ML20076B518
ML20076B518 | |
Person / Time | |
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Site: | Fermi |
Issue date: | 08/02/1983 |
From: | Wells D DETROIT EDISON CO. |
To: | James Keppler NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
References | |
10CFR-050.55E, 10CFR-50.55E, EF2-64307, NUDOCS 8308190389 | |
Download: ML20076B518 (2) | |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARNRC-97-0141, Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility1997-12-23023 December 1997
[Table view]Deficiency Rept Re Malfunction of EDG Number 11 Automatic Voltage Regulator (AVR) Printed Circuit Board Rev B,Due to Failure of Operational Amplifier U8 Chip.Avr Board Rev B Was Sent Offsite to Independent Engineering Facility ML20211M6491997-10-0808 October 1997 Addenda 1 to Part 21 Rept Re Weldments on Opposed Piston & Coltec-Pielstick Emergency stand-by Diesel gen-set lube-oil & Jacket Water Piping Sys.Revised List of Potentially Affected Utils to Include Asterisked Utils,Submitted ML20211H7911997-09-30030 September 1997 Part 21 Rept Re Failure of Weldment Associated w/lube-oil Piping Sys on 970804 at Millstone,Unit 2.Root Cause Is Not Yet Known.Quality of Weldment Is Being Considered.Listed Util Sites Affected NRC-97-0005, Part 21 Rept Re 961113,EDG 11 Failed Surveillance Test 24.307.01 for LOP Coincident W/Loca.Avr Board Rev B Was Sent Offsite to an Independent Engineering Test Facility. CA Include More Analysis & Testing of AVR Board1997-02-0606 February 1997 Part 21 Rept Re 961113,EDG 11 Failed Surveillance Test 24.307.01 for LOP Coincident W/Loca.Avr Board Rev B Was Sent Offsite to an Independent Engineering Test Facility. CA Include More Analysis & Testing of AVR Board NRC-94-0072, Part 21 Rept Re Improper Installation of Thermo-Lag Fire Barrier Matl Furnished & Delivered by Thermal Science,Inc. Eight of Ten Thermo-Lag Fire Barriers Installed by Pr Sussman Co Being Replaced1994-08-15015 August 1994 Part 21 Rept Re Improper Installation of Thermo-Lag Fire Barrier Matl Furnished & Delivered by Thermal Science,Inc. Eight of Ten Thermo-Lag Fire Barriers Installed by Pr Sussman Co Being Replaced ML20070H1471994-07-15015 July 1994 Part 21 Rept Re Problems W/Thermolag Fire Barriers.Initially Reported on 940715.Replaced Thermolag Fire Barriers ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical ML20058G5981993-11-17017 November 1993 Part 21 Rept Re Westronics Recorders,Model 2100C.Signal Input Transition Printed Circuit Board Assembly Redesigned to Improve Recorder Immunity to Electromagnetic Interference.List of Affected Recorders & Locations Encl ML20057G1511993-10-0707 October 1993 Part 21 Rept Re Westronics Model 2100C Series Recorders. 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... w, 4 Donald A Wells Meaum oo uf M .meo (113; .*17'M M Ecison Efn?E==
August 2, 1983 EF2-64307 1 Mr. Jamon G. Keppler, Regional Administrator Region III U. S. Nuclear Reguintory Commission 799 Roosevelt Road Glen Ellyn, Illinois 60137 i
Subject:
Interim Report of 10CFR50.55(e) Item on Possible ITE Circuit Brenker Failures (#87) l l
Dear Mr. Keppler:
This interim report involving ITE circuit breaker failures has been prepared to provide the current status of this problem.
This item was originally reported to Mr. P. Pelke of NRC Region III by
]
Detroit Edison's Mr. D. Ferencz, Acting Supervisor - Construction Quality Assurance on March 4,1983.
f A memo received f rom the NRC, concerning Brown Boveri Electric, Inc.
4 (formerly ITE) low voltage circuit breakers, described a problem involving a defective capacitator in the trip circuit which, upon failure, prevents the breaker from opening during an overcurrent condition. The failure of this capacitator and the trip device can result in failure to interrupt a fault.
The Edison Startup Organization has completed a survey of all solid l state trip devices in the 480V switchgear at Fermi 2. The survey found one hundred thirty (130) devicca equipped with a Type 400 capacit stor, which has been found to degrade over time.
Detroit Edison is awaiting a shipment of rep 1ncement solid state trip devices from Brown Bovert Electric, Inc. for all one hundred thirty devices.
i Another report on this item, either interim or finni, will be sent when further information is available. If you have questions concerning this matter, please contact Mr. G. M. Trahey, Assistant l Director - Project quality Assurance.
0308190309 030002
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DR ADOCK 05000 Very truly yours, t ,S. AN'~
p t s mL
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4 Mr. James G.-Keppler,. Regional Administrator 1
August 2, 1983-EF2-64307 4 Page 2 DAW /WEM/pn
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! cc: Mr. Richard DeYoung, Director Office of Inspection and Enforcement i
U. S. Nuclear Regulatory Commission l
Washington, D. C. 20555 j Mr. Paul Byron, Senior Resident Inspector U. S. Nuclear Regulatory Commission 6450 North Dixie Highway Newport, MI 48166 4
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