IR 05000336/2005005

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IR 05000336-05-005, 05000423-05-005; 10/01/2005 - 12/31/2005; Millstone Power Station, Units 2 and 3; Correction of Emergency Preparedness Weaknesses and Deficiencies, Other Activities
ML060330755
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 02/02/2006
From: Paul Krohn
NRC/RGN-I/DRP/PB6
To: Christian D
Dominion Resources
References
IR-05-005
Download: ML060330755 (63)


Text

ary 2, 2006

SUBJECT:

MILLSTONE POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000336/2005005 AND 05000423/2005005

Dear Mr. Christian:

On December 31, 2005, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Millstone Power Station Units 2 and 3. The enclosed inspection report documents the inspection results, which were discussed on January 19, 2006, with Mr. J. Alan Price and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents two NRC-identified findings of very low safety significance (Green).

One of these findings was determined to involve a violation of NRC requirements. However, because of its very low safety significance and because it has been entered into your corrective action program, the NRC is treating this issue as a Non-Cited Violation (NCV), in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the NCV, you should provide a response within 30 days of the date of these inspection reports, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Millstone Power Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Paul G. Krohn, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos.: 50-336, 50-423 License Nos.: DPR-65, NPF-49 Enclosure: Inspection Report 05000336/2005005 and 05000423/2005005 w/Attachment: Supplemental Information cc w/encl:

J. A. Price, Site Vice President, Millstone Station C. L. Funderburk, Director, Nuclear Licensing and Operations Support D. W. Dodson, Supervisor, Station Licensing L. M. Cuoco, Senior Counsel C. Brinkman, Manager, Washington Nuclear Operations J. Roy, Director of Operations, Massachusetts Municipal Wholesale Electric Company First Selectmen, Town of Waterford R. Rubinstein, Waterford Library B. Sheehan, Co-Chair, NEAC E. Woollacott, Co-Chair, NEAC E. Wilds, Director, State of Connecticut SLO Designee J. Buckingham, Department of Public Utility Control G. Proios, Suffolk County Planning Dept.

R. Shadis, New England Coalition Staff G. Winslow, Citizens Regulatory Commission (CRC)

S. Comley, We The People D. Katz, Citizens Awareness Network (CAN)

R. Bassilakis, CAN J. M. Block, Attorney, CAN P. Eddy, Electric Division, Department of Public Service, State of New York P. Smith, President, New York State Energy Research and Development Authority J. Spath, SLO Designee, New York State Energy Research and Development Authority

SUMMARY OF FINDINGS

IR 05000336/2005-005, 05000423/2005-005; 10/01/2005 - 12/31/2005; Millstone Power

Station, Units 2 and 3; Correction of Emergency Preparedness Weaknesses and Deficiencies,

Other Activities.

The report covered a 3-month period of inspection by resident inspectors and announced inspections by regional inspectors. One (Green) NCV was identified and one (Green) finding was identified. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Unit 3

!

Green.

The inspectors identified a violation of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, for the failure to properly assess compensatory actions and to take timely actions to correct the introduction of water into the Unit 3 B EDG rocker arm (RA) lubricating oil (LO) system. Following the discovery of elevated water content in the B EDG RA LO system on June 17, 2005, and the determination on July 11, that the EDG was fully qualified, Dominion; 1) did not specify compensatory actions to ensure the EDG was maintained in a fully qualified status while the degradation continued to exist, 2) did not establish a threshold for water content in the RA LO system beyond which the EDG would be considered inoperable, and 3) did not schedule the timely completion of maintenance activities to correct the in-leakage. While Dominion took several actions in response to the discovery of water in the LO system, these actions were not sufficient to preclude the development of significant water leakage into the RA LO system which resulted in the subsequent declaration of inoperability of the EDG on September 27, 2005, and the unavailability of the B EDG for approximately 5 days while corrective maintenance was performed. This finding is related to the cross-cutting area of problem identification and resolution in that, once the source of the water contamination had been identified, Dominion did not properly assess compensatory actions and take effective corrective actions to preclude significant water in-leakage into the B EDG RA LO system.

The finding was more than minor because it affected the equipment performance attribute of the mitigating system cornerstone and the availability and reliability of the B EDG to respond to initiating events. The inspectors determined that this finding was of very low safety significance because the finding was not a design or qualification deficiency, did not represent a loss of safety system function, did not represent an actual loss of safety function of a single train or one or more iii non-technical specification trains based on a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> probabilistic risk assessment mission time, and did not screen as potentially risk significant due to seismic, flooding, or severe weather initiating events. (Section 4OA5.2).

Cornerstone: Emergency Preparedness (EP)

Unit 2 and Unit 3

!

Green.

The inspector identified a Green finding for the failure to take effective corrective actions in that since 2004, on several occasions, staff assigned to the site emergency response organization (SERO) did not maintain their qualifications current. The corrective actions taken to prevent recurrence of this problem were not effective as highlighted by repeat examples of lapsed SERO qualifications. Individuals identified during the inspection with the lapsed qualifications were immediately removed from the SERO callout system until their training was completed. The cause of the finding is related to the cross-cutting element of problem identification and resolution in that the corrective actions taken were not effective in preventing reoccurrence.

The finding is more than minor because it is associated with the EP cornerstone attribute of emergency response organization readiness (training). It affects the cornerstone objective of ensuring the capability to implement measures to protect the health and safety of the public during an emergency. Specifically,

Dominions corrective actions to ensure personnel maintained their SERO qualifications current were ineffective and did not prevent recurrence. This finding is not suitable for SDP evaluation, but has been reviewed by NRC management and is determined to be a finding of very low safety significance.

(Section 1EP5).

Licensee-Identified Violations

None.

iv

REPORT DETAILS

Summary of Plant Status

Unit 2 operated at essentially 100 percent power for the duration of the inspection period with two exceptions. On November 8, 2005, operators reduced power to 94 percent for a planned outage of the B intake bay. Operators returned the unit to 100 percent power on November 10, 2005. On November 15, 2005, operators reduced power to 95 percent for a planned outage of the C intake bay. The unit was restored to 100 percent power on November, 16, 2005, and operated at essentially 100 percent power for the remainder of the inspection period.

Unit 3 began the inspection period shutdown for the 3R10 refueling outage. Unit 3 achieved criticality and synchronized to the grid on October 27, 2005, and then performed power ascension activities achieving full power on October 31, 2005. On November 2, 2005, Operations reduced power to 95 percent to repair a small steam leak on the first point feedwater heater. On November 4, 2005, Operations returned the unit to 100 percent power.

On December 1, 2005, Operations conducted a downpower in response to a reactor coolant system leak. During the downpower, the turbine generator exhibited increased vibrations and operators manually tripped the turbine. The reactor then tripped on low C steam generator water level. The unit achieved criticality on December 4, 2005, and returned to full power on December 6, 2005. On December 14, 2005, the unit conducted a downpower to 50 percent power due to degraded intake structure conditions. The unit was restored to 100 percent power on December 15, 2005, and operated at essentially 100 percent power for the remainder of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection

.1 Seasonal Site Inspection (One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

The inspectors performed a review of cold weather preparations during the onset of the cold weather season to evaluate the sites readiness for seasonal susceptibilities for both Unit 2 and Unit 3. The inspectors reviewed Dominions preparations/protection for cold weather and its impact on the protection of safety-related systems, structures and components. The inspection was intended to ensure that the indicated equipment, its instrumentation, and its supporting structures were configured in accordance with Dominions procedures and that adequate controls were in place to ensure functionality of the systems. The inspectors reviewed Dominions procedure which implements their cold weather protection program to determine if procedural expectations were being met. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

.2 System Inspection (One Unit 3 Sample)

a. Inspection Scope

The inspectors reviewed one sample of the readiness of the Unit 3 emergency core cooling system for extreme weather conditions, specifically, cold weather preparation.

The inspection was intended to ensure that the indicated equipment, its instrumentation, and its supporting structures were configured in accordance with Dominion procedures and that adequate controls were in place to ensure functionality of the system. The inspectors reviewed licensee procedures and walked down the system. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R02 Evaluations of Changes, Tests, or Experiments (71111.02 - Thirty one samples)

a. Inspection Scope

The inspectors reviewed 11 safety evaluations (SEs), all of which were either issued during the past two years or associated with plant modifications that were completed during the past two years. The SEs reviewed were in the Initiating Event, Mitigating Systems, and Barrier Integrity cornerstones. The selected SEs were reviewed to verify that changes to the facility or procedures as described in the Updated Final Safety Analysis Reports (UFSAR) were reviewed and documented in accordance with 10 CFR 50.59, and that the safety issues pertinent to the changes were properly resolved or adequately addressed. The reviews also included the verification that Dominion had appropriately concluded that the changes and tests could be accomplished without obtaining license amendments. The SEs reviewed are listed in the Attachment.

The inspectors also reviewed 20 screen evaluations for changes, tests and experiments for which Dominion determined that SEs were not required. This review was performed to verify that Dominions threshold for performing SEs was consistent with 10 CFR 50.59. The listing of the screened-out evaluations reviewed is provided in the

.

In addition, the inspectors reviewed the administrative procedures that were used to control the screening, preparation, and issuance of the SEs to ensure that the procedure adequately covered the requirements of 10 CFR 50.59.

c. Findings

No findings of significance were identified.

1R04 Equipment Alignment

Partial System Walkdowns (71111.04Q - Three Unit 2 Samples and Three Unit 3 Samples)

a. Inspection Scope

The inspectors performed six partial system walkdowns during this inspection period.

The inspectors reviewed the documents listed in the Attachment to determine the correct system alignment. The inspectors conducted a walkdown of each system to verify that the critical portions of selected systems were correctly aligned in accordance with these procedures and to identify any discrepancies that may have had an affect on operability. The inspectors verified that equipment alignment problems that could cause initiating events, impact mitigating system availability or function, or affect barrier functions, were identified and resolved. The following systems were reviewed based on their risk significance for the given plant configuration:

Unit 2

  • Partial equipment alignment of the turbine-driven auxiliary feedwater system, October 19, 2005; and
  • Partial equipment alignment of the service water system, October 20, 2005.

