05000318/LER-1980-009-03, /03L-0:on 800131,while Conducting Routine Test, Control Element Assembly (CEA) 32 Dropped Into Core.Cause Unknown.Technician Will Be Assigned During Next STP 0-29 to Monitor Operating Parameters of All CEAs on real-time Basi

From kanterella
(Redirected from ML19294B745)
Jump to navigation Jump to search
/03L-0:on 800131,while Conducting Routine Test, Control Element Assembly (CEA) 32 Dropped Into Core.Cause Unknown.Technician Will Be Assigned During Next STP 0-29 to Monitor Operating Parameters of All CEAs on real-time Basis
ML19294B745
Person / Time
Site: Calvert Cliffs 
Issue date: 02/29/1980
From: Bauer E, Davis S
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19294B743 List:
References
LER-80-009-03L-01, LER-80-9-3L-1, NUDOCS 8003050454
Download: ML19294B745 (2)


LER-1980-009, /03L-0:on 800131,while Conducting Routine Test, Control Element Assembly (CEA) 32 Dropped Into Core.Cause Unknown.Technician Will Be Assigned During Next STP 0-29 to Monitor Operating Parameters of All CEAs on real-time Basis
Event date:
Report date:
3181980009R03 - NRC Website

text

(7 771 LICENSEE EVENT REPORT control BLOCK: l l

l l

l l

lh (PLEASE PRINT oR TYPE ALL REQUIREo !NFORMATioN) 1 6

l MI ol cl cl Ni 2 l@l 0101 l 0101010101 10 0 @l4lllllllll@l I

l@

o i

UCENsE NUM8ER 25 26 LICENSE TYPE JO 5 7 CAT 58 7

8 9 LICENSEE COoE 14 con'T s 0 "c' l L j@l 0] 5 ] 0 l 0 ] 013 l 1 l 8 l@l 0 l 1 l 3 l l l 8 ] 0 }@l 0 l 2 l 2 l 9 l 8 0l@

o 7

8 60 61 oOCKET NUMBER 68 69 EVENT oATE 74 75 REPORT oATE 80 EVENT DESCRIPTION AND pro 8 ABLE CONSEQUENCES h l At 2212 while conductina a routine test, control element assembly (CEA) 32 i

o 2

i droceed into the core.

Reactor power was reduced to < 70% within one hour i

o 3

I cer T.S. 3.1.3.1.

CEA 32 was withdrawn to its group at 2350. All other l

o 4

l CEA's remained operable. As a result of the dropped CEA, Azimuthal Tilt l

0 s

l (TO) exceeded T.S. 3.2.4 limit of 0.03 at 0016 on 2/1/80. Tg returned to o

e l less than 0.03 at 0315 on 2/1/80.

I o

7 l

O 8

l su'8cIo'E sEEE

'cOI:'E

"#'d!

st 8c'$'E

'^

C0 couPONENT cooE lR lB l@ l Xl@ l Zl@ lZ lZ l Z j Z j Z j Z l@ lX l@ lZ l@

o 9

7 8

9 to 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVislON LER EVENT YEAR R EPORT NO.

COO 6' TYPE N O.

@ sug/RO l8l0l l-l 10l0l9l l/l l0l3l lL l l_]

l0l RE

,, 21 22 23 24 26 27 28 29 30 31 32 K N AC 0 ON P NT ME HoVRs 22 sB 1 POR S.

suPPLIE MANUFAC RER LZ,l@l X I@

lBl@

lZl@

l0l0l0l l W g lfl]g lZl@

lCl4l9l0lg 3J 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l It is not known at this time why CEA 32 dropped. The rod was raised i

i o

ITTTI I by the operator 68 minutes after it dropped.

It is planned during the I next STP 0-29 to have a technician monitor the operatino carameters of all i

2 l CEA's on a real-time basis in order to look for any intennittent problems l

i 3

~

i 4

l and take corrective action.

l oTHER status @ oisEOMRv' oiscovERv oEscRiPTiON @

's2E"s sPOwER l E l@ l l l 0 l 0 l@l NA l

lAl@l Operator Observation l

i s

80 A TIVITY CO TENT EgEAs AMOUNTgACnVITY @

RE Eo P NA j

7 8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUM8ER TYPE oEsCRIPTION 101010l@lZl@l N

l i

7 So PERsONN E L i~;ULs oEscRino~@

NUMBER lo 10 lo l@l NA l

i a

7 8 9 11 12 go

'ivi'E Esc"^PT O~ '^ "" @

8o03os e 4jr5a

' " ^

/ l l"1"Til Z l@l NA 7

8 9 10 go oEscRienON @

NRC USE ONLY ITITILN]E81 NA Illlllllllll{

issu 68 69 80 ;

7 8 9 10 (301)269-4742/4728 2

NAME oF PREPARER PHONE:

LER NO.

80-09/3L DOCKET NO.

50-318 EVENT DATE 01/31/80 REPORT DATE 02/29/80 ATTACH!1ENT EVENT DESCRIPTION Afl0 PROBABLE CONSEOUEi!CES:

(CONTINUED)

Tg returned to less than 0.03 at 0315 on 2/1/80.

Planar Radial and Integrated Radial Peaking Factors remained within Technical Specifi-cation limits.

LER's 79-03 (U-1) and 80-06 (U-1) describe similar events.