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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20151Y1191998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Calvert Cliffs Nuclear Power Plant Units 1 & 2.With ML20237B9371998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Calvert Cliffs Nuclear Power Plant ML20236R0881998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20249A7711998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ccnpp,Units 1 & 2 ML20247H5661998-04-30030 April 1998 Monthly Operating Repts for April 1998 for Ccnpp ML20216G4601998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20248L3641998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20202G6611998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20198N9441997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Calvert Cliffs Nuclear Power Plant,Units 2 & 3 ML20203H3081997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Calvert Cliffs Nuclear Power Plant ML20199D0801997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20198J6631997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Calvert Cliffs Nuclear Power Plant ML20210U7031997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for Ccnpp ML20210L0671997-07-31031 July 1997 Monthly Operating Repts for July 1997 for Ccnpp ML20149E2301997-06-30030 June 1997 Monthly Operating Repts for June 1997 for Calvert Cliffs Nuclear Power Plant ML20148L1761997-05-31031 May 1997 Monthly Operating Repts for May 1997 for CCNP ML20141F1401997-04-30030 April 1997 Monthly Operating Repts for Apr 1997 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20137W8781997-03-31031 March 1997 Monthly Operating Repts for Mar 1997 for Calvert Cliffs Nuclear Power Plant ML20136J4941997-02-28028 February 1997 Monthly Operating Repts for Feb 1997 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20134M2891997-01-31031 January 1997 Monthly Operating Repts for Jan 1997 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20133N1031996-12-31031 December 1996 Monthly Operating Repts for Dec 1996 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20132D1141996-11-30030 November 1996 Monthly Operating Repts for Nov 1996 for Calvert Cliffs Nuclear Power Plant,Unit 1 & 2 ML20134L6621996-10-31031 October 1996 Monthly Operating Repts for Oct 1996 for Calvert Cliffs Nuclear Power Plant Unit 1 & 2 ML20128Q8011996-09-30030 September 1996 Monthly Operating Repts for Sept 1996 for Calvert Cliffs Npp,Units 1 & 2 ML20117N2171996-08-31031 August 1996 Monthly Operating Repts for Aug 1996 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20116M6701996-07-31031 July 1996 Monthly Operating Repts for Jul 1996 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20115F7281996-06-30030 June 1996 Monthly Operating Repts for June 1996 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20112J1291996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20112A2421996-04-30030 April 1996 Monthly Operating Repts for Apr 1996 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20107C1831996-03-31031 March 1996 Monthly Operating Repts for Mar 1996 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20101D7831996-02-29029 February 1996 Monthly Operating Repts for Feb 1996 for Ccnpp ML20149K8721996-01-31031 January 1996 Monthly Operating Repts for Jan 1996 for Ccnpp ML20096D7031995-12-31031 December 1995 Monthly Operating Repts for Dec 1995 for Ccnpp Units 1 & 2 ML20095H3741995-11-30030 November 1995 Monthly Operating Repts for Nov 1995 for Calvert Cliffs Nuclear Power Plant Units 1 & 2 ML20096D7171995-11-30030 November 1995 Rev to Monthly Operating Rept for Nov 1995 for Ccnpp Unit 2 ML20094M0161995-10-31031 October 1995 Monthly Operating Repts for Oct 1995 for Calvert Cliffs Nuclear Plant ML20093G5881995-09-30030 September 1995 Monthly Operating Repts for Sept 1995 for Calvert Cliffs Nuclear Power Plants Units 1 & 2 ML20092G3521995-08-31031 August 1995 Monthly Operating Repts for Aug 1995 for Calvert Cliffs Nuclear Power Plant 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs LD-99-039, Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of