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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024A5401983-06-0202 June 1983 LER 83-021/03L-0:on 830504,containment Sump Alarms Declared Inoperable.Caused by Defective Alarm Card.Alarm Card Replaced.Annunciator Alarm Will Be Checked daily.W/830602 Ltr ML20028G4811983-01-31031 January 1983 LER 83-004/03L-0:on 830101,containment Sump Level Alarm Would Not Clear.Caused by Dirt & Debris Which Interfered W/Level Switch Operation.Level Switch Tube Flushed ML20028G3801983-01-27027 January 1983 Uptated LER 82-010/03X-1 on 820212,following Reactor Trip, Element Assembly 19 Discovered Stuck at 8-inch Withdrawn Position.Cause Undetermined.Control Element Assembly & Associated Bundle Inspected ML20028F4391983-01-21021 January 1983 LER 82-084/03L-0:on 821223,sequencer Initiated Alarm Failed to Clear When Diesel Generator 12 Shut Down.Caused by Failure of Breaker Lever to Operate Auxiliary Switch in Cubicle Due to Displaced Assembly.New Assembly Installed ML20052J0421982-05-14014 May 1982 LER 82-018/03L-0:on 820417,control Element Assembly 21 Dropped Into Core After Electricians Inadvertently Disconnected Power,Resulting in Pressurizer Level Deviation Exceeding Tech Spec Limit.Caused by Personnel Error ML20050D4691982-04-0202 April 1982 LER 82-014/03L-0:on 820304,water Observed in Emergency Diesel Generator Lube Oil Dry Tank.Caused by Filling Tank from Unsampled Barrel of Oil Which Had Significant Amount of Water.New Procedure Written ML20027D1261981-04-0303 April 1981 LER 81-013/03L-0:on 810304,while Installing Instrumentation, Temporary Shunt Opened,Causing Loss of Power to Low Pressure Safety Injection Pump 22 & Momentary Loss of Shutdown Cooling Flow.Caused by Opened Lead on One End of Shunt ML19347D5611981-03-13013 March 1981 LER 81-012/03L-0:on 810213,while Shifting from 1 to 2 Running Charging Pumps,Letdown Relief Valve CVC-345-RV Lifted & Failed to Reseat.Possibly Caused by Pressure Surge in Line.Valve Matls Review Being Conducted ML20003C6001981-03-0101 March 1981 Updated LER 81-002/03L-1:on 810108 & 0227,diesel Generator 12 Started Automatically.Generator Was Stopped & Start Failure Alarm Received.Caused by Insufficient Contact Wipe by Local Break Glass Start Switch.Actuator Fitting Removed ML20003A3881981-01-27027 January 1981 LER 80-066 Has Been Cancelled ML19351F6391981-01-0909 January 1981 LER 80-055/03L-0:on 801209,emergency Diesel Generator 12 Developed Fuel Oil Leak.Caused by Leak at Flared Type Brass Compression Fitting.Line Replaced ML19345B8391980-11-26026 November 1980 LER 80-050/03L-0:on 801027,wide Range ex-core Nuclear Instrument Channel B Failed.Caused by Greater than or Equal to 15-volt Dc Power Supply Having Low Supply W/Ac Ripple. Power Supply Replaced ML20002A7811980-11-17017 November 1980 LER 80-060/03L-0:on 801018,surveillance Testing Found RC-200 & RC-201 Lift Setpoints to Be 70 Psi & 56 Psi,Respectively, Above Max Tech Spec.Cause Not Stated.Setpoints Adjusted ML19323C4191980-05-13013 May 1980 LER 80-024/03L-0:on 800417,during Containment Entry ,Leak in Middle Seal Instrument Line Flexible Hose Discovered.Cause Unknown.Failed Part Is Inside Containment Bldg & Is Still Radiologically Contaminated ML19309G4451980-04-30030 April 1980 LER 80-022/03L-0:on 800412,charging Pump 23 Removed from Svc to Repair Weld on Suction Relief Valve.Leak Caused by Vibration Induced Metal Fatigue in Heat Affected Zone of Weld.Leak Repaired & Mods Approved for Charging Pumps ML19309F4001980-04-25025 April 1980 Updated LER 79-003/01X-2:on 790120,reactor Coolant Pump 22A Lower Seal Temp Alarm Activated & 2 Gpm Increase in Leak Rate Noted.Reactor Manually Tripped.Caused by Cracked Weld on Seal Pressure Sensing Line.Seal Assembly Replaced ML19309F4691980-04-25025 April 1980 LER 80-022/01T-0:on 800415,util Informed of Possible Deficiency in FSAR Section 14.3,boron Dilution Incident,For Case When RCS Is Drained to Hot Leg w/1% Shutdown Margin. Cause Not Stated.Procedures Changed ML19309F3841980-04-25025 April 1980 LER 80-016/03L-0:on 800325,during Surveillance Testing, Channel a Wide Range Nuclear Instrument Did Not Respond in Calibr Mode.Apparently Caused by Failure of Channel Preamplifier.Power Supply Replaced W/Spare ML19309E6641980-04-18018 April 1980 LER 80-021/03L-0:on 800318,during Performance of Surveillance Test 23,saltwater Pump Did Not Start Upon Receipt of Safety Actuation Signal.Caused by Faulty Pin. Pin Replaced ML19294B7451980-02-29029 February 1980 LER 80-009/03L-0:on 800131,while Conducting Routine Test, Control Element Assembly (CEA) 32 Dropped Into Core.Cause Unknown.Technician Will Be Assigned During Next STP 0-29 to Monitor Operating Parameters of All CEAs on real-time Basis ML19290E2321980-02-29029 February 1980 LER 80-007/03L-0:on 800130,while Performing Routine Surveillance Testing,Discovered Control Element Assembly 54 Would Not Drive Down Electrically.Cause Not Known.Rod Became Operable During Investigation of Rod Circuitry ML19296C8291980-02-27027 February 1980 LER 80-009/03L-0:on 800201,during Surveillance Testing, Discovered Hose for One of Two Containment Elevator Hose Stations Missing.Caused by Work Group Using Fire Sys for Cleaning Purposes on Elevation of Containment ML19296D1291980-02-22022 February 1980 LER 80-005/03L-0:on 