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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20090C4331975-12-29029 December 1975 AO-75-09:on 751123-29,licensee Failed to Analyze Stack Cartridges Weekly.Technician Reinstructed ML20090C4551975-11-28028 November 1975 AO-75-032:on 751117,acid Leak Occurred in Makeup Demineralizer Acid Storage Tank.Caused by Partially Open Discharge Valve.Valve Repaired ML20090C4491975-11-26026 November 1975 AO-75-031:on 751114,both Radiation Monitors in Reactor Bldg Ventilation Duct Failed to Provide Transfer to Emergency Ventilation Sys at 5 M/H.Caused by Incorrect Adjustment Made Prior to Calibr ML20090D8901975-08-29029 August 1975 AO 50-220/75-23:on 750826,during Audit of Contractor Facility Used in Analyzing Milk Samples,Required Sensitivity Not Achieved.Caused by Inadequate Procedure.Contractor Informed That Milk Counting Time Must Increase ML20090E0411975-04-0202 April 1975 AO 50-220/75-05:on 750401,during Routine Surveillance Testing,Emergency Vent Sys Failed to Function When Sys Inlet Ventilation Valve Bv 202-36 Failed to Open.Caused by Broken Stem in Solenoid Valve.Solenoids Will Be Replaced ML20090E1581975-01-0606 January 1975 AO 50-220/74-17:on 741227,source Range Monitor 14 Declared Inoperable.Caused by Component Failure.Detector Replaced W/Spare ML20090E1611974-12-19019 December 1974 AO 50-220/74-16:on 741210,intermediate Range Monitor 12 Found Inoperable.Cause Apparently Due to Defect in Cable or Detection.Repair Will Be Conducted on Sys ML20090E1631974-12-17017 December 1974 AO 50-220/74-15:during Markup of Motor Generator 167, Operator Tripped Supply Breaker for Power Board.Caused by Operator Error.Operator Educated in Proper Procedures. Training Sessions for All Operators Conducted ML20090E1591974-12-10010 December 1974 Ao:On 741110,fuel Channel Deflections Indicated Increase in Core Bypass Flow Over Calculations Assumed in Original Design.Channels Will Be Replaced.Finger Springs Will Be Used to Control Leakage ML20090E1651974-11-27027 November 1974 AO 50-220/74-14:on 741120,during Mgt Review of Monthly Surveillance Tests,Station Batteries Found Not Tested at Specified Intervals.Caused by Misinterpretation of Requirements by Maint Foreman.Foreman Notified ML20090E1661974-09-20020 September 1974 AO 74-13:on 740918,during Routine Testing,Containment Spray Pump Found Inoperable.Caused by Foreign Object Restricting Suction Flow of Pump.Object Removed ML20090E1681974-08-28028 August 1974 AO 50-220/74-12:on 740824,during Surveillance Testing,One Barton Instrument Used in Drywell High Pressure Reactor Protection Sys Drifted High.Caused by Setpoint Drift. Switch Recalibr ML20090E1701974-08-21021 August 1974 AO 74-10:on 740817,during Routine Surveillance Testing, Barton Differential Pressure Instrument 1 B05C (Emergency Cooling High Flow) Tripped at Lower than Required Value. Caused by Setpoint Drift ML20090E1731974-07-0101 July 1974 AO 74-9:on 740628,during Restart,Reactor Protection Sys Relay RE-230 Failed.Caused by Open Relay Coil.Relay Replaced ML20090E1751974-06-0303 June 1974 AO 50-220/74-8:on 740531,setpoint on Barton Instruments Used in Drywell High Pressure Reactor Protection Sys Drifted Higher than Required.Barton Switch Recalibr ML20090E1771974-05-0303 May 1974 AO 50-220/74-7:on 740425,eddy Current Testing Evaluation Showed Two Control Rod Blades W/Possible Inverted Tubes. Caused by Mfg Deficiency.Two Control Blades Will Be Changed ML20090E1791974-04-29029 April 1974 AO 50-220/74-6:during Releak Testing,Msiv Leaked Excessively.Cause Unknown & Being Investigated.Valve Will Be Inspected ML20090E1801974-04-24024 April 1974 AO 74-5:on 