ML20196J637
| ML20196J637 | |
| Person / Time | |
|---|---|
| Site: | Hope Creek |
| Issue date: | 10/20/1997 |
| From: | Miller H NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Eliason L Public Service Enterprise Group |
| Shared Package | |
| ML20196J644 | List: |
| References | |
| 50-354-97-01, 50-354-97-1, EA-97-160, NUDOCS 9812100158 | |
| Download: ML20196J637 (4) | |
See also: IR 05000354/1997001
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UNITED STATES
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NUCLEAR REGULATORY COMMISSION
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REGION I
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475 ALLENDALE ROAD
KING OF PRUSSIA, PENNSYLVANIA 1M061415
October 20, 1997
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EA 97-160
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Mr. Leon R. Eliason
Chief Nuclear Officer & President
Nuclear Business Unit
Public Service Electric and Gas Company
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Post Office Box 236
Hancocks Bridge, New Jersey 08038
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SUBJECT:
(NRC Inspection Report No. 50-354/97-01)
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Dear Mr. Eliason:
This letter refers to the NRC routine inspection conducted at the Hope Creek Generating
Station between February 2 and March 17,1997, the results of which were discussed with
Mr. L. Storz and other members of your staff at an exit meeting on March 27,1997. The
inspection report was sent to you on April 14,1997. During the inspection, the NRC
identified weaknesses in the safety evaluations for design change packages which added
crosstie piping and valves between the Residual Heat Removal (RHR) subsystems. In a
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teleconference between Mr. M. Bezilla of your staff and Mr. J. Linville of the NRC, on June
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26,1997, another exit meeting was held to inform you that the NRC had concluded that two
of the weaknesses in the safety evaluations involved apparent violations of NRC requirements.
On August 12,1997, a predecisional enforcement conference (conference) was conducted
with you and other members of your staff to discuss the apparent violations idsntified during
the inspection, their causes, and your corrective actions.
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Based on our review of the inspection findings, and information provided during the
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conference, one violation of NRC requirements is being cited and is described in the enclosed
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Notice of . Violation (Notice). The violation involves inadequate safety evaluations for a
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modification that was installed in April 1994. The modification involves the installation of
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crosstie piping, with two isolation valves, between the A and C RHR loops downstream of the
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RHR pumps to allow for additional flexibility during shutdown cooling operations. The safety
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evaluations were inadequate because you failed to identify that: 1) the change involved an
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tareviewed safety question (USO) since the change introduced the possibility of a loss of
independence of the low pressure coolant injection (LPCI) loops due to an erroneous valve
lineup; and 2) the crosstie isolation valves needed to be included h the monthly emergency
core cooling system (ECCS) flowpath verification required by Technical Specifications (TS),
which is required for any valve in the ECCS flowpath that is not locked closed.
Even though you recognized that installation of the crosstie piping changed the mechanical
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separation criteria of the LPCI subsystems, and you properly evaluated the potential for
intemal flooding events, you did not rigorously review the potential loss of more than one LPCI
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flow path resulting from an erroneous valve alignment, which is a malfunction of a different
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type than had been previously evaluated in the UFSAR. If a change introduces a malfunction
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9812100158 971020
ADOCK 05000354
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Public Service Electric and Gas
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of a different type than any evaluated previously in the UFSAR, it constitutes a USQ, and
Commission approval is required prior to implementation. In this case, the modification was
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installed without prior Commission approval. At the conference, you acknowledged that the
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original design of the crosstie piping was inadequate in that the design specified one of the
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two isolation valves to be normally open while tise reactor was at power. In such a
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configuration, valve misalignment such that the loops would be crosstied, should have been
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considered as a credible failure and, therefore, should have been identified as a USO.
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However, you also provided your view that the USQ associated with the RHR crosstie
modification was eliminated in March 1995, when you recognized the need to shut both
crosstie isolation valves when the reactor is at power. You determined that the probability of
unintentionally mispositioning the two manual crosstie isolation valves was several orders of
magnitude lower than the probability of other similar conditions evaluated in the UFSAR.
