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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARBSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 BSEP-98-0055, Monthly Operating Repts for Feb 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-98-0038, Monthly Operating Repts for Jan 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-98-0007, Monthly Operating Repts for Dec 1997 for Brunswick Steam Electric Plant,Unit 1 & 21997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Brunswick Steam Electric Plant,Unit 1 & 2 BSEP-97-0528, Monthly Operating Repts for Nov 1997 for Brunswick Steam Electric Plant,Units 1 & 21997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-97-0500, Monthly Operating Repts for Oct 1997 for Brunswick Steam Electric Plant,Units 1 & 21997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-97-0456, Monthly Operating Repts for Sept 1997 for Brunswick Steam Electric Plant1997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Brunswick Steam Electric Plant BSEP-97-0410, Monthly Operating Repts for Aug 1997 for Bsep,Units 1 & 21997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for Bsep,Units 1 & 2 BSEP-97-0373, Monthly Operating Repts for Jul 1997 for Brunswick Steam Electric Plant,Units 1 & 21997-07-31031 July 1997 Monthly Operating Repts for Jul 1997 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-97-0323, Monthly Operating Repts for June 1997 for Brunswick Steam Electric Plant,Units 1 & 21997-06-30030 June 1997 Monthly Operating Repts for June 1997 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-97-0266, Monthly Operating Repts for May 1997 for Brunswick Steam Electric Plant Units 1 & 21997-05-31031 May 1997 Monthly Operating Repts for May 1997 for Brunswick Steam Electric Plant Units 1 & 2 BSEP-97-0219, Monthly Operating Repts for Apr 1997 for Brunswick Steam Electric Plant,Units 1 & 21997-04-30030 April 1997 Monthly Operating Repts for Apr 1997 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-97-0142, Monthly Operating Repts for March 1997 for Bsep,Units 1 & 21997-03-31031 March 1997 Monthly Operating Repts for March 1997 for Bsep,Units 1 & 2 BSEP-97-0105, Monthly Operating Repts for Feb 1997 for Bsep,Units 1 & 21997-02-28028 February 1997 Monthly Operating Repts for Feb 1997 for Bsep,Units 1 & 2 BSEP-97-0055, Monthly Operating Repts for Jan 1997 for Brunswick Steam Electric Plant Units 1 & 21997-01-31031 January 1997 Monthly Operating Repts for Jan 1997 for Brunswick Steam Electric Plant Units 1 & 2 ML20138H7881996-12-31031 December 1996 Corrected Monthly Operating Rept for Dec 1996 for Brunswick Unit 1 BSEP-97-0015, Monthly Operating Repts for Dec 1996 for Brunswick Steam Electric Plant Units 1 & 21996-12-31031 December 1996 Monthly Operating Repts for Dec 1996 for Brunswick Steam Electric Plant Units 1 & 2 BSEP-96-0451, Monthly Operating Repts for Nov 1996 for Brunswick Steam Electric Plant,Units 1 & 21996-11-30030 November 1996 Monthly Operating Repts for Nov 1996 for Brunswick Steam Electric Plant,Units 1 & 2 ML20138H7821996-11-30030 November 1996 Corrected Monthly Operating Rept for Nov 1996 for Brunswick Unit 1 BSEP-96-0422, Monthly Operating Repts for Oct 1996 for Brunswick Steam Electric Plant,Units 1 & 21996-10-31031 October 1996 Monthly Operating Repts for Oct 1996 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-96-0375, Monthly Operating Repts for Sept 1996 for Brunswick Steam Electric Plant Unit 1 & 21996-09-30030 September 1996 Monthly