800122,five Channel B Trip Units Were Bypassed Due to Spurious High Power Levels.Caused by Noise from Excore Nuclear Instrument Upper Subchannel Detector. Troubleshooting Planned for Next Cold Shutdown ML19296A7041980-02-0808 February 1980 LER 80-003/03L-0:on 800110,repairs to Number 21 Diesel Generator Jacket Coolant Sys Required Diesel Be Out of Svc. Caused by Leaking Gasket on Jacket Cooling Water Discharge Header.Leak Located & Repaired ML19260D9751980-02-0707 February 1980 LER 80-002/03L-0:on 800107,refueling Water Tank Narrow Range Level Indicator Was in Alarm W/Low Level,But Instrument Did Not Indicate Alarm Conditions.Caused by Faulty Indicator Alarm light-emitting Diode.Diode Replaced ML19290C2781980-01-0404 January 1980 LER 79-047/03L-0:on 791204,while Performing post-refueling Low Power Physics Test,Average Temp Dropped Below Tech Specs.Caused by Operator & Erratic Control of Turbine Bypass Valves ML19210C4241979-11-0505 November 1979 LER 79-037/03L-0:on 791005,analog Meter in Channel Zf Containment Pressure Bistable for SIAS Found Nonlinear in Response to Surveillance Test Input Signals.Caused by Aging of Meter Movement.Meter Replaced ML19209C6791979-10-12012 October 1979 LER 79-049/03L-0:on 790924,loop Isolation Valve SI-617 Failed to Operate When Motor Operator Received Open Signal. Caused by Contact Misalignment of Movable Contactor. Contactor Realigned & Tested ML19209C8051979-10-11011 October 1979 LER 79-051/03L-0:on 790926,hydraulic Snubber Was Removed from Operation to Repair Anchors Attaching Snubber to Wall. Anchors Were Replaced & Hanger Restored to Operation ML19209C8601979-10-0909 October 1979 LER 79-035/03L-0:on 790922,plant Computer Failed.Caused by Printed Circuit Board Failure Which Generated Rapid Access Data Storage Disc Stop Signal.Circuit Board Replaced ML19249F3241979-10-0404 October 1979 LER 79-048/03L-0:on 790914,during Surveillance Test, Containment Spray Pump 12 Tripped on Ground Overcurrent. Caused by Motor Stator Coils Chafing Against Incoming Phase Lead,Thus Developing Short Circuits at Coil End ML19209C0091979-10-0404 October 1979 LER 79-032/03L-0:on 790905,channel D Nuclear Instrumentation Sys Linear Power Range Was Indicating Erratically High. Caused by Inadequate Chassis Ground.Signal Returned to Normal After Cleaning Drawer Rails ML19209A2951979-10-0101 October 1979 LER 79-031/03L-0:on 790903,spurious Trips on Reactor Protection Sys Channel C High Power Trip Units Occured.Cause Not Stated.Temp Element 2-TE-122HC Replaced ML19209A3041979-09-28028 September 1979 LER 79-038/03L-0:on 790829,115-volt Power Supply to Hydrogen Analyzer O-AE 6527 Was Inoperative.Caused by Shorted Winding in Power Transformer T-1 ML19249D8041979-09-14014 September 1979 LER 79-047/01X-0:on 790914,air Start Sys Hangers Found Not Meeting Seismic Requirement.New Hangers Will Be Installed Meeting Seismic Requirements in Approx 5 to 7 Days ML19208A8031979-09-13013 September 1979 LER 79-034/03L-0:on 790813,during Routine Surveillance Test, Control Element Assembly Deviation Exceeded 7.5 Inches Required to Initiate Assembly Motion Inhibit.Caused by Circuit Failing,W/High Conduction Affecting Other Failures ML19208A3091979-09-11011 September 1979 LER 79-036/03L-0 on 790812:during Surveillance Test,Wide Range Nuclear Instrument Channel D Would Not Indicate Properly While in Calibr Mode.Apparently Caused by Bad Connection in Test & Power Cables.Connector Replaced ML19253B0571979-08-31031 August 1979 LER 79-030/03L-0:on 790805,control Element Assemblies 6,7, 49,51 & 53 Failed to Initiate Motion Inhibit Function. Caused by Drifting of Motion Inhibit Setpoint Voltage Levels.Setpoints Will Be Reduced ML19270H4781979-08-17017 August 1979 LER 79-027/031-0 on 790718:channel C Trips Were Received from Power Level,Thermal margin-low Pressure & Axial Flux Offset.Cause of Intermittent Problem Is Suspected to Be Loose Connection or Faulty Switch Circuit ML19225C2021979-07-20020 July 1979 LER 79-023/03L-0 on 790621:diesel Tripped Repeatedly on Low Lube Oil Pressure During Test.Caused by Isolation of Engine Oil Pressure Switch Following 790620 Preventive Maint Calibr.Preventive Maint Procedure Changed ML19246A5801979-06-25025 June 1979 LER 79-019/03L-0 on 790606:discovered That Number 11 Control Room Air Conditioning Unit Breaker Had Tripped.Caused by Windings of Compressor Motor Exceeding Resistance Acceptance Criteria.Compressor Replaced ML19289F3821979-05-31031 May 1979 LER 79-018/04T-0 on 790517:oyster Samples Showed Ag-110m at 88 Plus or Minus 5% Pci/Kg & Decreasing.May Be Caused by Depuration.No Corrective Action Required ML19261B4881979-02-22022 February 1979 LER 79-005/03L-0 on 790129:during Operation,Flow Transmitter Output Was Found Pegged High & Was Bypassed.Caused by Packing Leak in Transmitter Equalizing & Reference Leg Isolation Valves ML19273A9981979-01-24024 January 1979 LER 79-001/03L-0 on 790106:excessive Reactor Coolant Sys Unidentified Leakage.Caused by Cracked Weld on Socket Weld Downstream of Second Isolation Valve.Study Planned to Propose Design Changes to Correct Fatigue Problem ML19269D5691978-09-26026 September 1978 LER 78-030/03L-0 on 780828:discovered Control Element Assembly Motion Inhibit Not Operable for Position Deviation. Caused by Bad K2 Relay on Relay Card.Relay Replaced & Motion Inhibit Returned to Svc 1993-07-09
