IR 05000261/2017002
ML17206A376 | |
Person / Time | |
---|---|
Site: | Robinson |
Issue date: | 07/25/2017 |
From: | Steven Rose NRC/RGN-II/DRP/RPB4 |
To: | Kapopoulos E Duke Energy Progress |
References | |
IR 2017002 | |
Download: ML17206A376 (29) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION uly 25, 2017
SUBJECT:
H. B. ROBINSON STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT 05000261/2017002
Dear Mr. Kapopoulos:
On June 30, 2017, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your H. B. Robinson Steam Electric Plant, Unit 2. On July 19, 2017, the NRC inspectors discussed the results of this inspection with you and members of your staff. On July 20, 2017, a re-exit meeting was conducted with Mr. Dave Huffman and other members of your staff, to discuss the final results of the inspection. Inspectors documented the results of this inspection in the enclosed inspection report.
The NRC inspectors did not identify any finding or violation of more than minor significance.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket No.: 50-261 License No.: DPR-23
Enclosure:
Inspection Report 05000261/2017002 w/Attachment: Supplemental Information
REGION II==
Docket Nos.: 50-261 License Nos.: DPR-23 Report No.: 05000261/2017002 Licensee: Duke Energy Progress, Inc.
Facility: H. B. Robinson Steam Electric Plant, Unit 2 Location: 3581 West Entrance Road Hartsville, SC 29550 Dates: April 1, 2017 through June 30, 2017 Inspectors: J. Zeiler, Acting Senior Resident Inspector G. Eatmon, Acting Senior Resident Inspector A. Beasten, Resident Inspector R. Kellner, Senior Health Physicist (Sections 2RS1, 2RS3, 2RS4)
J. Panfel, Health Physicist (Section 2RS2)
W. Pursley, Health Physicist (Sections 2RS5, 4OA1)
Approved by: Steven D. Rose, Chief Reactor Projects Branch 4 Division of Reactor Projects Enclosure
SUMMARY
Integrated Inspection Report 05000261/2017002, April 1, 2017, through June 30, 2017; Duke
Energy Progress, Inc., H. B. Robinson Steam Electric Plant, Unit 2, Operability Determinations and Functionality Assessments.
The report covered a 3-month period of inspection by resident inspectors and three regional inspectors. The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 6. No findings or violations of greater than minor significance were identified.
REPORT DETAILS
Summary of Plant Status
The unit began the inspection period shut down in Mode 4 for a planned refueling outage. The unit reached essentially 100 percent power on April 10, 2017, and remained there for the duration of the quarter.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection
a. Inspection Scope
.1 Summer Readiness of Offsite and Alternate AC Power System
The licensee did not implement equipment or procedure changes that potentially affect operation or reliability of offsite and alternate AC power systems since the last time the inspectors assessed grid reliability. The inspectors reviewed the material condition of offsite and onsite alternate AC power systems (including switchyard and transformers)by performing a walkdown of the switchyard. The inspectors reviewed outstanding work orders and assessed corrective actions for degraded conditions that impacted plant risk or required compensatory actions. Documents reviewed are listed in the attachment.
.2 Seasonal Extreme Weather Conditions
The inspectors conducted a detailed review of the stations adverse weather procedures written for extreme high temperatures. The inspectors verified that weather-related equipment deficiencies identified during the previous year had been placed into the work control process and/or corrected before the onset of seasonal extremes. The inspectors evaluated the licensees implementation of adverse weather preparation procedures and compensatory measures before the onset of and during seasonal extreme weather conditions. Documents reviewed are listed in the attachment. The inspectors evaluated the following risk-significant systems:
- Containment air recirculation cooling system
- Service water booster pumps
b. Findings
No findings were identified.
1R04 Equipment Alignment
a. Inspection Scope
.1 Partial Walkdown
The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the attachment.