740415,during Annual Refueling Shutdown Testing, Three High Temp Main Steam Line Tunnel Sensors Found to Actuate at Lower than Required Temp.Caused by Setpoint Drift on Sensor.Sensors Recalibr ML20090E1831974-04-11011 April 1974 AO 50-220/74-4:on 740402,during Refueling Outage Test,Low Condenser Vacuum Sensors Actuated Low Resulting in Reactor Scram.Caused by Switch Setpoint Drift.Sensor Switch Recalibr ML20090E1841974-04-0909 April 1974 AO 50-220/74-3:on 740402,both Inside MSIVs Failed to Meet Required Limit of 12.9 Std Cubic Ft Per Inch.Caused by Drift in Position Switch on Valve Controller.Valves Will Be Repaired & Retested ML20090E1871974-04-0202 April 1974 AO 50-220/74-3:on 740402,during Leak Testing,Both Inside MSIVs Exceeded Leakage Limit.Caused by Either Drifting Position Switch or Improper Seating of Disc.Investigation Continuing.Position Switch Will Be Readjusted ML20090E1941974-04-0101 April 1974 AO 50-220/74-2:on 740323,concentrator Steam Seeped Through Insulation Surrounding 12-inch Section of Pipe Leading from Side Arm Heater to Concentrator Bottom.Caused by Improper Installation.Pipe Will Be Replaced ML20090E2051974-03-25025 March 1974 AO 50-220/74-2:on 740323,during Routine Concentrator Steam Operation,Pipe Crack Found in Waste Concentrator Piping Leading from Side Arm Heater.Caused by Improper Installation.Pipe Section Will Be Replaced ML20090E2151974-03-0808 March 1974 AO 50-220/74-1:on 740225,during Routine Surveillance Testing,Core Spray Differential Pressure Instrument (Barton 288-4802,RV-30A) Actuated Low.Caused by Setpoint Drift. Instrument Will Be Modified ML20126F6041974-03-0404 March 1974 AO 50-220/74-1:on 740225,core Spray Differential Pressure Instrument RV-30A Found to Actuate Lower than Specified. Caused by Setpoint Drift.Barton Switch to Be Modified to Eliminate Drift ML20090E2311973-12-10010 December 1973 AO 73-12-1:on 731201,Magnetrol Switch 352624 in Scram Dump Vol Level Sys Failed.Caused by Oxidized Mercury in Switch Bulb.Bulb Replaced ML20090E2351973-12-0404 December 1973 AO 73-12-1:on 731201,during Surveillance Test,Magnetrol Switch 352624 in Scram Dump Vol Level Sys Failed to Operate. Caused by Oxidized Mercury in Bulb of Switch.Mercury Bulb Replaced ML20090E2931973-12-0303 December 1973 AO 73-11-29:on 731126,15 Control Rod Drives Failed to Insert to Position 00 Following Reactor Scram.Caused by Leakage Past Stop Piston Seals ML20090E3051973-11-30030 November 1973 AO 73-11-12:during Review of Spring 1973 Refueling Outage Tech Spec Update,Discrepancy Noted in Pressure Setpoint Trip of Recirculation Pumps.Caused by Design Error.Design Will Be Changed ML20090E3131973-11-28028 November 1973 AO 73-11-20:on 731120,during Routine startup,11 Control Rod Drives Failed to Insert to Position 00 Following High Flux Scram.Caused by Damaged Stop Piston Seals Resulting in Excessive Leakage.Control Rods Will Be Overhauled ML20083Q8111973-11-28028 November 1973 AO 73-11-17:on 731117,during Maint Work,Facility Experienced Loss of Offsite Power.Caused by Electrician Bumping 50FDS/SI Seal in Relay.Electricians Cautioned ML20083Q8061973-11-21021 November 1973 AO 73-11-17:on 731117,relay 945 de-energized,tripping Only 115-kV Line,Thus Leaving Plant W/O Offsite Power.Caused by Electrician Accidentally Bumping Relay.Power Restored in 10 ML20083Q8181973-11-19019 November 1973 AO 73-11-10:on 731110,reactor low-low Water Level Switch Setting Found to Actuate Above Normal Setpoint.Caused by Setpoint Drift.Switch Recalibr ML20083Q8151973-11-16016 November 1973 AO 73-11-13:on 731113,one Reserve Power Transformer Removed from Svc.Caused by Ground in Wire Supplying Duct Heater