Operating Repts for Sept 1996 for Brunswick Steam Electric Plant Unit 1 & 2 BSEP-96-0330, Monthly Operating Repts for Aug 1996 for Brunswick Steam Electric Plant,Units 1 & 21996-08-31031 August 1996 Monthly Operating Repts for Aug 1996 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-96-0295, Monthly Operating Repts for July 1996 for Brunswick Steam Electric Plant,Units 1 & 21996-07-31031 July 1996 Monthly Operating Repts for July 1996 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-96-0253, Monthly Operating Repts for June 1996 for Brunswick Steam Electric Plant Units 1 & 21996-06-30030 June 1996 Monthly Operating Repts for June 1996 for Brunswick Steam Electric Plant Units 1 & 2 BSEP-96-0236, Monthly Operating Repts for May 1996 for Brunswick Steam Electric Plant Units 1 & 21996-05-31031 May 1996 Monthly Operating Repts for May 1996 for Brunswick Steam Electric Plant Units 1 & 2 BSEP-96-0204, Monthly Operating Repts for April 1996 for BSEP1996-04-30030 April 1996 Monthly Operating Repts for April 1996 for BSEP BSEP-96-0146, Monthly Operating Repts for Mar 1996 for Brunswick Steam Electric Plant,Units 1 & 21996-03-31031 March 1996 Monthly Operating Repts for Mar 1996 for Brunswick Steam Electric Plant,Units 1 & 2 BSEP-96-0097, Monthly Operating Repts for Feb 1996 for BSEP1996-02-29029 February 1996 Monthly Operating Repts for Feb 1996 for BSEP BSEP-96-0053, Monthly Operating Repts for Jan 1996 for BSEP Units 1 & 21996-01-31031 January 1996 Monthly Operating Repts for Jan 1996 for BSEP Units 1 & 2 BSEP-96-0008, Monthly Operating Repts for Dec 1995 for Brunswick Steam Electric Plant1995-12-31031 December 1995 Monthly Operating Repts for Dec 1995 for Brunswick Steam Electric Plant 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 BSEP-98-0185, Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20151T5021998-08-0505 August 1998 Project Implementation Plan, Ngg Yr 2000 Readiness Program, Rev 2 BSEP-98-0164, Monthly Operating Repts for July 1998 for BSEP Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for BSEP Units 1 & 2 ML20236T1961998-07-0101 July 1998 Rev 1 to 2B21-0088, Brunswick Unit 2,Cycle 13 Colr ML20236T1921998-07-0101 July 1998 Rev 1 to 1B21-0537, Brunswick Unit 1,Cycle 12 Colr BSEP-98-0142, Monthly Operating Repts for June 1998 for BSEP Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for BSEP Units 1 & 2 ML20236T1971998-06-30030 June 1998 Rev 2 to 24A5412, Supplemental Reload Licensing Rept for Brunswick Steam Electric Plant Unit 2 Reload 12 Cycle 13 ML20249B9691998-06-11011 June 1998 Rev 1 to VC44.F02, Brunswick Steam Electric Plant,Units 1 & 2,ECCS Suction Strainers Replacement Project,Nrc Bulletin 96-003 Final Rept BSEP-98-0129, Monthly Operating Repts for May 1998 for Bsep,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Bsep,Units 1 & 2 ML20151S9041998-05-31031 May 1998 Revised Pages to Monthly Operating Rept for May 1998 for Brunswick Steam Electric Plant,Unit 1 BSEP-98-0104, Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Brunswick Steam Electric Plant,Units 1 & 2 ML20151S8991998-04-30030 April 1998 Revised Pages to Monthly Operating Rept for Apr 1998 for Brunswick Steam Electric Plant,Unit 1 ML20247N7501998-04-30030 April 1998 Rev 0 to BSEP Unit 1,Cycle 12 Colr ML20247N7721998-04-30030 April 1998 Rev 0 to J1103244SRLR, Supplemental Reload Licensing Rept for BSEP Unit 1,Reload 11,Cycle 12 ML20217K8461998-04-24024 April 1998 Safety Evaluation Approving Proposed Use of Code Case N-535 