|
---|
Category:Inspection Report
MONTHYEARIR 05000445/20240032024-10-30030 October 2024 Integrated Inspection Report 05000445/2024003 and 05000446/2024003 IR 05000445/20244042024-10-23023 October 2024 Security Baseline Inspection Report 05000445/2024404 and 05000446/2024404 (Public) IR 07200074/20244012024-10-10010 October 2024 Independent Spent Fuel Storage Installation Security Inspection Report 07200074/2024401 Public IR 05000445/20240052024-08-15015 August 2024 Updated Inspection Plan for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2024005 and 05000446/2024005) IR 05000445/20240022024-07-31031 July 2024 Units 1 and 2 - Integrated Inspection Report 05000445/2024002 and 05000446/2024002,and Independent Spent Fuel Storage Installation Inspection Report 07200074/2024001 IR 05000445/20244032024-07-16016 July 2024 Security Baseline Inspection Report 05000445/2024403 and 05000446/2024403 (Full Report) IR 05000445/20244012024-06-26026 June 2024 MC&A Program Inspection Report 05000445-2024401 and 05000446-2024401 Public-Final IR 05000445/20240122024-06-17017 June 2024 Design Basis Assurance Inspection (Programs) Inspection Report 05000445/2024012 and 05000446/2024012 IR 05000445/20240012024-04-26026 April 2024 Integrated Inspection Report 05000445/2024001 and 05000446/2024001 IR 05000445/20244022024-04-17017 April 2024 Security Baseline Inspection Report 05000445/2024402 and 05000446/2024402 (Full Report) IR 05000445/20243012024-02-28028 February 2024 Notification of NRC Initial Operator Licensing Examination 05000445/2024301 and 05000446/2024301 IR 05000445/20230062024-02-28028 February 2024 Annual Assessment Letter for Comanche Peak Nuclear Power Plant, Units 1 and 2 Reports 05000445/2023006 and 05000446/2023006 IR 05000445/20230132024-01-31031 January 2024 License Renewal Inspection Report 05000445/2023013 and 05000446/2023013 IR 05000445/20230042024-01-29029 January 2024 Integrated Inspection Report 05000445/2023004 and 05000446/2023004 ML24018A1072024-01-18018 January 2024 – Notification of Commercial Grade Dedication Inspection (05000445/2024012 and 05000446/2024012) and Request for Information IR 05000445/20234022023-11-30030 November 2023 NRC Security Inspection Report 05000445/2023402 and 05000446/2023402 IR 05000445/20230052023-08-23023 August 2023 Updated Inspection Plan for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2023005 and 05000446/2023005)- Mid Cycle Letter 2023 IR 05000445/20233012023-08-21021 August 2023 NRC Examination Report 05000445/2023301 and 05000446/2023301 IR 05000445/20230112023-07-20020 July 2023 Fire Protection Team Inspection Report 05000445/2023011 and 05000446/2023011 IR 05000445/20230022023-07-14014 July 2023 Integrated Inspection Report 05000445/2023002 and 05000446/2023002 IR 05000445/20230012023-04-13013 April 2023 Integrated Inspection Report 05000445/2023001 and 05000446/2023001 IR 05000445/20234012023-03-29029 March 2023 NRC Security Inspection Report 050004452023401 and 050004462023401 (Cover Letter Only) IR 05000445/20230102023-03-24024 March 2023 Biennial Problem Identification and Resolution Inspection Report 05000445/2023010 and 05000446/2023010 IR 05000445/20220062023-03-0101 March 2023 Annual Assessment Letter for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2022006 and 05000446/2022006) IR 05000445/20220042023-01-26026 January 2023 Integrated Inspection Report 05000445/2022004 and 05000446/2022004 IR 05000445/20220102023-01-23023 January 2023 TI-194 Report 05000445/2022010 and 05000446/2022010 IR 05000445/20224202022-12-0707 December 2022 Security Baseline Inspection Report Cover Letter 05000445/2022420 and 05000446/2022420 ML22319A0732022-11-15015 November 2022 Review of the Fall 2021 Steam Generator Tube Inspection Report ML22299A0562022-11-0101 November 2022 Integrated Inspection Report 05000445/2022003 and 05000446/2022003 and Notice of Violation IR 05000445/20220032022-11-0101 November 2022 Integrated Inspection Report 05000445/2022003 and 05000446/2022003 and Notice of Violation IR 05000445/20220052022-08-22022 August 2022 Updated Inspection Plan for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2022005 and 05000446/2022005) IR 05000445/20224032022-08-0909 August 2022 NRC Security Inspection Report 05000445/2022403 and 05000446/2022403 (Full Report) IR 05000445/20220022022-08-0505 August 2022 2nd Quarter 2022 Integrated Inspection Report 