Across One Phase of Secondary Transformer.Wire Removed & Transformer Returned to Svc ML20083Q8221973-11-13013 November 1973 AO 73-11-10:on 731110,reactor low-low Water Level Switch Setting Actuated Above Normal Setpoint.Caused by Setpoint Drift on Yarway RE02D Sensor.Sensor Recalibr 1975-08-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G2161999-10-15015 October 1999 Errata Pages 2 & 3 for Safety Evaluation Supporting Amend 168 Issued to FOL DPR-63 Issued on 990921.New Pages Change Description of Flow Control Trip Ref Cards to Be Consistent with Application for Amend ML20217K4631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Nine Mile Point, Unit 1.With ML20216J9251999-09-30030 September 1999 Suppl to Special Rept:On 990621,11 Containment Hydrogen Monitoring Sys Chart Recorder Was Indicating Below Normal Operating Range.Caused by Excessive Wear on Valve Body & Discs of Bypass Pump.Sample Pump Replaced ML20212F7301999-09-21021 September 1999 Special Rept:On 990907,CR Operators Declared 12 Containment Hydrogen Monitoring Sys Inoperable for Planned Maint.Cause of Low Flow Condition Was Determined to Be Foreign Matl. Replaced Sample Pump Valve Discs ML20212B9081999-09-14014 September 1999 Special Rept:On 990901, 12 Containment Hydrogen Monitoring Sys Was Declared Inoperable for Planned Maint.Caused by Planned Maint Being Performed as Corrective Action.Check Valves with O Rings Were Replaced ML20212C4601999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Nine Mile Point Nuclear Station,Unit 1.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 ML20210U4591999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Nine Mile Point, Unit 1.With ML20209D0291999-07-0202 July 1999 Special Rept:On 990621,operator Identified That Number 11 Hydrogen Monitoring Sys (Hms) Chart Recorder Was Indicating Below Normal Operating Range.Cause Indeterminate.Licensee Will Complete Troubleshooting of Subject Hms by 990709 ML20210B9081999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Nine Mile Point Unit 1.With ML20209F8811999-06-0808 June 1999 Rev 1 to NMP Unit 1 COLR for Cycle 14 ML20207G2261999-06-0707 June 1999 SER Accepting Proposed Mod to Each of Four Core Shroud Stabilizers for Implementation During Current 1999 Refueling Outage at Plant,Unit 1 ML20196E2111999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Nmp,Unit 1.With ML20207B0241999-05-18018 May 1999 Safety Evaluation of Topical Rept TR-107285, BWR Vessel & Intervals Project,Bwr Top Guide Insp & Flaw Evaluation Guidelines (BWRVIP-26), Dtd December 1996.Rept Acceptable ML20206U5351999-05-17017 May 1999 SER Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant, Units 1 & 2 ML20196L2301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Nmp,Unit 1.With ML20205L0541999-04-0101 April 1999 Nonproprietary Replacement Pages to HI-91738,consisting of Section 5.0, Thermal-Hydraulic Analysis ML20205S5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for NMP Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207G2671999-03-0101 March 1999 Special Rept:On 990315,Nine Mile Point,Unit 1 Declared Number 12 Containment Hydrogen Monitoring Sys Inoperable. Caused by Degraded Encapsulated Reed Switch within Flow Switch FS-201.2-1495.Technicians Replaced Flow Switch ML20204C9971999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Nine Mile Point,Unit 1.With ML20207E9311999-02-26026 February 1999 Part 21 Rept Re Sprague Model TE1302 Aluminum Electrolytic Capacitors with Date Code of 9322H.Caused by Aluminum Electrolytic Capacitors.Affected Capacitors Replaced ML17059C5501999-01-31031 January 1999 Rev 0 to MPR-1966(NP), NMP Unit 1 Core Shroud