Abb 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-035, Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re Abb 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on Abb CE ECCS Performance Evaluation Models ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 ML20153C1091998-09-18018 September 1998 Part 21 Rept Re Defective Capacity Control Valves.Trentec Personnel Have Been in Contact with Bg&E Personnel Re Condition & Have Requested Potentially Defective Valves ML20151U5441998-09-0404 September 1998 Bg&E ISI Summary Rept for Calvert Cliffs ML20151T5281998-09-0101 September 1998 Special Rept:On 980819,declared Rv Water Level Monitor Channel a Inoperable.Caused by Failure of Three Heated Junction Thermocouples (Sensors) in Lower Five Sensors. Channel a & B Rv Water Level Probes Will Be Replaced ML20151Y1191998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Calvert Cliffs Nuclear Power Plant Units 1 & 2.With ML20237D4981998-08-19019 August 1998 Safety Evaluation Accepting Licensee Request for Extension of Second ten-year Inservice Insp Interval ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML20237B9371998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Calvert Cliffs Nuclear Power Plant ML20237D5941998-07-22022 July 1998 Rev 2 to Ccnpp COLR for Unit 2,Cycle 12 ML20236L7521998-07-0606 July 1998 Safety Evaluation Granting Bg&E 980527 Request for Relief from Requirement of Section IWA-5250 of ASME Code for Calvert Cliffs Unit 2.Alternatives Provide Reasonable Assurance of Operational Readiness ML20236F7791998-06-30030 June 1998 Safety Evaluation Authorizing Request for Temporary Relief from Requirement of Subsection IWA-5250 of ASME Code,Section XI for Plant,Unit 1 ML20236R0881998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20236X3101998-06-19019 June 1998 Rev 1 to Calvert Cliffs Nuclear Power Plant COLR for Unit 2,Cycle 12 ML20249A9571998-06-15015 June 1998 Special Rept:On 980430,fire Detection Sys Was Removed from Svc to Support Mod to Purge Air Sys 27-foot Elevation & 5-foot Elevation East Piping Penetration Rooms.Installed Temporary Alteration & Returned Fire Detection Sys to Svc ML20249A7711998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Ccnpp,Units 1 & 2 1999-09-30
[Table view] |
Text
.
. e OPER ATlhG DAT A REPORT DOCKET NO. _50-317 DATE 7/15/82 COMPLETED BY Elaine lotito
. TELEPHONE (301) 787.5363 OPERATING STAIUS Notes
- 1. Uni: Name: Calvert Cliffs #1
- 2. Reporting Period: June, 1982
- 3. Licensed Thermal Power (MWr): 2,700
- 4. Nameplate Rating IGrms MWe p: 918
- 5. Design Elutrical Reting (Net MWe): 845
- 6. Maximum Dependable Capacity (Grass Mbe): -
- 7. Masimem Dependable Capacuy (Net MWe): 825
- 8. If Charges Ocet.r in Capsetty Ratings (Items Nunter 3 Through 7) Since Last Repurt.Gi'c Reasons.
- 9. Power Lesel To hhich licitricted. lf Any (Net Mhen:
10 Reasons For Restrictimu. lf Any:
This Month Yr.-to-Date Ct.mulative
^
I1. Hours in Reporting FerioJ -- 720.0 4.343.0 __ 62.652.0
- 12. Number Of Houes Reactor Was Critical 2.7 2,550.1 49,149.8
- 13. Reactor Resene $hurdown Hours 0.0 0.0 1,792.4
- 14. Ilours Generatoc On.Line 0.0 2,547.4 7 ,149.1 ,
- 15. UrJt Resene Shutdown linurs 0.0 0.0 0.'O
- 16. Gross Thermal Energy Generated (MWHI O 6,735, % 7 116,655,445 .
- 17. Gross Electrical Energy Genersted (MWill O 2,274,438 m,m,
- 18. Ne: Electrical Energy Generated (MWHi 0 2,178,927 _ 36,480,960
- 19. IJnit Senice f actor 0.0 58.7 76.9
- 20. Unit Assdability Facic,r 0.0 M.7 76.9
- 21. Unit Capacity Facter iUsing MDC Net) 0.0 60.8 70.6
- 22. Unit Capacity Factor (Using DER *ict) 0.0 59.4 68.9
- 23. Unit Iorced Outage Rate 0.0 0.0 8.4
- 24. Shutdowns Scheduled Over Nest 6 Months (Type. Date.ard Duration of Eacht.
No. I plant on a planned outage fran 4/17/82 for refueling, unit general irupection, and retube condenser.
%e plant was reported in service on 7/5/82 and is presently ranping back to full load.
- 25. If Shut ()own At End Of Report Feru>d. Estimated Date of Startup:
- 26. Unitsin Test Status (Prior to Commercial Optration). Forecast Achieved INITIA L CRITICALITY.