05000445/2022002 and 05000446/2022002 IR 05000445/20224012022-06-28028 June 2022 Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection 05000445/2022401; 05000446/2022401 ML22174A2792022-06-22022 June 2022 Notification of NRC Evaluations of Changes, Tests and Experiments Inspection (05000445/2022003 and 05000446/2022003) and Request for Information IR 05000445/20220012022-04-26026 April 2022 Integrated Inspection Report 05000445/2022001 and 05000446/2022001 IR 05000445/20224022022-04-25025 April 2022 Security Baseline Inspection Report 05000445/2022402 and 05000446/2022402 IR 05000445/20210062022-03-0202 March 2022 Annual Assessment Letter for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2021006 and 05000446/2021006) IR 05000445/20200112022-02-0707 February 2022 Amended - Comanche Peak Nuclear Power Plant - Triennial Fire Protection Inspection Report 05000445/2020011 and 05000446/2020011 and Notice of Violation IR 05000445/20210042022-01-25025 January 2022 Integrated Inspection Report 05000445/2021004 and 05000446/2021004 IR 05000445/20210122022-01-13013 January 2022 TI-194 Report 05000445/2021012 and 05000446/2021012 IR 05000445/20214052021-12-15015 December 2021 Security Baseline Inspection Report 05000445/2021405 and 05000446/2021405 IR 05000445/20214032021-12-0909 December 2021 Powerplant, Units 1 and 2 - Security Baseline Inspection Report 05000445/2021403 and 05000446/2021403 IR 05000445/20210032021-11-0303 November 2021 Integrated Inspection Report 05000445/2021003 and 05000446/2021003 IR 05000445/20213012021-10-19019 October 2021 NRC Examination Report 05000445/2021301 and 05000446/2021301 IR 05000445/20210102021-10-0707 October 2021 Biennial Problem Identification and Resolution Inspection Report 05000445/2021010 and 05000446/2021010 IR 05000445/20214012021-09-0909 September 2021 Security Baseline Inspection Report 05000445/2021401 and 05000446/2021401 IR 05000445/20210052021-09-0101 September 2021 Mid-Cycle Inspection Plan Transmittal Letter for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2021005 and 05000446/2021005) IR 05000445/20214022021-08-19019 August 2021 Security Baseline Inspection Report 05000445/2021402 and 05000446/2021402 IR 05000445/20210022021-08-10010 August 2021 Integrated Inspection Report 05000445/2021002 and 05000446/2021002 2024-08-15
[Table view] Category:Letter
MONTHYEARIR 05000445/20240032024-10-30030 October 2024 Integrated Inspection Report 05000445/2024003 and 05000446/2024003 IR 05000445/20244042024-10-23023 October 2024 Security Baseline Inspection Report 05000445/2024404 and 05000446/2024404 (Public) IR 07200074/20244012024-10-10010 October 2024 Independent Spent Fuel Storage Installation Security Inspection Report 07200074/2024401 Public 05000445/LER-2024-002-01, Condition Prohibited by Technical Specifications Due to Inoperable Remote Shutdown System Functions2024-10-0303 October 2024 Condition Prohibited by Technical Specifications Due to Inoperable Remote Shutdown System Functions 05000446/LER-2024-001-01, Unit Two, Recurring Reactor Scrams Associated with Main Feedwater System Modifications2024-09-30030 September 2024 Unit Two, Recurring Reactor Scrams Associated with Main Feedwater System Modifications CP-202400335, License Amendment Request to Adopt TSTF-51, TSTF-471, and TSTF-571-T to Eliminate Use of the Term Core Alterations and Revise Requirements During Handling of Irradiated Fuel2024-09-12012 September 2024 License Amendment Request to Adopt TSTF-51, TSTF-471, and TSTF-571-T to Eliminate Use of the Term Core Alterations and Revise Requirements During Handling of Irradiated Fuel ML24031A6322024-09-11011 September 2024 Exemption from the Requirements of 10 CFR 50.71(e)(4), Final Safety Analysis Report Update Schedule (EPID L-2023-LLE-0023) - Letter ML24243A0152024-09-0303 September 2024 – Notification of Comprehensive Engineering Team Inspection (05000445/2025012 and 05000446/2025012) and Request for Information ML24194A1332024-08-28028 August 2024 Issuance of Amendment Nos. 190 and 190, Respectively, Revision to Technical Specifications to Adopt TSTF-589, Eliminate Automatic Diesel Generator Start During Shutdown ML24228A2252024-08-22022 August 2024 Relief to Use Later Code Edition for Inservice Inspection Program ML24179A0772024-08-20020 August 2024 Issuance of Amendment Nos. 189 and 189, Respectively, Extension of Allowed Outage Time for an Inoperable Emergency