ML18009A743

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LER 90-022-00:on 901108,missed Surveillance Test for Secondary Waste Sample Tank Due to Incorrect Procedure Rev
ML18009A743
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 12/06/1990
From: RICHEY R B, VERRILLI M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
HO-900202-(O), LER-90-022-01, LER-90-22-1, NUDOCS 9012120132
Download: ML18009A743 (5)


Text

ACCELERATED DISTR BUTION DEMONSTRATION SVS>aiVI REGULATORY INFORMATION DXSTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9012120132 DOC.DATE: 90/12/06 NOTARIZED:

NO FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION VERRILLI,M.

'arolina Power 6 Light Co.RICHEY,R.B.

Carolina Power 6 Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET N 05000400

SUBJECT:

LER 90-022-00:on 901108,missed surveillance test for secondary waste sample tank due to incorrect procedure rev.DXSTRIBUTION CODE: IE22T COPXES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Inciden Rpt, etc.NOTES:Application for permit renewal filed.05000400 A RECIPIENT ID CODE/NAME PD2-1 LA BECKER, D, INTERNAL: ACNW AEOD/DOA AEOD/ROAB/DS P NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB EXTERNAL EG&G BRYCE i J H NRC PDR NSIC MURPHY,G.A COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2'1 1.1 1 2.2 1 1 1 1 1 1 3 3 1 1 1 1 RECIPIENT ID CODE/NAME PD2-1 PD ACRS AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFBll NRR/DOEA/OEAB NRR/DST/SELB 8D NRR/BBDl REG FILE 02 RGN2 01 L ST LOBBY WARD NSIC MAYS,G NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 D D D NOTE TO ALL"RIDS" RECIPIENTS:

A D D PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT.20079)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUXRED: LTTR 33 ENCL 33 CNIL Carolina Power 8 Ljght Company P.O.Box 165~New Hill, N.C.27562 DEC 0 6 1990 R.8.AICHEY Vice Preaideflt Harria Nuclear Project Letter Number.'H0-900202 (0)U.S.Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO.50-400 LICENSE NO NPF-63 LICENSEE EVENT REPORT 90-022-00 Gentlemen.'I In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted.

This report fulfills the requirement for a written report within thirty (30)days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September 1983.Very truly yours, p/,/i R.B.Richey Vice President Harris Nuclear Project RBR:msb Enclosu're cc: Mr.R.A.Becker (NRR)Mr.S.D.Ebneter (NRC-RII)Mr.J.E.Tedrow (NRC-SHNPP)90i2i20132 90i206.PDR ADOCK 05000400 8 PDC MEM/LER-90-022/1/Osl l~iilC FORM 355 (549)US.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LERI PPROVED OMB NO.3)504)OC EXPIRES: C/30/9'2 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REGUESTr 50.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS ANO REPORTS MANAGEMENT BRANCH IP430).U.S.NUCLEAR REGULATORY COMMISSION.

WASHINGTON, OC 20555.AND TO THE PAPERWORK REDUCTION PROJECT (3150410CI.

OFFICE OF MANAGEMENT ANO BUDGET, WASHINGTON.

OC 20503.FACILITY NAME (1)Shearon Harris Nuclear Power Plant-Unit//1 TITLK Iel Missed Surveillance Test Due to Incorrect Procedure Revision DOCKET NUMBER (2)PA 5 3 0 5 0 0 04 0 0 1 OFO 3 MONTH OAY YEAR YEAR EVENT DATE (5)I.ER NUMBER (Sl SSOVSNTIAL NVMSSR REVISION rrvMBSR REPORT OATK (7)MONTH OAY YEAR OOCKFT NUMBER(s)0 5 0 0 0 FACILITY NAMES OTHER FACILITIES INVOLVED IS)0 8 909 0 022 0 0 12 069 0 0 5 0 0 0 OPERATING MODE (Sl POWER LEYEL 1 0 0 r"'r+a e4kk<20A02(bl 20AOS(el(1)(i) 20AOSI~)(1)(SI 20 ASS(e)ll I ()BI 20AOS(el(1)(ie) 20.COS(el(1 l(el 20AOSIcl SOM(cl(II SOM(cl(2)50.73(ell2) li)50.73(el(2)

(9)50.73(el(2)

IIII)LICENSEE CONTACT FOR THIS LER H2)50.73(e I (2)I Ie)50,73(el(2)(e) 50.73(el(2)(eSI 50,73(e I (2)(riii)(A)50.73(e)12)lriS)(5)50.73(~l(2)(el THIS REPORT IS SUBMITTED PURSUANT T 0 THE RLGUIRKMENTS OF 10 CFR (): IChecrr one or more o/the/orrorrin/I (11 73.71(SI 73.71(cl OTHER/Speclly/n AOrtrect Oererrenr/

ln Teer,//RC FOrm 3661/NAME Michael Verrilli-Regulatory Compliance Technician TELEPHONE NUMBER AREA CODE 91 936 2-230 3 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE OKSCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAC.TURKR CAUSE SYSTEM COMPONENT MANUFAC.TURER F.PORTABLE TO NPRDS A&k SUPPLEMENTAL REPORT EXPECTED (ICI X NO YES II/yer, complete EXPECTED Sr/8M/SS/D//

DATE/ABsTRAcT IL/mlt to/coo rp>>cct,/.A.epproelmerely

/llrecn rrnprccpece typcrrrrtrcn

/incr/llsl EXPECTED SU 5 MISSION OATS II Sl MONTH OAY YEAR On November 8, 1990, the plant was operating in Mode 1 at 100K power.Upon evaluation of a Significant Operational Occurrence Report (SOOR)it was determined that part of the required surveillance test for the Secondary Waste Sample Tank (SWST)Radiation Monitor HAREM"21WS-3542 had not been performed within its quarterly time interval.This was due to a revisi."n of the applicable maintenance surveillance test procedure (MST-I0330 Secondary Waste Tank Dx,scharge Monitor Operational Test).This revision incorrectly deleted the"loss of counts test" portion of the procedure that was required by Technical Specification (TS)Section 4.3.3.10 table 4.3-8 item l.a.3 table notation (1)b.As a result, the"loss of counts test" was not performed within its 92 day frequency (plus 23-days for 25K margin)and violated TS Section 4.3.3.10 for a period of 25 days.The cause of this incident was a misinterpretation of TS requirements on the part of maintenance procedure personnel.