Unit 3

  • Partial equipment alignment of the A motor-driven auxiliary feedwater system while the turbine-driven feedwater system was out of service for maintenance, October 26, 2005; and
  • Partial equipment alignment of the B quench spray system following maintenance, October 27, 2005.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

Quarterly Sample Review (71111.05Q - Six Unit 2 Samples and Six Unit 3 Samples)

a. Inspection Scope

The inspectors performed twelve walkdowns of fire protection areas during the inspection period. The inspectors reviewed Dominion's fire protection program to determine the required fire protection design features, fire area boundaries, and combustible loading requirements for the selected areas. The inspectors walked down these areas to assess Dominion's control of transient combustible material and ignition sources. In addition, the inspectors evaluated the material condition and operational status of fire detection and suppression capabilities, fire barriers, and any related compensatory measures. The inspectors then compared the existing conditions of the inspected fire protection areas to the fire protection program requirements to ensure all program requirements were being met. Documents reviewed during the inspection are listed in the Attachment. The fire protection areas reviewed included:

Unit 2

  • High Pressure Safety Injection (HPSI) Pump Room, Auxiliary Building, -45'-6" Elevation (Fire Area A-4);
  • Low Pressure Safety Injection (LPSI) Pump Room, Auxiliary Building, -45'-6" Elevation (Fire Area A-3);
  • Containment Spray and HPSI/LPSI Pump Room, Auxiliary Building, -45'-6" Elevation (Fire Area A-8, Zone A);
  • Reactor Building Closed Cooling Water Pump and Heat Exchanger Area, Auxiliary Building, -25'-6" Elevation (Fire Area A-1, Zone B);
  • Diesel Generator Room A, Auxiliary Building, 14'-6" Elevation (Fire Area A-15);and
  • Diesel Generator Room B, Auxiliary Building, 14'-6" Elevation (Fire Area A-16).

Unit 3

  • East Motor Control Center and Rod Control Area, Auxiliary Building, 4'-6, 24'-6",

and 43'-6" Elevation (Fire Area AB-5);

  • Containment Structure, -24'-6" thru 51'-4" Elevation (Fire Area RC-1);
  • East Fuel Oil Vault, 14'-6" Elevation, (Fire Area EG-1);
  • Station Blackout Diesel Generator Fuel Oil Storage Tank, 24'-6" Elevation (Fire Area SBO-2).

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures (71111.06 - One Unit 2 Sample)

Internal Flooding Inspection

a. Inspection Scope

The inspectors reviewed one sample of flood protection measures for equipment in the safety related room listed below. This review was conducted to evaluate Dominions protection of the safety-related system from internal flooding conditions. The inspectors performed a walkdown of the area, reviewed the Final Safety Analysis Report, the internal flooding evaluation and related documents. The inspectors compared the as-found equipment and conditions to ensure that they remained consistent with those indicated in the design basis documentation, flooding mitigation documents, and risk analysis assumptions. Documents reviewed during the inspection are listed in the

.

Unit 2

b. Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities (71111.08P - Two Unit 3 Samples)

a. Inspection Scope

The purpose of this inspection is to assess the effectiveness of Dominions program for monitoring degradation of vital system boundaries including the reactor coolant system and other risk significant systems. The inspectors assessed the inservice inspection activities using the criteria specified in the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code. During this inspection period, no sample reviews were conducted because there were no recordable indications accepted for continued service during the previous refueling outage.

The inspectors observed in-process non-destructive examination (NDE) activities, reviewed documentation and interviewed personnel to verify that the activities were performed in accordance with the ASME Boiler and Pressure Vessel Code Section XI requirements. The sample selection was based on the inspection procedure objectives and risk priority of those components and systems where degradation would result in a significant increase in risk of core damage. The inspectors reviewed a sample of condition reports to assess Dominions effectiveness in problem identification and resolution. The specific inspection activities included:

  • Radiographic Test (RT) of pressurizer head safety nozzle penetrations 03X5644-A-T and 03X5648-B-T, bi-metallic welds attaching nozzle to the safe end on the pressurizer, carbon steel to stainless steel, RT tested using Procedure VPROC-ISI00-00 Rev 0. Acceptance criteria of ASME Section XI, 1989 edition.
  • Ultrasonic Test (UT) of Main Steam System (MSS), field weld MSS-31-FW-6, 8 inch diameter pipe to pipe butt weld, carbon steel to carbon steel, ASTM A 106 Grade B, UT tested using Procedure MP-PDI-UT-1, Rev 2. Acceptance criteria is all indications are reported for evaluation.
  • Penetrant Test (PT) of Auxiliary Feedwater System, 16 inch diameter butt weld, field welds FWS-11-FW-70 and FW-72, carbon steel to carbon steel, SA 106 Grade C to SA 216 Grade WCB and SA 234 Grade WPC to SA 106 Grade C respectively, PT tested using procedure MP-LP-4, Rev 04. Acceptance criteria of ASME Section XI, 1989 edition.
  • Magnetic Particle Test (MT) of MSS, field weld MSS-31-FW-6, 8 inch diameter butt weld, pipe to pipe, carbon steel to carbon steel, ASTM 106 Grade B, MT tested using procedure MP-MT-1, Rev 03. Acceptance criteria of ASME Section XI, 1989 edition.

Additionally, the inspectors reviewed the Millstone Unit 3 Steam Generator Eddy Current Data Analysis Reference Manual to determine whether selected steam generator tube inspections were performed consistent with the Electric Power Research Institute (EPRI)

Pressurized Water Reactor Steam Generator Examination Guidelines. The inspectors reviewed and compared the Millstone Unit 3 Steam Generator Integrity Degradation Assessment to the EPRI Steam Generator Aging Management Guidelines. The inspectors reviewed the retrieval of a small section of bare metal weld wire located in the secondary side of one steam generator. The discovery was discussed with the steam generator inspection program manager. The loose part condition was entered into the corrective action program and the loose part was removed from the steam generator.

Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Requalification Activities Review by Resident Staff (71111.11Q - One Unit 2 Sample and

One Unit 3 Sample)

a. Inspection Scope

The inspectors observed one sample of Unit 2 licensed operator simulator training on November 17, 2005, and one sample of Unit 3 licensed operator simulator training on November 18, 2005. The inspectors verified that the training evaluators adequately addressed that the applicable training objectives had been achieved. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

.2 Biennial Review by Regional Specialist (71111.11B - One Unit 2 Sample and One Unit 3

Sample)

a. Inspection Scope

An inspector performed inspection activities from October 31, 2005, to November 2, 2005, using Inspection Procedure Attachment 71111.11, Licensed Operator Requalification Program, and NRC Manual Chapter 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP), as acceptance criteria to evaluate conformance with simulator requirements specified in 10 CFR 55.46. This inspection focused primarily on assessment of the effectiveness of the facility licensee's process for continued assurance of simulator fidelity with regard to identifying, reporting, correcting, and resolving simulator discrepancies via a corrective action program. In particular, the inspection concentrated on followup of several previously documented simulator fidelity concerns, including the following:

  • deficiencies associated with the April 17, 2005, event involving a reactor trip and safety injection;
  • an unresolved item related to several simulator deficiencies identified during development and administration of the March 2005 Millstone Unit 2 initial license examination (URI 05000336/2005301-01);
  • an unresolved item related to simulator scenario-based testing methodology (URI 05000336 and 05000423/2005008-01); and
  • an unresolved item related to simulator demonstration of expected plant response (05000423/2005008-02).

Additionally, an inspection followup was conducted to evaluate licensee actions related to an unresolved item on technical specification requirements for nuclear instrument operability (URI 05000336/2005301-02).

A sample of simulator deficiency reports (DRs) closed in 2004 and 2005 were reviewed for the scope of each deficiency and the effectiveness of corrective actions.

On December 20, 2005, an inspector conducted an in-office review of licensee annual operating test results for 2005. The inspection assessed whether pass rates were consistent with the guidance of NRC Manual Chapter 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process. For both units, the inspectors verified that:

  • Crew failure rate was less than 20 percent (Crew failure rate was 8.5 percent);
  • Individual failure rate on the dynamic simulator test was less than or equal to 20 percent (Individual failure rate was 0 percent at both units);
  • Individual failure rate on the walk-through test was less than or equal to 20 percent (Individual failure rate was 0 percent); and
  • Overall pass rate among individuals for all portions of the exam was greater than or equal to 75 percent (Overall pass rate was 91.5 percent).

b. Findings

No significant findings were identified.

1R12 Maintenance Effectiveness (71111.12 - Two Unit 2 Samples and Two Unit 3 Samples)

Routine Maintenance Effectiveness Inspection (71111.12Q)

a. Inspection Scope

The inspectors reviewed four samples of Dominion's evaluation of degraded conditions, involving safety-related structures, systems and/or components for maintenance effectiveness during this inspection period. The inspectors reviewed licensee implementation of the Maintenance Rule (MR), 10 CFR 50.65, and verified that the conditions associated with the referenced condition reports (CRs) were appropriately evaluated against applicable MR functional failure criteria as found in licensee scoping documents and procedures. The inspectors also discussed these issues with system engineers and maintenance rule coordinators to verify that they were appropriately tracked against each system's performance criteria and that the systems were appropriately classified in accordance with MR implementation guidance. Documents reviewed during the inspection are listed in the Attachment. The following conditions were reviewed:

Unit 2

Unit 3

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - Three Unit 2

Samples and Five Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed eight samples of the adequacy of maintenance risk assessments of emergent and planned activities during the inspection period. The inspectors utilized the Equipment Out of Service quantitative risk assessment tool to evaluate the risk of the plant configurations and compared the results to Dominion's stated risk. The inspectors verified that Dominion entered appropriate risk categories and implemented risk management actions as necessary. Documents reviewed during the inspection are listed in the Attachment. The inspectors verified the conduct and adequacy of scheduled maintenance risk assessments for plant conditions affected by the conduct of the following maintenance and testing activities:

Unit 2

  • Risk assessment for work scheduled on October 5, 2005;
  • Risk assessment for work scheduled on October 12, 2005; and
  • Risk assessment for work scheduled on October 25, 2005.

Unit 3

  • Shutdown safety assessment scheduled on October 4, 2005;
  • Shutdown safety assessment scheduled on October 9, 2005;
  • Shutdown safety assessment scheduled on October 17, 2005;

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Evolutions and Events (71111.14 - Four Unit

3 Samples)

a. Inspection Scope

The inspectors reviewed four samples of events on Unit 3 that demonstrated personnel performance in coping with non-routine evolutions and transients. The inspectors observed operations in the control room and reviewed applicable operating and alarm response procedures, technical specifications, plant process computer indications, and control room shift logs to evaluate the adequacy of Dominion's response to these events. The inspectors also verified the events were entered into the corrective action program to resolve identified adverse conditions. Documents reviewed during the inspection are listed in the Attachment.

