ML18011A214

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Monthly Operating Rept for Sept 1993 for Harris Nuclear Plant Unit 1.W/931015 Ltr
ML18011A214
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 09/30/1993
From: CRENSHAW A, ROBINSON W R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9310210073
Download: ML18011A214 (12)


Text

ACCEI ERAT%9 DOCUMENT DIST UTION SYSTEM REGULAT~INFORMATION DISTRIBUTIO SYSTEM (RIDS)!I FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION CRENSHAW,A.

Carolina Power&'ight Co.ROBINSON,W.R.

Carolina Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET N 05000400

SUBJECT:

Monthly opera for Sept 1993 for Harris Nuclear Plant Unit 1/931015 1 r.DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTR ENCL SIZE: TITLE: Monthly Operating Report (per Tech Specs NOTES:Application for permit renewal filed.D 05000400/RECIPIENT ID CODE/NAME PD2-1 IA LE,N COPIES LTTR ENCL 3 3 1 1 RECIPIENT ID CODE/NAME PD2-1 PD COPIES LTTR ENCL 1 1 D INTERNAL: ACRS AEOD/DSP/TPAB NRR/DRIL/RPEB RGN2 10 10 AEOD/DOA 1 1 NRR/DORS OEAB 1 1~~LE Ol 1 1 1 1 1 1 1 1 D EXTERNAL: EG&G BRYCE,J.H NSIC 1 1 1 1 NRC PDR 1 1 R i I D i/i A D NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTEI CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2065)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!D TOTAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24

~j Carolina Power&Light Company P.O.Box 165 New Hill, NC 27562 OCT 1 5 1995 File Number: SHF/10-15505 Letter Number: H0931039 Document Control Desk United States Nuclear Regulatory Commission Washington, DC 20555 HARRIS NUCLEAR PLANT DEPARTMENT UNIT NO.1 DOCKET NO.50-400 LICENSE NO.NPF-63 MONTHLY OPERATIONS REPORT

Dear Sirs:

In accordance with Technical Specification 6.9.1.5 for the Harris Nuclear Power Plant, Unit No.1;Carolina Power 6 Light Company herewith submits the report of operation statistics and shutdown experience for the month of September 1993.Yours vc"y truly, W.R.Robinson General Manager Harris Nuclear Plant APC:bdd Enclosure I c: Mr.S.D.Ebneter (NRC-RII).Mr.J.E.Tedrow (NRC-SHNPP)