[Table view] Category:RO)
MONTHYEARML20045G8611993-07-0909 July 1993 LER 93-003-00:on 930610,dual Unit Trip Occurred Due to Partial Loss of Offsite Power.Flashover Protection Relay for Breaker 552-61 Replaced & Training for Personnel W/ Access to Relays Will Be reinforced.W/930709 Ltr ML20043A7871990-05-21021 May 1990 LER 90-016-00:on 900421,determined That Waste Gas Decay Tank (Wgdt) 13 Discharged Instead of (Wgdt) 11 for Discharge Permit Issued.Caused by Inadequate Communications.Training Performed for Operators Re event.W/900521 Ltr ML20005D6611989-12-0606 December 1989 LER 89-018-00:on 891106,discovered That Many Air Operated Control Valves & piston-operated Dampers Which Utilize safety-related Air Accumulators Would Not Have Performed as Expected After Loss of air.W/891206 Ltr ML19325F3951989-11-10010 November 1989 LER 89-002-01:on 890228,discovered That Fire Barrier Penetration Inoperable & Action Statement Requirements Not Satisfied.Caused by Inadequate Administrative Controls. Penetration Returned to Operable status.W/891115 Ltr ML20024E1721983-07-14014 July 1983 Updated LER 81-015/03X-1:on 810226,sample Pump for Control Room Radiation Monitor Found Out of Svc,Rendering Automatic Recirculation of Control Room Ventilation Sys on High Radiation Inoperable.Caused by seizure.W/830714 Ltr ML20024A5401983-06-0202 June 1983 LER 83-021/03L-0:on 830504,containment Sump Alarms Declared Inoperable.Caused by Defective Alarm Card.Alarm Card Replaced.Annunciator Alarm Will Be Checked daily.W/830602 Ltr ML20028G4811983-01-31031 January 1983 LER 83-004/03L-0:on 830101,containment Sump Level Alarm Would Not Clear.Caused by Dirt & Debris Which Interfered W/Level Switch Operation.Level Switch Tube Flushed ML20028G3801983-01-27027 January 1983 Uptated LER 82-010/03X-1 on 820212,following Reactor Trip, Element Assembly 19 Discovered Stuck at 8-inch Withdrawn Position.Cause Undetermined.Control Element Assembly & Associated Bundle Inspected ML20028F4391983-01-21021 January 1983 LER 82-084/03L-0:on 821223,sequencer Initiated Alarm Failed to Clear When Diesel Generator 12 Shut Down.Caused by Failure of Breaker Lever to Operate Auxiliary Switch in Cubicle Due to Displaced Assembly.New Assembly Installed ML20052J0421982-05-14014 May 1982 LER 82-018/03L-0:on 820417,control Element Assembly 21 Dropped Into Core After Electricians Inadvertently Disconnected Power,Resulting in Pressurizer Level Deviation Exceeding Tech Spec Limit.Caused by Personnel Error ML20050D4691982-04-0202 April 1982 LER 82-014/03L-0:on 820304,water Observed in Emergency Diesel Generator Lube Oil Dry Tank.Caused by Filling Tank from Unsampled Barrel of Oil Which Had Significant Amount of Water.New Procedure Written ML20027D1261981-04-0303 April 1981 LER 81-013/03L-0:on 810304,while Installing Instrumentation, Temporary Shunt Opened,Causing Loss of Power to Low Pressure Safety Injection Pump 22 & Momentary Loss of Shutdown Cooling Flow.Caused by Opened Lead on One End of Shunt ML19347D5611981-03-13013 March 1981 LER 81-012/03L-0:on 810213,while Shifting from 1 to 2 Running Charging Pumps,Letdown Relief Valve CVC-345-RV Lifted & Failed to Reseat.Possibly Caused by Pressure Surge in Line.Valve Matls Review Being Conducted ML20003C6001981-03-0101 March 1981 Updated LER 81-002/03L-1:on 810108 & 0227,diesel Generator 12 Started Automatically.Generator Was Stopped & Start Failure Alarm Received.Caused by Insufficient Contact Wipe by Local Break Glass Start Switch.Actuator Fitting Removed ML20003A3881981-01-27027 January 1981 LER 80-066 Has Been Cancelled ML19351F6391981-01-0909 January 1981 LER 80-055/03L-0:on 801209,emergency Diesel Generator 12 Developed Fuel Oil Leak.Caused by Leak at Flared Type Brass Compression Fitting.Line Replaced ML19345B8391980-11-26026 November 1980 LER 80-050/03L-0:on 801027,wide Range ex-core Nuclear Instrument Channel B Failed.Caused by Greater than or Equal to 15-volt Dc Power Supply Having Low Supply W/Ac Ripple. Power Supply Replaced ML20002A7811980-11-17017 November 1980 LER 80-060/03L-0:on 801018,surveillance Testing Found RC-200 & RC-201 Lift Setpoints to Be 70 Psi & 56 Psi,Respectively, Above Max Tech Spec.Cause Not Stated.Setpoints Adjusted ML19323C4191980-05-13013 May 1980 LER 80-024/03L-0:on 800417,during Containment Entry ,Leak in Middle Seal Instrument Line Flexible Hose Discovered.Cause Unknown.Failed Part Is Inside Containment Bldg & Is Still Radiologically Contaminated ML19309G4451980-04-30030 April 1980 LER 80-022/03L-0:on 800412,charging Pump 23 Removed from Svc to Repair Weld on Suction Relief Valve.Leak Caused by Vibration Induced Metal Fatigue in Heat Affected Zone of Weld.Leak Repaired & Mods Approved for Charging Pumps ML19309F4001980-04-25025 April 1980 Updated LER 79-003/01X-2:on 790120,reactor Coolant Pump 22A Lower Seal Temp Alarm Activated & 2 Gpm Increase in Leak Rate Noted.Reactor Manually Tripped.Caused by Cracked Weld on Seal Pressure Sensing Line.Seal Assembly Replaced ML19309F4691980-04-25025 April 1980 LER 80-022/01T-0:on 800415,util Informed of Possible Deficiency in FSAR Section 14.3,boron Dilution Incident,For Case When RCS Is Drained to Hot Leg w/1% Shutdown Margin. Cause Not Stated.Procedures Changed ML19309F3841980-04-25025 April 1980 LER 