Unit 3

  • On October 19, 2005, Operations commenced a vacuum fill on the A loop in accordance with Operating Procedure 3216, Reactor Coolant System Drain IPTE, during the 3R10 outage. While operators were attempting to draw a vacuum on the A loop, they noticed water in the vacuum pump hoses and stopped the vacuum pump. Dominion conducted an investigation and discovered that the A loop drain path was isolated and therefore unable to provide an adequate drain path. Operators drained approximately 3000-4000 gallons from the A loop and successfully drew a vacuum on the A loop and filled the loop on October 21, 2005.
  • On October 27, 2005, Operations personnel responded to an unexpected reduction in primary plant pressure during a plant startup. During the transient, primary plant pressure dropped from the normal operating system pressure (2250 psig) to 2206 psig. The station entered Technical Specification (TS) 3.2.5, Departure from Nucleate Boiling (DNB) Parameters, since primary plant pressure dropped below the DNB Technical Specification limit of 2218 psig.

Control room operators took prompt action and restored pressure to above the DNB limit in approximately three minutes and exited the Limiting Condition of Operation. Dominion determined that the pressure drop was caused by the main turbine load set controller, operating in load set mode, responding to a high grid frequency transient. There were no safety consequences associated with the transient.

  • On November 2, 2005, Operations personnel discovered a small turbine building steam leak coming from a steam supply to the first point feedwater heater. The inspectors observed a 6" steam plume leaking around a 1/2" test connection plug located on top of a non-return check valve. Dominion evaluated the steam leak and decided to reduce power to 95 percent, isolate the feedwater heater, and cap the test plug to stop the steam leak. Following the repair, operators returned the feedwater heater back to service and increased power to 100 percent.
  • On December 1, 2005, Operations personnel responded to indications of an approximate three to five gallon per minute reactor coolant system (RCS) leak.

The inspectors responded to the control room and observed operator response.

Operators implemented Abnormal Operating Procedure (AOP) 3555, Reactor Coolant System Leak, and entered TS 3.4.6.2, RCS Operational Leakage.

Operators noted a rise in level of the containment drain transfer tank (CDTT).

The CDTT, in part, collects leak-off from RCS loop stop and bypass valves and pressurizer spray valves. Operators conducted a rapid downpower, in accordance with AOP 3575, Rapid Downpower, to support containment entry to isolate the RCS leak to the CDTT. At approximately 39 percent power, the turbine was manually tripped due to high vibrations on the number 7 turbine bearing. Shortly afterward, the reactor automatically tripped on low steam generator water level in the C steam generator due to steam generator indicated water level shrink from the turbine trip.

  • Operators implemented Emergency Operating Procedure (EOP) 35 E-O, Reactor Trip or Safety Injection, EOP 35 ES-0.1, Reactor Trip Response, and AOP 3550, Turbine/Generator Trip, for the reactor trip and turbine trip respectively. Following recovery actions from the reactor and turbine trip, operators entered containment and identified that the RCS leakage was coming from a leak-off line from the B loop cold leg stop valve. Operators closed the leak-off line isolation valve and secured the RCS leakage to the CDTT.

Dominion subsequently determined that the primary packing of the B loop cold leg stop valve was leaking and that the loop stop valve was not fully backseated. Dominion backseated the loop stop valve which isolated the valve packing from RCS pressure, and reopened the leak-off isolation valve to the CDTT. Dominion investigated the event, implemented corrective actions, conducted Operations training, and started up the plant on December 4, 2005.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15 - Three Unit 2 Samples and Four Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed seven operability determinations associated with degraded or non-conforming conditions to ensure that operability was justified and that mitigating systems or those affecting barrier integrity remained available and no unrecognized increase in risk had occurred. The inspectors also reviewed compensatory measures to ensure that the compensatory measures were in place and were appropriately controlled. The inspectors reviewed licensee performance to ensure all related TS and Final Safety Analysis Report requirements were met. Documents reviewed during the inspection are listed in the Attachment. The inspectors reviewed the following degraded or non-conforming conditions:

Unit 2

  • Heat Trace for #2 Atmospheric Dump Valve is not Working (CR-05-13096);
  • Intermittent A Charging Pump Low Lube Oil Pressure Alarm (CR-05-13163);and
  • Potential for Significant Air Entrainment in Refueling Water Storage Tank Emergency Core Cooling Suction Lines (OD:MP2-014-05).

Unit 3

  • Errors Identified in Loss of Coolant Accident Analysis (CR-05-11563);
  • Receipt of Over-temperature Delta-temperature Alarms (CR-05-12217); and

b. Findings

No findings of significance were identified.

1R16 Operator Work-Arounds (71111.16 - One Unit 3 Sample)

Selected Operator Work-arounds

a. Inspection Scope

The inspectors reviewed one risk significant operator work-around (OWA) for Unit 3 during the inspection period. The inspectors evaluated the conditions to determine if there were any effects on human reliability in responding to an initiating event or any adverse effects on the function of mitigating systems. The work-arounds were also reviewed to ensure compliance with licensee documents which administratively control OWAs. Documents reviewed during the inspection are listed in the Attachment.

Unit 3

  • C Service Water Pump Strainer Blowdown Every 4 Hours During Operation

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17B - Sixteen samples)

a. Inspection Scope

The inspectors reviewed 16 risk-significant plant modification packages selected from the design changes that were completed within the past two years. The review was performed to verify that:

(1) the design bases, licensing bases, and performance capability of risk significant structures, systems, and components had not been degraded through the modifications; and,
(2) the modifications performed during increased risk configurations did not place the plant in an unsafe condition. The modifications reviewed are listed in the attachment.

The selected plant modifications were distributed among the Initiating Event, Mitigating Systems, and Barrier Integrity cornerstones. For these selected modifications, the inspectors reviewed the design inputs, assumptions, and design calculations to determine the design adequacy. The inspectors also reviewed field change notices that were issued during the installation to confirm that the problems associated with the installation were adequately resolved. In addition, the inspectors reviewed the post-modification testing, functional testing, and instrument and relay calibration records to determine readiness for operations. Finally, the inspectors reviewed the affected procedures, drawings, design basis documents, and UFSAR sections to verify that the affected documents were appropriately updated.

For the accessible components associated with the modifications, the inspectors also walked down the systems to detect possible abnormal installation conditions.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing (71111.19 - Five Unit 2 Samples and Four Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed nine samples of post-maintenance tests (PMT) during this inspection period. The inspectors reviewed these activities to determine whether the PMT adequately demonstrated that the safety-related function of the equipment was satisfied given the scope of the work specified and that operability of the system was restored. In addition, the inspectors evaluated the applicable test acceptance criteria to verify consistency with the associated design and licensing bases, as well as TS requirements. The inspectors also verified that conditions adverse to quality were entered into the corrective action program for resolution. Documents reviewed during the inspection are listed in the Attachment. The following maintenance activities and their post maintenance tests were evaluated:

Unit 2

  • Troubleshoot Control Element Assembly 18 Abnormal Voltage (M2-05-10549);
  • Replace Refueling Water Storage Tank Level Indicator LI-3004 (M2-05-09591);
  • B Reactor Building Component Cooling Water Heat Exchanger Temperature Control Valve Repair (M2-05-08956);
  • Replace Degraded Tubing in Vital AC Switchgear Room Cooling System (M2-05-05878); and

Unit 3

  • Repack Charging System Bypass Control Valve (M3-04-13022);
  • Control Room Pressurization Manual Isolation Valve Repair (M3-05-13890); and

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities (71111.20 - Two Unit 3 Samples)

Unit 3

.1 Unit 3 Refueling Outage

a. Inspection Scope

The inspectors reviewed the Shutdown Risk Review Team Pre-outage Report for the Unit 3 refueling outage, conducted September 29 through October 27, 2005, to confirm that Dominion had appropriately considered risk, industry experience, and previous site-specific problems in developing and implementing a plan that assured maintenance of defense-in-depth. During the refueling outage, the inspectors observed portions of the shutdown and cooldown processes and monitored licensee controls over the risk significant outage activities listed below. Additionally, the inspectors conducted a walkdown of containment prior to final closeout to ensure no loose material or debris was present which could be transported to the containment sump. Documents reviewed during the inspection are listed in the Attachment. The inspectors reviewed selected aspects of the following evolutions:

  • New fuel receipt inspection;
  • Fuel handling, core loading, and fuel element assembly tracking;
  • Reactor cooling system pressure, level, and temperature instrument operability;
  • Mid-loop and reduced inventory operations;
  • Tagout control;
  • Vacuum fill operations;
  • Reactor Startup; and
  • Power Ascension.

b. Findings

No findings of significance were identified.

.2 Forced Outage

a. Inspection Scope

The inspectors reviewed one sample of a forced outage following a Unit 3 reactor trip on December 1, 2005, for conformance to technical specification requirements and approved procedures. Selected activities were verified for the following evolutions:

  • Site Organization Review Committee (SORC) meeting;
  • Plant shutdown to mode 3;
  • Plant heatup;
  • Reactor startup and criticality; and
  • Power ascension.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22 - Five Unit 2 Samples and Eight Unit 3 Samples)

a. Inspection Scope

The inspectors reviewed thirteen samples of surveillance activities to determine whether the testing adequately demonstrated the equipments operational readiness and its ability to perform its intended safety-related function. The inspectors attended pre-job briefs, verified that selected prerequisites and precautions were met and that the tests were performed in accordance with the procedural steps. Additionally, the inspectors evaluated the applicable test acceptance criteria to verify consistency with associated design basis, licensing bases and TS requirements, and that the applicable acceptance criteria were satisfied. The inspectors also verified that conditions adverse to quality were entered into the corrective action program for resolution. Documents reviewed during the inspection are listed in the Attachment. The following surveillance activities were evaluated:

Unit 2

  • Engineered Safeguards Actuation System Undervoltage Sequencer Calibration and Functional Test (SP-2403BA); and
  • Reaction Protection System Matrix Logic and Trip Path Relay Test (SP-2401D).

Unit 3

  • Pressurizer Level Protection Set 1 Transmitter Calibration (SP-3442D01);
  • Containment Sump Wide Range Level Transmitter Calibration (SP-3447B01);
  • Pressurizer Pressure Narrow Range Channel 1 Transmitter Calibration (SP-3442C10);
  • A Safety Injection Pump Bearing Oil Cooler Relief Valve IST (MF 3762WD-001);
  • Low Power Physics Testing (SP-31008); and

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23 - One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

The inspectors reviewed two samples of temporary modifications to verify that the temporary modifications did not affect the safety function of important safety systems.