MIS/MTH-OPR.RPT/1/OS4 V3i 0210073.930930 PDR ADOCNP,05000400 8"'.~'"PDR'

~~~'

DOCKET NO.: 050-400 UNIT: Harris Unit 1 DATE: September 1993 COMPLETED BY: Amanda Crenshaw OPERATIONS

SUMMARY

Harris Unit 1 operated at 100 percent Availability Factor for the referenced month and a 98.16 percent Capacity Factor.There were two significant power reductions.

There are 157 fuel assemblies in the reactor vessel and 1031 spent fuel assemblies stored in the spent fuel pools.583 of the spent fuel assemblies are BWR, which were shipped to Harris from CP&L's Brunswick Plant.224 of the spent fuel assemblies are from CP&L's Robinson Plant.MISNMTH-OPR.RPTN2%0S4 CPKLCO RUN DATE (9/66/93 RUN TIME f 3:87'16 ,NT PERFORMANCE DATA SYSTEM OPERATING DATA REPORT HARR1S UNIT 3 PAGE RPD36-000 OPERATING STATUS DOCKET NO.050-400 COMPLETED BY AMANDA CRENBHAW TELEPHONE (919)362-2868 2~3 J 4, 5 4 6.7 1 8.UNIT NAME: HARRIS UNIT t NOTES REPORTIHG PERIOD: SEPTEMBER 93 I LICENSED THERMAL POWER (MWT): 2775 See Operations Summary.HAMEPLATE RATING (GROSS MWE): 950.9 I DESIGN ELECTRICAL RATING<NET MWE): 909.0 MAX DEPENDABLE CAPACITY (GROSS MWE): 920.0 (MAX DEPENDABLE CAPACITY (NET MWE): 860.0 IF CHAHGES OCCUR IH CAPACITY RATIHGS (ITEMS 3 THRU 7)SIHCE LAST REPORT i GIVE REASONS: None.9.19.POWER LEVEL TO WHICH RESTRICTED IF AHY (NET MWE): None.REASONS FQR RESTRICTION IF ANY: N/A THIS MONTH YR TO DATE CUMUL ATIVE 12.f3.14.15.16.$7.18.20.22 23.24.HOURS IH REPORTIHG PERIOD 720.00 NUMBER OF HOURS REACTOR CRITICAL 728.00 REACTOR RESERVE SHUTDOWN HRB.98 HOURS GENERATOR OH LIHE 720.00 UNIT RESERVE SHUTDOWN HOURS.00 GROSS THERMAL ENERGY GEH.(MWH)$969357.88 GROSS ELEC.ENERGY GEH.(MWH)647691.98 HET ELEC.ENERGY GENERATED (MWH)607827.00 UNIT SERVICE FACTOR 399.68 UNIT AVAILABILITY FACTOR 166.96 UNIT CAP.FACTOR<UBIHG MDC NET)98.16 UNIT CAP.FACTOR (USING DER HET)93.80 UNIT FORCED OUTAGE RATE.00 SHUTDOWNS SCHED.OVER NEXT 6 MOHTHS (TYPE, DATE, Unit scheduled for shutdown on March 5, 1994 for 6551.60 6524.41.00 6512.45.60 17859694.86 5980693.00 5612887.99 99.41 5'9.41 99.63 95.20.08 AND DURATION 56256.00 46693.33.60 45568.63.00 12329)730.30 40395534.00 37618563.98 8$.60 81.09 77.76 74.30 3.49 OF EACH): Refueling Outage Number 5.25.26.IF SHUTDOWN AT EHD QF REPORT PERIOD, ESTIMATED DATE OF START UP: UNITS IH TEST STATUS (PRIOR TO COMMERCIAL OPERATION):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATIOH f.f6" 9 MIS/MTH-OPR.

RPT/3/OS4

~~

~CPKLCO NT PERFORMANCE DATA SYSTEM RUH-DATE 10/06/93 APPENDIX B-AVERAGE DAILY POWER LEVEL RUN TIME 11:07: 36 HARRIS UNIT 1 PAGE RPD39-000 SEPTEMBER 3993 DAY AVG.DAILY POWER LEVEL (MWE-NET)DOCKET NO.050-400 COMPLETED BY AMAHDA CRENSHAW TELEPHOHE (919)362-2808 DAY AVG.DAILY POWFR LEVEL (MWE-HET)860 860 10 856 86)860 859 859 857 873 2()24 25 27 865 862 864 864 748 472 820 858 873 859 858 29 30 877 878 880 859 1.$6-8 MIS/MTH-OPR.RPT/4/OS4

~~t"i'~

UNIT SHUTDOWNS AND POWER REDUCTION I Q 7 O REPORT MONTH: September 1993 UNIT NAME: Harris DATE: September 1993 COMPLEIED BY: A.P.Crenshaw TELEPHONE:

(919)362-2808 93-005 Date 930924 T y P e Duration (Hours)0.0 R~e a s 0 n Method of Shutting Down Reactor'icensee Event Report¹N/A System Code 4 HH Component Code 5 Pump Cause and Corrective Action to Prevent Recurrence Unit power reduced to 85%to repair leak on the"B" Heater Drain Pump.A turbine valve test was also performed while at 85%power.During this event, power was further reduced to 50%for a period of time for repairs to the"B" Main Feed Pump (see event¹93-006).Unit was returned to 100%on September 26, 1993.1 F: Forced S: Scheduled 2 Reason: A-Equipment Failure (Explain)B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training 5.License Examination F-Administrative G-Operational Error (Explain)H-Other (Explain)3 Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-Continued 5-Reduced Load 6-Other 4 Exhibit G-Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER)File (NUREG-01 61)5 Exhibit 1-Same Source tg v UNIT SHUTDOWNS AND POWER REDUCTION I O O REPORT MONTH: September 1993 UNIT NAME: Harris DATE: September 1993 COMPLETED BY: A.P.Crenshaw TELEPHONE:

(919)362-2808 No.93406 Date 930924 T y P e Duration (Hours)0.0 R~e a s 0 A Method of Shutting Down Reactor'icensee Event Report¹N/A System Code 4 CH Component Code 5 Pump Cause and Corrective Action to Prevent Recurrence Unit power reduced to 50%for repairs of a seal pipiri'g leak on the"B" Main Feed Pump.This power reduction occurred while the plant was at 85%(see event¹93%05).Unit power returned to 85%on September 25, 1993 then to 100%on September 26, 1993.1 F: Forced S: Scheduled 2 Reason: A-Equipment Failure (Explain)8-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training&License Examination F-Administrative G-Operational Error (Explain)H-Other (Explain)3 Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-Continued 5-Reduced Load 6-Other 4 Exhibit G-Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER)File (NUREG-01 61)5 Exhibit 1-Same Source A A 4