80-016/03L-0:on 800325,during Surveillance Testing, Channel a Wide Range Nuclear Instrument Did Not Respond in Calibr Mode.Apparently Caused by Failure of Channel Preamplifier.Power Supply Replaced W/Spare ML19309E6641980-04-18018 April 1980 LER 80-021/03L-0:on 800318,during Performance of Surveillance Test 23,saltwater Pump Did Not Start Upon Receipt of Safety Actuation Signal.Caused by Faulty Pin. Pin Replaced ML19294B7451980-02-29029 February 1980 LER 80-009/03L-0:on 800131,while Conducting Routine Test, Control Element Assembly (CEA) 32 Dropped Into Core.Cause Unknown.Technician Will Be Assigned During Next STP 0-29 to Monitor Operating Parameters of All CEAs on real-time Basis ML19290E2321980-02-29029 February 1980 LER 80-007/03L-0:on 800130,while Performing Routine Surveillance Testing,Discovered Control Element Assembly 54 Would Not Drive Down Electrically.Cause Not Known.Rod Became Operable During Investigation of Rod Circuitry ML19296C8291980-02-27027 February 1980 LER 80-009/03L-0:on 800201,during Surveillance Testing, Discovered Hose for One of Two Containment Elevator Hose Stations Missing.Caused by Work Group Using Fire Sys for Cleaning Purposes on Elevation of Containment ML19296D1291980-02-22022 February 1980 LER 80-005/03L-0:on 800122,five Channel B Trip Units Were Bypassed Due to Spurious High Power Levels.Caused by Noise from Excore Nuclear Instrument Upper Subchannel Detector. Troubleshooting Planned for Next Cold Shutdown ML19296A7041980-02-0808 February 1980 LER 80-003/03L-0:on 800110,repairs to Number 21 Diesel Generator Jacket Coolant Sys Required Diesel Be Out of Svc. Caused by Leaking Gasket on Jacket Cooling Water Discharge Header.Leak Located & Repaired ML19260D9751980-02-0707 February 1980 LER 80-002/03L-0:on 800107,refueling Water Tank Narrow Range Level Indicator Was in Alarm W/Low Level,But Instrument Did Not Indicate Alarm Conditions.Caused by Faulty Indicator Alarm light-emitting Diode.Diode Replaced ML19290C2781980-01-0404 January 1980 LER 79-047/03L-0:on 791204,while Performing post-refueling Low Power Physics Test,Average Temp Dropped Below Tech Specs.Caused by Operator & Erratic Control of Turbine Bypass Valves ML19210C4241979-11-0505 November 1979 LER 79-037/03L-0:on 791005,analog Meter in Channel Zf Containment Pressure Bistable for SIAS Found Nonlinear in Response to Surveillance Test Input Signals.Caused by Aging of Meter Movement.Meter Replaced ML19209C6791979-10-12012 October 1979 LER 79-049/03L-0:on 790924,loop Isolation Valve SI-617 Failed to Operate When Motor Operator Received Open Signal. Caused by Contact Misalignment of Movable Contactor. Contactor Realigned & Tested ML19209C8051979-10-11011 October 1979 LER 79-051/03L-0:on 790926,hydraulic Snubber Was Removed from Operation to Repair Anchors Attaching Snubber to Wall. Anchors Were Replaced & Hanger Restored to Operation ML19209C8601979-10-0909 October 1979 LER 79-035/03L-0:on 790922,plant Computer Failed.Caused by Printed Circuit Board Failure Which Generated Rapid Access Data Storage Disc Stop Signal.Circuit Board Replaced ML19249F3241979-10-0404 October 1979 LER 79-048/03L-0:on 790914,during Surveillance Test, Containment Spray Pump 12 Tripped on Ground Overcurrent. Caused by Motor Stator Coils Chafing Against Incoming Phase Lead,Thus Developing Short Circuits at Coil End ML19209C0091979-10-0404 October 1979 LER 79-032/03L-0:on 790905,channel D Nuclear Instrumentation Sys Linear Power Range Was Indicating Erratically High. Caused by Inadequate Chassis Ground.Signal Returned to Normal After Cleaning Drawer Rails ML19209A2951979-10-0101 October 1979 LER 79-031/03L-0:on 790903,spurious Trips on Reactor Protection Sys Channel C High Power Trip Units Occured.Cause Not Stated.Temp Element 2-TE-122HC Replaced ML19209A3041979-09-28028 September 1979 LER 79-038/03L-0:on 790829,115-volt Power Supply to Hydrogen Analyzer O-AE 6527 Was Inoperative.Caused by Shorted Winding in Power Transformer T-1 ML19249D8041979-09-14014 September 1979 LER 79-047/01X-0:on 790914,air Start Sys Hangers Found Not Meeting Seismic Requirement.New Hangers Will Be Installed Meeting Seismic Requirements in Approx 5 to 7 Days ML19208A8031979-09-13013 September 1979 LER 79-034/03L-0:on 790813,during Routine Surveillance Test, Control Element Assembly Deviation Exceeded 7.5 Inches Required to Initiate Assembly Motion Inhibit.Caused by Circuit Failing,W/High Conduction Affecting Other Failures ML19208A3091979-09-11011 September 1979 LER 79-036/03L-0 on 790812:during Surveillance Test,Wide Range Nuclear Instrument Channel D Would Not Indicate Properly While in Calibr Mode.Apparently Caused by Bad Connection in Test & Power Cables.Connector Replaced ML19253B0571979-08-31031 August 1979 LER 79-030/03L-0:on 790805,control Element Assemblies 6,7, 49,51 & 53 Failed to Initiate Motion Inhibit Function. Caused by Drifting of Motion Inhibit Setpoint Voltage Levels.Setpoints Will Be Reduced ML19270H4781979-08-17017 August 1979 LER 79-027/031-0 on 790718:channel C Trips Were Received from Power Level,Thermal margin-low Pressure & Axial Flux Offset.Cause of Intermittent Problem Is Suspected to Be Loose Connection or Faulty Switch Circuit ML19225C2021979-07-20020 July 1979 LER 79-023/03L-0 on 790621:diesel Tripped Repeatedly on Low Lube Oil Pressure During