Therefore, misalignment of both crosstie valves did not have to be considered as creating the
possibility of a malfunction of a different type because it was not a credible event. You
indicated that this determination was based on guidance in Nuclear Safety Analysis Center
(NSAC)-125, " Guidelines for 10 CFR 50.59 Safety Evaluations." ^ Nevertheless, this
arrangement created the possibility for a malfunction of a different type.
This violation is significant because between April 1994, when the crosstie piping was
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installed, and March 1995, when changes were made to require both isolation valves to be
closed whenever the reactor was at power, a single valve alignment error could have resulted
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in the loss of independence of the LPCI subsystems. Fortuitously, both valves were always
closed while the reactor was at power due to an errorin the system drawings, but there were
no administrative controls in place to ensure that the valves were in the correct position and
remained in that position. The violation is also of regulatory concern because the NRC relies
upon licensees correctly assessing proposed modifications to ensure that USQs do not exist.
Therefore, this violation has been categorized at Severity Level lliin accordance with the
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" General Statement of Policy and Procedure for NRC Enforcement Actions," (Enforcement
Policy), NUREG-1600.
In accordance with the Enforcement Policy, a base civil penalty in the amount of $50,000 is
considered for a Severity Level lil problem or violation that occured prior to November 12,
1996. Hope Creek has been the subject of escalated enforcement actions within the last 2
years'. Therefore, the NRC considered whether credit was warranted for /denti// cation and
Corrective Action in accordance with the civil penalty assessment process in Section VI.B.2
of the Enforcement Policy. Credit is warranted forIdentification because, even though you
did not identify the inadequacies in your safety evaluations until prompted by the NRC, you
did recognize the need to shut both crosstie isolation valves during a safety system functional
review in March 1995, and identified the need for administrative controls to ensure that the
valves are shut when the reactor is at power during review of the safety evaluation for the B
and D loop crosstie in December 1995. Subsequent to the conference, you submitted a TS
A Notice of Violation and Proposed imposition of Civil Penalties in the amount of $150,000
was issued to PSE&G on October 23,1996, for several violations, including a similar failure to
obtain NRC approval prior to implementing a change to the Hope Creek service water system
which involved a USQ. (EAs96-125 and 96-281)
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amendment request for the RHR crosstie modification. Credit is also warranted for Corrective
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Action since your corrective actions to address the inadequate safety evaluations were
considered both prompt and comprehensive after the violation was identified. These actions
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included, but were not limited to: (1) reassessment of the safety evaluations for the RHR
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crosstie modifications; (2) evaluation of 50.59 and engineering performance issues; (3)
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enhanced training for engineering staff and Station Operations Review Committee (SORC)
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members; (4) implementation of an independent peer review process; and (5) modification of
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your safety evaluation process to be consistent with NRC guidance.
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Therefore, to encourage prompt identification and comprehensive correction of violations, I
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have been authorized, after consultation with the Director, Office of Enforcement, not to
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propose a civil penalty in this case. However, significant violations in the future could result
in a civil penalty.
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You are required to respond to this letter and should follow the instructions specified in the
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enclosed Notice when preparing your response. The NRC will use your response, in part, to
determine whether further enforcement action is necessary to ensure compliance with
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regulatory requirements.
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In accordance with 10 CFR 2.790 of the NRC's " Rules of Practice," a copy of this letter,its
enclosure, and your response will be placed in the NRC Public Document Room (PDR).
Sincerely,
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H
rt . Miller
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Regional Administrator
Docket No. 50-354
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License No. NPF-57
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Enclosure: Notice of Violation
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Public Service Electric and Gas
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cc w/ encl:
L. Storz, Senior Vice President - Nuclear Operations
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E. Simpson, Senior Vice President - Nuclear Engineering
E. Salowitz, Director - Nuclear Business Support
A. Kirby, lit, External Operations - Nuclear, Delmarva Power & Light Co.
J. Isabella, Manager, Joint Generation Atlantic Electric
M. Bezilla, General Manager - Hope Creek Operations
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J. McMahon, Director - Quality Assurance & Nuclear Safety Review
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D. Powell, Manager - Licensing and Regulation
R. Kankus, Joint Owner Affairs
A. Tapert, Program Administrator
J. Keenan, Esquire
Consumer Advocate, Office of Consumer Advocate
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W. Conklin, Public Safety Consultant, Lower Alloways Creek Township
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State of New Jersey
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State of Delaware
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