The inspectors selected the following systems or trains to inspect:
- Charging pumps A and C while charging pump B was out of service for repair
- Motor driven auxiliary feedwater (MDAFW) pump A while MDAFW B was out of service for scheduled preventative maintenance
- Service water booster pump (SWBP) A while SWBP B was out of service for scheduled rotating assembly replacement
- B emergency diesel generator (EDG) while A EDG out of service for scheduled oil replacement
b. Findings
No findings were identified.
1R05 Fire Protection
a. Inspection Scope
.1 Quarterly Inspection
The inspectors evaluated the adequacy of selected fire plans by comparing the fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the fire plans, the inspectors assessed the following items:
- control of transient combustibles and ignition sources
- fire detection systems
- water-based fire suppression systems
- gaseous fire suppression systems
- manual firefighting equipment and capability
- passive fire protection features
- compensatory measures and fire watches
- issues related to fire protection contained in the licensees corrective action program (CAP)
The inspectors toured the following five fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the attachment.
- MDAFW pump room, fire zone 6
- Turbine building - Building 350 - west end ground level
- North and South cable vaults, fire zones 9 and 10
- Emergency 4160 volt switchgear rooms E1/E2, fire zone 20
- B EDG room, fire zone 1
b. Findings
No findings were identified.
1R06 Flood Protection Measures
a. Inspection Scope
.1 Internal Flooding
The inspectors reviewed related flood analysis documents and walked down the areas listed below containing risk-significant structures, systems, and components susceptible to flooding. The inspectors verified that plant design features and plant procedures for flood mitigation were consistent with design requirements and internal flooding analysis assumptions. The inspectors also assessed the condition of flood protection barriers and drain systems. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the CAP. Documents reviewed are listed in the attachment.
- Component cooling water pump room (internal flood zone FLC050)
- A and B EDG rooms (internal flood zones FLC020 and FLC010)
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program and Licensed Operator Performance
a. Inspection Scope
.1 Resident Inspector Quarterly Review of Licensed Operator Requalification
On May 23, 2017, the inspectors observed an evaluated simulator scenario administered to an operating crew as part of the annual requalification operating test required by 10 CFR 55.59, Requalification.
The scenario consisted of three events, starting with a pressurizer level transmitter failure, continuing with a loss of normal power to an emergency electrical bus, coupled with the A EDG failure to start. The final event consisted of a large-break loss of coolant accident, with one train of safeguards available.
The inspectors assessed the following:
- licensed operator performance
- the ability of the licensee to administer the scenario and evaluate the operators
- the quality of the post-scenario critique
- simulator performance Documents reviewed are listed in the attachment.
.2 Resident Inspector Quarterly Review of Licensed Operator Performance in the Actual
Plant/Main Control Room On April 5-6, 2017, the inspectors observed licensed operator performance in the main control room during reactor restart and reactor physics testing following the refueling outage.
The inspectors assessed the following:
- use of plant procedures
- control board manipulations
- communications between crew members
- use and interpretation of instruments, indications, and alarms
- use of human error prevention techniques
- documentation of activities
- management and supervision Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors assessed the licensees treatment of the issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. Documents reviewed are listed in the attachment.
- NCR 02121535, No output DC voltage on A-1 battery charger
- NCR 02115268, Significant steam leak and damage to steam dump valve PRV-1324B-1 during unit startup
b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed the maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the CAP. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities. Documents reviewed are listed in the attachment.
- April 17, 2017, Green risk for MDAFW pump 'B' out of service for planned maintenance
- May 12, 2017, Green risk for emergent RCS Loop 3 Low Flow bistable switch replacement
- April 27-29, 2017, emergent Yellow grid system reliability condition due to low generation capacity
- June 13-15, 2017, planned Yellow risk for maintenance on steam driven auxiliary feedwater pump, with multiple revisions of station risk profile
- May 25, 2017, emergent elevated Green risk for tornado watch
b. Findings
No findings were identified.
1R15 Operability Determinations and Functionality Assessments
a. Inspection Scope
.1 Operability and Functionality Review
The inspectors selected the operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.
Documents reviewed are listed in the attachment.