The following corrective actions were taken'.MST-I0330 was revised to re-insert the"loss of counts test" into the procedure and maintenance procedure personnel were counseled on the incident to provide emphasis on the importance of understanding surveillance requirements in MST procedures to prevent future recurrence.

In addition, Radiation Monitor HAREM-21WS-3542 will be tested upon completion of maintenance and returned to operable status.A review of composite samples taken revealed no non-natural activity present in the SWST release;therefore, no significant safety consequences resulted from this event.This event is being reported in accordance with lOCFR50.73 (a)(2)(i)(B)as a TS violation.

NRC Form 355 (549)

NRC FORM366A I~o$9)US.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)TEXT CONTINUATION APPROVED 0 M 0 NO.31504)04 EXPIRES: a/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 50J)HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (F430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (3150410al.

OFFICE OF MANAGEMENT AND BUDGET,WASHINGTON, DC 20503.FACILITY NAME (1)Shearon Harris Nuclear Power Plant Unit 81 TEXT///more space/s IeEIa)ed, use ddd/dona/HRC ferns 3564's/OT)DOCKET NUMBER (2)o s o o o 40 YEAR LER NUMBER (6)SEOVENTIAL k.: NVMSEA 0 2 2 (@AEVISION NVMSEA 0 0 PAGE (3)02 oFO 3 EVEHT DESCRIPTION:

On November 6, 1990, the plant was operating in Mode 1 at 100X power.Maintenance procedure personnel submitted a SOOR to the Shift Foreman in the Main Control Room.This was in regard to the requirements of TS Table 4.3-8.Upon evaluation by the Regulatory Compliance group on November 8, 1990, it was determined that section 4.3.3.10 table 4.3-8 item l.a.3 table notation (1)b.required a quarterly (once per 92 days)"loss of counts test" for Radiation Monitor REM-21WS-3542.

This test had last been performed satisfactorily on April 26, 1990, as a part of MST-I0330 (Secondary Waste Tank Discharge Monitor Operational Test).A revision to this procedure was issued on July 7, 1990, to comply with corrective action number 5 of LER-90-005.

This corrective action required the deletion of steps in procedure MST-Z0356 that disconnected and subsequently reconnected coaxial cables.This revision was to prevent pin breakage in these cables, specifically for Radiation Monitor REM-1LT-3502A (RCS Leak Detection System).The corrective action also stated that this revision would apply to other applicable maintenance procedures.

This corrective action was incorrectly applied to MST-I0330.

Therefore, a time period of 140 days elapsed between the last satisfactory"loss of counts test", which occurred on April 26, 1990, and the day that the monitor was declared inoperable (for maintenance) on September 13, 1990.The 92 day frequency plus 23 days (25X margin)would have elapsed on August 20, 1990.This resulted in violation of TS section 4.3.3.10 for a period of 25 days.CAUSE: The cause of this event was a misinterpretation of TS requirements on the part of the individuals revising and reviewing the MST procedure while attempting to comply with the intent of LER 90-005-00 corrective action number 5.SAPETY SIGNIFICANCE:

There were no significant safety consequences as a result of this event.Although the"loss of counts" surveillance test was not performed within the required frequency, the monitor was verified twice a day to be operating properly by the performance of a trend check.This check is conducted and documented by Health Physics radiation monitoring system personnel.

Additionally, a composite sample is collected and analyzed on a weekly basis when continuous releases are made from the SWST.A review of these samples for the time period during which the surveillance interval was exceeded, revealed no non-natural activity present in the SWST release.NRC Foam 366A (669)

NRC FORM 355A etYT49)O ILS.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT ILER)TEXT CONTINUATION APPROVED OMB NO.31500)0l EXPIRES: e/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST1 50.0 HRS.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P430), U.S.NUCLEAR REGULATORY COMMISSION, WASHINGTON.

OC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE, OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503.FACILITY NAME (I)Shearon Harris Nuclear Power Plant Unit I/1 TEXT///more epece/e relrrkaL rree er///1/rme/HRC Fomr 3/l//49/(17)CORRECTIVE ACTIOHS: DOCKET NUMBER (2)o e o o o 4 o LER NUMBER (BI YEAR+%5 SECVENTIAL

'+@REVISION YRB NUMBER~?Nr NUMBEII 9 0 0 22 00 PAGE (3)0 3 03 DF 1.Procedure MST"I0330 was revised to re-insert the"loss of counts test" back into the procedure.

2.Maintenance procedure personnel were counseled on this incident to provide emphasis on the importance of understanding surveillance requirements in MST procedures.

3.Radiation Monitor gRITM-21WS-3542 will be tested upon completion of maintenance and returned to operable status.EISS CODE IMFORMATION:

Radiation Monitoring System IL NRC Form 355A (559)