05000272/LER-2077-035-03, Inoperability of Pressurizer Level

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Inoperability of Pressurizer Level
ML19031B053
Person / Time
Site: Salem  PSEG icon.png
Issue date: 06/02/1977
From: Librizzi F
Public Service Electric & Gas Co
To: O'Reilly J
NRC/IE, NRC Region 1
References
LER 1977-035-03
Download: ML19031B053 (4)


LER-2077-035, Inoperability of Pressurizer Level
Event date:
Report date:
2722077035R03 - NRC Website

text

Public Service Electric and Gas Company 80 Park Place Newark, N.J. 07101 Phone 201 /622-7000 Mr. James P. O'Reilly Director of USNRC June 2, 1977 Office of Inspections and Enforcements Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. O'Reilly:

LICENSE NO. DPR-70 DOCKET NO. 50-272 REPORTABLE OCCURRENCE 77-35/03L Pursuant to the requirements of Salem Generating Station Unit No. 1 Technical Specifications, Section 6.9.1, we are submitting Licensee Event Report for Reportable Occurrence 77-35/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

~/v(~-f,.,"

Frank P. Libriz91' General Manager -

Electric Production CC Director, Office of Inspection and Enforcement (30 copies)

Director, Office of Management Information and Program Control (3 copies)

The Energy People 95-2001 (400M) 6-76

Report Number:

Report Date:

Occurrence Date:

Facility:

~35/03L 5/20/77 5/7/77 Salem Generating Station Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Pressurizer Level Channel I Inoperable CONDITIONS PRIOR TO OCCURRENCE:

Mode 3, Tave 547°F, Pressure 2235 psig DESCRIPTION OF OCCURRENCE:

At 0700 hours0.0081 days <br />0.194 hours <br />0.00116 weeks <br />2.6635e-4 months <br />, pressurizer level channel I was declared inoperable due to it reading 3 to 5% higher than other channels.

Pressurizer level channel I was placed in the 'tripped condition.

Action State-ment No. 7 for LCO 3.3.1.1, Table 3.3.1 and Action Statement A for LCO 3.3.2.l were placed in effect.

Power operation continued until 5/18/77 when the unit was taken out of service to repair the channel.

DESIGNATION OF APPARENT* CAUSE OF OCCURRENCE:

Two problems were identified that caused this occurrence.

Gas was trapped in condensate pot causing a false high level signal.

Addi-tionally, the low pressure isolation valve and the equalizing valve were found to be leaking through.

With the equalizing valve leaking through a false differential pressure signal was being applied to the transmitter.

ANALYSIS OF OCCURRENCE:

Action Statement No. 7 for LCO 3.3.1.1 and Action Statement A for LCO 3.3.2.1 allow operation to continue until the next required functional test provided the inoperable channel is placed in the tripped condi-tion within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

Channel I pressurizer level was placed in the tripped condition within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, therefore, the LCO was not violated.

The function test for this channel was due on 5/19/77.

At no time was there any danger to the health and safety of the general public or site personnel.

CORRECTIVE ACTION

On 5/18/77, the unit was placed in Mode 2 to facilitate venting of the pressurizer level condensate pot.

The pot was vented and the indica-tion decreased to approximately 3%.

The equalizing valve and low side

Report No. 77-3S/03L *e 5/20/77 isolation valve were replaced and the channel output came to within 2 millivolts of other operable channels.

Channel I was declared operable and all action statements terminated.

FAILURE DATA:

Not Applicable Prepared by T. Spencer

~~~~~=--~~~~~

Manager _I/Salem Generating Station SORC Meeting No. ~~~~~~~~-

57-77

CONTROL BLOCK LICENSEE EVENT REPORT

  • 6 77-35/03L 5/7 /77

!_ICENSEE LICENSE EVENT NAME LICENSE NUMBER TYPE TYPE REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT OATC:

f011l CON'TL_Lj LlJ UJ I 0 I 51 0 I -I 0 I 21 71 21 r--""1 5 7 58 59 60 6,

68 I 0 I 5 I 0 I 7 I 7 I 7 I I 0 I 5 I 2 I 0 j7 I 7j 69 74 75

EVENT DESCRIPTION

~I During Mode 3 operation, Channel I pressurizer level was 7

8 9 declared inopert so

@))!able due to it indicating 3-5% greater than other operable channels.

1 as

@))!Channel I was placed in the tripped condition and Action Statements for 7

8 9 J

J

~ILCO 3.3.1.1 & 3.3.2.1 were implemented.

Condensate pot was vented and 7

8 9

~!equalizing valve was replaced.

(77-35/03L) 7 8 9 SYSTEM

CAUSE

cooE. cooE

@E]LLllLJ

~

7 8 9 10 11 CAUSE DESCRIPTION COMPONENT CODE IX IX IX IX IX..JXJ 12 17 PRIME COMPONENT SUPP!_IER LbJ 43 COMPONENT MANUFACTURER IZ!9i9191 44 47 VIOLATION LBJ 48

@:01 Gas trapped in the condensate pot caused a false high level signal.

~9 l2Jfil I age thru the equalizing valve on the 6P transmitter attributed to the 7

s 9

[!]£]I false level indication.

7 8 9 FACILITY STATUS ITEl LUJ.

1 a

s FORM OF

'!<.POWER IO 10 IO I 10 12 ACTIVITY CONTENT MET HOO OF OTHEfl STATUS DISCOVERY IL:-~N~;_.A~~--.J' l_g,J 13 44 45 01scov*ERY pESCRIPTION N;A I

00 l

so Leal!:-

I BO I

ao so RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE

~ w w

l~ ___

N__:./_A __

_JI I

NI A I

1 a

s 10 11 44 4'="5:---------'--,;.._-------~oo PERSONNEL EXPOSURES NUMBER TYPE

DESCRIPTION

~1010101 lZJ NA 1

a s 11 12 1b3;-----~<-.,;;..;=---------------------------=:!so PERSONNEL INJURIES NUMBER

DESCRIPTION

GEJIOIOIOI NA 1

a 9 11 12 so OFFSITE CONSEQUENCES

~

NA LOSS OR DAMAGE TO FACILITY G:@l9~i ICESCRIPTION N/A 1

a

~10.-----~----_::.;.L....;;..;;..._ _______________________ __,....

PUBLICITY

@iJ 7 8~9------------...U.,<-C~------------------------80~

ADDITIONAL FACTORS II@'n-~~~~~~~~~-N==-~A'--~~~~~~~~~~~~~~~~~~~..,.,i 7

8 9 o::lil~~~~~~~~~~~~~~~~~~~~~~~~~~~~_;_~~~~..;.....J 7

89 00 NAME:

T." L. Snencer

=-='------

PHONE: (609) 365-7000 Ext. Salem 628 J