ML17304B158

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Special Rept 2-SR-89-004:on 890406,preplanned Alternate Sampling Program Initiated When RCS Reached Temp of 555 F on 890330.Temporary Mod Request to Isolate Demineralized Water Sys Approved & Addl Sampling Performed
ML17304B158
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 05/03/1989
From: Haynes J
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
192-00475-JGH-T, 192-475-JGH-T, 2-SR-89-004, 2-SR-89-4, NUDOCS 8905160247
Download: ML17304B158 (8)


Text

A.C CELEPXTED Dl STR1Bt'TION DEMONg~gTlON 0 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8905160247 DOC.DATE: 89/05/03 NOTARIZED:

NO DOCKET Tent FACIL:STN-50-529 Palo Verde Nuclear Station, Unit, 2, Arizona Publi 05000529 AUTH.NAME AUTHOR AFFILIATION HAYNES,J.G.

Arizona Nuclear Power Project'.(formerly Arizona Public Serv RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Special Rept 2-SR-89-004:on 890406,post-accident sampling sys inoperable for period greater than 7 days.DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR

$ENCL g SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:Standardized plant.05000529 8 RECIPIENT ID CODE/NAME PD5 LA CHAN,T INTERNAL: ACRS MICHELSON ACRS WYLIE AEOD/DSP/TPAB DEDRO NRR/DEST/ADE SH NRR/DEST/CEB SH NRR/DEST/ICSB 7 NRR/DEST/MTB 9H NRR/DEST/RSB SE NRR/DLPQ/HFB 10 NRR/DOEA/EAB 11 SIB 9A REG FILE 02 E PRAB EXTERNAL: EG&G WILLIAMS,S L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A NOTES COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 4 4 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD5 PD DAVIS,M ACRS MOELLER AEOD/DOA AEOD/ROAB/DS P IRM/DCTS/DAB NRR/DEST/ADS 7E NRR/DEST/ESB SD NRR/DEST/MEB 9H NRR/DEST/PSB 8D NRR/DEST/SGB SD NRR/DLPQ/QAB 10 NRR/DREP/RPB 10 NUDOCS-ABSTRACT RES/DSIR/EIB RGN5 FILE 01 FORD BLDG HOY I A LPDR NSIC MAYS,G COPIES LTTR ENCL 1 1 1 1 2 2 1 1 2 2 1 1 1 0 1 1 1 1 1 1 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 R I NOIK'IO ALL"RIDS" RECIPZEPIS'IZASE HELP US IO REDUCE HASTE.'ORI'ACT

'%HE DOQ3MENI'OÃIROL DESK, RXN Pl-37 (EXT.20079)TO ELIMINATE~RQK EKR DZPHGEPZIGN LISTS H)R DOCUMENI'S YOU DON'T NEZDf h D D S TOTAL NUMBER OF COPIES REQUIRED: LTTR 46 ENCL 45

Arizona Nuclear Power Project P,O, BOX 52034~PHOENIX, ARIZONA 85072.2034 192-00475-JGH/TDS/JEM May 3, 1989 U.S.Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C.20555

Dear Sirs:

Subject:

Palo Verde Nuclear Generating Station (PVNGS)Unit 2 Docket No.STN 50-529 (License No.NPF-51)Special Report 2-SR-89-004 File: 89-020-404 Attached please find Special Report 2-SR-89-004 prepared and submitted pursuant to Technical Specifications 3.3.3.1 ACTION 28 and 6.9.2.This report discusses the Post Accident Sampling System being inoperable for more than 7 days.If you have any questions, please contact T.D.Shriver, Compliance Hanager, at (602)393-2521.Very truly yours, dQ J.G.Haynes Vice President Nuclear Production JGH/TDS/DAJ/kj Attachment cc: D.B.Karner E.E.Van Brunt, Jr.J.B.Hartin T.J.Polich H.J.Davis A.C.Gehr INPO Records Center (all w/attachments)