The inspectors reviewed the temporary modifications and their associated 10 CFR 50.59 screening against the Final Safety Analysis Report and Technical Specification to ensure the modifications did not affect system operability or availability. Documents reviewed during the inspection are listed in the Attachment.

Unit 2

  • B Reactor Coolant Pump Reactor Building Closed Cooling Water Low Flow Alarm Set Point Lowered (CR-05-08516).

Unit 3

  • Control Building Service Water Enclosure Tube Closure Plate Control Room Habitability Seal (MP3-05-01).

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Testing (One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

An onsite review of the Millstone public alert system was conducted to ensure that the system was capable of promptly notifying the public for taking protective actions.

The inspector reviewed the following emergency preparedness (EP) procedures:

MP-26-EPA-FAP-09, Public Alert System Test and Maintenance, and MP-26-EPA-FAP08, Public Alerting System Administration. In addition, the inspector reviewed maintenance and test records for calendar years 2004 and 2005 to determine:

1) if test failures were properly trended and assessed; 2) inoperable sirens were promptly repaired; and 3) preventative maintenance was routinely performed. The inspection was conducted in accordance with NRC Inspection Procedure 71114,

2. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1EP3 Emergency Response Organization Augmentation (One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

An onsite review of the site emergency response organization (SERO) training records and augmentation staffing requirements was conducted to review the readiness of key staff to respond to an event. In addition, SERO pager test records from 2004 and 2005 were reviewed to determine Dominions capability to meet their Emergency Plan (E-Plan) staffing commitments and timely activation of their emergency facilities.

Condition reports associated with the pager tests were assessed to ensure pagers were properly maintained and effectively repaired. Finally, the E-Plan qualification records for key SERO positions were reviewed to ensure that the SEROs qualifications were current. The inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment 3. Documents reviewed during the inspection are listed in the

.

b. Findings

A Green finding was identified by the inspector regarding ineffective corrective actions associated with individuals not maintaining their SERO qualifications current (Refer to Section 1EP5 for specific details).

1EP4 Emergency Action Level and Emergency Plan Changes (One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

During the period of June through September 2005, the NRC received changes made to Dominions E-Plan in accordance with 10 CFR 50.54(q). Dominion had determined that the changes did not result in a decrease in effectiveness of the E-Plan and continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. A selected sample of E-Plan changes were reviewed in-office by the inspector. This review does not constitute approval of the changes and, as such, the changes and the associated 10 CFR 50.54(q) reviews are subject to future NRC inspection. The inspection was conducted in accordance with NRC Inspection Procedure 71114,

4. Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (One Unit 2 Sample and One Unit 3 Sample)

a. Inspection Scope

The inspector reviewed CRs generated by Dominion (listed in the Attachment)pertaining to issues identified from drills and exercises conducted since 2003 and the overall conduct and maintenance of the EP program. The review was conducted to determine the significance of the issues, associated corrective actions, and whether repeat problems were occurring. Included in that review were several CRs related to the SERO not maintaining their qualifications current in 2004 and 2005. The inspector also conducted a review of Dominions nuclear oversight program and the associated 2004 audit assessment reports to determine if the audits met the requirements of 10 CFR 50.54(t) and were self-critical. This inspection was conducted in accordance with NRC Inspection Procedure 71114, Attachment 5.

b. Findings

Introduction.

The inspector identified a Green finding for not implementing effective corrective actions to prevent repeat problems associated with maintenance of the training qualifications for the SERO staff.

Description.

In 2004, a nuclear oversight quality assurance audit identified a deficiency regarding compliance issues in the area of maintaining, monitoring, and trending SERO qualifications. It was identified as a deficiency because it was a repeat finding from the 2003 audit. In six of the twelve months of 2004, Dominion identified examples of lapsed SERO staff qualifications. Dominion reviewed this problem and identified several causal factors including: weak program ownership; personnel not being informed when the qualifications had lapsed; and the training tracking system was not user friendly and not routinely utilized. Dominion implemented additional corrective actions to ensure that the SERO staff would maintain their qualifications including: development of an electronic notification when qualifications were due to expire and senior management review of program expectations with appropriate staff personnel.

Subsequently, during an actual event in April 2005, an individual reported to his assigned facility with qualifications that had expired in February 2005. The individual was not allowed to perform his assigned duties and was instructed to complete the re-qualification process. However, during this inspection, the NRC found the individual still had not completed the required training, and had remained in the SERO callout system. Additionally, the inspector identified two more individuals with lapsed qualifications. Dominion verified that all three individuals had received the reminder electronic messages. The inspector concluded that the corrective actions for resolving this issue were ineffective to prevent recurrence.

Two of the three individuals identified during the inspection with lapsed qualifications, immediately completed the required training specific to their assigned position. The third individual was immediately removed from the SERO callout system pending the completion of the required training.

Analysis.

A performance deficiency occurred in which Dominion did not implement effective corrective actions to ensure that staff assigned to the SERO maintained their qualifications current. Since 2004, there were several examples in which the qualifications for SERO staff had expired. The corrective actions taken to prevent recurrence of this problem were ineffective as highlighted by the multiple repeat examples. The finding is more than minor because it is associated with the EP cornerstone attribute of emergency response organization readiness (training).

It affected the cornerstone objective of ensuring the capability to implement measures to protect the health and safety of the public during an emergency. The inspector also determined that this finding was indicative of a cross-cutting issue in the area of problem identification and resolution in that the corrective actions taken were not effective in precluding recurrence.

This finding is not suitable for significance determination process evaluation, but has been reviewed by NRC management and determined to be a finding of very low safety significance (Green) since Dominion always maintained sufficient numbers of qualified SERO staff.

Enforcement.

No violation of regulatory requirements occurred because the performance deficiency did not involve an explicit violation of a requirement.

Dominions failure to implement effective corrective actions to ensure that staff assigned to the SERO maintained their qualifications current, was considered a finding of very low safety significance (Green) (FIN 05000336,423/2005005-01, Ineffective Corrective Actions to Prevent SERO Qualification Lapses). Following the inspector's identification of the issue, SERO individuals with lapsed qualifications either immediately completed required training or were removed from the SERO callout system. This issue has been entered into Dominions corrective action program as CR-05-10819.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety [OS]

2OS1 Access Control to Radiologically Significant Areas (71121.01 - Ten Unit 3 Samples)

a. Inspection Scope

During the period October 17 - 20, 2005, the inspector conducted the following activities to verify that Dominion was properly implementing physical, administrative, and engineering controls for access to locked high radiation areas and other radiologically controlled areas, and that workers were adhering to these controls when working in these areas during the Unit 3 refueling outage. Implementation of these controls was reviewed against the criteria contained in 10 CFR 20, Unit 3 TS, and Dominions procedures. This inspection activity represents completion of ten

(10) samples relative to this inspection area.

Plant Walkdown and RWP Reviews

  • During the Unit 3 refueling outage, the inspector identified exposure significant work areas in the Unit 3 containment building. The inspector reviewed radiation survey maps and radiation work permits (RWP) associated with these areas to determine if the radiological controls were acceptable. Work areas reviewed included the pressurizer spray line, reactor vessel lower head, and regenerative heat exchanger cubicle.
  • The inspector performed independent surveys of selected areas in the Unit 3 containment building to confirm the accuracy of survey maps, the adequacy of postings, and that Technical Specification locked high radiation areas (TSLHRA)and very high radiation areas (VHRA) were properly secured and posted. Areas surveyed included the seal table, steam generator cubicles, reactor cavity drain line, and locked gates to the regenerative heat exchanger room and under reactor vessel area.
  • In evaluating RWPs, the inspector reviewed electronic dosimeter dose/dose rate alarm reports to determine if the setpoints were consistent with the survey indications and plant policy. The inspector verified that workers were knowledgeable of the actions to be taken when a dosimeter alarms or malfunctions for tasks being conducted under selected RWPs. Work activities reviewed included surveying the under reactor vessel area for downgrading from a VHRA to a TSLHRA (RWP-392/1), boric acid removal from regenerative heat exchanger valves (RWP-343/3), and pressurizer spray line weld repairs (RWP-360/2).
  • The inspector reviewed the RWPs and associated as low as reasonably achievable respiratory protection evaluations for potential airborne radioactivity areas located in the Unit 3 containment building. Respiratory protection evaluations reviewed included reactor cavity decontamination (No. 305/2),reactor disassembly (No. 301/2), pit seal repairs (No. 314/1), and steam generator primary side channel head entries (RWP 306/4).
  • The inspector reviewed Personnel Contamination Reports (PCRs) and the dose assessments, for personnel contaminations whose internal dose could potentially exceed 50 mrem, to evaluate the assessment methods. PCR Nos. M3-05-001 through M3-05-009 were reviewed.

High Risk Significant, High Dose Rate High Radiation Areas, and VHRA Controls

  • The inspector attended the pre-job briefings and reviewed the preparations for tasks involving entries into potential VHRAs and TSLHRAs. Tasks reviewed included radiation protection technicians surveying under the reactor vessel, following incore thimble insertion, for the purpose of down grading the area from a VHRA to TSLHRA; and decontamination personnel entering the regenerative heat exchanger cubicle, a TSLHRA, to clean boric acid build-up on various valves.
  • The inspector inventoried keys to VHRA and TSLHRAs stored at the Unit 3 control point and in the Unit 3 control room to verify that all keys were accounted for.
  • The inspector verified that VHRA, such as the under vessel hatchway and incore instrument area, were properly secured and posted and that surrounding area dose rates met regulatory criteria.
  • The inspector reviewed CRs relative to controlling work activities in the Unit 3 radiological controlled areas to assess the threshold for which problem reports were initiated and the timeliness of the corrective actions.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02 - Five Unit 3 Samples)

a. Inspection Scope

During the period October 17 - 20, 2005, the inspector conducted the following activities to verify that Dominion was properly implementing operational, engineering, and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for tasks conducted during the Unit 3 refueling outage.

Implementation of these controls was reviewed against the criteria contained in 10 CFR 20, applicable industry standards, and Dominions procedures. This inspection activity represents completion of five

(5) samples relative to this inspection area.

Radiological Work Planning

  • The inspector reviewed pertinent information regarding cumulative exposure history, current exposure trends, and ongoing activities to assess current performance and outage exposure challenges. The inspector determined the sites 3-year rolling collective average exposure and compared it to current trends.
  • The inspector reviewed the refueling outage work scheduled during the inspection period and the associated work activity exposure estimates.

Scheduled work included, reactor cavity drain-down and decontamination, pressurizer spray line weld repairs, and containment demobilization.