Vertical Weld Repair Design Rept. ML20199M0891999-01-22022 January 1999 Part 21 Rept Re Failure of Square Root Converters.Caused by Failed Aluminum Electrolytic Capacitory Spargue Electric Co (Model Number TE1302 with Mfg Date Code 9322H).Sent Square Root Converters Back to Mfg,Barker Microfarads,Inc ML20199K9331998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20210R8441998-12-31031 December 1998 1998 Annual Rept for Energy East ML20206P2391998-12-31031 December 1998 Special Rept:On 981222,operators Removed non-TS Channel 12 Drywell Pressure Recorder & Associated TS Pressure Indicator from Svc.Caused by Intermittent Measuring Cable Connection in non-TS Recorder Circuitry.Replaced Cable ML20206P2421998-12-30030 December 1998 Special Rept:On 981219,number 12 Hydrogen Monitoring Sys (Hms) Was Declared Inoperable When Operators Closed Valve 201.2-601.Caused by Indeterminate Failure of Valve 201.2-71. Supplemental Rept Will Be Submitted After Valve Is Repaired ML20198M3571998-12-23023 December 1998 Special Rept:On 981210,operators Declared Number 11 Inoperable,Due to Failure of CR Chart Recorder.Caused by Inverter Board in Power Supply Circuitry of Recorder Due to Component Aging.Maint Personnel Replaced Failed Inverter ML20198D9361998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Nine Mile Point,Unit 1.With ML20155E2001998-11-0202 November 1998 Safety Evaluation Approving NMP 980227 Request for Extension of Reinspection Interval for Core Shroud Vertical Welds at NMP1 from 10,600 Hours to 14,500 Hours of Hot Operation ML20195J4141998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20154D8401998-10-0505 October 1998 Safety Evaluation Accepting Proposed Changes Related to PT Limits in Plant,Unit 1 TSs ML20154P1821998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Nine Mile Point Nuclear Station,Unit 1.With ML20153B2001998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Nmpns,Unit 1.With ML20237C6351998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20236T5911998-07-20020 July 1998 LER 98-S01-00:on 980618,security Force Member Left Nine Mile Point,Unit 2 Vehicle Gate Unattended Without Ensuring,Gate Alarm Had Been Reactivated.Caused by Inadequate Work Practice.Vehicle Gate Alarm Was Activated ML18040A3491998-07-0202 July 1998 LER 98-017-00:on 980602,control Room Ventilation Sys Was Declared Inoperable.Caused by Original Design Deficiency. Mod Designed,Tested & Implemented Prior to Startup from RF06 to Correct Design deficiency.W/980702 Ltr ML20236Q1701998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1011998-06-24024 June 1998 LER 98-014-00:on 980525,noted Differences Between Actual Valve Weights & Weights Shown on Engineering Drawings.Caused by Vendor Failing to Provide Accurate Valve Weights.Revised Valve Drawings & Associated Calculation,Per 10CFR21 ML20151P1751998-06-16016 June 1998 Rev 0 to SIR-98-067, Evaluation of NMP Unit 2 Feedwater Nozzle-to-Safe End Weld Butter Indication (Weld 2RPV-KB20, N4D) ML18040A3451998-06-0404 June 1998 LER 98-004-01:on 980302,TS Required LSFT of Level 8 Trip of Main Turbine Was Missed.Caused by Knowledge Deficiency of EHC Sys.Revised Applicable LSFT Procedures Prior to Refueling Outage 6.W/980604 Ltr ML20249B4971998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20198B4991998-05-15015 May 1998 Non-proprietary Replacement Pages for Attachment F to Which Proposed to Change TS 5.5, Storage of Unirradiated & Sf ML20247R1141998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Nine Mile Point Nuclear Station,Unit 1 ML20217B0621998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Nine Mile Point Nuclear Station,Unit 1 ML17059C1681998-03-19019 March 1998 Revised Niagara Mohawk Powerchoice Settlement Document for NMPC PSC Case Numbers 94-E-0098 & 94-E-0099, Vols 1 & 2 ML20217F4341998-03-19019 March 1998 SER Related to Proposed Restructuring New York State Electric & Gas Corp,Nine Mile Point Nuclear Station,Unit 2 ML17059B9051998-02-28028 February 1998 NMP Unit 1 Boat Samples Analyses Part Iii:Tension Tests, RDD:98:55863-004-000:01 1999-09-30
