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{{#Wiki_filter:NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION wm.LICENSEE EVENT REPORT CONTROL BLOCK: l llllll(PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 Ol@l 0 l0 l-0 l0 l0 l0 l0
{{#Wiki_filter:NRC FORM 366                                                                                                                                         U. S. NUCLEAR REGULATORY COMMISSION wm               .
-l 0 0 l@l4 1 l1 11 l1 l@l l@VAlN lA S 1 o i l 8 9 LICENSEE CODE 14 IS LIL E N5E NU*.'d E H 23 26 LICEN5E T YPE 30 Si LAIS3 CON'T 5C i t i@l 01 51 01 o f 01 31 31 81@] 01 I 01417 ] 91@l 1 l 0 ] ol a l 71 9@
LICENSEE EVENT REPORT CONTROL BLOCK: l                       l      l      l    l    l      l                    (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1                                           O o    i            VAlN lA                  S        1 l@lIS 0 l0 l- 0 l0 14 l0 l0 l0 -l 0 023l@l426 1LICEN5E LIL E N5E NU*.'d E H l1 11T YPE l1 30l@lSi    LAIS3 l@
" o i l 6 t. 0 f> l DOCK E T N U'.* 3 E R
l          8 9            LICENSEE CODE CON'T
(.3 fra EVENT OATE 14 5 REPORT D ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 21 l On September 4, 1979, durino Mode 1 operation. the motor driven auxiliarv co n +.. u n ,-
                        "
I o 3l pump 1-FW-P-3A became inoperable when the pump's lube oil strainer was removed for 1 o 4l maintenance after a lower than usual lube oil pressure was Observed. Tha hnalth and I o s j safety of the general public were not af fec+ed by this incident because the redundant I o cl auxiliary feedwater pumps 1-FW-P-3B and 1-FW-P-2 remained available for naaratio if l0 7l required.
o    i 5C i t i@l 01 51 01DOCK                            o fE T01      31 31 81@]       (.3 01 fra I 01417 ] 91@l5 1 l 0 EVENT OATE              14
Reportable pursuant to T.S. 6.o.l.9.b.
                                                                                                                                                                              ] ol a l 71 809@
l0 all80 7 8 9 SYSTE\1 CAUSE CAUSE COYP VALVE CODE CODE SUSCODE COVPONENT CODE SU8 CODE SUSCODEl Hl H @ l E h l X l@ l Fl ll L Tl E R h l z lh [_Z_j h o 9 1 8 9 10 11 12 73 18 19 20 SEQUEN TI AL OCCURRENCE REFORT REVISION EVENT YE AR RE POR T NO.
REPORT D ATE l           6                         t. 0           f> l                         N U'.* 3 E R EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 21 l On September 4, 1979, durino Mode 1 operation. the motor driven auxiliarv co n +.. u n ,-                                                                                                         I o   3      l pump 1-FW-P-3A became inoperable when the pump's lube oil strainer was removed for                                                                                                         1 o   4        l maintenance after a lower than usual lube oil pressure was Observed. Tha hnalth and                                                                                                       I o   s j safety of the general public were not af fec+ed by this incident because the redundant I o   c        l auxiliary feedwater pumps 1-FW-P-3B and 1-FW-P-2 remained available for naaratio                                                                                                 if l 0    7      l required.                   Reportable pursuant to T.S. 6.o.l.9.b.                                                                                                                       l 0  a                                                                                                                                                                                                    l l
CODE TYPE N o.@ "LE R RO l217 l9 ll-ll1 l0 l8 l I/ll0'.3[L_jl-l0 lug t_22 23 24 26 2/28 29 30 31 31 ACTION FUTURE EFFECT SHU T Do c.N ATT ACHV ENT N P R D-4 PHIVE COM; COYPONENT TAKEN ACTION ON PLANT METHOD HOURS SUSVITTED FORM Suts.
80 7           8 9 SYSTE\1                 CAUSE             CAUSE                                                             COYP             VALVE CODE                     CODE         SUSCODE                     COVPONENT CODE                       SU8 CODE           SUSCODE 1
SUPP LI E R MAN UF AC TUR EFs IDI@lzig zgl zig 10 l010l[vjgl N g Al@lCl714l5l@
o    9 8
33 34 35 36 3/40 41 42 43 44 4;CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O The decrease in the pu r.p's lube oil pressure was caused by a partially cloaced lobe 1[i li l l oil strainer.
l Hl H @ l E h l X l@ l Fl ll L Tl E R h l z lh [_Z_j h 9           10             11               12               73                                 18           19               20 SEQUEN TI AL                             OCCURRENCE             REFORT                     REVISION EVENT YE AR                                       RE POR T NO.                                 CODE                 TYPE                         N o.
After bei.: removed and disassembled, the strainer was cleaned. adjm t-i ed, and reinsta led.