at Brunswick Unit 1 During Second 10-yr Interval,Pursuant to 10CFR50.55a(a)(3)(i).Authorizes Use of Code Case N-535 Until Code Case Included in Future Rev of RG 1.147 ML20217K3941998-04-24024 April 1998 SER Approving Relief Request for Pump Vibration Monitoring, Brunswick Steam Electric Plant,Units 1 & 2 ML20217E6841998-04-23023 April 1998 Safety Evaluation Accepting Code Case N-547, Alternative Exam Requirements for Pressure Retaining Bolting of CRD Housings ML20217E7471998-04-21021 April 1998 Safety Evaluation Accepting Alternative to Insp of Reactor Pressure Vessel Circumferential Welds ML20217B5241998-04-20020 April 1998 SE Accepting Licensee Request for Approval to Use Alternative Exam Requirement for Brunswick,Unit 1,reactor Vessel Stud & Bushing During Second 10-yr ISI Interval Per 10CFR50.55a(a)(3)(ii) BSEP-98-0080, Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 21998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Bsep,Units 1 & 2 ML20216B1041998-03-0404 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Brunswick Steam Electric Plant, Unit 1 1999-09-30
[Table view] |
Text
-
l V l l
l l
l D?Eii ATI:!G DATA REP 0f;T l l
DOCKET NO. 091-0325 l nATE 12/n5/7-C0hPLETEr) ny EULIS ILLI c TELEPHO:;E 919-457-6701 OPERATI'IU STATUS
- l. U.11 T S A"E r 3RUl!SP!ICK UNIT 1 I >!nTES I
- 2. REP 0iiTI!!U PERIOD: 93VEMBEI? 76 I I
- 3. LICE:! SED THE RI.!AL PO'9ER ( lU"T ) : 2435 I I 4 .! A."EPL ATE RAIII'O ( GR OS S ,D'E ) : 867.0 I I S. DES I D:t ELECTi?IC AL R ATI NG ('IET 'dP!E) : b2I.O I I
- 5. ...AX TTEPENDADLE C APACITY (GRDSS P!E): 315.0 I I
- 7. AX DEPE.'IDAjLE C AP ACITY (:lET O!E ): 790.0 - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
- d. IF C :A'.'JES GCCUR I!' CAPACITY HTI'!G9 (ITEIS 3 THPU 7) SI'CC LAST 4:r>DRT, biVE .iASODS:
V. P3,'ER LEVEL TO MHICH deers!CTED IF AW( ( 1ET U'J!E ) : '!J' E
- 10. REA50,1S FJE RESTRICTIUM IF AJY:
CU UL THIS YR TO VONTH D iTE ATIVE
- 11. :UURS l'l PEPORTING PERIDU 720.0 8914.0 14v53.^
- 12. '!J.mER JF h0URS REACTOR P'A9 CRITICAL 667.3 711/.6 1 15 56. '>
- 13. REAUTOR RESERVE SHUTJU"'.4 HOURS -
0.0 0.0 1647.I 14 ii]UdS DE!iER ATnn U:1 LINE 621.1 6tw .6 loo 75.m 15 . UlIT RESERVE ShUTu0*l.! HDU7S 0.1 c. 0 0.'
Id. U30SS THEh:AL E!:ERGY GE'!ERATED (,WH) In61045.2 15nn039I.4 22Vi1217.o
- 17. GRUSS ELECTi;ICAL E'!ERGY GEliERATED (W"!) 347265.0 4971551.0 7593b47.1 lo. NET ELECTRICI AL Eh'ER3Y GE'IER ATED (l!.'."H) 334140.0 4799253.0 7315042.0
- 19. U'!II SERVICE F ACTOR 86.3 65.9 72.3
- 20. UNIT AVAILABILITY FACTOR e6.3 35.9 72.3
- 21. U:ili C AP ACITY FACTO 7 (USI?l0 PDC tiET) 56.7 75.6 61.9
- 22. U!!IT CAPACITY FACTOR (USING DER 'fET) 56.5 72.9 59.6
- 23. U?IT FC7CEu OUTAGE 7 ATE 7.0 10.0 24.c 24 SHUrDJ "fS SCHEDULE 9 DVER ?! EXT 5 '0::TH3 (TYPE, DATE, AlD DU" ATIT GF E ACH)-
Refueling 79,01,13 1656.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br />
- 26. IF ShuTJ3"'; AT Ei!D JF REP 07T PERI 1U, ESTI"ATEn DATE 0.: STADT UP: n/ n/ 0
- 26. U-IIiC I'! TEST STATUS (PRIDD TO C0'mERICIAL DPERATIO1): FOT W .c. , I V E P l
l I !ITI AL CrITICALITl - - - - - - - - --------
l
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APPEDIX E
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uAt AVG. DAILi 'i>OhE7 LEVEL DAY AVG. DAILY P31-lED LEVEL
,: = 4 )
( , ,,. .. :
. 3 7 ..1_ ) (;,4,.,. =
I 790. 17 345.
2 435 16 ".
. .%. 1. I9 n.
J 7ba. 20 165. ,
O 503. 21 349, 6 647. 22 353 7 7e6. 23 357.
t 7c5. 24 242.
767. 540.
V 25 10 705. 26 58'.
11 212. 27 e 12.
12 7]. 2d 5n6 13 607. 29 567.
