ML19320C134

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Second Interim Part 21 Rept Re Steel Liner Plate in Reactor Containment Bldg.Progress on Repair Includes Completed Removal of Deformed Liner Plate & Detailed Mapping of Removed Plate Submitted to Contractor
ML19320C134
Person / Time
Site: South Texas  STP Nuclear Operating Company icon.png
Issue date: 06/06/1980
From: Eric Turner
HOUSTON LIGHTING & POWER CO.
To:
References
REF-PT21-80-210-001 ST-HL-AE-477, NUDOCS 8007160219
Download: ML19320C134 (6)


Text

ATTAGED IS A PART 21 REPORT FR01 IE tall BilT - ROOM 359 E/W

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7 o i-11 o -oo /

HA ou + Pm PART 21 IDENTIFICATION NO. COMPANY KVE l

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IMTE OF LETiER  %/ fr o DOCKET NO. So-49 r , ro -Y9 e IMTE DISTRIBUTED 4/ 9/ Fo DRIGINAL REPORT SUPPLFJENTARY L DISTRIBUTION:

REACIOR (R) [ FUEL CYCE & SAFEGUARDS (S)

FATERIALS (FD IE FIES

, IE FIES AD/RDI (2) IE FIES AD / SG AD/RCI AD / FFFSI AD / ROI EGIONS PEGIONS PEGIONS VENDORBR,RIV VENDOR BR R IV VEILDOR BR R IV ,

L0EB / MPA FT4B 5715 ffES / FCFS NRR / DDR AE0D Fi4B7602 L0EB / FPA FliB5715 NFES / SG SS-881 NRR / DDR (2) AEOD F14B7602 LOEB / MPA T14B 5715 NRR / DPM (2) CENTRAL FIES 016

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AEOD t4B 7602 Z CENTRAL FIES1 016 .

CENTRAL FIES (GRONL l' ~

~CDUPAL FIES 016 CEhTRAL FIES (GRON) PDR CBITRAL FIES (CHROM PDR LPDR - -

CENTPAL FIES SS -3:

PDR JERA' LPDR TERA ,

ACTION:

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PREL15}i55Y E dEbAYld 'Of THE TTN6HED 'REPORTfINDICATES LUPRESPONSIBIC'T T 5' ~

FOLLOW-UP AS SH M4 BELOW:

IE g NRR _ NFES [ OTHER 'i

@FFMSI 80072 60  ; REV. 6/L3/E.

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'$he Light COET.)dEE[ Hmim>n UMig n,wer m m>x Uno Hmim>n.'lexas ,,001 GW 22M2H June 6, 1980 ST-HL-AE-477 SFN: V-0530 fC)--1 l 0 -o a (

. Director, Region IV -

Nuclear Regulatory Commission 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76102

Dear Sir:

South Texas Project Units'l & 2 Docket Nos. STN 50-498, STN 50-499 Second Interim Report on Damage to The Steel Liner Plate in the Unit 2 Reactor Containment Building In the first interim report (ST-HL-AE-433) dated March 24, 1980, Houston Lighting and Power provided a logic for the Unit 2 Reactor Con-M tainment Building liner bulge repair. Provided for your information is -

a summary of the progress performed to date regarding the repair of the liner bulge.

- Pittsburgh Des Moines Steel Company, the containment liner sub-

. -.--2. . -. contractor, has completed.the. removal of the defonned liner .__ - . . . .

plate.

- A detailed mapping of the extent of the removed liner plate has .

been completed. This infonnation has in turn been provided to Pittsburgh Des Moines Steel Company in order that they may de-velop detailed shop drawings and procedures for the repair of the liner plate. . Discussions with Pittsburgh Des Moines Steel .

-Company have indicated that the detailed drawings and procedures.

_ should be-received shortly, m t.~owmerw-+Examinationcof-therconcrete-following-the -removal _of'the> deformedw--%ma

liner plate has- failet to disclose any unexpected or unusual con-- - --

crete void formations.

.The logic previously issued is currently undergoing revisions and will be submitted upon its completion.