INITIA L ELECTRICITY COMMERCI AL OPER ATION
'82072'10276 SGI5i715 -
' (a[77)
PDR ADOCK 05000317 R PDR.
. ._ L
l OPER ATING DAT 4 REPORT DOCKET No. _% 11 A DATE 7/15/82 COMPLETED BY yintne totito TELEPHONE _ (101) 787a161 OPER ATING STA T US
- 1. Uni: Name: C.ilvert Cliffs #2 bot *5
- 2. Reporting Period. June, 1982 2,700
- 3. Li:ensed Thermal Power (MW ).
- 4. Nameplate I.ating (Cross MWel: 911
- 5. Desi;;n Elettrica! Rating (Net Mwe): 845
- 6. Maximum Dependable Capacity (Gross MWe): 860
- 7. Masimum Dependable Capacity (Net MWe): 825
- 8. If Charges Occur in Capseity Ratings litems Nur,ter 3 Through 7) Since Last Report.Gise Reasons:
- 9. Power Leiel To hhich Hestricted.lf Any (Net 4the):
- 10. Reasons For Restnctions. If Any:
This Month Yr..to Date Ct.mubtive 720.0
- 11. ilours in Reporting PreioJ 4.343.0 46,007.0
- 12. Nember Oi Hours Reactor was Critical 720.0 4,033.7 39,601.7
- 13. Rescror Resene Shutdown Hours 0.0 9.4 723.6
- 14. Hours Generator On Line 0.0 <+,u11.2 w ,vaa.6
- 15. Unit Resene Shutdown llouri 0.0 0.'O 0.0
- 16. Gross Thermal Energy Generated iMWHI 1,856,153 10,561,111 % ,605,667 .
- 17. Gross Electrical Energy Generated lMWill 5 % ,014 3,487,526 31,902,929
~
- 18. Nc Electrical Enctgy Generated (MWti, 576,895 3,346,757 _ 30,432,568
- 19. Urut Senice Factot 100.0 92.4 84.9
- 20. Unit Avalability Factor 100.0 92.4 84.9
- 21. Unit Capacity Factor (Using MDC Nett 97.1 ~ 93.4 80.2
- 22. Unit Capacity factor tusing DER Net) 94.8 91.2 78.3
- 23. Unit Forced Outage Rate 0.0 7.6 5.6
- 24. Shutdowns Scheduled Over Nest 6 Months (Type. Date.snd Duration of Eacht:
(
- 25. If Shut Down At End Of Report Period. Estimated Date of Staitup:
- 26. Units in Test StatuilPrior to Commercial 0perstion): Forecast Achieved INITIA L CRITICA LITY .
INITIA L EL ECTRICITY COMstERCI AL OPER ATION (9/77)
6., ., .
IVERAC,E D AILY UNIT POWER LEVEL DOCKET NO. 50-317 Calvert Cliffs #1 UNIT DATE 7/15/82 COMPLETED BY Elaine lotito TELEPflONE 1) 787- M MONTH June 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe Net) (MWe-Neti 1 l7 -
2 18 -
3 -
19 -
4 20 5 --
21 6 22 7 23 8 24 9 -
25 -
10 . 26 1I 27 12 23 13 , 29 14 30 15 3l -
16 INSTRUCTIONS On this format.Itst the nerage daily unit power levelin MWe. Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/77)
L
s., .'- .
~
kVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-318 UNIT Calvert Cliffs #2 DATE 7/15/82 COMPLETED BY Elaine lotito TELEPHONE (301) 787 5363 MONTil --J e 1982 DAY AVERAGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL
- (MWe Net) (Mwe-Net p i 855 17 760' 2 784 gg 687 840 737 3 g9 4 844 20 757 5 741 731 21 6 801 22 782 7 829 833 23 8 24 E
849 834 9 25 820 832 10 . 26 11 851 27 75; 12 746 28 831 13 770 831 29 14 853 824 30 855 _
15 3, 16 822 INSTRUCTIONS On this format.hst the average daily unit power levelin MWe. Net for each day in the reporting month. Compute to the nearest whole megawatt.
(9/771
DOCKET NO. 91317 UNIT SHUTDOWNS AND POWER REDUCTIONS UNIT NAME r ,1 ~ r, enrr_ q DATE 7/1 W 2 F1,f re Y e+ 4 e ,
COMPLETED BY REPORT MONT11 Jum, 1%', TELEPHONE (301) 787 s363 e.
