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 Issue dateTitleTopic
ML20090C43329 December 1975AO-75-09:on 751123-29,licensee Failed to Analyze Stack Cartridges Weekly.Technician Reinstructed
ML20090C45528 November 1975AO-75-032:on 751117,acid Leak Occurred in Makeup Demineralizer Acid Storage Tank.Caused by Partially Open Discharge Valve.Valve Repaired
ML20090C44926 November 1975AO-75-031:on 751114,both Radiation Monitors in Reactor Bldg Ventilation Duct Failed to Provide Transfer to Emergency Ventilation Sys at 5 M/H.Caused by Incorrect Adjustment Made Prior to Calibr
ML20090D89029 August 1975AO 50-220/75-23:on 750826,during Audit of Contractor Facility Used in Analyzing Milk Samples,Required Sensitivity Not Achieved.Caused by Inadequate Procedure.Contractor Informed That Milk Counting Time Must Increase
ML20090E0412 April 1975AO 50-220/75-05:on 750401,during Routine Surveillance Testing,Emergency Vent Sys Failed to Function When Sys Inlet Ventilation Valve Bv 202-36 Failed to Open.Caused by Broken Stem in Solenoid Valve.Solenoids Will Be Replaced
ML20090E1586 January 1975AO 50-220/74-17:on 741227,source Range Monitor 14 Declared Inoperable.Caused by Component Failure.Detector Replaced W/Spare
ML20090E16119 December 1974AO 50-220/74-16:on 741210,intermediate Range Monitor 12 Found Inoperable.Cause Apparently Due to Defect in Cable or Detection.Repair Will Be Conducted on Sys
ML20090E16317 December 1974AO 50-220/74-15:during Markup of Motor Generator 167, Operator Tripped Supply Breaker for Power Board.Caused by Operator Error.Operator Educated in Proper Procedures. Training Sessions for All Operators Conducted
ML20090E15910 December 1974Ao:On 741110,fuel Channel Deflections Indicated Increase in Core Bypass Flow Over Calculations Assumed in Original Design.Channels Will Be Replaced.Finger Springs Will Be Used to Control Leakage
ML20090E16527 November 1974AO 50-220/74-14:on 741120,during Mgt Review of Monthly Surveillance Tests,Station Batteries Found Not Tested at Specified Intervals.Caused by Misinterpretation of Requirements by Maint Foreman.Foreman Notified
ML20090E16620 September 1974AO 74-13:on 740918,during Routine Testing,Containment Spray Pump Found Inoperable.Caused by Foreign Object Restricting Suction Flow of Pump.Object Removed
ML20090E16828 August 1974AO 50-220/74-12:on 740824,during Surveillance Testing,One Barton Instrument Used in Drywell High Pressure Reactor Protection Sys Drifted High.Caused by Setpoint Drift. Switch Recalibr
ML20090E17021 August 1974AO 74-10:on 740817,during Routine Surveillance Testing, Barton Differential Pressure Instrument 1 B05C (Emergency Cooling High Flow) Tripped at Lower than Required Value. Caused by Setpoint Drift
ML20090E1731 July 1974AO 74-9:on 740628,during Restart,Reactor Protection Sys Relay RE-230 Failed.Caused by Open Relay Coil.Relay Replaced
ML20090E1753 June 1974AO 50-220/74-8:on 740531,setpoint on Barton Instruments Used in Drywell High Pressure Reactor Protection Sys Drifted Higher than Required.Barton Switch Recalibr
ML20090E1773 May 1974AO 50-220/74-7:on 740425,eddy Current Testing Evaluation Showed Two Control Rod Blades W/Possible Inverted Tubes. Caused by Mfg Deficiency.Two Control Blades Will Be ChangedShutdown Margin
ML20090E17929 April 1974AO 50-220/74-6:during Releak Testing,Msiv Leaked Excessively.Cause Unknown & Being Investigated.Valve Will Be Inspected
ML20090E18024 April 1974AO 74-5:on 740415,during Annual Refueling Shutdown Testing, Three High Temp Main Steam Line Tunnel Sensors Found to Actuate at Lower than Required Temp.Caused by Setpoint Drift on Sensor.Sensors Recalibr