Diesel Generator ML24232A2262024-08-19019 August 2024 Information Request, Security IR 2024404 ML24232A2412024-08-19019 August 2024 Information Request, ISFSI Security IR 2024401 CP-202400294, (CPNPP) - Response to RAI for Exemption Request from 10 CPR 50.71(e)(4) Final Safety Analysis Update Schedule2024-08-15015 August 2024 (CPNPP) - Response to RAI for Exemption Request from 10 CPR 50.71(e)(4) Final Safety Analysis Update Schedule IR 05000445/20240052024-08-15015 August 2024 Updated Inspection Plan for Comanche Peak Nuclear Power Plant, Units 1 and 2 (Report 05000445/2024005 and 05000446/2024005) CP-202400319, (CPNPP) - Revision to CPNPP Letter to the NRC, Multiple Relief Requests for Unit 2 Third Ten-Year Inservice Inspection Interval from 10CFR50.55(a) Inspection Requirements Due to Impracticality2024-08-13013 August 2024 (CPNPP) - Revision to CPNPP Letter to the NRC, Multiple Relief Requests for Unit 2 Third Ten-Year Inservice Inspection Interval from 10CFR50.55(a) Inspection Requirements Due to Impracticality ML24177A2692024-08-0707 August 2024 Issuance of Amendment Nos. 188 and 188, Respectively, Revision to Technical Specifications to Adopt TSTF-591, Revise Risk Informed Completion Time (RICT) Program CP-202400315, (Cpnpp), Multiple Relief Requests for Unit 2 Third Ten-Year Inservice Inspection Interval from 10CFR50.55(a) Inspection Requirements Due to Impracticality2024-08-0505 August 2024 (Cpnpp), Multiple Relief Requests for Unit 2 Third Ten-Year Inservice Inspection Interval from 10CFR50.55(a) Inspection Requirements Due to Impracticality IR 05000445/20240022024-07-31031 July 2024 Units 1 and 2 - Integrated Inspection Report 05000445/2024002 and 05000446/2024002,and Independent Spent Fuel Storage Installation Inspection Report 07200074/2024001 IR 05000445/20244032024-07-16016 July 2024 Security Baseline Inspection Report 05000445/2024403 and 05000446/2024403 (Full Report) ML24187A0372024-07-15015 July 2024 Withdrawal of Requested Licensing Action Exemption from Select Requirements of 10 CFR Part 55, Operators Licenses ML24192A1862024-07-10010 July 2024 Notification of Inspection (NRC Inspection Report 05000445/2024003 and 05000446/2024003) and Request for Information ML24185A1382024-07-0202 July 2024 Inservice Inspection Request for Information CP-202400253, (Cpnpp), Units 1 & 2 Inservice Testing Plan for Pumps & Valves Third Interval, Revision 52024-06-26026 June 2024 (Cpnpp), Units 1 & 2 Inservice Testing Plan for Pumps & Valves Third Interval, Revision 5 IR 05000445/20244012024-06-26026 June 2024 MC&A Program Inspection Report 05000445-2024401 and 05000446-2024401 Public-Final CP-202400235, (Cpnpp), Units 1 & 2, Inservice Testing Plan for Pumps & Valves Fourth Interval, Revision 02024-06-18018 June 2024 (Cpnpp), Units 1 & 2, Inservice Testing Plan for Pumps & Valves Fourth Interval, Revision 0 IR 05000445/20240122024-06-17017 June 2024 Design Basis Assurance Inspection (Programs) Inspection Report 05000445/2024012 and 05000446/2024012 ML24120A3632024-06-10010 June 2024 Issuance of Amendment Nos. 187 and 187, Respectively Adoption of 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Plants 05000445/LER-1924-002, (Cpnpp), Unit 1, Condition Prohibited by Technical Specifications Due to Inoperable Remote Shutdown System Functions2024-06-0303 June 2024 (Cpnpp), Unit 1, Condition Prohibited by Technical Specifications Due to Inoperable Remote Shutdown System Functions CP-202400205, (Cpnpp), Units 1and 2, Submittal of the Snubber Inservice Program Plan for the Fourth Ten Year Interval2024-05-30030 May 2024 (Cpnpp), Units 1and 2, Submittal of the Snubber Inservice Program Plan for the Fourth Ten Year Interval CP-202400175, (CPNPP) - Supplement to License Amendment Request to Extend the Allowed Outage Time for an Inoperable Emergency Diesel Generator2024-05-16016 May 2024 (CPNPP) - Supplement to License Amendment Request to Extend the Allowed Outage Time for an Inoperable Emergency Diesel Generator 05000446/LER-2024-001, (Cpnpp), Unit 2, Two Recurring Reactor Scrams Associated with Main Feedwater System Modifications2024-05-13013 May 2024 (Cpnpp), Unit 2, Two Recurring Reactor Scrams Associated with Main Feedwater System Modifications 05000445/LER-2024-001, Re Potential Loss of Safety Function Due to Inoperability of Both Trains of Uninterruptible Power Supply Heating, Ventilation & Air Conditioning2024-05-0606 