Test.Caused by Isolation of Engine Oil Pressure Switch Following 790620 Preventive Maint Calibr.Preventive Maint Procedure Changed ML19246A5801979-06-25025 June 1979 LER 79-019/03L-0 on 790606:discovered That Number 11 Control Room Air Conditioning Unit Breaker Had Tripped.Caused by Windings of Compressor Motor Exceeding Resistance Acceptance Criteria.Compressor Replaced ML19289F3821979-05-31031 May 1979 LER 79-018/04T-0 on 790517:oyster Samples Showed Ag-110m at 88 Plus or Minus 5% Pci/Kg & Decreasing.May Be Caused by Depuration.No Corrective Action Required ML19261B4881979-02-22022 February 1979 LER 79-005/03L-0 on 790129:during Operation,Flow Transmitter Output Was Found Pegged High & Was Bypassed.Caused by Packing Leak in Transmitter Equalizing & Reference Leg Isolation Valves ML19273A9981979-01-24024 January 1979 LER 79-001/03L-0 on 790106:excessive Reactor Coolant Sys Unidentified Leakage.Caused by Cracked Weld on Socket Weld Downstream of Second Isolation Valve.Study Planned to Propose Design Changes to Correct Fatigue Problem ML19269D5691978-09-26026 September 1978 LER 78-030/03L-0 on 780828:discovered Control Element Assembly Motion Inhibit Not Operable for Position Deviation. Caused by Bad K2 Relay on Relay Card.Relay Replaced & Motion Inhibit Returned to Svc 1993-07-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000317/LER-1999-006, :on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With1999-10-22022 October 1999
- on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With
ML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With 05000317/LER-1998-011, :on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With1999-09-20020 September 1999
- on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With
ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20211J3531999-09-0101 September 1999 Safety Evaluation Supporting Amends 231 & 207 to Licenses DPR-53 & DPR-69,respectively ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-005, :on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With1999-08-23023 August 1999
- on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With
05000317/LER-1999-004, :on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With1999-08-23023 August 1999
- on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With
ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-003, :on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With1999-07-30030 July 1999
- on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With
ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-039, Part 21 Rept Re Defect of ABB 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of ABB 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified LD-99-035, Part 21 Rept Re ABB 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re ABB 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-002, :on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With1999-05-25025 May 1999
- on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With
ML20206U7031999-05-18018 May 1999 Rev 1 to Ran 97-031, Main CR Fire Analysis for IPEEE Section 4-1 ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on ABB CE ECCS Performance Evaluation Models ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20205J8331999-04-0707 April 1999 Safety Evaluation Concluding That Security Lighting,Portable Lighting & Helmet Lights,As Described by Licensee Satisfies Underlying Purpose of 10CFR50,App R,Section Iii.J.Grants Licensee Request for Exemption ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20204B5961999-03-17017 March 1999 Corrected Page 7 to SER for Amend 205 for License DPR-69. Staff Deleted Word Not on Line One of Page 7 ML20207L2991999-03-0808 March 1999 Safety Evaluation Supporting Amend 205 to License DPR-69 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons 05000317/LER-1997-010, :on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With1999-01-29029 January 1999
- on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With
ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors 05000317/LER-1998-009, :on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With1999-01-0808 January 1999
- on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With
ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative 05000317/LER-1998-008, :on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With1998-11-11011 November 1998
- on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With
ML20195D4271998-11-0505 November 1998 Safety Evaluation Supporting Amend 203 to License DPR-69 ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 1999-09-30
[Table view] |
Text
- _.
. ,' B ALTIMORE GAS AND ELECTRIC CALVERT CLIFFS NUCLEAR POWER PLANT 1650 CALVERT CLIFFS PARKWAY
- LUSBY. MARYLAND 20657-4702 CHARLES H. CRUSE
^ "
c vin rrs July 30, 1993 U.S. Nuclear Regulatory Commission Washington, D.C. 20555 ATTENTION: Document Cc.ntrol Desk
SUBJECT:
Calvert Cliffs Nuclear Power Plant Unit No. 1; Docket No. 50-317; License No. DPR 53 Licensee Event Report 93-005 TS 3.0.3 Entered, Due to Both Containment Spray Systems Inorerable The attached report is being c o nt to you as required under 10 CFR 50.73 guidelines. Should you have any questions regarding this report, we will be pleased to discuss them with you.