- NCR 02118558, All turbine valves lost indication on the control room turbine control panel
- NCR 02012658, Main steam line break unanalyzed condition due to single failure vulnerability with bypass feedwater regulating valves
- NCR 02125988 and NCR02120069, Evaluate service water booster pump B cloudy oil and suspended sediment
- NCR 02127683 and NCR 0212686, Failed infared detector in Reactor Coolant Pump bay B
b. Findings
No findings were identified.
1R18 Plant Modifications
a. Inspection Scope
The inspectors verified that the plant modifications listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. Documents reviewed are listed in the attachment.
- Engineering Change (EC) 259629, CS/SI Full Flow Test Line - Closeout of Acceptance Testing (Permanent Modification)
- EC 408455, Charging pump C lubricating collection tank Belzona leak repair (Temporary Modification)
b. Findings
No findings were identified.
1R19 Post-Maintenance Testing
a. Inspection Scope
The inspectors either observed post-maintenance testing or reviewed the test results for the maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.
- Work Orders (WOs) 20133334, 20121841, and 20045301, AFW (Auxiliary Feedwater) pump 'B' post maintenance testing following scheduled preventative maintenance in accordance with OST-201-2, MDAFW (Motor Driven Auxiliary Feedwater) System Component Test - Train B
- WO 20034740, Limitorque grease inspection of valve SI-880C-MO in accordance with PM-112, Limitorque Inspection No. 1
- WOs 20156906 and 20089787, Perform maintenance and testing of reactor trip bypass bkr (breaker)
- WO 20161947, FC-435, RCS Loop 3 bistable switch post maintenance testing following emergent troubleshooting and repair
- WO 13422523, SWBP B post maintenance testing following scheduled rotating assembly replacement in accordance with OST-303-2, Service Water Booster Pump B test
- WO 20014772, Charging pump C post maintenance testing following repair of leak in lubricating collection tank in accordance with OP-301C, Chemical and Volume Control System Charging Pump C Operation
- WO 20031124, AFW pump A discharge flow control valve FCV-1424 post maintenance testing following scheduled controller calibration in accordance with PIC-033, Auxiliary Feedwater Flow Indicating Controller FIC-1424 and OST-210-1, MDAFW System Component Test - Train A The inspectors evaluated these activities for the following:
- Acceptance criteria were clear and demonstrated operational readiness
- Effects of testing on the plant were adequately addressed
- Test instrumentation was appropriate
- Tests were performed in accordance with approved procedures
- Equipment was returned to its operational status following testing
- Test documentation was properly evaluated Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
1R20 Refueling and Other Outage Activities
a. Inspection Scope
For the refueling outage which was ongoing at the start of the inspection period and ended April 8, 2017, the inspectors evaluated the following outage activities:
- decay heat removal and spent fuel pool cooling system operation
- containment closure
- reactivity control
- heatup and startup The inspectors verified that the licensee:
- controlled plant configuration in accordance with administrative risk reduction methodologies
- developed work schedules to manage fatigue
- developed mitigation strategies for loss of key safety functions
- adhered to operating license and TS requirements Inspectors verified that safety-related and risk-significant structures, systems, and components not accessible during power operations were maintained in an operable condition. The inspectors also reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with outage activities. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the surveillance tests listed below and either observed the test or reviewed test results to verify testing activities adequately demonstrated that the affected SSCs remained capable of performing the intended safety functions (under conditions as close as practical to design bases conditions or as required by technical specifications) and maintained their operational readiness.
The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.
Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the attachment.
Routine Surveillance Tests
- MST-020, Reactor Protection Logic Train A at Power
- EST-050, Refueling Startup Procedure
- OST-160, Pressure Isolation Check Valve Back Leakage Test In-Service Tests
- OST-151-3, Safety Injection System Components Test - Pump C
b. Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
a. Inspection Scope
The inspectors observed the emergency preparedness drill conducted on May 31, 2017.
The inspectors observed licensee activities in the simulator and technical support center to evaluate implementation of the emergency plan, including event classification, notification, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures.
Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the CAP. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
RADIATION SAFETY
[RS]
Cornerstones: Occupational Radiation Safety and Public Radiation Safety
2RS1 Radiological Hazard Assessment and Exposure Controls
a. Inspection Scope
Hazard Assessment and Instructions to Workers The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys of the independent spent fuel storage installation (ISFSI) pad. The inspectors reviewed survey records of gamma and neutron surveys around the ISFSI.
b. Findings
No findings were identified.
2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls
a. Inspection Scope
Work Planning and Exposure Tracking The inspectors reviewed work activities and their collective exposure estimates for Refueling Outages 29 and 30 (RO29 and RO30). The inspectors reviewed ALARA planning packages for activities related to the following RO30 high collective exposure tasks: Bottom Vessel Instrumentation Inspection, In-Service Inspections, Steam Generator Primary and Secondary Side Maintenance, and Refueling/Reactor Head Activities. For the selected tasks, the inspectors reviewed established dose goals and discussed assumptions regarding the bases for the current estimates with responsible ALARA planners. The inspectors evaluated the incorporation of exposure reduction initiatives and operating experience, including historical post-job reviews, into RWP requirements. Where applicable, the inspectors discussed changes to established estimates during the RO29 and RO30 outages with ALARA planners and evaluated them against work scope changes or unanticipated elevated dose rates.
Source Term Reduction and Control The inspectors reviewed the collective exposure three-year rolling average from 2012 -
2015. The inspectors evaluated historical dose rate trends for reactor coolant system piping and compared them to levels during both RO29 and RO30. Source term reduction initiatives, including cobalt reduction and zinc injection, were reviewed and discussed with radiation protection (RP) staff. The inspectors also reviewed temporary shielding packages for the 2RO30.
Radiation Worker Performance In conjunction with Inspection Procedure (IP) 71124.01, the inspectors observed pre-job ALARA briefings and radiation worker performance for higher risk jobs that were performed during the inspection. While observing job tasks, the inspectors evaluated the use of remote technologies to reduce dose including teledosimetry and remote visual monitoring.
Problem Identification and Resolution The inspectors reviewed and discussed selected CAP documents associated with ALARA program implementation. The inspectors evaluated the licensees ability to identify and resolve the issues. The inspectors also reviewed recent self-assessment results.
Inspection Criteria ALARA program activities were evaluated against the requirements of UFSAR Chapters 11 and 12, TS Section 5.7, 10 CFR Part 20, and approved licensee procedures. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
2RS3 In-Plant Airborne Radioactivity Control and Mitigation
a. Inspection Scope
Engineering Controls The inspectors reviewed the use of temporary and permanent engineering controls to mitigate airborne radioactivity during RO30. The inspectors reviewed the use of portable air filtration units for work in contaminated areas of the radiologically controlled area (RCA) and reviewed filtration unit testing certificates. The inspectors evaluated the effectiveness of continuous air monitors to provide indication of increasing airborne levels and the placement of air samplers in work area breathing zones, and verified that the licensee is accounting for alpha emitting nuclides in setpoint determination.
Respiratory Protection Equipment The inspectors reviewed the use of respiratory protection devices to limit the intake of radioactive material. This included review of devices used for routine tasks and devices stored for use in emergency situations. The inspectors reviewed selected ALARA evaluations for the use of respiratory protection performed since the last inspection.
Selected Self-Contained Breathing Apparatus (SCBA) units and negative pressure respirators (NPR)s staged for routine and emergency use in the Main Control Room and other locations were inspected for material condition, SCBA bottle air pressure, number of units, and number of spare masks and availability of air bottles. The inspectors reviewed maintenance records for selected SCBA units for the past two years and evaluated SCBA and NPR compliance with National Institute for Occupational Safety and Health certification requirements. The inspectors also reviewed records of air quality testing for supplied-air devices and SCBA bottles.