May 2024 Re Potential Loss of Safety Function Due to Inoperability of Both Trains of Uninterruptible Power Supply Heating, Ventilation & Air Conditioning ML24120A3042024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Sylestine, R, Alabama-Coushatta Tribe of Texas ML24120A2902024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Bunch, J, United Keetoowah Band of Cherokee Indians ML24120A2912024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Cooper, D, Apache Tribe of Oklahoma ML24120A3032024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-SpottedBird, L, Kiowa Indian Tribe ML24107B1012024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Cernek, J, Coushatta Tribe of Louisiana ML24120A3022024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Pierite, M, Tunica-Biloxi Tribe of Louisiana ML24120A2922024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Dotson, Delaware Nation ML24120A2952024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Johnson, L.J., Seminole Nation of Oklahoma CP-202400153, (Cpnpp), Registration of Dry Spent Fuel Storage Canisters2024-04-29029 April 2024 (Cpnpp), Registration of Dry Spent Fuel Storage Canisters ML24120A3052024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Woommavovah, M, Comanche Nation ML24120A3072024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Yargee, W, Alabama-Quassarte Tribal Town ML24120A2932024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Garza, Jr, Juan, Kickapoo Traditional Tribe of Texas ML24120A3002024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Morrow, R K, Thlopthlocco Tribal Town ML24120A2942024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Gonzalez, B, Caddo Nation ML24120A3012024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Parton, T, Wichita and Affiliated Tribes ML24120A2972024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Martin, R, Tonkawa Tribe of Oklahoma ML24120A2962024-04-29029 April 2024 Lr Feis Section 106 Consultation Letters, Tribes-Kaskaske, D, Kickapoo Tribe of Oklahoma 2024-09-30
[Table view] |
Text
January 23, 2023
SUBJECT:
COMANCHE PEAK NUCLEAR POWER PLANT, UNITS 1 AND 2 -
TI-194 REPORT 05000445/2022010 AND 05000446/2022010
Dear Ken Peters:
On January 19, 2023, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Comanche Peak Nuclear Power Plant, Units 1 and 2 and discussed the results of this inspection with Mr. S. Sewell, Acting Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Nicholas H. Taylor, Chief Engineering Branch 2 Division of Operating Reactor Safety
Docket Nos. 05000445, 05000446 License Nos. NPF-87, NPF-89
Enclosure:
As stated
Inspection Report
Docket Numbers: 05000445 and 05000446
License Numbers: NPF-87 and NPF-89
Report Numbers: 05000445/2022010 and 05000446/2022010
Enterprise Identifier: I-2022-010-0058
Licensee: Vistra Operations Company, LLC
Facility: Comanche Peak Nuclear Power Plant, Units 1 and 2
Location: Glen Rose, TX 76043
Inspection Dates: November 14, 2022 to November 18, 2022
Inspectors: J. Drake, Senior Reactor Inspector S. Graves, Senior Reactor Inspector R. Deese, Senior Reactor Analyst
Approved By: Nicholas H. Taylor, Chief Engineering Branch 2 Division of Operating Reactor Safety
Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a Temporary Instruction 2515/194, Inspection of the Licensees Implementation of Industry Initiative Associated with the Open Phase Condition Design Vulnerabilities in Electric Power Systems (NRC Bulletin 2012-01), at Comanche Peak Nuclear Power Plant, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL
2515/194 - Inspection of the Licensees Implementation of Industry Initiative Associated With the Open Phase Condition Design Vulnerabilities In Electric Power Systems (NRC Bulletin 2012-01)
The inspectors reviewed the licensees implementation of revision three to Nuclear Energy Institute Voluntary Industry Initiative, (ADAMS Accession No. ML19163A176) dated June 6, 2019. This review focused on modifications to the open phase detection system designed and manufactured by Power System Sentinel Technologies, LLC. The inspectors also reviewed the licensee's application of risk screening techniques to determine that the risk associated with an open phase condition (OPC) event is significantly reduced through the implementation of detection circuits and the use of operator manual actions in lieu of automatic trip functions.