14 4E7. 33 575, 15 397. >
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 050-0325 ,.
UNIT NAME Brimnwick No. 1 DATE December 4, 1978 COMPLETEiJ gy Eults A. Willis REPORT MONTH .Hoyombar 1978 TELEPHONE (919) 457-6701 1 - E E
, ,{g 3 j .y] Licensee h in. Cause & Corrective a No .' Date H
& Eg s j g@ Event gg gu3 Action to yI E Report # mO j ;g g g Prevent Recurrence 6
1
, 035 781102 F 18.1 G 3 N/A MB INSTRU- I&C technician replacing steam jet
., air ejector switch 1-0G-TIS-2752 with jumper installed. Screwdriver slipped, blowing the control power fuse. SJAE inlet valves shut and -
could not be recet. Reector scrammed when turbine control valve fast
, closure resulted from loss of conden-ser vacuum.
- l. The events leading to the scram will. be reviewed in training classes for all I&C technicians.
- 2. An EWR will be submitted for engineering to determine the
' feasibility'of installing separate control power fuses on the SJAE's.
I 2 3 4 F: Forced Reason: Method: Exhibit G-Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data
, B Maintenance of Test . 2-Manua! Scram. Entry Sheets for 1.icensee C-Refueling 3-Automatic Scram. Event Report (LER) File (NURLG-
- D-Regulatory Restriction 4-Other (Explain) 0161)
E-Operatur Training & License Examination F-Administrative 5-G-Operational Error (Explain) Exhibit I - Same Source (9/77) Il-Other (Explain)
__ _ _ _ _ _ _ _ _ _ _ . -.2_* *_ _ _ . .- _ wi + ---*-ase'+ aW - W w 2 ----e a_. -PT- -
se
^
.~~.
. m UNIT SHUTDOWNS AND POWER REDUCTIONS ' DOCKET NO. 050-0325 .
UNIT NAME Brunswicit No. 1 DATE no, hor A_ io7g COMPLETED By Eulis A. Willis REPORT MONT11 November 1978 TELEPilONE (919) 457-6701 e
+ -
E E
'g
.! E '3 $ .! 5 Licensee ,Eg j*t Cause & Corrective +
{ No. Date ]g s ,@ j $ Event g po - Action to 4
8-f5 5 2t 6; ;g:
Report # mO o
o Prevent Recurrence 6
036 781111 F 28.3 H 3 N/A 'HB ZZZZZZ Separated unit from grid due to high i
reactor vessel conductivity. Re actor scrammed due to level control problem f Reactor vessel conductivity was .
1 corrected and unit returned to i service. . Reactor' vessel conductivity l was caused by MSR control system
- l. being unstable. The system was
- . placed in menual control and-l stabilized.
i t
4 4
i 1- .
i i 1 2 3 4 F: Forced ' Reason: Methed: Exhibit G-Instructiims S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance of Test .
2-Manual Scram.- Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (LER) File (NURLG-D-Regula:ory Restriction 4-Other (Explain) 0161)
- E-Operator Training & License Examination j- F-Administrative 5 i G-Operational Error (Explain) Exhibit I - Same Source t
19/77) Il-Other (Explain) i a
- _ , . ._ _ - , . , . , - _ . . _ _ _ . - . - - . . . . ~ . _ - . , ~ . - ~ . - . . ~ . _ - - . . - - - , , - - - - - . , . . - . . . - . -
- - , _ , . . _ . . , . . . , . _ . . . . _ , - - - _ - - - _ - _ . . - . ~ . - - - . . , , .
, m m Page 1 of 2 i
UNIT SIIUTDOWNS AND POWER REDUCTIONS DOCKET NO. 050-0325 ,
' UNIT NAME Brunswick No. .1 1 DAT E December 4. 1978 REPORT MONTII November 1978 COMPLETED BY Eulis A. Willis TELEPilONE (919) 457-6701 i
n.
- B E No. Date
- , .$ ? 3g $Y5 Licensee ,E% {% Cause & Corrective e g- g Ej _g g 5 Event ' gi o-3 Action to H $ I., E 3 ;g F Report # to u $U Prevent Recurrence o
1 a g O
i -
037 781117 S 52 5 B 3 N/A CB PIPEXX Power level uas being reduced to 3 . separate from the grid to begin a .
planned outage to reinspect 4 1
recirculating system nozzle safe-end's. While descending in power, a stator cooling runback periodic -
test was performed on the unit tur-bine/ generator. The runback failed to stop at the low power stop and the reactor scrammed on high pressure when the bypass valve capacity was exceeded. The nozzle safe-ends were inspected and no changes in previous-ly identified indications were found.
