ML20196J637

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Discusses Insp Rept 50-354/97-01 Conducted on 970202 & 0317 & Forwards Notice of Violation Re Inadequate Safety Evaluations for Mod That Was Installed in Apr 1994
ML20196J637
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 10/20/1997
From: Miller H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Eliason L
Public Service Enterprise Group
Shared Package
ML20196J644 List:
References
50-354-97-01, 50-354-97-1, EA-97-160, NUDOCS 9812100158
Download: ML20196J637 (4)


See also: IR 05000354/1997001

Text

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UNITED STATES

[ g NUCLEAR REGULATORY COMMISSION

3 E REGION I

f 475 ALLENDALE ROAD

%g*****,e KING OF PRUSSIA, PENNSYLVANIA 1M061415

October 20, 1997

[ EA 97-160

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!

Mr. Leon R. Eliason

Chief Nuclear Officer & President

Nuclear Business Unit

, Public Service Electric and Gas Company

l Post Office Box 236

Hancocks Bridge, New Jersey 08038  !

!

! SUBJECT: NOTICE OF VIOLATION

(NRC Inspection Report No. 50-354/97-01)

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Dear Mr. Eliason:

This letter refers to the NRC routine inspection conducted at the Hope Creek Generating

Station between February 2 and March 17,1997, the results of which were discussed with 1

Mr. L. Storz and other members of your staff at an exit meeting on March 27,1997. The  !

inspection report was sent to you on April 14,1997. During the inspection, the NRC

identified weaknesses in the safety evaluations for design change packages which added

,

crosstie piping and valves between the Residual Heat Removal (RHR) subsystems. In a

teleconference between Mr. M. Bezilla of your staff and Mr. J. Linville of the NRC, on June

t

26,1997, another exit meeting was held to inform you that the NRC had concluded that two l

of the weaknesses in the safety evaluations involved apparent violations of NRC requirements.  !

On August 12,1997, a predecisional enforcement conference (conference) was conducted

with you and other members of your staff to discuss the apparent violations idsntified during

the inspection, their causes, and your corrective actions.

,

[  ;

l Based on our review of the inspection findings, and information provided during the l

l conference, one violation of NRC requirements is being cited and is described in the enclosed i

y Notice of . Violation (Notice). The violation involves inadequate safety evaluations for a I

l- modification that was installed in April 1994. The modification involves the installation of

l crosstie piping, with two isolation valves, between the A and C RHR loops downstream of the

l RHR pumps to allow for additional flexibility during shutdown cooling operations. The safety i

l

evaluations were inadequate because you failed to identify that: 1) the change involved an '

tareviewed safety question (USO) since the change introduced the possibility of a loss of

independence of the low pressure coolant injection (LPCI) loops due to an erroneous valve

lineup; and 2) the crosstie isolation valves needed to be included h the monthly emergency

core cooling system (ECCS) flowpath verification required by Technical Specifications (TS),

which is required for any valve in the ECCS flowpath that is not locked closed.

'

Even though you recognized that installation of the crosstie piping changed the mechanical

separation criteria of the LPCI subsystems, and you properly evaluated the potential for

intemal flooding events, you did not rigorously review the potential loss of more than one LPCI

l flow path resulting from an erroneous valve alignment, which is a malfunction of a different

type than had been previously evaluated in the UFSAR. If a change introduces a malfunction

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9812100158 971020

PDR

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ADOCK 05000354 'k iI

PDR

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Public Service Electric and Gas 2

l Company

of a different type than any evaluated previously in the UFSAR, it constitutes a USQ, and

.

Commission approval is required prior to implementation. In this case, the modification was

l installed without prior Commission approval. At the conference, you acknowledged that the

l original design of the crosstie piping was inadequate in that the design specified one of the

{ two isolation valves to be normally open while tise reactor was at power. In such a

j configuration, valve misalignment such that the loops would be crosstied, should have been

j considered as a credible failure and, therefore, should have been identified as a USO.

l

However, you also provided your view that the USQ associated with the RHR crosstie

modification was eliminated in March 1995, when you recognized the need to shut both

crosstie isolation valves when the reactor is at power. You determined that the probability of

unintentionally mispositioning the two manual crosstie isolation valves was several orders of

magnitude lower than the probability of other similar conditions evaluated in the UFSAR.