The inspectors reviewed the number and types of respirators used for various jobs during RO30 and observed fit testing of SCBA and negative pressure respirator face pieces. The inspectors discussed training for various types of respiratory protection devices with licensee staff and interviewed radworkers and control room operators on use of the devices including SCBA bottle change-out and use of corrective lens inserts.
The inspectors reviewed respirator qualification records (including medical qualifications)for several Main Control Room operators and emergency responder personnel. In addition, inspectors evaluated qualifications for individuals responsible for testing and repairing SCBA vital components.
Problem Identification and Resolution The inspectors reviewed and discussed selected CAP documents associated with airborne controls and respiratory protection activities. The inspectors evaluated the licensees ability to identify and resolve the issues. The inspectors also reviewed recent self-assessment results.
Inspection Criteria RP program activities associated with airborne radioactivity monitoring and controls were evaluated against details and requirements documented in the UFSAR Chapters 11 and 12; 10 CFR Part 20; Regulatory Guide (RG) 8.15, Acceptable Programs for Respiratory Protection and approved licensee procedures. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
2RS4 Occupational Dose Assessment
a. Inspection Scope
Source Term Characterization The inspectors reviewed the plant radiation characterization (including gamma, beta, alpha, and neutron) being monitored and verified the use of scaling factors to account for hard-to-detect radionuclides in internal dose assessments.
External Dosimetry The inspectors reviewed National Voluntary Laboratory Accreditation Program (NVLAP)certification data for the licensees optimically stimulated luminescence (OSL) processor for the current year for ionizing radiation dosimetry. The inspectors observed and evaluated onsite storage of thermoluminescent dosimeters (TLDs). Comparisons between electronic dosimeter (ED) and OSL results, including correction factors, were reviewed and discussed. The inspectors also evaluated licensee procedures for unusual dosimetry occurrences. ED alarm logs were reviewed as part of Inspection Procedure 71124.01. The inspectors reviewed contamination logs and evaluated events with the potential for external dose.
Internal Dosimetry The inspectors reviewed and discussed the in vivo bioassay program with the licensee.
Inspectors reviewed procedures that addressed methods for determining internal or external contamination, releasing contaminated individuals, and the assignment of dose.
The inspectors evaluated the licensees program for in vitro monitoring and reviewed in vivo bioassay results, and in vitro sample information, for personnel involved in recent diving activities. The inspectors also reviewed contamination logs and evaluated events with the potential for internal dose.
Special Dosimetric Situations The inspectors reviewed records for declared pregnant workers (DPW)s from March 2015 through June 2017 and discussed guidance for monitoring and instructing DPWs. Inspectors reviewed the licensees program for monitoring external dose in areas of expected dose rate gradients, including the use of multi-badging and extremity dosimetry. The inspectors evaluated the licensees neutron dosimetry program including instrumentation used to perform neutron surveys. In addition, the inspectors reviewed the licensees program for evaluation of shallow dose equivalent (SDE). The inspectors also reviewed contamination logs and evaluated events with the potential for SDE.
Problem Identification and Resolution The inspectors reviewed and discussed selected CAP documents associated with occupational dose assessment including self-assessments. The inspectors evaluated the licensees ability to identify and resolve issues.
Inspection Criteria The licensees occupational dose assessment activities were evaluated against the requirements of U-2 UFSAR Chapter 12; TS Section 5.4 and 5.7; 10 CFR Parts 19 and 20; and approved licensee procedures. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
2RS5 Radiation Monitoring Instrumentation
a. Inspection Scope
The inspectors reviewed the licensees radiation monitoring instrumentation programs to verify the accuracy and operability of radiation monitoring instruments used to monitor areas, materials, and workers to ensure a radiologically safe work environment during normal operations and under postulated accident conditions.
Walkdowns and Observations During tours of the site areas, the inspectors observed installed radiation detection equipment including the following instrument types: area radiation monitors (ARMs),continuous air monitors (CAMs), personnel contamination monitors (PCMs), small article monitors (SAMs), and portal monitors (PMs). The inspectors observed the calibration status, physical location, material condition and compared technical specifications for this equipment with UFSAR requirements. In addition, the inspectors observed the calibration status and functional checks of selected in-service portable instruments and discussed the bases for established frequencies and source ranges with RP staff personnel. The inspectors reviewed periodic source check records for compliance with plant procedures and manufacturers recommendation for selected instruments and observed the material condition of sources used.