Sections 03.01.a, Detection, Alarms and General Criteria, and 03.01.b, Protective Actions, were previously inspected and documented in Inspection Report 05000445/2018012 and
===05000446/2018012 with noted exceptions. Because the licensee chose to demonstrate compliance with Revision 3 of the Open Phase Condition Initiative using the Risk Informed Evaluation Method in lieu of the designs automatic protective functions, section 03.01.c, Use of Risk-Informed Evaluation Method was inspected and documented in Inspection Report 05000445/2021012 and 05000446/2021012 with one noted exception. The licensee implemented modifications to the OPC equipment installed on the XST2 transformer due to a high impedance condition which prevented the OPC equipment from being able to detect an open phase condition with the transformer lightly loaded. This modification has been inspected by the NRC staff and the results documented in this report. This included reviewing how the licensee updated their licensing basis to reflect the need to protect against open phase conditions.
Inspection of the Licensees Implementation of Industry Initiative Associated With the Open Phase Condition Design Vulnerabilities In Electric Power Systems (NRC Bulletin 2012-01)===
- (1) Vistra Operations Company, LLC selected the open phase detection system designed and manufactured by Power System Sentinel Technologies, LLC, as the design vendor for Comanche Peak Nuclear Power Plant. Due to a high impedance condition on the XST2 transformer neutral preventing the use of active injection to identify unbalanced phase conditions, the licensee elected to modify the Open Phase Condition (OPC) equipment installed on the XST2 transformer. At the end of this inspection the licensee had installed complete systems in monitoring mode on all four startup transformers but removed the Active Injection signal capability for identifying unbalanced conditions under low loading from the OPC equipment installed on the XST2 transformer. The inspectors reviewed the engineering change documents for the modifications to the open phase detection equipment for the XST2 transformer, including loading calculations and scenarios and electrical load diagrams to verify that the XST2 transformer would be loaded in excess of the vendor-identified minimum loading (600 kVA) necessary to ensure open phase conditions would be detected.
Exceptions:
None
Observations:
1. The XST2 transformer OPC equipment has been modified by removal of relay CR112 from the open phase monitoring equipment and revision of SEL2411 code (Schweitzer Engineering Laboratories). This modification eliminated the injection abnormal and injection source failure alarms from the channel general alarm and disabled the test initiate and injection signal reference pushbuttons.
2. The modification requires that the XST2 transformer always have a minimum loading of 600 kVA to ensure on open phase conditions will be detected by the passive mode of the OPC equipment. Inspectors reviewed electrical drawings and diagrams which showed that normal and likely conditions the loading on the XST2 transformer would be above this threshold when in service.
INSPECTION RESULTS
No findings were identified.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On January 19, 2023, the inspectors presented the TI-194 post modification exit meeting inspection results to Mr. S. Sewell, Acting Site Vice President, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision or
Procedure Date
2515/194 Calculations EE-VP-U1-Unit 1 Class 1E System Voltage Profile 5
1E_05
Engineering FDA-2016-Revise FDA to removed relay CR112 from the 2
Changes 000005-04 Byron open phase modification
FDA-2016-Final Design Authorization 10/31/2022
000005-04-
Miscellaneous 6.9 kV / 480 VAC Big Book 12/07/2013
EE-VP-U1-Specification - OPEN PHASE PROTECTION 2
1E_05 SYSTEM
IEGR-DD-OPPSys_protection_settings_CPNPP_U2_XST2-
1741 A
IEGR-DD-OPPSys_protection_settings_CPNPP_U2_XST2
2564 (003)
SL-011517 Report - Open Phase Evaluation - Transformers 0
XST1, XST2 and XST2A
VDRT-Open Phase Protection (OPP) System Failure 0
6034826 Modes and Effects Analysis (FMEA) Comanche
Peak NPP XST2
VDRT-Open Phase Protection (OPP) System Operating 0
6034827 and Maintenance Manual-Comanche Peak for
Transformer XST-2
Procedures SOP-602 138 KV AND 345 KV TRANSFORMERS AND 14
SWITCHYARD AIR SWITCHES
SOP-602 138 KV AND 345 KV TRANSFORMERS AND 15
SWITCHYARD AIR SWITCHES
5