ML20090E18311 April 1974AO 50-220/74-4:on 740402,during Refueling Outage Test,Low Condenser Vacuum Sensors Actuated Low Resulting in Reactor Scram.Caused by Switch Setpoint Drift.Sensor Switch Recalibr
ML20090E1849 April 1974AO 50-220/74-3:on 740402,both Inside MSIVs Failed to Meet Required Limit of 12.9 Std Cubic Ft Per Inch.Caused by Drift in Position Switch on Valve Controller.Valves Will Be Repaired & Retested
ML20090E1872 April 1974AO 50-220/74-3:on 740402,during Leak Testing,Both Inside MSIVs Exceeded Leakage Limit.Caused by Either Drifting Position Switch or Improper Seating of Disc.Investigation Continuing.Position Switch Will Be Readjusted
ML20090E1941 April 1974AO 50-220/74-2:on 740323,concentrator Steam Seeped Through Insulation Surrounding 12-inch Section of Pipe Leading from Side Arm Heater to Concentrator Bottom.Caused by Improper Installation.Pipe Will Be Replaced
ML20090E20525 March 1974AO 50-220/74-2:on 740323,during Routine Concentrator Steam Operation,Pipe Crack Found in Waste Concentrator Piping Leading from Side Arm Heater.Caused by Improper Installation.Pipe Section Will Be Replaced
ML20090E2158 March 1974AO 50-220/74-1:on 740225,during Routine Surveillance Testing,Core Spray Differential Pressure Instrument (Barton 288-4802,RV-30A) Actuated Low.Caused by Setpoint Drift. Instrument Will Be Modified
ML20126F6044 March 1974AO 50-220/74-1:on 740225,core Spray Differential Pressure Instrument RV-30A Found to Actuate Lower than Specified. Caused by Setpoint Drift.Barton Switch to Be Modified to Eliminate Drift
ML20090E23110 December 1973AO 73-12-1:on 731201,Magnetrol Switch 352624 in Scram Dump Vol Level Sys Failed.Caused by Oxidized Mercury in Switch Bulb.Bulb Replaced
ML20090E2354 December 1973AO 73-12-1:on 731201,during Surveillance Test,Magnetrol Switch 352624 in Scram Dump Vol Level Sys Failed to Operate. Caused by Oxidized Mercury in Bulb of Switch.Mercury Bulb Replaced
ML20090E2933 December 1973AO 73-11-29:on 731126,15 Control Rod Drives Failed to Insert to Position 00 Following Reactor Scram.Caused by Leakage Past Stop Piston Seals
ML20090E30530 November 1973AO 73-11-12:during Review of Spring 1973 Refueling Outage Tech Spec Update,Discrepancy Noted in Pressure Setpoint Trip of Recirculation Pumps.Caused by Design Error.Design Will Be Changed
ML20090E31328 November 1973AO 73-11-20:on 731120,during Routine startup,11 Control Rod Drives Failed to Insert to Position 00 Following High Flux Scram.Caused by Damaged Stop Piston Seals Resulting in Excessive Leakage.Control Rods Will Be Overhauled
ML20083Q81128 November 1973AO 73-11-17:on 731117,during Maint Work,Facility Experienced Loss of Offsite Power.Caused by Electrician Bumping 50FDS/SI Seal in Relay.Electricians Cautioned
ML20083Q80621 November 1973AO 73-11-17:on 731117,relay 945 de-energized,tripping Only 115-kV Line,Thus Leaving Plant W/O Offsite Power.Caused by Electrician Accidentally Bumping Relay.Power Restored in 10
ML20083Q81819 November 1973AO 73-11-10:on 731110,reactor low-low Water Level Switch Setting Found to Actuate Above Normal Setpoint.Caused by Setpoint Drift.Switch Recalibr
ML20083Q81516 November 1973AO 73-11-13:on 731113,one Reserve Power Transformer Removed from Svc.Caused by Ground in Wire Supplying Duct Heater Across One Phase of Secondary Transformer.Wire Removed & Transformer Returned to Svc
ML20083Q82213 November 1973AO 73-11-10:on 731110,reactor low-low Water Level Switch Setting Actuated Above Normal Setpoint.Caused by Setpoint Drift on Yarway RE02D Sensor.Sensor Recalibr