Very truly yours,
-f V CHC/RCG/bj d Attachment cc: D. A. Brune, Esquire J. E. Silberg, Esquire R. A. Capra, NRC D. G. Mcdonald, Jr. , NRC T. T. Martin, hTC P. R. Wilson, NRC R. I. McLean, DNR J. H. Walter, PSC Director, Office of Management Information and Program Control 9309040253 930730 030040- 3n f#,#j ADOCK 05000317 PDR >
S PDR gg
- N N NRC FORM 366 U. S. NUCLEAR REoVLATORY COMMISSION N *
- ESTMTED EURDEM FER ESFDPRITo COMFLYWITHTK3 NfC3MATION
- ** COLLECRON EOUEsT: 500 HFE FCMAFO COMMDRS EGARDWG Bm ESTmTE Tome EMMTON AND RECORDS MMAGEMENT LICENSEE EVENT REPORT (LER) LVWCH (MNBS 7714). U S NUCLEAR FEGULATORV FNMcW(
WASHirGTOtt DC 20'Hr0001. ANDTo THE PAPOWoHK FE. DUCTION PFulECT (See reverse for reauired number of diaits/ characters for each block) Q1500104) OFFICE OF M4%GEMENT AND BUDGET,WASHirGTOf( DC20'in FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
Calvert Clif f s, Unit 1 05000 317 1 OF 07 TITLE (4)
TS 3.0.3 Entered, Due to Both Containment Spray Systems inoperable EVENT DA1E (5) LER NUMBER (6) REPORT DATE (7) OTHER F ACILITIE S INVOLVED (8)
^' I MOMTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NUMBER 05000 06 30 93 93 - 005 -
00 07 30 93 05000 OPERATING THff REPORT tS SUDMfTTED PURSUANT TO THE REOUIREMENT9 OF 10 CFR -(Check one or more) f11)
MODE (9)
I 20.402(b) 20 405(c) 50 73(a)(2)(ev) 73 73 gy POWER 73 7DC)
LEVEL 100 20 405(a)(1)@ w.3c(c)(2) 2 73(a)(2)(vii) X mm CD) X 20.405(a)(1)(iii) 50 73(a)(2)(i) 50.73(a)(2)(viii)(A) (Speedy in Atatract below and in 20.405(a)(1)0v) Text, NRC Form 30/A) 50.73(a)(2)0i) 50.73(a)(2)(viii)(B) 20 405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER Dnclude Area Code)
R. C. Gradle, Compliance Engineer 401 260-3738 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE SYST E M COMPONENT ABE M CAUSE SYSTEM COMPONENT TURER NPRDS TURER NPRDS B CC V M120 Y SUPPLEME NTAL REPORT f YPECTED (14) EXPECTED MONTH DAY YEAR YES 8 "8 " '**' "
X No (if yes complete FXPFCTFD SUBMISSION DATF) DATE (15)
ABSIRAC1 (LJmit to 1400 spaces,i.e , approxamarely15 single 4p < t, pewntien hnes) (10) on June 30, 1993, at 2:00 p.m., Calvert Cliffs Unit 1 entered Technical Specification 3.0.3 for 45 minutes because both independent Containment Spray (CS) Systems were inoperable. No. 12 CS System was inoperable for scheduled maintenance. No. 11 CS System was determined to be inoperable because the outlet valve for component cooling water supplying its shutdown cooling heat exchanger was broken. Immediate corrective action restored No. 11 CS System to OPERABLE status while the Unit was at 100 percent power. This event l resulted in no public health or safety consequences.
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l The affected valve actuator had disconnected. We believe the actuator connecting linkage separated due to pivot locking plate failure. The replacement plcte subsequently cracked. Similar cracked plates were found on two identical Unit 2 valves. Plate material was a sintered alloy. The cracked plates were replaced with carbon steel plates. We plan to install carbon steel pivot locking plates on similar style valves. This report satisfies 10 CFR Part 21 requirements.
1 l
PRC Form 3E pg5
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 31504104 f! Lea EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE To COMPLY W!TH THIS INFoRMATioN CoufCTloN REQUEST: 50.0 HRS FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARCMG BURDEN ESTIMATE To THE INFoRMATON AND RECORDS MANAGEMENT BRANCH (MNBB 7714L U.S NUCLEAR TEXT CONTINUATION REcutAToRy CoMMssON. WASHINGTON. DC aosssmoi. AND To THE PAPERWORK REDUCTON PROJECT (31sG 0104L oFFCE oF MANAGEMENT AND BUDGET, WASHINGTON. DC 20503 F ACluTY NAME (1) DOCKET NUMBER A LER NUMBER @ PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
005 - 00 02 OF 07 TtxT y mo. .p.c. w.a. .m on.i wp.= or NRC ro, 38eA3 ci7)
I. DESCRIPTION OF EVENT On June 30, 1993, at 2:00 p.m. Calvert Cliffs Unit 1 entered Technical Specification (TS) 3.0.3 for 45 minutes because both independent Containment Spray (CS) Systems were inoperable. No. 12 CS System was inoperable for scheduled maintenance. No. 11 CS System was subsequently determined to be inoperable because the outlet valve for Component Cooling Water (CCW) supplying its shutdown cooling (SDC) heat exchanger was broken. Immediate corrective action restored No. 11 CS System to OPERABLE status while the Unit was at 100 percent power.
Technical Specification 3.6.2.1 Limiting Condition for Operation (LCO) for the CS System requires that two independent CS Systems and associated SDC heat exchangers be OPERABLE in Modes 1-3. The associated ACTION requirement for this LCO allows one CS System to be inoperable for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> ACTION limit for No. 12 CS System was entered on June 30, 1993, at 2:50 a.m.
when No. 12 Saltwater (SW) loop was removed fron service for scheduled maintenance. The removal of No. 12 SW loop also rendered one group of containment air coolers out of service.
On June 27, 1993, at 4:00 a.m., SDC was secured with No. 11 SDC heat exchanger CCW outlet control valve (1-CC-3828-CV) shut. This is the last time this valve was operated prior to June 30, 1993.
On June 30, post-maintenance flow testing of No. 13 CCW pump was in progress.
Control Room operators were aware that Control Room valve position indication for 1-CC-3828-CV was inoperable due to a broken open position indicator limit switch. When 1-CC-3828-CV was opened an expected increase in CCW flow did not occur. Immediate inspection of the valve, revealed that the connecting link from the actuator stem had disconnected from the vane arm. This failure rendered the valve inoperable in the shut position. The Control Room was immediately informed of the valve failure. With both CS Systems inoperable, the Snift Supervisor entered TS 3.0.3 at 2:00 p.m.