Calibration and Testing Program The inspectors reviewed calibration data for selected ARMs, PCMs, PMs, SAMs, and laboratory instruments as well as the last calibration and methodology for the whole body counter. The inspectors reviewed calibration data, methodology used and the source certification for the Containment High Range Radiation Monitors R-32A and R-32B. In addition, the inspectors observed a functional test of all ARMs outside containment in accordance with plant procedures. The current output values for the portable instrument calibrator and the instrument certifications used to develop them were reviewed by the inspectors. The inspectors reviewed the licensees process for investigating instruments that are removed from service for calibration or response check failures and discussed specific instrument failures with plant staff. In addition, the inspectors reviewed 10 CFR Part 61 data to determine if sources used in the maintenance of the licensees radiation detection instrumentation were representative of radiation hazards in the plant and scaled appropriately for hard to detect nuclides.
Problem Identification and Resolution The inspectors reviewed and discussed selected CAP documents associated with radiological instrumentation including licensee sponsored assessments. The inspectors evaluated the licensees ability to identify and resolve issues. The inspectors also reviewed recent self-assessment results.
Inspection Criteria Operability and reliability of selected radiation detection instruments were reviewed against details documented in the following: 10 CFR Part 20; NUREG-0737, Clarification of TMI Action Plan Requirements; TS Sections 3 and 5; UFSAR Chapter 12 and applicable licensee procedures. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
a. Inspection Scope
The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 1 and Unit 2 PIs listed below. The inspectors reviewed plant records compiled between April 1, 2016, and March 31, 2017, to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI.
In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data.
Cornerstone: Initiating Events
- unplanned scrams with complications
Cornerstone: Mitigating Systems
- safety system functional failures Public Radiation Safety Cornerstone The inspectors reviewed the Radiological Control Effluent Release Occurrences PI results for the Public Radiation Safety Cornerstone and reviewed PI records generated between January 2016 and May 2017. For the assessment period, the inspectors reviewed cumulative and projected doses to the public contained in liquid and gaseous release permits and NCRs related to Radiological Effluent Technical Specifications/Off-site Dose Calculation Manual issues. Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
4OA2 Problem Identification and Resolution
.1 Routine Review
The inspectors screened items entered into the licensees CAP to identify repetitive equipment failures or specific human performance issues for followup. The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.
.2 Semi-Annual Trend Review
a. Inspection Scope
The inspectors reviewed issues entered in the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on the human performance trend associated with procedure use and adherence that lead to repetitive equipment issues but also considered the results of inspector daily condition report screenings, licensee trending efforts, and licensee human performance results. The review nominally considered the 6-month period of January 2017 through June 2017, although some examples extended beyond those dates when the scope of the trend warranted. The inspectors compared their results with the licensees analysis of trends. Additionally, the inspectors reviewed the adequacy of corrective actions associated with a sample of the issues identified in the licensees trend reports. The inspectors also reviewed corrective action documents that were processed by the licensee to identify potential adverse trends in the condition of structures, systems, and/or components as evidenced by acceptance of long-standing non-conforming or degraded conditions. Documents reviewed are listed in the attachment.
b. Findings and Observations
No findings were identified. However, the inspectors noted there were five NCRs generated during the first half of 2017 relating to human performance issues, specifically procedure use and adherence with the potential to impact plant health. Most events were significant enough to warrant a Human Performance Review Board. One of these events resulted in an inadvertent actuation of the AFW system, discussed in 4OA3 of this report. Several other events involved missed procedural steps which had the potential to impact or did impact equipment important to safety. The licensee is aware of the trend in human performance as it relates to procedure use and adherence, and took immediate corrective actions in each instance, however human performance continues to be an item of interest. The inspectors also observed the procedure use and adherence trends extended into log keeping as it related to entering and exiting procedures, severe weather alerts, and changes in risk. The logkeeping observations have been captured by the licensee in NCR 02132554.
