05000272/LER-2077-031-01, Inoperability of Valves Due to Excessive Closure Time

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Inoperability of Valves Due to Excessive Closure Time
ML19031B057
Person / Time
Site: Salem  PSEG icon.png
Issue date: 05/20/1977
From: Schneider F
Public Service Electric & Gas Co
To: O'Reilly J
NRC/IE, NRC Region 1
References
LER 1977-031-01
Download: ML19031B057 (4)


LER-2077-031, Inoperability of Valves Due to Excessive Closure Time
Event date:
Report date:
2722077031R01 - NRC Website

text

....

Frederick W. Schneider Vice President Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 201/622-7000 Production Mr. James P. O'Reilly Director of USNRC May 20, 1977 Off ice of Inspections and Enforcements Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. O'Reilly:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 77-31/03L 1R.egu\\atory Docket tit~

Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 77-31/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours, CC:

Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control

( 3 copies)

  • Report Number:

Report Date:

Occurrence Date:

Facility:

--31/03L 5/5/77 4/29/77 Salem Generating Station

  • Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Inoperable Containment Isolation Valves 1WL99 and lWLlOB CONDITIONS PRIOR TO OCCURRENCE:

Mode 3, Surveillance Testing in progress.

DESCRIPTION OF OCCURRENCE:

While performing surveillance during Mode 3, 1WL99 (RC Drain Tank -

Vent Header Connection) and 1WL108 (RC Drain Tank ~ N2 Connection) were de-clared inoperable because they failed to close within. the time allowed by Technical Specifications.

Action Statement for LCO 3. 6. 3-.1 was placed in effect and 1WL99 and 1WL108 were closed and isolated.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

The valve operator vent solenoid was determined to be undersized.

The 3/64" ports were too small to allow adequate bleed off of air from operator.

Aging of existing solenoid combined with undersized ports, caused valve stroke time to exceed the allowed 10 seconds.

ANALYSIS OF OCCURRENCE:

Technical Specification LCO 3.6.3.1 Action Statement requires that the inoperable valves be secured in the isolation posi~ion and de-energized.

1WL99 and 1WL108 were isolated and de-energized, therefore, the LCO was not violated.

At no time was there any danger to. the health and safety of the general public or site personnel.

CORRECTIVE ACTION

Solenoid vent valves (Asco, type FT8314B6) were replac-ed with larger_

size (Asco, type FT8321A2) *valves to d_ecrease _the bleed off time.

- 1WL99 and ___ lWLlOB were then timed and declared operable.

The Action Statement was then terminated.

FAILURE DATA:

Asco Solenoid Valves Type:

FT8314B6 Prepared by~~~T_.~L_.~S~p~e~n.;.;;..:...c~e~r~-"-

SORC Meeting No.

51-77

~~~~~~~~

5/5/77

LICENSEE EVENT REPORT e CONTROL BLOCK LICENSEE NAME REPORT REPORT I I 6

LICENSE NUMBER CATEGORY TVl"E SOURCE COCKET NUMBER LICENSE.

TYPE EVENT TYPE EVENT CATE REPORT CATE ram coN'TlRlQJ L!J Ll:!..l 1 o 1 s 1 o 1 -1 o 1 2 1 11 2J s1 sa 59 so 61 10141219 17 17 I 101510 !5 !717J 69 74 75 EVENT OESCRIPT10N

~!.'While performing surveillance in Mode 3. valves 1WL99 and 1WL108 were 7

8 9 I

SQ

@:Ell declared inoperable due to closure time being in excess of Tech Spec.

7 8 9 J*

@)) 3.6.3.1. Vent solenoid valves were replaced with larger size to decrease 1

a This is the first occurrence of this type. (77-31/03L).

[2N) I closure time.

I 7

~9 so

~1::----~~~~~~~~~~-,----~~~~~~~~------~~~------~~....;,_J 7

8 9 PRIME 60 SYSTEM

CAUSE

COMPONENT COMPONENT COO£ COO£ COMPONENT COCE SUPPLIER MANUFACTURER

@rr]1M IA I

@J IV IA IL IV 10.E.J 11J IX 19 I 919 I VIOLATION lli.I 7

8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION

~l 9

Undersized bleed off ports combined with aging increased valve closure

~I time to above that allowed by Tech Spec.

Asco, tvpe: FT8314B6 I

so I

7 8 9 so [Ifil 7 8~9~----------------'-----~--------------..;.._------90~

FACILITV STATUS

'l(o POWER OTHER STATUS [ill LQJ.

10 10 !O I I NIA 1

a 9

10 12 13 FORM OF ACTIVITV CONTENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY GE

~ ~ I N/A 7

8 9

10 11 PERSONNEL EXPOSURES NUMBER TVPE CESCRIPTION METHOO OF CISCOVERV I Lill 44 45 CISCOVERV CESCRIPTION

!Surveillance Testing 80 LOCATION OF RELEASE I

~I ________

__;.;N~/=A ____________ -=:!I 44

~

so f2E)!OIOIOl,lZJ NA 1

e s 11 12 l"=13;-----_;:.:~~-------------------------80 d

PERSONNEL INJURIES NUMBER CESCRIPTION G:EJI0/0101 NA 1

a 9 11 12 OFFS1TE CONSEQUENCES

~

NA LOSS OR OAMAGE TO FACILITY TVPI!:

CESCRIPTION GJ!l I Z I I.**

N/A*

j 1

a~.. ~10..------------"-'-'"--';;...;...--~--------------'-----'-.,..----------...i~

PUSLJCITY

.GE 7

8 9 AOOITIONAL FACTORS

!IJ!1 N/A 1

a~9~---------------..;.._--~-----------------------~eo N.a.ME: _____

T_. ___ L

._s~p....;e;..;n=c-"e;;..;;r;;...._ _______ _

PHONE: (609) 365-7000 Ext.Salem-528