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Ilonst.,n 1.igining & Power (:omp.iny ST-HL-AE-477 SFN: V-0530 June 6, 1980 Page 2 The next interim report will be submitted on July 11, 1980.

Should you have any questions, please contact Mr. S. S. Rodgers at (713) 676-7953.

Very truly yours ,

eq. . . ;

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E. A. Turner Vice President Power Piant Construction

& Technical Services RRH/mf O

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Houston tighti:*.3 & Paser Company ST-HL-AE-477 Page 3 cc: G. W. Oprea, Jr.

D. G. Barker C. L. McNeese H. R. Dean R. L. Waldrop G. B. Painter A. J. Granger R. A. Frazar M. D. Schwarz (Baker & Botts)

R. Gordon Gooch (Baker & Botts)

J. R. Nevtman (Lowenstein, Newman, Reis, Axelrad & Toll)

Director, Office of Inspection & Enforcement Nuclear Regulatory Commission

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Washington, D.C. 20555 M. L. Borchelt Executive Vice President Central Power & Light Company P. O. Box 2121 Corpus Christi, Texas 78403 _ _

R. L. Range Central Power & Light Company P. O. Box 2121 Corpus Christi, Texas 78403 R. L. Hancock Director of Electrical Utilities -

City of Austin P. O. Box 1088 - -

Austin, Texas 78767 M. C. Nitcholas City of Austin .

P. O. Box 1088 Austin, Texas 78767 J. B. Poston Assistant General Manager of Operations City Public Service Board ,

P. O. Box 1771 ~ ~ '

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San Antonio, Texas 78296 -

A.~vonRosenberg City Sublic Service Board P. O. Box 1771 San Antonio, Texas 78296 v -

Houston, Ugh:mg & her Company ST-HE-AE477 Page 4 Charles'Bechoefer, Esquire Chairman,' Atomic Safety & Licensing Board U.S. Nuclear ~ Regulatory Commission Washington,'D.C. 20555-Dr.' James C. Lamb, III 313 Woodhaven Road 4

Chapel-Hill, North Carolina 27514 Dr. Emmeth A. Luebke Atomic' Safety & Licensing Commission U.S. Nuclear Regulatory Commission

- Washington, D.C.20555 Steven A. Sinkin, Esquire 116 Villita Street

' San Antonio, Texas 78205 Citizens for Equitable Utilities c/o Ms. Peggy Buchorn Route 1, Box 432 Brazoria, Texas 77422 Richard W. Lowerre, Esquire Assistant Attorney General for the State of Texas P. 0.. Box 12548 .

Capitol Station Austin, Texas 78711 Henry J. McGurren, Esquire Hearing Attorney Office of the Executive Legal Director U.S. Nuclear Regulatory Commission Washington, D.C. 20555 v w e h

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instrument and control sysfems Effo"M' ,3L*$'*

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Tb40s 0 7-4?"9 April 24, lh00 RO: 604/

IIounton Lichting and Power Company bT- CD- HL - 1666 P.O. Etox 1700 Brown and Root Building $3 <

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Houcton, Texco 77001 g Centlemen:

Purcuant to the recent investigations of nomal nuclear power plant operation, Comsip, Inc.-has found that substantial '

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damage to the containment gas analysin cyte:nc may occur uhon the samplo inlet and return linec are cloced off whild the containment can , cyntem pumps are otill runninc.

Since the plant ' operating procedures- are boyond our' contro'1, _

end the recultinc damace may pose a cafety hazard once these lince are opened, Corm ni p , Inc. Lo issuing the following wor!:

Instructionc to modify the systea pumpc. Oneo implemented, tho - (lutomatic or manually operated nample line icoIntion valveu may be cloced without cubsequent dacago to the containment can cystem.

P2ecce find enclosed a copy of 'the- report to the 1:fic which d. .

initinted thic field rnodification. i~ote that i.t wee reporte under the requirements of 10Crn?1. The above modificatico ic r.icndatory and Cranip uracc you to contact uo cc ac>on ac

-possibic co^ce +we-may- providemthe - mod irication.. kit, to tha ,_ , _ ,

proper individuale.

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cuctome:- Set-vice t:anager a E C EIV ED .

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