IR 05000369/1979039
| ML19294B851 | |
| Person / Time | |
|---|---|
| Site: | McGuire |
| Issue date: | 01/23/1980 |
| From: | Donat T, Martin R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML19294B849 | List: |
| References | |
| 50-369-79-39, NUDOCS 8003060176 | |
| Download: ML19294B851 (4) | |
Text
.
.
'o UNITED STATES
' ~,
NUCLEAR REGULATORY COMMISSION
,
n
$
-"
sE REGION 11 e
o,,
- f 101 MARIETTA ST., N.W.. SUITE 3100
p*
ATLANTA, G EORGIA 30303
% e*
Report No. 50-369/79-39 Licensee: Duke Power Company 422 South Church Street Charlotte, North Carolina 28242 Facility: McGuire Nuclear Station Docket No. 50-369 License No. CPPR-83 Inspection at McGuire Nuclear Station near Charlotte, North Carolina Inspector:
/
7[(t( e
'
5 fo
~
T. J'. Donat C
'Date/ Signed Approved by:
[74(cu[
/
J fo R. D. Martin, Section Chief, RONS Branch
/Dat/ Signed SUMMARY Inspection on December 5-7, 1979 Areas Inspected:
This routine, unannour.ced inspection involved 19 inspector-hours onsite in the areas of preoperational test witnessing, observations of Ice loading operations, review of plant status, and review of previous inspection findings.
Results:
Of the four areas inspected, no items of noncompliance or deviations were identified.
/76 i
8003000 9"
.
-
-
.
,
)
DETAILS 1.
Persons Contacted Licensee Employees
- M.
D. McIntosh, Plant Manager
- W. M. Sample, Technical Services and Licensing Engineer
- E.
Estek, Associate Engineer
- D. Lampke, Assistant Engineer
- T.
L. McConnell, Supervisor Technical Services
- L. E. Weaver, Performance Engineer
- M.
Pacetti, Test Engineer D. Marquis, Assistant Engineer J. Bowles, Assistant Test Engineer M. Halls, Assistant Test Engineer D. Smith, Assistant Test Engineer Other licensee employees contacted included technicians, operators, and mechanics.
.
- Attended exit interview 2.
Exit Interview The inspection scope and findings were summarized on December 7, 1979 with those persons indicated in Paragraph I above. The inspector and licensee also discussed various organizational changes at the site.
,
3.
Licensee Action on Previous Inspect a Findings Not inspected.
4.
Unresolved Items Unresolved items were not identified during this inspection.
5.
Preoperational Test Witnessing The inspector witnessed the verification of plant initial condition, including establishing of minimum flows for the service water system loads, for preoperational test TP/1/A/1200/01.
Specific loads were:
(a) Waste Gas Compressor heat exchangers (b) Sample heat exchangers (c) Waste Evaporator condenser and cooler
.
%
-2-s (d) Recycle Evaporator condenser and cooler The inspector also witnessed the licensee trouble-shoot electrical problems encountered in preparation for Diesel Generator lA Load Sequencer Functional Test, TP/1/A/1350/08/A. Specifically, the time delay had been set on three relays in accordance with an instrumentation procedure, yet when checked in accordance with the test procedure were found to be out of specification.
Investigation by the licensee determined that the relays' time delay was in specification but that the onset of the time interval was effected by the length of time that a "Special Test Reset" button was depressed. Once this was identified the licensee corrected his test procedure to preclude this effect and was in the process of correcting problems with local diesel generator instruments before resuming the test.
6.
Unit 2 Preoperational Tests The licensee notified the inspector that he did not intend to perform a full pressure blow-down test of the upper head injection system on unit 2.
The basis for this decision was a Westinghouse letter (OBP-280, DUKE-4952)
from R. S. Howard to S. K. Blockley (Duke) dated 11/5/79.
In this letter Westinghouse stated that based on their analysis of the Unit 1 blowdown data, that a normal pressure blowdown of the Unit 2 Upper Head injection system would not be necessary and provided revised acceptance criteria for the low (90 PSIG) pressure blowdown. The letter states that meeting the revised acceptance criteria would insure that the final volume of water delivered to the reactor vessel during a normal blowdown would be within the band used in the ECCS analysis.
The licensee stated that an ammendment to the FSAR in sections 6.3 and 14.1 would be proposed identifying that a normal pressure UHI system blowdown would not be performed on unit 2.
The inspector acknowledged receipt of a copy of the Westinghouse letter and a memorandum on the proposed FSAR changes. The licensee though still must address how the isolation valves will be tested against maximum differential pressure as required by Reg Guide 1.79.
The resolution of the test program for the UHI system will be followed as Open Item 79-39-01.
7.
Unit 1 Ice Loading The inspector monitored the Unit 1 ice loading activities in progress which consisted of clearing ice chips and debris from around the baskets which had been already loaded. Repairing the conveyor feed belt between the ice machine storage hopper and the ice chopper / blower assembly had delayed resumption of loading operations. Recalibration of the spring scale and the dillon load cell had interrupted ice basket weighing.
8.
Site Personnel Reorganization The licensee informed the inspector of the following personnel and organiza-tional changes at McGuire Nuclear Station:
An Onshift Radiological / Chemistry group has been organized to handle waste processing activities. They will report to the station chemist and organiza-
.
-
s-3-t tionally be part of the chemistry department. The goal is to relieve the shift operators of all unnecessary tasks.
....
-