LR-N03-0518, November 2003 Monthly Operating Report for Salem Unit 1

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November 2003 Monthly Operating Report for Salem Unit 1
ML033570223
Person / Time
Site: Salem PSEG icon.png
Issue date: 12/15/2003
From: Fricker C
Public Service Enterprise Group
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LR-N03-0518
Download: ML033570223 (3)


Text

. PSEG Nuclear LLC P.O. Box 236, Hancocks Bridge, New Jersey 08038-0236 DEC 1 5 2003 § NuclearLLC PSEG LR-N03-051 8 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:

MONTHLY OPERATING REPORT SALEM GENERATING STATION UNIT I DOCKET NO. 50-272 In compliance with Section 6.9, Reporting Requirements for the Salem Unit I Technical Specifications, the operating statistics for November 2003 are being forwarded.

Sincerely, Ca I J. Fricker Salem Plant Manager Attachments C Distribution 95-2168 REV. 7199

DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 12/11/03 COMPLETED BY: F. Todd TELEPHONE: (856) 339-1316 Reporting Period November 2003 OPERATING DATA REPORT Design Electrical Rating (MWe-Net) 1130 __ _

Maximum Dependable Capacity (MWe-Net) 1096 I :_-

Month Year-to-date Cumulative No. of hours reactor was critical 720 7734 149922 No. of hours generator was on line (service 720 7658 145209 hours)

Unit reserve shutdown hours 0 0 0 Net Electrical Energy (MWH) 770870 8294908 148198874 UNIT SHUTDOWNS NO. DATE TYPE DURATION REASON METHOD OF CORRECTIVE ACTIONI F=FORCED (HOURS) (1) SHUTTING COMMENT S=SCHEDULED DOWN THE REACTOR (2)

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip/Scram C - Refueling 3 - Automatic Trip/Scram D - Regulatory Restriction 4 - Continuation E - Operator Training/License Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other

DOCKET NO.: 50-272 UNIT: Salem 1 DATE: 12/11/03 COMPLETED BY: R. Ritzman TELEPHONE: (856) 339-1445 Summary Of Monthly Operating Experience

  • Salem 1 entered the month at approximately 100% power.
  • On November 15, power was reduced for a scheduled line outage. Power was restored to 100% later that day.
  • On November 25, power was reduced to approximately 76% due to circulator repairs and river grass intrusion. Salem 1 ended the month at this reduced power level.
  • At the end of the month, Salem 1 completed 42 days of continuous on-line operation.