 22, May 17, and September 9, 2003

Section 1EP4: Emergency Action Level and Emergency Plan Changes

OM10.ID2, Emergency Plan Revision and Review

Section 1EP5: Correction of Emergency Preparedness Weaknesses and Deficiencies

Action Requests: 0547774, 0550693, 0551200, 0554959, 0555070, 0558465, 0558491,

0558493, 0559139, 0566575, 0567256, 0567309, 0570531, 0572729, 0579860, 0580113,

0580122, 0580152, 0580154, 0582237, 0583140, 0583142, 0583391, 0584767, 0587734,

0589170, 0592987

A-3 Attachment

Section 4OA2: Problem Identification and Resolution

Self-Assessment for NRC Information Notice 2002-14, October 3, 2003

Self-Assessment, Bravo Team Graded Exercise, October 23, 2002

Self-Assessment, Charlie Team Drill, May 28, 2003

Self-Assessment, Alpha Team Drill, July 17, 2003

Section 2OS2: ALARA Planning and Controls

Procedures:

AD2.ID1 Procedure Use and Adherence, Revision 11

RP1 Radiation Protection, Revision 3

RP1.DC4 Radiological Hot Spot Identification and Control Program, Revision 1A

RP1.ID1 Requirements For The ALARA Program, Revision 2B

RP1.ID2 Use and Control of Temporary Radiation Shielding, Revision 5B

RP1.ID10 Embryo/Fetus Protection Program, Revision 2A

RCP D-205 Performing ALARA Reviews, Revision 13

RCP D-240 Radiological Posting, Revision 12A

Temporary Shielding Packages:

91-163

98-059

Hot Spot Packages:

113

116

Action Requests:

ETR-V0042728, AR- A0536032, A0571273, A0572734, A0572911, A0575867, A0577951,

A0578496, A0579604, A0581774, A0585060, A0589289, A0591813, and A0592291

A-4 Attachment

LIST OF ACRONYMS

ADAMS agency document access and management system

AFW auxiliary feedwater

ALARA as low as is reasonably achievable

AR action request

DEG diesel engine generator

CFR Code of Federal Regulations

DEP drill and exercise performance

EOF Emergency Operations Facility

ERO emergency response organization

FEMA Federal Emergency Management Agency

FIN finding

FSAR Final Safety Analysis Report

IMC Inspection Manual Chapter

LER licensee event report

NCR nonconformance report

NCV noncited violation

NEI Nuclear Energy Institute

NOUE notification of unusual event

NRC Nuclear Regulatory Commission

PARS publicly available records system

PG&E Pacific Gas and Electric Company

RCP reactor coolant pump

RHR residual heat removal

RI resident inspector

RWP radiation work permit

SDP significance determination process

SRI senior resident inspector

URI unresolved item

A-5 Attachment