S905160247 890503 PDR ADOCK 05000529 9 PDC/r

PALO VERDE NUCLEAR GENERATING STATION PASS Inoperable for Greater Than 7 Days License No.NPF-51 Docket No.50-529 Special Report 2-SR-89-004 This Special Report is being submitted in accordance with Technical Specifications 3.3.3.1 ACTION 28-2 and 6.9.2 to report an event in which the Post Accident Sampling System (PASS)was inoperable for a period greater than 7 days.The 7 day limit for inoperability was exceeded at approximately 0800 MST on April 6, 1989.At approximately 0800 HST on March 30, 1989, Palo Verde Unit 2 was in Mode 3 (HOT STANDBY)at approximately 565 degrees F Reactor Coolant System (RCS)temperature and approximately 2255 psia pressurizer pressure when PASS was declared inoperable due to the planned isolation of the demineralized water supply to PASS.In accordance with Technical Specification 3.3.3.1 ACTION 28-1 the Preplanned Alternate Sampling Program (PASP)was initiated at 1924 HST on April 3, 1989.Prior to the event, at approximately 1630 HST on March 27, 1989, Palo Verde Unit 1 Chemistry personnel identified that a portion of the Demineralized Water System (DW)was contaminated.

Subsequent investigation in Unit 1 identified backflow from the Reactor Coolant System Hot Leg Loop 1 sample line backwards through two (2)check valves and one (1)normally closed solenoid valve into the DW system.The DW system is connected into the RCS sample line to provide flush water for sample lines routed to the sample sink in the Chemistry Hot Laboratory.

Flushing of the sample lines is to maintain radi ation exposure As Low As Reasonably Achievable (ALARA)in the event that PASP is utilized for PASS.On March 30, 1989, Unit 1 Operations personnel informed Units 2 and 3 personnel of the contamination of the Unit 1 DW lines.Unit 3 personnel investigated, but did not identify any contamination of the DW system.Unit 2 personnel investigated and identified contamination in the Unit 2 DW system.At approximately 0800 MST on March 30, 1989, Unit 2 personnel isolated the contaminated portion of the DW system by shutting isolation valve DWN-V-122.

Shutt'ing DWN-V-122 isolated several DW service lines including the DW supply to PASS and the DW supply to the RCS Hot Leg sample line that is used when PASP is being utilized.Unit 2 personnel determined that the valves in the DW supply line to PASP had leaked contaminated RCS back to the DW header.These valves were SSN-UV-564 (solenoid valve), SSN-V-856 (check valve), and SSN-V-857 (check valve).The DW supply line to PASS is required for operability of PASS, therefore, PASS was declared inoperable when DWN-V-122 was shut at approximately 0800 MST on March 30, 1989.The cause of the valves backleakage is not known at this time.A Root Cause of Failure will be performed by August 31, 1989.As an interim corrective action a Temporary Modification Request was approved on March 31, 1989.This modification isolates the DW system from the RCS Hot Leg sample line.This is

Special Report 2-SR-89-004 Page 2 accomplished by removing a section of the DW line between the first check valve and the tee into the RCS sample line and then capping the two open ends of the line.The modification was completed in Unit 2 on April 9, 1989.After successful completion of Surveillance Test 74ST-2SS04 (PASS functional Test)PASS was declared operable at 1140 MST on April 11, 1989.The modification was completed in Unit 1 on April 7, 1989 and will be implemented in Unit 3 by May 23, 1989.Additional sampling and analysis of the DW systems have been performed in Units 1 and 2 since the modification was completed.

No further radioactive contamination has been identified in the DW systems.Additionally, an investigation is being performed to review other similar connections between contaminated systems and"clean" flushing water systems.This investigation will be conducted to determine if additional controls are required to preclude other situations of cross-contamination.

This report will be supplemented by December 31, 1989, to report the root cause of the valves'eakage and any further corrective action that may be required due to the investigation.