[Table view] |
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FJIAGARA .-t MOHAWK l 300 ErtlE COULEV AFID. WLtiT
- SYtt ACUSE. ii. Y.13 202 December 19, 1974
50-220 Rect?vgg e lit. Kari R. Gotter -2 DEC 23 ISIA 2 Assis. tant Dinector of ,0peAa. ting Reactors Q "kaj up :
N Dihectorate of Lxccas.usg s,4 United States Atcmic Energij Cosr. mission (*e
Ocar Itt. Gotter:
In accordance tolth .the Teclutical Specifications for the N.ine !.fiic Point !!ucleat Station, Unit til, the enclosed Abnormat Ocetoutance Report (14-16) is being submitted.
This is in .the accepted for=t a!. detai.Ced in Regulatony I".' f{.
Guide 1.16, Rev. 1.
Ver(: thuit) tjourb, Original signed by R.R. Schneider R.R. Schneider Vice Presidentt Electric Cperations -
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O-NIAGARA MOHAWK POWER CORPORATION NI AGARA ', MOHAWK DATE: December 16, 1974 ,
SUBJECT:
Abnonnal Occurrence Report No. 50-220 /74-16' ;
The-enclosed Abnormal Occurrance Report is being submitted in accordance with Technical Specifications-Section 6.
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TO: James P. 0?Reilly '
Directorate of Regulatcry Operations Region'1' 631 Park Avenue King of Prussia, Pennsylvahia 19406 FROM: Niagara Mohawk Power Corporation Nine Mile Point - James A. FitzPatrick Site P.0, Rnv #32 Lycoming, New York 13093 t
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SUBJECT:
Abnormal' Occurrence 10 Day Letter ,
REFERENCE:
Licenso DPR 17 .
i Report No.: 50-220 /74-16 .
l Report Date: 12/10/74 .
Occurrence Date: 12/10/74 Facility: NY NMP #1 l .
Identification of Occurrence:
One inoperable IRM (12), in Safety System 11 l Conditions Prior to l
Occurrence: Steady State Power Routine Shutdown-llot Standby Cold Shutdown Load Changes Refueling Shutdown 3 X Routine Startup other Description of f.he Occurrence:
During routine surveillance it was found that IRM (12) was -
inoperabic. Technical Specifications Tabic 3.6.2a requires -3 operabic Instrument Channels per trip. system. This LCO-was satisfied as the other 3 IRM's in safety system 11 were operable.
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Apparent Cause of the Occurrence:
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Design ,Procedurc Manufacture Unusual Service Installation /Const. Condition Operator X Component Failurc Other (Specify)
Cable or detector failurc Analysis of Occurrence:
The IM1 system is used to detect and indicate neutron flux 1cvel between the source range and the power range instrum-entation. Trip signals are provided to the RPS in a one out of two r.wice logic. It is possibic to bypass an inoperative IIG! channel from the RPS. The switches for this function are arranged so that only one channcI in a safety system bus ca_n be bypassed at one time. The number and locations of the IIBl detectors have been analytically and experimentally determined to provide sufficient intermediate range flux levn1 information'under the worst permitted bypass or detector failure conditions. A range of rod withdrawal accidents has been analyzed. In the most severe case the reactor is just sub-critical with one fourth of the control rods plus one more rod removed in the normal operating sequence.