  • The inspector reviewed the ALARA Reviews (AR), ALARA Challenge Board meeting minutes, and Work-In-Progress ALARA Evaluations that addressed estimating and controlling dose for specific work activities. Work activities reviewed included steam generator inspection and maintenance activities, pressurizer spray line repairs, valve repairs, various in-service inspection activities, and reactor refueling tasks.
  • The inspector reviewed 3R10 dose summary reports, detailing worker estimated and actual exposures through October 19, 2005, for jobs performed during the refueling outage to compare actual exposures with forecasted data.
  • The inspector evaluated exposure mitigation requirements specified in RWPs and associated ARs. Jobs reviewed included reactor vessel disassembly/reassembly (RWP 301/302/303, AR 3-05-01), scaffolding installation/removal (RWP 231/331, AR 3-05-13), and snubber inspections (RWP 232/332, AR 3-05-06).
  • The inspector evaluated the departmental interfaces between radiation protection, operations, maintenance crafts, and engineering to identify missing ALARA program elements and interface problems. The evaluation was accomplished by interviewing the ALARA Supervisor and Radiation Protection Manager, and reviewing recent ALARA Council meeting minutes and ALARA Challenge Board minutes. The inspector also attended two
(2) ALARA Council meetings, and two
(2) pre-job briefings to assess interdepartmental coordination.

The inspector also interviewed the Unit 3 Health Physics Shift Supervisor regarding dose challenges in completing outage preparations and coordinating activities during the outage.

  • The inspector determined if work activity planning included the use of temporary shielding, system flushes, and operational considerations; i.e., scheduling work when the steam generators were filled, to further minimize worker exposure.

The inspector performed independent measurements on various system components including the excess letdown heat exchangers, reactor vessel level indication system, and various Unit 3 reactor building work areas to determine if temporary shielding was appropriately utilized.

Verification of Dose Estimates and Exposure Tracking Systems

  • The inspector reviewed the assumptions and basis for the annual site collective exposure estimate and the Unit 3 refueling outage dose projection.
  • The inspector reviewed personnel contamination reports for selected personnel to evaluate the contamination control measures.
  • The inspector reviewed Dominions method for adjusting exposure estimates, and re-planning work, when actual dose approached the estimated dose. The inspector attended ALARA Council meetings regarding repairing the pressurizer spray line and evaluated the exposure controls applied to this task (RWP 360/2).
  • The inspector reviewed Dominions exposure tracking system to determine whether the level of dose tracking detail, exposure report timeliness, and exposure report distribution was sufficient to support the control of collective exposures. Included in this review were departmental dose compilations, and individual dose records.

Job Site Inspection and ALARA Control

  • The inspector observed maintenance activities being performed for containment demobilization, pressurizer spray line repair, and boric acid removal from regenerative heat exchanger valves. The inspector verified that the appropriate radiological controls were implemented including radiation protection technician coverage, contamination mitigation, properly worn dosimetry, and that workers were knowledgeable of job site radiological conditions.
  • The inspector reviewed the exposure of individuals in selected work groups, including maintenance crafts to determine if supervisory efforts were being made to equalize doses among the workers.

Source Term Reduction and Control

  • The inspector reviewed the current status and historical trends of the Unit 3 source term. Through interviews with the Radiation Protection and Chemistry Manager and the ALARA Supervisor, the inspector evaluated Dominions source term measurements and control strategies. The inspector reviewed reactor coolant chemistry data to evaluate the effectiveness of post shutdown source term reduction efforts. Specific strategies being employed included system flushes, installation of temporary shielding, and chemistry controls.

Radiation Worker Performance

  • The inspector observed radiation worker and radiation protection technician performance for selected tasks. Tasks observed included steam cleaning of regenerative heat exchanger valves, under reactor vessel surveying, and containment demobilization. The inspector determined whether the individuals were aware of radiological conditions, access controls, that the skill level was sufficient with respect to the radiological hazards and the work involved.
  • The inspector reviewed condition reports, related to radiation worker and radiation protection technician errors, and personnel contamination reports to determine if an observable pattern traceable to a common cause was evident.

Declared Pregnant Workers

  • The inspector determined that no declared pregnant workers were employed to perform outage related activities in the radiologically controlled areas.

Problem Identification and Resolution

  • The inspector reviewed elements of Dominions corrective action program related to implementing the radiological controls program to determine if problems were being entered into the program for resolution. Details of this review are contained in Section 4OA2 of this report.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

[OA]

4OA1 Performance Indicator Verification

.1 Occupational Exposure Control Effectiveness (One Unit 2 and One Unit 3 Sample)

a. Inspection Scope

The inspector reviewed implementation of Dominions Occupational Exposure Control Effectiveness Performance Indicator Program. Specifically, the inspector reviewed CRs, and associated documents, for occurrences involving locked high radiation areas, VHRAs, and unplanned exposures against the established performance indicator criteria to verify that all occurrences that met the criteria were identified and reported. This inspection activity represents the completion of one

(1) sample relative to this inspection area; completing the annual inspection requirement.

b. Findings

No findings of significance were identified.

.2 RETS/ODCM Radiological Effluent Occurrences (One Unit 2 and One Unit 3 Sample)

a. Inspection Scope

The inspector reviewed relevant effluent release reports for the period January 1, 2004, through June 30, 2005, for issues related to the public radiation safety performance indicator, which measures radiological effluent release occurrences that exceed 1.5 mrem/qtr whole body or 5.0 mrem/qtr organ dose for liquid effluents; 5mrads/qtr gamma air dose, 10 mrad/qtr beta air dose, and 7.5 mrads/qtr for organ dose for gaseous effluents. This inspection activity represents the completion of one

(1) sample relative to this inspection area; completing the annual inspection requirement.

The inspector reviewed the following documents to ensure Dominion met all requirements of the performance indicator from the first quarter 2004 to the third quarter 2005:

  • monthly projected dose assessment results due to radioactive liquid and gaseous effluent releases;
  • quarterly projected dose assessment results due to radioactive liquid and gaseous effluent releases; and
  • dose assessment procedures.

b. Findings

No findings of significance were identified.

.3 Emergency Preparedness (Three Unit 2 Samples and Three Unit 3 Samples)

a. Inspection Scope

The inspector reviewed Dominions procedure for developing the data for the Emergency Preparedness PIs which are:

(1) Drill and Exercise Performance;
(2) Emergency Response Organization Drill Participation; and
(3) Alert and Notification System (ANS) Reliability. The review covered the period of September 2004 to September 2005. The inspector also reviewed Dominions 2004 and 2005 drill and exercise reports, training records and ANS test data to verify the accuracy of the reported data. The review was conducted in accordance with NRC Inspection Procedure 71151. The acceptance criteria used for the review were 10 CFR 50.9 and NEI 99-02, Revision 3, Regulatory Assessment Performance Indicator Guideline.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Review of Items Entered into the Corrective Action Program

As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and in order to help identify repetitive equipment failures or specific human performance issues for followup, the inspectors performed a daily screening of items entered into Dominion's corrective action program. This was accomplished by reviewing the description of each new problem evaluation report and attending daily management review committee meetings.

.2 Semi-Annual Review to Identify Trends

a. Inspection Scope

The inspectors performed a semi-annual review to identify trends that might indicate the existence of a more significant safety issue. The inspectors reviewed Unit 2 and Unit 3 performance indicator monthly reports, CRs, system health reports, quality assurance audits, self-assessment reports, maintenance reports, and NRC inspection reports and interviewed key personnel to evaluate if a trend existed.

b. Findings and Observations

Operability Determinations. No findings of significance were identified, however, the inspectors continue to follow operability determination (OD) issues in relation to a trend originally identified in NRC Inspection Report 05000336/2004008 and 05000423/2004008. In that report, the inspectors discussed a lack of rigor by Dominion relating to both the understanding of the effects of degraded conditions and the technical bases used in evaluating degraded conditions in ODs. Additionally, the inspectors identified that a contributing factor was the failure to appropriately apply Dominions OD procedure. Multiple examples of both non-cited and minor violations were discussed that exemplified this negative trend.

During 2005, the inspectors have identified additional concerns with the quality of ODs and the implementation of Dominions OD procedure. Most notably, a finding was issued in NRC Inspection Report 05000336/2005004 and 05000423/2005004 which discussed several examples where Dominion did not adequately implement their OD process. Dominion has identified OD quality as a key site issue that is being addressed under a senior site management initiative for improvement. An OD improvement team has been established, procedural guidance has been reviewed and revised, and Operations training is being developed to improve performance in this area.

Additionally, revised Generic Letter 91-18, Operable/Operability: Ensuring the Functional Capability of a System or Component, guidance will be reviewed for incorporation into Dominion procedural guidance and training forums. In consideration of additional OD issues during 2005 and in-progress corrective actions by Dominion, the resident inspectors will continue to follow OD issues and programmatic corrective actions within the framework of the baseline inspection program.

.3 Annual Sample Review

Inservice Inspection Activities Unit 2

a. Inspection Scope

The inspector reviewed a sample of corrective action reports shown in the Attachment, which identified problems related to in-service inspection issues. The inspector verified that problems were being identified, evaluated, appropriately dispositioned, and entered into the corrective action program.

b. Finding No findings of significance were identified.

.4 ALARA Planning and Controls

a. Inspection Scope

The inspector reviewed eight

(8) CRs, four
(4) Nuclear Oversight Department Field Observation reports, and twelve
(12) Quality Control Quick Data Check-lists, relating to maintaining personnel exposure ALARA during the Unit 3 refueling outage, to evaluate the threshold for identifying, evaluating, and resolving radiological control problems.

This review was conducted against the criteria contained in 10 CFR 20, TS, and Dominions procedures.

b. Findings

No findings of significance were identified.

.5 10CFR 50.59 and Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed CRs associated with 10 CFR 50.59 and plant modification issues to ensure that Dominion was identifying, evaluating, and correcting problems associated with these areas and that the planned or completed corrective actions for the issues were appropriate. The inspectors also reviewed a sample of Dominions self-assessments related to 10 CFR 50.59 SEs and plant modification activities.

The listing of the condition reports and self assessments reviewed is provided in

1.

b. Findings

No findings of significance were identified.

.6 Cross-References to Problem Identification and Resolution Findings Documented

Elsewhere Section 1EP5 describes a failure to implement effective corrective actions to ensure SERO staff maintained their qualifications current in that the corrective actions taken were not effective in precluding recurrence.

Section 4OA5.2 describes a failure to formally disposition leakage into the B EDG rocker arm lube oil system.