(1) The stator cooling runback limiter will be repaired during the upcoming Unit No. I refueling outage.
. (2) The recirculating nozzle safe-(Cont'd.on Page Z of Z)
I 2 3 4 F: Forced Reason: '
Method: Exhibit G -Instructions S: Scheduled A-Equipment Failure (Explain) I-Manual for Preparation of Data i B-Maintenance of Test 2-Manual Scram. Entr> Sheets for Licensee C-Refocling 3 Automatic Scram. Event Report (LER) File (NUREG-D-Regulatory kestriction 4-Other (Explain) 0161)
E-Operator Training & License Examination F Administrative 5 G. Operational Error (Explain) Exhibit I - Same Source p7/77) Il-Other (Explain)
_ _ - . _ ~. -
./ 3 ,
. Page 2 of 2 ,
UNITSIIUTDOWNS kND POWER RE')UCTIONS DOCKET NO. 050-0325 UNIT NAME Brunswicit No. I DATE Daca=har 4- 1978
~
N ovember 1978 COMPLETED BY Eulis A. Willis REPORrMONT11 TELEPiiONE (919) 457-6701 e.
c
--, jE 3 E5 ' Licensee ,E-r, h Cause & Corrective No. Date i 3g 4 } s'5
.2 Event g3 o-3 Action to -
t-fE E y ;5 ::
<. f Report n in O !O u
Prevent Recurrence 6
037 781117 S 52.5 B . 3 N/A ' CB 'PIPEXX '(cont'd) ends wilI be inspected during the *
. upcoming Unit No. I refueling outage to determine if there have been any changes in indications which were-
I 2 3 . 4 F: Forced Reason: Method: Exhibit G -Instructions S: Scheduled A.1:quipment Failure (Explain) 1-Manual for Preparation of Data .;
B. Maintenance or Test 2-Manual Scram. Entry Shecis for Licensee C-Refuel;ng 3-Automatic Scram. Event Report (LER) File (NUREG-D. Regulatory Restriction ..
4-Other (Explain) 0161)
E-Operator Training & License Examination F-Administrative i 5 G-Operational Error (lixplain) ;e Exhibit I- S,ame Source l'8/77) II-Oiher (Explain)
l APPENDIX ]
i DOCKET NO. 050-0325 UNIT Brunswick No. 1 DATE December 5. 1978 l COMPLETED BY Eulis A. Willis 1 BRUNSWICK NO. 1 Availability factor for Brunswick Unit No. I was 86.3% for November, with 1 three shutdowns lasting a total of 98.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> occurring this month: ,
P November 2: A technician error while replacing steam jet air ejector switch 1-0G-TIS-2752 caused a reactor scram. The unit was down for 18.1 bours.
November 11: The unit was separated from the grid due to high reactor vessel -
conductivity. The conductivity was caused by MSR control system being unstable. "Down time" 28 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> November 17: Power was being reduced to separate from the grid to begin a planned outage to reinspect 4 recirculating system nozzle safe ends, when the reactor scrammed due to stator cooling runback limiter problems. "Down time" 52.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
Capacity factor was limited to 58.7% because of load following as per the dispatchers request, high reactor vessel conductivity and " preconditioning" the fuel, i
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OPERATING DATA REPORT DOCKET'NO. 057-0324 DATE I2/01/7.>