Plant engineering and maintenance personnel inspected the valve actuator linkage and discovered that the pivot locking plate, which resembles a square washer, was missing from the pivot screw (see Figure 1). The pivot screw is part of an assembly that connects the actuator connecting link to the valve vane arm.
Emergency maintenance was conducted on 1-CC-3828-CV. Replacement parts were obtained off a similar spare valve actuator and the valve was repaired and returned to service. Technical Specification 3.0.3 was exited at 2:45 p.m.
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ . _ _ _ _ _ _ _ . _.._____.___-__-.__-.__.___m_ _ _ . _ _ _ _ _ - _ _ . _ _ - - - _ .__._
NRC [ORM 36CA U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 per) EXPIRES 5/31/95 l ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS INFORMATON CoLLECTON REQUEST 60.0 HRS. FORWARD UCENSEE EVENT REPORT (LER) couuENTs ReGARaNo BURoEN ESTuATE To TwE mroRuATON :
AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U 8. NUCLEAR TEXT CONTINU ATION REGutATony couussON, wAsMuGroN. oC rosssoooi, ANo To THE PAPERWORK REDUCTON PROJECT (315CLO104), OFFICE oF j MANAGEMENT AND BUDGET, WASHINGTON, oC 20603.
F ACILITY NAME (1) DOCKET NUMBER (4 LER NUMBER (3) PAGE (4) ;
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
005 - 00 03 OF 07 TEXT Of more space a requited, use aoMonal copees of NRC Form 366A) (17)
II. CAUSE OF EVENT The immediate cause of this event was the separation of the valve actuator connecting link from the valve vane arm. We believe that the pivot locking .
plate on 1-CC-3828-CV cracked in half allowing the connecting linkage to slip !
free of the vane arm. ,
l On June 30, 1993, a visual inspection was conducted on the identical Unit 2 valves (2-CC-3828-CV and 2-CC-3830-CV). Both valves were found to have cracks in their pivot locking plates. The Shift Supervisor was informed and maintenance orders were issued to replace these pivot locking plates.
Ten other similar style safety-related valves were identified in the Unit 1 and ;
Unit 2 CCW and Service Water (SRW) Systems. These valves were visually inspected on June 30, 1993, and no cracks were found.
On July 9 and 10, 1993, the cracked pivot locking plates on 2-CC-3828-CV and i 2-CC-3830-CV, were replaced. The old cracked plates were mistakenly discarded, i so the opportunity was lost to perform a metallurgical failure analysis. l I
Replacement plates were purchased from the vendor as non-stock commercial grade ;
and were dedicated for use as safety-related items. Critical characteristics for the plate described the material as either carbon steel or sintered iron copper alloy. The same part number (370295-111-779) applies to both materials.
During receipt inspection both plates were verified to be ferrous material.
Discussions with the vendor revealed that they currently supply only carbon steel pivot locking plates with improved ductility characteristics under this part number. They stated that in October 1989, a drawing change was made to include carbon steel as a material for the plates.
On July 2 a small crack in the replacement pivot locking plate for 1-CC-3828-CV was discovered. This plate had been obtained from a similar spare valve assembly on June 30. A maintenance order was issued to replace this pivot locking plate. ,
On July 22, 1993, the cracked pivot locking plate on 1-CC-3828-CV was replaced with a carbon steel pivot locking plate. The replaced plate had two cracks oriented 90 degrees apart and was verified to be sintered alloy material. A detailed failure analysis on the replaced plate identified the brittle nature of the material as susceptible to this type of inservice failure.
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NRC FORM 36CA U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (sea EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE To COMPLY WW THIS INFoRMATON CodICTON REQUEST 50 0 HMS FORWARD ,
LICENSEE EVENT REPORT (LER) CouuEwTS ReoARDiNG BURDEN tsnuATE To THE iNFoRuaTON i AND RECORDS MANAGEMENT BRANCH {MNBB 7714L U.S. NUCLEAR !
TEXT CONTINUATION REovuToRY Couw SSON. WASHINGTON. oC asseooi, AND To ,
THE PAPERWORK REDUCTON PROJECT Cit 60-0104), OFFICE OF j UANAGEMENT AND BODGET, WASHINGTON. DC 20$C3 F ACluTY NAME (1) DOCKET NUMBER (a LER NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
005 -
00 04 0F 07 TEXT y mo,. .o.r a,.o. o .ooit on.i cop or Nrc Form assA) tit) t A review of previous maintenance orders was conducted for the eight similar CCW ;
control valves, but did not identify any previous valve inoperability due to -
failed pivot locking plates. We also conducted two historical queries of the Nuclear Plant Reliability Data System (NPRDS) under the general valve model number (34000) and the valve actuator (Case No. 18L, 37-18), but no pivot t locking plate failures were identified. ,
III. ANALYSIS OF EVENT The CS System is designed to provide sufficient heat removal capability to ,
maintain containment pressure and temperature below established design values i following a loss-of-coolant accident (LOCA). Each CS System consists of a 50 percent capacity pump, a SDC heat exchanger, and a spray header. The SDC heat exchanger is cooled by the CCW System. After a LOCA, suction for the CS pumps is taken directly from the refueling water tank and discharged through the SDC heat exchangers to containment.
The CS System is redundant to the Containment Air Cooling System which consists of two independent groups of containment air coolers, with two units in each ;
group cooled by a SRW System. With three of four cooling units in operation, the Containment Air Cooling System provides the same heat removal capability as ,
the two CS Systems.
The short time that both CS Systems and one group of containment air coolers was inoperable resulted in no public health or safety consequences. The safety significance of this event was minimized based on the following.
The scenario of concern is a LOCA concurrent with a loss of offsite power (IDOP), a highly unlikely scenario. We have identified that 1-CC-3828-CV was shut from the Control Room on June 27, 1993. Thus, the maximum hypothetical time of CS System inoperability concurrent with one group of inoperable containment air coolers is limited to the approximate 12-hour period following the securing of No. 12 SW loop and the restoration of 1-CC-3828-CV to OPERABLE status. The probability of such an event occurring in so short a period of time was extremely low.