4OA3 Event Followup

a. Inspection Scope

On December 1, 2005, Operations personnel responded to a RCS leak, turbine trip, and automatic reactor trip. See Section 1R14 for a detailed discussion on this event.

Resident inspectors responded to the control room, verified emergency action level and notification considerations, and reviewed the event in accordance with Inspection Procedure 71153, Event Follow-up, and Management Directive 8.3, NRC Incident Investigation Program.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 Temporary Instruction 2515/160 Pressurizer Penetration Nozzles and Steam Space

Piping Connections in U.S. Pressurized Water Reactors (NRC Bulletin 2004-01)

a. Inspection Scope

At Millstone Unit 3, a bare metal visual (BMV) and volumetric (VT) examination was performed on all five pressurizer penetration nozzles fabricated from Alloy 82/182/600 material to verify the absence of boric acid crystals and to verify the integrity of the pressurizer penetrations and steam space connections. As stated in its response to the NRC Bulletin 2004-01, there is a total of five penetration nozzles fabricated from Alloy 82/182/600 material at Millstone Unit 3. Dominion committed to perform BMV as well as VT examinations of the five nozzles. The only impediment to the BMV examinations was the installed insulation around the five penetrations. After removing the insulation, the observed penetrations were free of material that could adversely affect viewing the pressurizer penetrations. BMV showed no evidence of boric acid leakage or material deficiencies (i.e., cracks, corrosion, etc.) at any of the penetration nozzles. VT examinations identified indications in the PZR spray nozzle. The inspections conducted at Millstone Unit 3 during this outage were consistent with Dominions bulletin response dated July 27, 2004, and supplemental response dated October 4, 2004. Documents reviewed during the inspection are listed in the Attachment.

Bare Metal Visual Examination (03.02)a., b. Direct BMV examination of the Alloy 82/182/600 pressurizer penetrations were performed by Dominions NDE technicians certified to ASME,Section XI, Level II or Level III for visual examiners qualification and training requirements as described in ASME Code Section XI. The NDE technicians performing the VT examinations were qualified in conformance with Dominions inspection procedures.

c.

The inspectors reviewed Dominions examination procedures contained in its Boric Acid Control Program, MP-24-BACCFAP01, Rev. 000-01. The examination procedures for boric acid corrosion control and visual inspection for evidence of boric acid leakage were adequate to identify reactor coolant leakage in the penetration nozzles or steam space piping components.

d.

All five pressurizer penetration nozzles were inspected by a qualified NDE technician using direct visual examinations. The examiners achieved a visual examination coverage of 360E around the circumference of the nozzles.

e.

The inspectors independently examined the physical condition of the five Alloy 82/182/600 penetration nozzles with Dominions examiners. The nozzles were free of debris, dirt, and boron deposits. There was no viewing obstruction to perform direct visual examination of the five penetration nozzles.

f.

The inspectors confirmed that insulation was removed from the pressurizer nozzles. The inspectors visually examined 360E around the circumference of each of the penetration nozzles. No debris, dirt, or boric acid deposits were identified.

g.

No boric acid deposits were identified.

h., I. No anomalies, deficiencies, or discrepancies associated with RCS structures or the examination process were identified.

Volumetric Examination (03.03)a.

As committed in its response to the Bulletin 2004-01, Dominion performed VT examinations of the five pressurizer nozzles containing Alloy 82/182/600 welds.

The examination scope is consistent with the requirements set forth by the Bulletin.

b.

Dominions VT examination methodologies were reviewed and found to be sufficient in identifying indications that would exist in the welds. Dominion chose to perform RT and manual UT of the nozzles. If indications are detected, an automatic UT, capable of identifying and sizing flaws, would be performed to better characterize any flaws that exist.

VT examinations of the Alloy 82/182/600 pressurizer penetrations were performed by Dominions and its contracted NDE technicians using RT and UT.

The technicians were certified Level II or Level III examiners.

c.

Dominion performed manual UT examinations of the five nozzles. Because of geometry restraint of the nozzles surface, only 50 percent coverage of the examination volume was obtained. No reportable indications were detected.

Dominion performed RT examinations of the five nozzles. The RT radiographs were examined by Dominions qualified Level III examiner. The examination showed two indications in its PZR spray nozzle, Weld # 03-X-5641-E-T. No indications were found in the other four nozzles. The inspector reviewed the RT radiographs of all five nozzles with Dominions examiner. The two indications were evaluated as three flaws as described below.

Dominion performed an automatic UT examination of the PZR 6" spray nozzle which included surface machining and preparation to provide a better UT transducer access. The examination was performed by qualified Level II and Level III examiners with Procedure WDI-STD-119A Revision 1. This is a fully qualified procedure for flaw detection and sizing in accordance with the EPRI Performance Demonstration Initiative Program. The inspector observed the surface preparation and automatic UT examination process. Dominion performed the examination consistent with the procedures.

Results provided by Dominion are as follows: Flaw #1 was characterized as lack of fusion located at or near the ID surface 360E circumferentially. It is in the butter to weld region with 16.4 inch in length, and a maximum depth of 0.214 inches. Flaw #2 is also a circumferential flaw characterized as lack of fusion about 7.7 inches in length near the safe-end side of the weld. Max depth is 0.219 inches. Flaw #3 is an axial flaw originated from the ID surface located in the butter. It was measured 0.25 inches in length, 0.214 inches through-wall (depth).

Dominion performed a structural weld overlay on the spray nozzle to address these flaws.

b. Findings

No findings of significance were identified.

.2 (Closed) URI 05000423/2005003-04, Failure to Formally Disposition Leakage into the

B EDG Rocker Arm (RA) Lubricating Oil (LO) System This URI was opened to assess Dominions response to an abnormal LO sample result for the B EDG identified on June 17, 2005, and to follow-up on Dominions cause determination and corrective actions. Documents reviewed are listed in the Attachment.

Introduction.

The inspectors identified a Green violation of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, for the failure to properly assess compensatory actions and to take timely actions to correct the introduction of water into the Unit 3 B EDG RA LO system. Specifically, following the discovery of elevated water content in the B EDG RA LO system on June 17, 2005, and the determination on July 11, that the EDG was fully qualified, Dominion; 1) did not specify compensatory actions to ensure the system was maintained in a fully qualified status while the degradation continued to exist, 2) did not establish a threshold for water content in the RA LO system beyond which the EDG would be considered inoperable, 3) and did not schedule the timely completion of maintenance activities to correct the in-leakage. While Dominion took several actions in response to the discovery of water in the LO system, these actions were not sufficient to preclude the development of significant water leakage into the RA LO system which resulted in the subsequent declaration of inoperability of the B EDG on September 27, 2005, and the unavailability of the B EDG for approximately 5 days while unplanned corrective maintenance was performed.

Description.

On June 17, 2005, Dominion identified water in the B EDG RA LO system.

The inspectors generated an URI at that time to assess Dominions corrective actions and cause analysis. On September 27, 2005, Dominion drained the RA LO reservoir and replaced the LO with fresh oil in preparation for a B EDG surveillance run.

Approximately 1.5 ounces (47 milliliters) of water was drained from the reservoir prior to the surveillance run. Dominion then conducted the monthly operability run for approximately one hour and sampled the RA LO at which point approximately one quart of water was drained from the reservoir. The RA LO sump capacity is approximately 36 quarts. Dominion removed the cylinder rocker arm covers and identified water leaking from an exhaust valve on the #7 cylinder head. Dominion declared the B EDG inoperable and initiated a maintenance activity to replace cylinder exhaust valve O-rings.

This was an unplanned TS entry which caused the unavailability of the EDG for approximately 5 days during subsequent corrective maintenance. The B EDG was restored to service on October 2, 2005.

Dominion determined that four additional cylinders (3-5-6-8) had water leakage similar to the #7 cylinder. The inspectors noted that the O-rings for the exhaust cages associated with these cylinders exhibited brittle characteristics compared to the O-rings for the cylinders that did not experience water leakage. Dominion determined that it was likely that these O-rings were the original rings installed in the B EDG approximately 20 years ago and had not been replaced at the 10 year interval as recommended by the Fairbanks-Morse owners group in 1998. Dominion did, however, find adequate documentation to support that the other non-leaking O-rings had been replaced between 1989 and 1999. Dominion determined that the jacket water that cools these exhaust valve cages was leaking through the brittle O-rings into the RA LO system.

As documented in the corrective action program, on July 11, Dominion recognized that there appeared to be a small cooling water leak into the RA LO system. A reasonable Expectation of Continued Operability and an Operability Determination (OD) were generated in which Operations determined the EDG to remain operable. Dominion subsequently closed the OD on July 12 because they determined that the EDG was fully qualified. On August 2, Dominion identified that the cause of the water in-leakage was from leaking jacket water O-rings. Dominion subsequently scheduled corrective maintenance for February 2006. The inspectors noted that the B EDG was a risk significant component as demonstrated by the Millstone 3 Probabilistic Risk Assessment (PRA) model.

On December 20, 2005, Dominion completed an evaluation (AR 05005955) to determine the effect the water discovered in the RA LO system on September 27 had on the B EDGs ability to run for a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period. This evaluation and the previous July 11 OD did not ensure that the B EDG was fully qualified per Generic Letter 91-18 in that the evaluations did not specify compensatory actions, such as, staging equipment needed to recover from O-ring failures or performing time studies, operator pre-briefs on the degraded condition and its implication on EDG operation, or walkdowns to drain and refill the RA LO reservoir tank in the event that in-leakage caused a high level alarm in the reservoir. Also, the OD and CR evaluation did not establish a threshold for water content in the RA LO system beyond which the EDG would be considered inoperable. Dominions December 20 evaluation did determine that water would enter the RA LO system through the leaking exhaust valve cage O-rings and accumulate in the bottom of the reservoir tank. Dominion determined that this condition would not have affected the B EDG from operating as designed during an assumed PRA mission time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Dominions evaluation, however, did not adequately address EDG function beyond 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The inspectors conducted a review of Dominions evaluation. The inspectors determined that Dominions evaluation did provide an adequate basis that concluded the B EDG could have operated for up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> during an event. However, Dominion did not provide a basis describing how the machine would have operated during a design basis event beyond 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors determined that it was reasonable to believe that the B EDG would have failed at some point beyond 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> once the RA LO pump began to pump water to the rocker arm components. While this failure was unlikely to occur within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following an event, it was likely that the B EDG would have failed at a subsequent point prior to completion of the design basis mission time (absent manual action in response to a RA LO oil reservoir tank high level alarm to drain and refill the tank while the engine was running).