.3 Annual Followup of Selected Issues
a. Inspection Scope
The inspectors conducted a detailed review of the following condition reports:
- NCR 02117314, ENG identified trend in charging pump discharge relief valve
- NCR 02118679, Small oil leak at upper crank case bolts on EDG B The inspectors evaluated the following attributes of the licensees actions:
- complete and accurate identification of the problem in a timely manner
- evaluation and disposition of operability and reportability issues
- consideration of extent of condition, generic implications, common cause, and previous occurrences
- classification and prioritization of the problem
- identification of root and contributing causes of the problem
- identification of any additional condition reports
- completion of corrective actions in a timely manner Documents reviewed are listed in the attachment.
b. Findings
No findings were identified.
4OA3 Follow-up of Events and Notices of Enforcement Discretion
.1 (Closed) License Event Report (LER) 05000261/2017-001-00, Auxiliary Feedwater
System Actuation During Surveillance Testing
a. Inspection Scope
On April 3, 2017, with the plant in Mode 3 at 0 percent power, Unit 2 experienced an actuation of the AFW system during turbine trip logic surveillance testing. The licensee determined that the direct cause of the AFW system actuation was inadequate procedure adherence during the surveillance procedure. In accordance with the test procedure, the single running main feedwater pump was tripped, however the AFW system actuated because the AFW defeat switches were not in the defeat position, as required by the test procedure. MDAFW pumps A and B started as designed in response to the trip of the main feedwater pump. The licensee took immediate corrective actions to re-emphasize the need to verify all steps in the procedure are completed. The inspectors reviewed the licensee event report, appropriateness of corrective actions, violations of requirements, and generic issues.
b. Findings
The inspectors concluded that the failure to follow licensee procedure MST-551, Turbine Trip Logic Channel Testing, was a violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which required that activities affecting quality be accomplished in accordance with instructions and procedures. Due to the fact that no actual loss of auxiliary feedwater occurred during the incident and because the Unit was in Mode 3, there was no adverse impact on plant operation, the failure to comply with this requirement constituted a violation of minor safety significance that was not subject to enforcement action in accordance with the NRCs Enforcement Policy. The licensee entered this issue into their CAP as NCR 02113929. This LER is closed.
4OA6 Meetings, Including Exit
On July 19, 2017, the resident inspectors presented the inspection results to Mr. Kapopoulos and other members of the licensees staff. On July 20, 2017, a re-exit meeting was conducted with Mr. Dave Huffman and other members of your staff, to discuss the final results of the inspection. The inspectors confirmed that no proprietary information was retained by the inspectors or documented in this report.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- J. Barber, Radiation Protection Supervisor
- C. Caudell, Regulatory Affairs
- F. Giannone, Training Manager
- T. Giese, Manager, Operations Training
- D. Hall, Nuclear Oversite Manager
- S. Hall, Radiation Protection Superintendent / Manager
- G. Hartzer, Chemistry Manager
- D. Hoffman, Manager, Operations
- J. Kammer, General Manager, Engineering
- E. Kapopoulos, Site Vice President
- T. Kirwin, Manager, Maintenance
- J. Krakuszeski, Plant General Manager
- A. Maysam, Regulatory Affairs
- C. Orr, Manager, Nuclear Work Management
- T. Pilo, Regulatory Affairs Manager
- D. Pitsley, Manager, Emergency Preparedness
- C. Sherman, Organizational Effectiveness Director
- J. Wild, Regulatory Affairs
NRC personnel
- J. Zeiler, Senior Resident Inspector
G.Eatmon, Senior Resident Inspector
- A. Beasten, Resident Inspector
- P. Niebaum, Acting Chief, Reactor Projects Branch 4
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Closed
- 05000261/2017-001-00 LER Auxiliary Feedwater System Actuation During Surveillance Testing (Section 4OA3)