- E E
$E 3 jU Li6cnsec Eg yi Cause & Corrective .
No. Date Q 3? 4 .s j $ Event g sg0 I' Action to 3: 5 jgg Report a mL g Present Recurrence d
i 82-01 820417 S 720.0 C 4 XX Fuel X Refueling, unit general inspection and retube l condenser.
t
/
J l
/
l
' +
/
4 )
- 3 4 1 .'l F: Forced . ' ' ' Reason: Method: Exhibit G -Instructions for Preparation of Data l S: Scheduled A Equipment Failure (Explain) I-Manual .
24tanual Scram. Entry Sheets for Licensee l B Maintenance of Test C-Refueling 3 Autunutic Scram. Event Report tLER) File (NUREG-D Regulator) Restriction 44 entinuation 016I)
I; Operator Tsaining& Liecus Examination 5-Load Reduction F Adm.mstrative 5 9-Other Exhibis I Same Source G-Operational Ersur (Explain)
(9/77) Il4hher (Explain) a
DOCKET NO.56-318 UNIT SHUTDOhNS AND POWER REDUCllONS UNIT NAME Cahen Cliffs 4 DATE 7 'i s 'O N TED {jg RFPORT MONTH June 1982 l
.$3 3 h[ Lwensec En, fg Cauw & Corrective .
No. Daic h 3g ( .g g e Escrit a7 EU a? Action to u!'
$E 3 g =f e
No outages or reductions.
I 2 3 4 F: Forced Reason: Method: Exhibit G - Instructions A Equipment Failure (Explain) 1 -Manual for Preparation of Data 5: Scheduled B Maintenance of Test 2-Manual Scram. Entry Sheets for Licensee C-Refueling 3- Automatie Scram. Event Report t1.ER) File (NUREG-D Regulatory Restriction 44 cntinuation 0161) 1:-Operator Tsaining A License Eumination 5-Load Reduction F Adnunntrative $
-Otlier Exhibit I - Same Source G-Operational Essur (Explain)
(9/77) IlOther (Explain)
July 7,1982 REFUELING INFORMATION REQUEST
- 1. Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No.1
- 2. Scheduled date for next Refueling Shutdown: October 15,1983*
- 3. Scheduled date for restart following refueling: December 9,1983*
- 4. Will refueling or resumption of operation thereaf ter require a technical specification change or other license amendment?
Resumption of operation after refueling will require changes to Technical Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core.
- 5. Scheduled date(s) for submitting proposed licensing accion and supporting Information.
July 13,1983*
- 6. Important licensing considerations associated with the refueling.
Reload fuel will be similar to that reload fuel inserted into the previous cycle.
- 7. The number of fuel assemblies (a) in the core and (b) in the spent fuel storage pool.
(a) 217 (b) 656 Spent Fuel Pools are common to Units 1 and 2
- 8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies.
1830 Licensed
- 9. The projected date of 'M last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load.
April,1991
- Information changed since last report.
I i
. . l' July 7,1982 REFUELING INFORMATION REQUEST
- 1. Name of Facility: Calvert Cliffs Nuclear Power Plant, Unit No. 2.
- 2. Scheduled date for next refueling shutdowm October 15,1982.
- 3. Scheduled date for restart following refueling: January 5,1982
- 4. Will refueling or resumption of operation thereafter require a technical specification change or other licensed amendment?
Resumption of operation after refueling will require changes to Technical Specifications. The changes will be such as to allow operation of the plant with a fresh reload batch and reshuffled core.
- 5. Scheduled date(s) for submitting proposed licensing action and supporting information.
October 4,1982
- 6. Important licensing considerations associated with refueling.
Reload fuel will be similar to that reload fuel inserted in the previous cycle.
- 7. The number of fuel assemblies (a) in the core and (b) in the Spent Fuel Storage Pool.
1 (a) 217 (b) 656 Spent Fuel Pool is common to Units 1 and 2.
- 8. The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been required or is planned, in number of fuel assemblies.
1830 Licensed 1358 Currently Installed
- 9. The projected date of the last refueling that can be discharged to the Spent Fuel Pool assuming the present licensed capacity and maintaining space for one full core off load.