The performance deficiency was the failure to take effective corrective actions to properly assess compensatory actions and correct water leakage into the B EDG RA LO system prior to the development of significant water leakage into the RA LO system on September 27, 2005.

Analysis.

Traditional enforcement does not apply to this finding since there were no actual safety consequences, no impact on the NRCs ability to perform its regulatory function, and no willful aspects. The finding was more than minor because it affected the equipment performance attribute of the mitigating system cornerstone and the availability and reliability of the B EDG to respond to initiating events. The inspectors determined that this finding was of very low safety significance (Green) by performing a Phase 1 significance determination using NRC IMC 609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. Specifically, this finding screened to Green because the finding was not a design or qualification deficiency, did not represent a loss of safety system function, did not represent an actual loss of safety function of a single train or one or more non-technical specification trains based on a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> PRA mission time, and was not potentially risk significant due to seismic, flooding, or severe weather initiating events.

This finding was related to the cross-cutting issue of problem identification and resolution because Dominion failed, once the source of the water contamination had been identified, to properly assess compensatory actions and take effective corrective actions for water in-leakage into the B EDG RA LO system. The delay resulted in the unplanned unavailability of the B EDG and the likely failure of the EDG if it had been called upon to perform its design function for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Enforcement.

Code of Federal Regulation 10 CFR Part 50 Appendix B, Criterion XVI, Corrective Action, requires, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. Contrary to this requirement, from June 17 to September 27, 2005, Dominion failed to properly assess and correct known water leakage into the B EDG rocker arm lubricating oil system prior to EDG inoperabilty despite the source and cause of the leakage having been identified on July 11. Also, Dominion failed to properly assess the degraded condition, in that, compensatory measures to ensure the system was maintained in a fully qualified status while the degradation continued to exist were not identified or implemented despite performance of a July 11 operability determination. This issue was determined to be of very low safety significance (Green) and has been addressed in Dominions corrective action program (CR-05-10248). After declaring the B EDG inoperable on September 27, Dominion performed corrective maintenance to replace the leaking O-rings, returning the EDG to service on October 2. This violation is being treated as non-cited violation consistent with Section VI.A of the NRC Enforcement Policy (NCV 05000423/2005005-02, Failure to properly assess and correct known water leakage into the B EDG rocker arm lube oil system).

.3 (Closed) URI 05000336/2005003-03, FSAR statements do not support CEDM design

attribute As a result of inspector questions during an NRC inspection of the Unit 2 reactor vessel head replacement in February 2005, Dominion determined it could not locate any actual test or other reference material to support a statement in the UFSAR regarding the control element drive mechanisms (CEDMs). Specifically, section 3.3.3.3 of the UFSAR stated that a loss of cooling air would not prevent the CEDM from releasing the control element assembly (CEA) if a reactor trip was initiated, and that tests had shown that the CEDM was capable of dropping the CEA after four hours of operation in the hold mode without cooling air. Dominion initiated CR-05-01483 to address the issue, and generated a Reasonable Assurance of Continued Operability. The URI was opened to evaluate the adequacy of Dominions resolution of the issue.

As part of the corrective actions for this issue, Dominion initiated a change to the UFSAR to replace the reference to the test with additional design information regarding the CEDMs. To evaluate the adequacy of the UFSAR change, the inspector reviewed FSAR Change Request 04-MP2-015 and its associated 10 CFR 50.59 Screen Form, the associated vendor technical manual and design specifications, and UFSAR section 8.9.1, Control Element Drive Mechanism Cooling System. The inspector noted that the function of the CEDM cooling system is to provide acceptable coil life and maintain an acceptable coil replacement cycle, and that the CEDMs themselves are designed to operate at temperatures and pressures significantly higher than those at normal operating conditions. The inspector also noted that the CEDM is designed to withstand a complete loss of cooling for a four-hour period in the hold mode with the plant at normal operating temperature and pressure, and be capable of normal operation after restoration of cooling. The inspector verified that demonstration of this requirement was documented in the test report. The inspector did not identify a specific design specification or test requirement regarding the ability of the CEDM to drop the CEA after four hours of operation in the hold mode without cooling air. Finally, the inspector noted that Dominion had procedures in place which direct the operators to trip the reactor upon a loss of CEDM cooling. As a result, the inspector found the 50.59 screen to be adequate, and no violations of requirements were identified. A list of documents reviewed is included in the attachment to this inspection report. Based on the above, this Unresolved Item is closed.

.4 (Closed) URI 05000336/2005301-01, Unit 2 Simulator Deficiencies Identified During

NRC Exam Process The inspector reviewed three deficiencies related to simulator fidelity and addressed them as closed issues. They had previously been documented in an Initial Examination Report 05000336/2005301 (June 2005).

URI 05000336/2005301-01 described three examples of potentially inaccurate fidelity between the Unit 2 simulator and the reference plant:

  • Modeling of Air Flow in Enclosure Building Filtration (EBFS) and Hydrogen Purge Systems - Attempted to align Facility 1 and 2 EBFS cross-train with Facility 2 and 1 hydrogen purge valves to depressurize containment during validation of the NRC exam on the Unit 2 simulator. Containment pressure did not respond as expected.

Dominion entered this issue into their simulator corrective action process under DR #2005-2-0013 and modified the logic of the air flow calculation in the EBFS and hydrogen purge system to properly model these containment depressurization flowpaths. The modeling discrepancy appeared to be beyond the scope of current simulator operational testing. The discrepancy had apparently not been identified during model verification and validation testing performed several years ago and had apparently not been previously encountered through use of plant procedures on the simulator.

  • Primary Makeup Water (PMW) Flow Controller and Flow Totalizer Indicated Flow With the Valve Closed - Observed approximately 0.1 gpm flow indicated on the PMW flow controller during an NRC exam on the simulator with the flow control valve closed.

Dominion entered this issue into their simulator corrective action process under DR#2005-2-0023. It was determined to be a minor hardware issue and was corrected through recalibration of the flow controller hardware.

  • VCT Outlet Valve Opened When Control Switch Placed in Auto - During the validation of the NRC exam in February 2005, VCT outlet valve CH-501 was observed to automatically open when its control switch was returned to the AUTO position from the CLOSE position. VCT level had remained in its normal operating range during the time that the handswitch was in CLOSE. A review of the valves electrical schematic (dwg no. 25203-32009 sht 6) revealed that the valve, by design, will only receive an open signal automatically from the AUTO position for a two-second period following the clearing of a VCT low-low level condition.

Dominion entered this issue into their simulator corrective action process under DR#2005-2-0021. The valve control logic in the simulator coding was modified to include relays associated with the valve automatic operation and the DR was closed with no further corrective action. In August 2005, several months after identification of this simulator modeling deficiency, an operations training supervisor who was assisting in the plant during the refueling outage, and aware of the recent simulator change, observed a problem with the same valve in the plant. He noted that CH-501 in the plant incorrectly stroked open from the AUTO position just as the simulator had prior to correction of the modeling problem.

Condition Report CR-05-08322 was generated to address the difference between CH-501 operation and design and is currently scheduled for troubleshooting and repair in the next refueling outage. This plant problem has been evaluated by the facility as not impacting valve operability as it does not affect the ability of the valve to close on a safety injection actuation signal or to be closed manually. A Condition Report action has been generated for engineering to conduct a review of the implementation of this modification prior to performing the CR-05-08322 troubleshooting activity.

Further investigation by Dominion has determined that the plant design change was implemented in 1997 as part of 14 modifications to address hot short concerns. These modifications were incorrectly assessed at the time as not impacting the simulator. A review of these changes has revealed that a total of 3 of the 14 modifications required simulator changes and should have been identified as impacting the simulator. All 3 of these modeling deficiencies (affecting CH-501, CH-504 and SI-651) have been corrected. Condition Report CR-05-13556 was initiated for extent of condition to evaluate whether hot short modifications on Unit 3 have been fully implemented on the Unit 3 simulator.

Inspector discussions with Dominion, and review of their actions taken, resulted in the NRC determining that, for one of the apparent simulator fidelity issues (PMW flow controller indication), no actual lack of simulator fidelity existed.

Corrective actions fine-tuned the controller indication to better match reference plant indications.

The inspector further determined that for the other two apparent simulator fidelity issues (EBFS flow and CH-501 response), simulator modeling was incorrect and simulator fidelity had not been maintained. NRC Inspection Manual Chapter 0612 defines a performance deficiency as an issue that is the result of a licensee not meeting a requirement or standard where the cause was reasonably within Dominions ability to foresee and correct, and which should have been prevented. Although Dominion did not meet the simulator fidelity requirements of 10 CFR 55.46 for these two issues, the inspector determined that the causes of each of these issues were not reasonably within Dominions ability to foresee and correct within the current simulator operational testing program, and therefore no performance deficiency was identified. This conclusion was based on the fact that these issues would not be apparent during conduct of normal simulator periodic testing or normal simulator operations. The EBFS flow deficiency was so readily apparent when the system was aligned for venting containment that it is unlikely the evolution had been previously conducted during any training session. The VCT outlet valve handswitch is taken to CLOSE during some simulated evolutions. By procedure, operators are directed to open the valve later during these evolutions. Through questioning, the inspector determined that an operator will typically take the handswitch from CLOSE, through the center AUTO position to the OPEN position before allowing it to spring-return back to the AUTO position. The typical operation of the switch therefore masked the modeling deficiency of the valve opening when the handswitch was taken from CLOSE to AUTO.

Inspector review of the three issues described in this unresolved item resulted in the determination that, in one case, no actual simulator fidelity problem existed.

In the other two cases, the simulator did not match reference unit design but, as explained, no licensee performance deficiency existed. In the cases where fidelity was inaccurate, timely and effective corrective actions have been taken.

For the reasons given above, the inspector determined no findings related to simulator fidelity existed, and therefore, URI 05000336/2005301-01 is closed.

.5 (Closed) URI 05000423/2005008-02, Millstone Unit 3 Simulator Demonstration of

Expected Plant Response to Operator Input and to Normal Conditions (Reactor Heat-up Operations) Using Only Operator Actions Normal to the Reference Unit The inspector reviewed a potential Unit 3 simulator fidelity issue and addressed it as a closed issue. It was related to the method used to establish simulated hot standby plant conditions for simulator normal evolution testing. This unresolved item had been documented in Inspection Report 05000423/2005008 (April 2005).

URI 05000423/2005008-02 described a potential failure to maintain Unit 3 simulator fidelity when establishing hot standby conditions for simulator normal evolution testing.