CDP.PLETED BY EULIS '?ILLIS TELEPHONE 919-457-6701 OPERATI NG STATUS
- 1. UNIT IAME: BRUliSI'.'ICK UNIT 2 I NOTES I
- 2. REPORTING PERIOD: NOVEMBER 76 I I
- 3. LICENSED THERMAL PO3!ER (#MT): 2435 I I:
- 4. NAiiEPLATE RATING (GROSS JP!E) * 'S67.0 I I
- 6. DESIGN ELECTRICAL RATING-(NET '4WE): 821.0. I I
- 6. MAX DEPENDABLE CAPACITY (GROSS MNE): 615.0 I- I
- 7. hAX DEPENDADLE CAPACITY (NET Mt1E ): 790.0 - - - - - - - - - - - - - - - - - - - - - - - - - - - -
- s. IF CHA1GES OCCUR IN CAPACITY R ATINGS (ITEl.iS 3' THRU 7) SIUCE LAST 9:PD7T, GIVE REASOUSi
- 9. PJ'dR LEVEL TO WHICH RESTRICTED IF ANY ( NET MPlE) * . NONE
- 10. REASONS FOR RESTRICTION IF ANY:
THIS YP TO CUdUL -
MONTH DATE ATIVE-
- 11. HJURS IN REPORTING PERIOD 720.0 8016.0 26977.0
- 12. NURSER OF HOURS REACTOP PAS CRITICAL 531.4 657c.5 13545.4
- 13. RE^ ACTOR RESERVE SHUTDOWN HOURS 0.0 3.0 0.0
- 14. HOURS GENERATOR D': LIHE 514.5 6285.0 17392.0
- 15. UNIT RESERVE SHUTDO'!N HOURS 0.0 0.0 0. 0
- 16. GROSS THERMAL E!.' ERG ( GEiERATED (MWH) 939249.0 13137233.2 39358992.9
- 17. GROSS ELECTRICAL ENER'iY G NERATED (Mv!H) 315333.0 4427232.0 10275292.0 ,
- 16. NET ELECTRICI AL ENERGY GENERATED (WlH) 303056.0 4271073.0' 9864856.0' r
- 19. UNIT SERVICE FACTOR 71.5 70.4 54.5:
- 20. UNIT AVAILABILITY FACTOR 71.5 7s.4 $3.5
- 21. U'IIT CAP ACIT( FACTOR (USING "DC NET) 53.3 67.4 e6.3
- 22. UNIT CAPACITY FACTOR (USING DER HET) 51'.3 64.-9 da.5
- 23. U'MT FORCED OUTAGE R ATE 28.5 9.6 15.6 r 24 SHUTDTINS SCHEDULED DVER NEXT 6 HONTHS (TYPE, DATE, AND DUDATION-D.: EA.CH):
Refueling 79,02,18 1488.0 hour0 days <br />0 hours <br />0 weeks <br />0 months <br />s-Modification- 78,12,23 48.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> (78-269) 25.'IF SHUTOOMU AT END OF REPORT PERIOD, ESTI: FATED DATE OF START UP: I2/ I/71 '
- 26. U:iITS I:1 TEST STATUS (PRIOR TO C0!ZERICIAL OPERATION): ForAST ACHEIVED IRITIAL CRITICALITY - - - - - - - - - - - - - -
IUITI AL ELECTRICITi -------- -------- i
'CO LERICIAL OPERATION -------- - - - - - - -
1.16 - 9 ,
. _ , - . . _ . . . - -_.u._..._._ -._ .. ..-.-_.- _ _.....--.-.._ _. _ . _ _._ , _ . _ . _ - _ , _ . . . _ - _.
APPENDIX B AVERAGE DAILY PO!';ER LEVEL DOCKET NO. 050-0324 UiIIT nR'Jt!S'?ICK UN'IT 2 DATE 12/01/70 COMPLETED BY EULIS "'ILLIS TELEPHO'JE 91v-457-67ni dQVEi?ER To vAY AVG. DAILY POWER LEVEL DAY AVG. DAILY P011ER LEVEL (MNE-NET) ( Ml'!E-!!ET )
1 794. 17 283.
2 79I. 18 335.
3 7b6. 19 -449.
4 3c6. 20 504.
5 699 21 545.
6 441. 22 573.
7 0. 23 623.
6 0. 24 666.
9 0. 25 770 10 0. 25 707.
1i 0. 27 775.
12 0. 2d 770.
13 c. 29 .771.
14 93. 33 363.
15 302.
16 272.
1.16 - 8
.~. . m . n i -
!. 050-0324 UNITSifUTDOWNS AND POWER REDUCTIONS - DOCKET NO. .
~- -
i UNIT NAME Brunswick No. 2 ,
DATE December 4. 1978 REPORT MONT11 November 1978 COMPLETED BY _Eulis A. Willis l; .
TELEPlf0NE (919) 457-6701 "c.