The error is the removal of the control rod adjacent-to-the-last rod withdrawn. This 16 cation is chosen to maximize the-distance to the second nearest detector for cach RPS trip system. The nearest detector in cach trip system:is usumed to be bypassed. The rod withdrawal is '.'seen" and a trip. initiated, y n,q
.s Therefore, it can be concluded that one IRM being inoperable would not have prevented the performance of the intended safety function of the IRM system. Further, no hazard would have.
been presented to the plant safety or health and welfare 'of the general public from this event.
Corrective Action: ,
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- The failure is apparently in either the-cable or the. detect'or ~
itself. Therefore, a power reduction and de-inertion of the drywell would be required to repair the IRM. This repair will be under-taken during a refueling shutdown and the nature of repair included in the annual report.
Conclusion:
1The 1141 will remain bypassed or in a trippe'd condition-until-repairs can be made. The LCO Table 3.6.2a is satisfied. There-fore,,it is concluded that no hazard is presented to the general public. ,
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- inAo^ter aQ monnu DNIII
- Deceber 10, 1974
SUBJECT:
Abnormal Occun ence Repet No. 50-220 r74-16 The enc.losed prc)ir.tinary AOR is being submittet. in accordance with Technical Specifications 'Section 6.
'fo: Jasaes P. O'Reilly -
Directorate of Regulutory Operations .. f ~
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SDDJ ECT:._ Abnornal Occurrence 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Notification Confirming ffr. T..Perkins phone conversation With __Mr'. Y. She.ilonky .
AEC RO:1 office on '
17f10/74 .
REFJ3RTECB: License DPR 17 _.
Rrport No : 50 220 /74-16 Rsport Date: 12/I_0/74
- Occurrence Dato: 12/10/74 - -
Puoility: IN TC'#. # 1 2 -
Identification of" Occurrence:
One inoperablo IRM (12), in Safety System :1 ,
Conditions Prior to Ocettrrenco: Steady Stute Power- Routino Shutdown llot Standby ,
Cold Simtdown Load Change.*
Rofuoling Shutdown x Routine Sturtup _ Other Ducription. of the Docurrence:
During routino aurve511once it uns found that IR4 (12) was inoperable. Technical Specifications Table 3.6.2a requirer -3 operabic Inntrtnwnt channels per trip systera. This LCO wp untinfled as the othor 3 IRM's in safety system 11 were operable. ,
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Cable or detector failure. ,
Analysis of Occurrences b IRM Syster: is used to detect and indicate neutron flux level' botuoca the source ranne and the power range .instruzz-entation. Trip signaln are provided to the HPS in a one out of tuo tuice logic. It is por.sible to bypass an inoperativt.-
IPJS chttuni fro:n the RP3. Tho switches for this function ure-prec.t':cd'.sc tbar only our chunnel in a sat *ety system bus cun be bypnosed'at one tine. The rnnbur and'. Iocations of the 11tn detectora Irm been unalytically ani experiuant.nlly dhterrained to provido sui'ficient in:crraediate range flur.IcVet infornntion under the worct permitted bypnos or deteetor failuro conditions, A ronce of red uithdr teni occidents hno been unnly:ud. In the most .'wveir cace th:r rc=ctor in ju::.t sub-critical with. ons+ 1'ourth of the control roda plus ona corn rod recoved in tho normni operatin;; sequence.
Tha cerez- is the remval of the cent.rol rod adjacent to the inst rod withdruyn. This location is chosen to noxioite ttne
. diatsuco to tho ..ecoral nenrost dotee. tor for cash IWS trip cyt.t c.v . The ncatest detector in. cach trip sy.vten in umraed -
to be bypsused. 'lhe rod' withdraual is "scen" and a trip initiated.
Therefore>. it can be concluded that one IRM bein; inoperablu Hould not have preventexi the part' ore.2nco of the intended safety function of thu IlUI systen. Further.. no hazard.vould have bcon. presented to tha plant safety or hvalth and welfore, of the general public from this ovcnt..
Corrective /iction Luter-Failtire Datu: : ,-
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