Millstone Nuclear Station Unit 3 reference plant does not have any means for changing a reactor coolant pumps frictional heat output characteristics; it is established by design based, in part, on the amount of work being required and performed by pump operation.

The reference plant reactor coolant pump frictional heat output is predetermined by design and cannot be adjusted during reactor operations under any conditions. Other factors such as time and rate of heat addition on the temperature of vessel head, flanges, and nozzles as well as thermal-hydraulic operating characteristics that influence reactor heat-up cannot be artificially changed during the heat-up from cold shutdown conditions in the reference reactor plant.

Inspectors previously found that the simulation facility licensee had conducted required normal evolution performance testing on the Unit 3 plant-referenced simulator using mathematical model changes instead of using only operator actions normal to the reference unit to artificially manipulate the effect and response of reactor coolant pump frictional heat output (e.g., allowing unrealistic reactor vessel temperature and pressure responses during reactor coolant pump operations when this capability is not in the reference plant and is not part of the design data for the reactor coolant system).

Incorrect generation of simulator initial condition sets, and the use of artificial means to effect reactor coolant pump frictional heat changes, could impact operator actions on the reference plant as a result of licensed operators and senior operators being negatively trained on initial condition sets that were derived from an incorrect representation of the reactor core and reactor coolant system used to inappropriately demonstrate nuclear and thermal hydraulic characteristics and subsequently leading to misunderstandings of the expected reference plant response.

Dominion entered this issue into their simulator corrective action process under DR #2005-3-0016 and ran a comparison of resulting conditions from a 150-degree Fahrenheit RPS heatup in normal time versus fast time. Some differences were noted in the resulting final conditions. The fast time heatup yielded a greater response in pressurizer parameters. However, no abnormal alarms were received and the operator was able to follow plant procedures. Stabilization of the simulated plant after reaching the desired conditions restored plant parameters to desired values such that the conditions saved for further testing and operator training matched expected plant conditions.

Although no fidelity issue was identified between final conditions established using fast time as compared to normal time, the facility determined that there was not a clear benefit to using the feature during required testing or operator training. Condition Report CR-05-12389 was written to initiate a change to the Nuclear Simulator Engineering Manual to administratively restrict the use of the simulator fast-time heatup function.

Inspector discussions with Dominion, and review of their actions taken, resulted in the inspector determining that tests performed by Dominion demonstrated simulator fidelity was not adversely affected in this case. However, ANSI/ANS-3.5-1998 Section 3.1.1 provides guidance that the simulator shall support the conduct of reference unit evolutions, using only operator action normal to the reference unit, including reactor startups and shutdowns, in a continuous manner without any mathematical model or initial condition changes. In light of this guidance, the plant staff actions to prohibit future use of non-real-time features such as fast heatup in testing or development of operating conditions was appropriate.

Inspector review of the issue described in this unresolved item resulted in the conclusion that no simulator fidelity problem existed. Therefore, URI 05000423/2005008-02 is closed.

.6 (Discussed) URI 05000336,423/2005008-01, Acceptability or Suitability of Millstone Unit

2 and Unit 3 Simulator Scenario-Based-Tests (SBTs) For Meeting ANSI/ANS-3.5-1998 Performance Testing Criteria The inspector updated actions taken in regard to the open unresolved issue on simulator scenario-based testing (SBT) methodology. This unresolved item had been documented in Inspection Report 05000336 and 05000423/2005008 (April 2005). The NRC staff has been in discussions over this issue throughout 2005 with industry through the NEI and the Mid-Atlantic Nuclear Training Organization (MANTG). In August 2005, MANTG hosted a training conference at the Millstone Station where the Millstone training staff put on a demonstration of a proposed methodology for documentation of scenario-based tests. The facility is awaiting outcome of industry / NRC meetings on this topic and has not made any changes to their SBT methodology. This unresolved issue will remain open, pending final decision reached by the Operator Licensing Program Office.

.7 (Discussed) URI 05000336/2005301-02, Potential Gap in Technical Specification

Requirements for Nuclear Instrument Operability The inspector updated actions taken in regard to the open unresolved issue on technical specification requirements for nuclear instrument operability. This unresolved item had been documented in Inspection Report 05000336/2005301 (June 2005).

A potential issue was noted with the TSs during development of the written examination as follows:

- Wide Range Nuclear Instruments (WRNIs) are required operable in Modes 3, 4, 5

- Power Range Nuclear Instruments (PRNIs) are required operable in Modes 1, 2

- Mode 2 is defined as Keff > 0.99

- Power Range Nuclear Instruments come on scale at 0.1 percent power It thus appears possible to be in compliance with Technical Specifications with the plant in Mode 2, with power still below the range of the PRNIs, but with no requirement for operable WRNIs.

Dominion initiated Condition Report CR-05-03176 to address the issue. Millstone engineering evaluated the situation and concluded that no problem exists since WRNIs are not credited to mitigate any existing FSAR Chapter 14 design basis event and no auto or manual action is credited based on this indication.

The NRC staff is currently evaluating this issue further. The unresolved issue will remain open pending outcome of this evaluation.

4OA6 Meetings, Including Exit

Emergency Preparedness

Exit Meeting Summary

On October 7, 2005, the inspector presented the inspection results to Mr. J. Alan Price and other Dominion staff. The inspector confirmed that no proprietary information was provided or examined during the inspection.

Occupational Radiation Safety

Exit Meeting Summary

On October 20, 2005, the inspector presented the inspection results to Mr. J. Alan Price and other members of Dominion management. Dominion acknowledged the conclusions presented.

Inservice Inspection Activities

Exit Meeting Summary

On October 28, 2005, the inspector presented the inspection results to Mr. Skip Jordan and other members of Dominion management. Dominion acknowledged the conclusions presented.

10 CFR 50.59 and Permanent Plant Modifications Report

Exit Meeting Summary

The inspectors presented the inspection results to Mr. J. Alan Price and other members of Dominion management on November 18, 2005. Dominion management stated that none of the information reviewed by the inspectors was considered proprietary.

Integrated Report

Exit Meeting Summary

On January 19, 2006, the resident inspectors presented the overall inspection results to Mr. J. Alan Price and other members of his staff, who acknowledged the findings. The inspectors asked Dominion whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

D. Bajumpa, Engineering
B. Barron, Engineering
B. Bartron, Licensing
P. Bandaru, Engineering
W. Bellows, Engineering
B. Burnham, Operations
P. Calandra, ALARA Coordinator
M. Chalbert, Engineering
S. Chang, Software Systems Engineer Specialist (Simulator)
A. Chyra, Engineering
G. Closius, Licensing Engineer
K. Connor, Reactor Engineering
M. Cote, Supervisor, Unit 2 Licensed Operator Requalification Training
T. Dagata, Radiation Protection Technician
D. DelCore, Supervisor, Health Physics Operations
D. Dodson, Supervisor, Station Nuclear Licensing
J. Follett, I&C Instructor
J. Fuller, Senior EP Instructor
R. Fuller, ISI Level III
P. Grossman, Manager-Nuclear Engineering
J. Hawxhurst, Nuclear Quality Specialist
G. Huang, Software Systems Engineer Specialist (Simulator)
S. Heard, Manager-Nuclear Oversight
T. Horner, Operations Training Supervisor
S. Jackson, Simulator Systems Analyst (Test Operator)
N. Jaycox, Engineering
A. Jordan, Director, Nuclear Station Operations & Maintenance
J. Jozwick, Radiation Protection Technician
E. Laine, Manager, Radiological Protection & Chemistry
J. Langan, Manager- Nuclear Site Engineering
L. Loomis, Operations
P. Luckey, Manager, EP
D. MacNeill, Operations
P. Malzahn, Operations Instructor
F. Matovic, Radiation Protection Technician
R. MacManus, Director, Nuclear Engineering
M. Nappi, Supervisor, Radiation Protection - ALARA
F. Perkins, System Engineer
A. Price, Site Vice President - Millstone
D. Regan, Supervisor, Radiation Protection Support (ALARA)
D. Robinson, Information Technology Manager (Simulator)
C. Ryan, Operations Instructor
S. Scace, Director, Nuclear Station Safety and Licensing
M. Stark, SG Project Manager
S. Stricker, Design Manager
C. Tan, Software Systems Engineer Specialist (Simulator)
S. Turowski, Supervisor-HP Technical Services
R. Zeiber, Engineering

NRC Personnel

J. C. Benjamin, Resident Inspector, Division of Reactor Projects (DRP)
T. F. Burns, Reactor Inspector, Division of Reactor Safety (DRS)
J. M. DAntonio, Operations Engineer, DRS
Z. B. Fu, Reactor Inspector, DRS
D. C. Johnson, Reactor Inspector, DRS
G. X. Johnson, Reactor Inspector, DRS
S. R. Kennedy, Resident Inspector, DRP
K. S. Kolaczyk, Senior Resident Inspector, Ginna, DRP
N. T. McNamara, Emergency Preparedness Inspector, DRS
M. C. Modes, Senior Reactor Inspector, DRS
T. A. Moslak, Health Physicist, DRS
A. C. Patel, Reactor Inspector, DRS
P. A. Presby, Operations Engineer, DRS
R. J. Prince, Health Physicist, DRS
S. M. Schneider, Senior Resident Inspector, DRP

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000336,423/2005005-01 FIN Ineffective Corrective Actions to Prevent SERO Qualification Lapses (1EP5)
05000423/2005005-02 NCV Failure to properly assess and correct known water leakage into the B EDG rocker arm lube oil system (4OA5.2)

Closed

05000423/2005003-04 URI Failure to Formally Disposition Leakage into the B EDG Rocker Arm Lube Oil System (4OA5.2)
05000336/2005003-03 URI FSAR statements do not support CEDM design attribute (4OA5.3)
05000336/2005301-01 URI Simulator Deficiencies Identified During NRC Exam Process (4OA5.4)
05000423/2005008-02 URI Millstone Unit 3 Simulator Demonstration of Expected Plant Response to Operator Input and to Normal Conditions (Reactor Heat-up Operations) Using Only Operator Actions Normal to the Reference Unit (4OA5.5)

Discussed

05000336,423/2005008-01 URI Acceptability or Suitability of Millstone Unit 2 and Unit 3 Simulator Scenario-Based-Tests (SBTs) For Meeting ANSI/ANS-3.5-1998 Performance Testing Criteria (4OA5.6)
05000336/2005301-02 URI Potential Gap in Technical Specification Requirements for Nuclear Instrument Operability (4OA5.7)

LIST OF DOCUMENTS REVIEWED