.5 E 3g Y Licensee E-t b Cause & Currective --i No. Date h 3g ;g g & Event E5 8.% '8 Action to gu H 5 5 Report # t#G e di g c$ 5 Prevent Recurrence
. 0 t o 4 031 781106- F 193.0 A 3 N/A EB ELECON A broken shield cable caused phase to .-'
l' phase short on. the Delco West 230 KV transmission line causing severe trans-i mission system instability. The-
, instability caused a generator lockout 4 on loes of excitation resulting in a- -
, turbine. trip and a reactor scram.
liechanical seals.were damaged on both reactor recirculating pumps.
I ,
An investigation was performed by the r c) 4 generator manufacturer.(General ~Electri
' to determine if the exciter controls failed to perform as required in re-sponse to the transient. The results t- of the investigation are pending the manufacturer's review. An investigation is being performed 'by Transmission 4
Substation Maintenance Service to deter ruine '
j d.ct cacccd the tc;;._ission instability'
- y y and correctgi ve action. Mechanical seals ,
i F: Forced Reason: Method: on the reacto1EnMei Cifd#Akiq3nPumps E .were
- 5: Scheduled A-Equipment Failure (Explain) 14tanual replaced. . for Preparation of Data B-Maintenance of Test .
2-Manual Scram. Entry Shuts for Licensee ,
4 C-Refueling 3-Automatic Scram. Escent ReporI (LERI File iNUREG. -
1 D-Regulatory Restriction 4-Other (Explain) 0161) r
. E-Operator Training & License Examination t 4
F-Administrative 5
, G. Operational Error (Explain) Eihibit 1 - Same Source
- t9/77) II-Othes (Explain)
I ,
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.e---geWq- amr saw a .-w-p- s -e->" **y ow,-w g- -e-r g wwgv-ww w*rg er W7 Mmmm+-r-.eeeq- y+yw--,w,%-va we+a-13 rew,-- --rv e wcy--wrw, ,.-m-e w wowi+ y me.- 1 m-wwr-*vrd -'- --- vv--
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050-0324 UNIT SIIU11) OWNS AND POWER REDUCTIONS DOCKET NO. ,
UNIT N AME Brunswick No. 2 DATE December 4. 1978 REPORTMONT1f _ November 1978 COMPLETED BY Eulis A. Willis TELEPIIONE (919) 457-6701
- E c
-o $E 3 $ .Y 5 Licensee ,E t, jn. Cause & Corrective s No. Date g g Ej $ jgE Event y Q Action to E
$E $ 5g= Report # mV $U Prevent Recurrence f
O u
032 781130 F 12.5 G 3 N/A CII INSTRU Reactor scram on reactor low level while technician working on recorder C32-R006 (Total Steam Flow). Record-er was pegged high. When lead to recorder was lifted,.the 3 element level control loop was interrupted, -
the feed pump level control s~aw zero and ran the feed pumps back. Level dropped to scram set point.
(Continued Next Month) 4
, t 2 3 4 F: Forced Reason: Method: Exhibit G-Instructions S: Scheduled A-Equipment Failure (Explain) 14tanual for P eparation of Data B Maintenance of Test ,
2-Manual Scram. Entry Sheets for Licensee C-Refueling 3-Automatic Scram. Event Report (LERI File (NUREG.
D-Regulatory Restriction 4-Other (Explain) 01611 E-Operator Training & l_icense Examination F Administrative 5 G-Operational Error (Explain) Exhibit I - Same Source (9/77) 1I-Other (Explain) l
APPENDIX DOCKET NO. 050-0324 I UNIT Brunswick No. 2 DATE December 5, 1978 COMPLETED BY Eulis A. Willis BRUNSWICK NO. 2 Capacity factor for Brunswick Unit No. 2 was 53.3% for the month of November because of high reactor vessel conductivity, " preconditioning" the fuel, two forced outages, and " load following" near the end of the month. Total "down time" for the month was 205.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />s:
November 6: A broken shield cable caused a generator lockout which caused a turbine trip and a reactor scram. Mechanical seals on both reactor recirculating pumps were damaged. The unit was.down for 193 hours0.00223 days <br />0.0536 hours <br />3.191138e-4 weeks <br />7.34365e-5 months <br />.
November 30: A technician error caused a reactor scram which lasted through the end of the report period (12.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />). Unit back on-line 12-1-78. 7 Brunswick Unit No. 2 availability factor for the month of November 71.5%. For ,
, further explanation of outages, see the unit shutdowns and power reductions log (Appendix D) for the month of November.
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