Therefore, misalignment of both crosstie valves did not have to be considered as creating the

possibility of a malfunction of a different type because it was not a credible event. You

indicated that this determination was based on guidance in Nuclear Safety Analysis Center

(NSAC)-125, " Guidelines for 10 CFR 50.59 Safety Evaluations." ^ Nevertheless, this

arrangement created the possibility for a malfunction of a different type. I

1

This violation is significant because between April 1994, when the crosstie piping was {

installed, and March 1995, when changes were made to require both isolation valves to be  ;

closed whenever the reactor was at power, a single valve alignment error could have resulted I

in the loss of independence of the LPCI subsystems. Fortuitously, both valves were always

closed while the reactor was at power due to an errorin the system drawings, but there were

no administrative controls in place to ensure that the valves were in the correct position and  ;

remained in that position. The violation is also of regulatory concern because the NRC relies

upon licensees correctly assessing proposed modifications to ensure that USQs do not exist. 1

Therefore, this violation has been categorized at Severity Level lliin accordance with the i

" General Statement of Policy and Procedure for NRC Enforcement Actions," (Enforcement

Policy), NUREG-1600.

In accordance with the Enforcement Policy, a base civil penalty in the amount of $50,000 is

considered for a Severity Level lil problem or violation that occured prior to November 12,

1996. Hope Creek has been the subject of escalated enforcement actions within the last 2

years'. Therefore, the NRC considered whether credit was warranted for /denti// cation and

Corrective Action in accordance with the civil penalty assessment process in Section VI.B.2

of the Enforcement Policy. Credit is warranted forIdentification because, even though you

did not identify the inadequacies in your safety evaluations until prompted by the NRC, you

did recognize the need to shut both crosstie isolation valves during a safety system functional

review in March 1995, and identified the need for administrative controls to ensure that the

valves are shut when the reactor is at power during review of the safety evaluation for the B

and D loop crosstie in December 1995. Subsequent to the conference, you submitted a TS

l

A Notice of Violation and Proposed imposition of Civil Penalties in the amount of $150,000

was issued to PSE&G on October 23,1996, for several violations, including a similar failure to

obtain NRC approval prior to implementing a change to the Hope Creek service water system

which involved a USQ. (EAs96-125 and 96-281)

,

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Public Service Electric and Gas 3

i Company -

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} amendment request for the RHR crosstie modification. Credit is also warranted for Corrective

j Action since your corrective actions to address the inadequate safety evaluations were

. considered both prompt and comprehensive after the violation was identified. These actions

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included, but were not limited to: (1) reassessment of the safety evaluations for the RHR  :

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crosstie modifications; (2) evaluation of 50.59 and engineering performance issues; (3) )

enhanced training for engineering staff and Station Operations Review Committee (SORC) i

members; (4) implementation of an independent peer review process; and (5) modification of I

i, your safety evaluation process to be consistent with NRC guidance.

.

!

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1.

j -

Therefore, to encourage prompt identification and comprehensive correction of violations, I

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have been authorized, after consultation with the Director, Office of Enforcement, not to l

! propose a civil penalty in this case. However, significant violations in the future could result  !

in a civil penalty. '

i

You are required to respond to this letter and should follow the instructions specified in the

j enclosed Notice when preparing your response. The NRC will use your response, in part, to

.: determine whether further enforcement action is necessary to ensure compliance with

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regulatory requirements.

In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter,its

enclosure, and your response will be placed in the NRC Public Document Room (PDR).
Sincerely,

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l H rt . Miller  !

j Regional Administrator

Docket No. 50-354 l

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License No. NPF-57 l

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Enclosure
Notice of Violation

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Public Service Electric and Gas 4

Company

cc w/ encl:

L. Storz, Senior Vice President - Nuclear Operations '

E. Simpson, Senior Vice President - Nuclear Engineering

E. Salowitz, Director - Nuclear Business Support

A. Kirby, lit, External Operations - Nuclear, Delmarva Power & Light Co.

J. Isabella, Manager, Joint Generation Atlantic Electric

M. Bezilla, General Manager - Hope Creek Operations '

J. McMahon, Director - Quality Assurance & Nuclear Safety Review i

D. Powell, Manager - Licensing and Regulation  !

R. Kankus, Joint Owner Affairs  ;

A. Tapert, Program Administrator

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J. Keenan, Esquire

Consumer Advocate, Office of Consumer Advocate

{

W. Conklin, Public Safety Consultant, Lower Alloways Creek Township

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State of New Jersey i

State of Delaware

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