April,1991
- Information changed since last report.
SilMMARY OF IJNIT I OPER ATING EXPERIENCE - JtJNE 1982 6/1 At the beginning of this reporting period Unit I was shutdown for its 5th scheduled refueling outage.
6/25 Completed filling the Reactor Coolant System at 2300.
6/29 Reactor Coolant System heatup was completed at 0900.
6/30 The reactor was brought critical at 2116. Commenced low power physics testing. At the end of this reporting period Unit I was critical with low power physics testing in progress.
l
SUMMARY
OF UNIT 2 OPERATING EXPERIENCE - JUNE 1982 6/1 At the beginning of this reporting period Unit 2 was operating at 875 M've with the reactor at 100% power.
6/2 At 1130 Control Element Assembly (CEA) 64 dropped into the core. Reactor power was immediately reduced to less than 70% in accordance with the Technical Specifications. CEA 64 was withdrawn back to its group at 1257.
Load had been increased to 655 MWe at 1437 when CEA 64 again dropped into the core. Reactor power was immediately reduced to 70%. CEA 64 was S withdrawn back to its group at 1530. Load was increased to capacity (865 MWe) at 1900, 6/3 At 0800 load was decreased to 830 MWe, due to Axial Shape Index swings caused by the dropped CEA's. Resumed full load operation (860 MWe) at 1200.
6/5 Decreased load to 700 MWe at 0100 to clean main condenser water boxes.
Resumed full load operation (880 MWe) at 1800.
6/6 Decreased load to 750 MWe at 0600 for Travelling Screen maintenance. Load was increased to capacity (880 MWe) at 1722.
6/7 At 2100 load was reduced to 750 MWe to investigate saltwater leakage into the main condenser. Af ter plugging I condenser tube resumed full load operation (865 MWe) at 1340.
6/10 At 1000 loed was reduced to 730 MWe to investigate saltwater leakage into the main condenser. Load was increased to 865 MWe at 1500 when indications of saltwater leakay,e disappeared.
6/12 At 0125 load was reduced to 740 MWe to investigate saltwater leakage into the main condenser. Increased load to capac?ty (870 MWe) at 2300 af ter plugging 3 condense" tubes.
SUMMARY
OF UNIT 2 OPER ATING EXPERIENCE - JUNE 1982 CONTINUED 6/13 At 0200 load was reduced to 780 MWe to investigate saltwater leakage into the main condenser. Located and plugged 3 leaking condenser tubes at 0630. Load had been increased to 820 MWe at 1045 when indications of saltwater leakage into the main condenser returned. Load was decreased to 760 MWe at 1200 to investigate. After plugging 3 condenser tubes resumed full load operation (870 MWe) at 2100.
6/16 At 0645 load was reduced to 740 MWe to investigate saltwater leakage into the main condenser. Load was increased to 870 MWe at 1300 when indications of saltwater leakage disappeared.
6/17 At 2l00 load was reduced to 720 MWe to investigate saltwater leakage into the main condenser.
6/19 increased load to capacity (875 MWe) at 1730 after plugging 2 condenser tubes.
6/20 Decreased load to 715 MWe at 0115 to clean main condenser water boxes.
Completed water box cleaning at 0600 but remained at reduced load to investigate saltwater leakage into the main condenser. Load was increased to 870 MWe at 1400 when indications of saltwater leakage disappeared.
6/21 At 0400 load was reduced to 720 MWe to investigate saltwater leakage into the main condenser. After plugging I condenser tube resumed full load operation (860 MWe) at 2200.
6/22 At 0100 load was reduced to 735 MWe to investigate saltwater leakage into the main condenser. Increased load to capacity (865 MWe) at 0950 af ter plugging I condenser tube.
6/24 Decreased load to 700 MWe at 0400 to clean main condenser water boxes.
Resumed full load operation (365 MWe) at 0830.
I t
9 I
4
SUMMARY
OF UNIT 2 OPERATING EXPERIENCE - JUNE 1982 CONTINUED 6/27 Decreased load to 720 MWe at 0730 for travelling screen replacement. Load was increased to capacity (865 MWe) at 2100.
I 6/30 At the e.nd of this reporting period Unit 2 was operating at 860 MWe with the reactor at 100% power.
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