This event is considered reportable in accordance with 10 CFR 50.73(a)(2)(1)(B),
10 CFR 50.73(a)(2)(v), and 10 CFR Part 21.
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 313 0104 f5 e2) EXPIRES 5/31/95 ESTIMATED BURDEN PER NBPoNSE TO COMPLY WlTH THIS INFoRMATiON COLLECTON REQUEST: SO 0 HRS. FORWARD LICENSEE EVENT REPORT (LER) CouuCNTs REsAmNG BURDEN EsTiuaTE To THE iNroRuAfoN AND RECoRDB MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR TEXT CONTINUATION REGULATORY COMMSSON. WASHWGToN, DC 205554xH, AND TO THE PAPERWORK REDUCTON PROJECT (31500104), oFFtCE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20$03.
F ACluTV NAME (1) DOCKET NUMBER (2) LER HUMBER (3) PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
005 -
00 05 0F 07 TtxT e mm..p.c ..w.o. .amons cop or NRC r awn on IV. CORRECTIVE ACTIONS Immediate corrective actions are completed as follows:
A. The CCW outlet valve actuator connecting link assembly from No. 11 SDC heat exchanger was replaced and TS 3.0.3 was exited at 2:45 p.m. on June 30, 1993.
B. The pivot locking plates on Unit 2 CCW valves for 21 and 22 SDC heat exchangers were replaced with carbon steel pivot locking plates on July 9 and 10,1993.
C. The appropriate maintenance personnel were sensitized to the importance of retaining the replaced, cracked pivot locking plate ;
for failure analysis.
Actions to prevent recurrence include:
A. On July 22, 1993, a carbon steel pivot locking plate was installed on 1-CC-3828-CV. I 1
B. Sintered alloy plates will be replaced with carbon steel pivot locking plates on other similar style safety-related valves in the plant.
C. The stock description for this pivot locking plate has been revised I such that only carbon steel pivot locking plates will be accepted in the future.
D. An Issue Report was generated concerning the inadvertent discarding of the cracked locking plates for 2-CC-3828-CV and 2-CC-3830-CV.
Corrective action to preclude this problem from recurring will be taken in accordance with our corrective action process. )
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' NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 maa EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE To COMPLY WITH THIS INFoRMATION COLLECTION REQUEST: 20 HRS. FORWARD UCENSEE EVENT REPORT (LER) CouuENTs REcAFoNG BuRoEN tsTiuATE To THE iNroRMATiON AND RECORDS MANAGEMENT BRANCH (MNB0 7714), U.S. NUCLEAR TEXT CONTINUATlON REGULATORY COMMISS40N, WASHINGTON, DC 2055540, AND To THE PAPERWORK REDUCTION PROJECT (3150 c104). OFFICE oF MANAGEMENT AND BUDGET, WASHINGTON, DC 23503, F ACILITY NAME (1) DOCKET NUMBER (33 LER NUMBER (3) PAGE (4)
Calvert Cliffs, Unit 1 05000 3 1 7 93 -
005 - 00 06 0F 07 TEXT pf more space is requued, peo addMkmal copese of NRC Form 36eA) (17)
V. ADDITIONAL INFORMATION A. Identification of Components and Systems referred to in this LER:
IEEE 803A/83 IEEE 805/84 Component or System Function ID System ID Containment Spray System N/A BE Component Cooling Water System N/A CC Saltwater System N/A BI Service Water System N/A BI' Containment Fan Cooling System N/A BK Pump P N/A Valve V N/A ;
Heat Exchanger HX N/A Cooler CLR N/A B. Previous Similar Events: I There has been one previous similar event involving entry into TS <
3.0.3 due to a concurrent inoperability of both CS Systems, but the !
cause is not related to this event. Details of the previous event I were provided in LER 318/92-002.
The valves which experienced pivot locking plate cracking are Masonellan model number 37-34211. The part number for the pivot locking plate is 370295-111-779. The vendor stated that carbon steel pivot locking plates have square edges and pivot locking plates made of sintered iron carbon alloy have rounded edges.
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HRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO.3150-0104 as21 EXPIRES 5/31/95 ESTIMATED BUFOEN PER e4ESPONSE TO COMPLY WriH THIS it#0RMATON COLLECTON REQUEST: 50 o HHS. FORWARD LICENSEE EVENT REPORT (LER) coMuEurs REaAroNo suRDEN EsTiMAtt TO THE wORuATON AND RECORDS MANACEMENT BRANCH (MNBB 7714) U.S. NUCLEAR TEXT CONTINUATION HEGULATORY COMMIC3ON WWUNGTON. DC 20555@01, AND TO THE PAPERWORK REDUC'ON PROJECT (31BC104). OFFCE OF MANAGEMENT AND BUDGET. W ASHINGTON. DC 20$03.
F ACluTY NAME (9) DOCKETNUMBER Q LER NUMBER (3) PAGE l4)
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FIGURE 1 34000 Butterfly Valves with 1-1/2" -- 4" Stroke Actuators PARTS REFERENCE No. Part Name No. Part No. No. Part No.
- 1. Body 13 Lock Washer 25. Clevis I
- 2. Vane 14. Body Cap Screw 26. Lock Nut
'3. Elastorner Liner 15 Bushing 27. Actuator Stem
- 4. Vane Shaft 16. Setscrew 28. Actuator Mounting Plate
- 5. Teper Pina 17. Key 29. Cap Screw
'6. Vane Shaft Bushing 18. Vane Arm 30. Lock Washer
'7. Pm nng 19. Pivot Screw 31. Nut
- 8. Pe:6ng Box Gland 20. Pivot Locking Plate 32. Cotter Pin
- 9. Gland Flange Stud 21. Castle Nut
- 10. Giand Fiange 22. Cotter Pan
- 11. Gland Flange Nut 23 Connecting Lie -
- 12. Actuator Mounting Bracket 24 Clevis Psn
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