                  @ "LE   ugR RO t
I , 7 IiI3I L I i g 7 8 9 80 STA S% PO/JER OTHER STATUS blSC V RY DISCOVERY DESCRIPTION NAlB l@lSurveillance Test ll E @ l 0l ol2l@l i 5 AC TIVI TY CO TENT RELEASED OF RELE ASE AVOUNT OF ACTIVITY LOCATION OF RELE ASE NAllNAl@@l Zl@li c 7 8 9 10 11 44 45 80 PERSONNE L E XPOSURES 0 l@TQl[ll0 0 1 7 7 8 9 11 12 13 80 PERSONNE L INJURIES f h'l h NUMHER DESCF, N C-lli p l l 0l 0 0l@l NA 7 8 9 11 12 80 LOSS OF OR D AVAGE TO FACILITY TYPE DESCHIPTION Lzjgj NA-) ) ~7li o 7 910100 W /
l-l              l1 l0 l8 l                 I/l              l  0'. 3               [L_j            l-l          0l
*, s 9 m Pus t iCi TY NHC USE ONLY
_  l217 22l9 l                23               24               26         2/             28       29           30               31         31 ACTION FUTURE                         EFFECT               SHU T Do c.N                                     ATT ACHV ENT         N P R D-4     PHIVE COM;               COYPONENT TAKEN ACTION                       ON PLANT                 METHOD                       HOURS               SUSVITTED         FORM Suts.         SUPP LI E R         MAN UF AC TUR EFs IDI@lzig 33           34                     35 zg                l zig 36 10 l010 3/                       40 l    [vjg 41 lNg 42                   43 Al@        lCl714l5l@
*ISSUEn DtSCR'PTION
44                   4; CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i   O           The decrease in the pu r.p's lube oil pressure was caused by a partially cloaced lobe                                                                                                   1
[219 ] [Njhl NA Tllllllllllll l}68 69 80 5 I d 9 10 NAMF OF PREPARER
[i li l l oil strainer.                                   After bei.: removed and disassembled, the strainer was cleaned. adjm t-
.. Ca ght 703-894-5151 2 pggyg; Virginia Electric and Power Company North Anna Power Station, Unit #1
      ,    7      i ed, and reinsta led.                                                                                                                                                                       I IiI3I L I
i g 7         8 9                                                                                                                                                                                           80 STA S                   % PO/JER                             OTHER STATUS                     blSC V RY                                 DISCOVERY DESCRIPTION i    5 l E @ l 0l ol2l@l                                           NA                          l      B l@l                  Surveillance Test                                                    l AC TIVI TY       CO TENT RELEASED OF RELE ASE                                   AVOUNT OF ACTIVITY                                                               LOCATION OF RELE ASE 7
i  c 8 9
                  @@l Zl@l          10             11 NA 44 l            l 45 NA 80 l
PERSONNE L E XPOSURES 1    7      l0        0 0 l@TQl                                 [                                                                                                                                 l 7         8 9                     11       12               13                                                                                                                                       80 PERSONNE L INJURIES NUMHER                  DESCF,              N f     h   'l h C-li p l l 0l 0 0l@l                                     NA 80 l
7           8 9                   11         12 LOSS OF OR D AVAGE TO FACILITY TYPE         DESCHIPTION i    o      Lzjgj                   NA                                                                                                     -) ) ~7                                                     l
  ,           s 9 ISSUEn m
Pus t iCi TY DtSCR'PTION 7 910100 W /                                                NHC USE ONLY
                                                                                                                                                                                                            *
                                                                                                                                                                                                                  *
[219 ] [Njhl                                 NA                                                                                                   T                l 68 69 llllllll              lll l}
I         d 9               10                                                                                                                                                                         80 5 NAMF OF PREPARER                                   .     . Ca             ght                                       pggyg;        703-894-5151                                 2
 
Virginia Electric and Power Company North Anna Power Station, Unit #1                


==Attachment:==
==Attachment:==
Page 1 of 1 Doc ke t No . 50-338 Report No. LER 79-103/03tc0 Description of Event On September 4,1979, during the performance of the monthly surveillance test, the lube oil pressure for the motor driven auxiliary feedwater pump 1-FW-P-3A was observed to be lower than usual.
Page 1 of 1 Doc ke t No . 50-338 Report No. LER 79-103/03tc0 Description of Event On September 4,1979, during the performance of the monthly surveillance test, the lube oil pressure for the motor driven auxiliary feedwater pump 1-FW-P-3A was observed to be lower than usual. The pump's lube oil strainer was removed for maintenance rendering 1-FW-P-3A inoperable. This event is contrary to T.S. 3.7.1.2.a.                                                                  .
The pump's lube oil strainer was removed for maintenance rendering 1-FW-P-3A inoperable.
Probable Consequences of Occurrence The consequences of this event were limited because the redundant motor driven auxiliary feedwater pump as well as the steam driven auxiliary feedwater pump were both available for operation if required. As a result, the public health and safety were not af fected by this event. There are no generic implications associated with this occurrence.
This event is contrary to T.S. 3.7.1.2.a.
Cause of Occurrence The low lube oil pressure was caused by the lube oil strainer being partially clogged.
.Probable Consequences of Occurrence The consequences of this event were limited because the redundant motor driven auxiliary feedwater pump as well as the steam driven auxiliary feedwater pump were both available for operation if required.
Immediate Corrective Action The lube oil strainer was removed and disassembled to allow for cleaning.
As a result, the public health and safety were not af fected by this event.
There are no generic implications associated with this occurrence.
Cause of Occurrence The low lube oil pressure was caused by the lube oil strainer being partially clogged.Immediate Corrective Action The lube oil strainer was removed and disassembled to allow for cleaning.
Af ter being thoroughly cleaned, the strainer was adjusted and reinstalled.
Af ter being thoroughly cleaned, the strainer was adjusted and reinstalled.
Scheduled Corrective Action No scheduled corrective action required.
Scheduled Corrective Action No scheduled corrective action required.
Actions Taken to Prevent Recurrence No further actions are required.
Actions Taken to Prevent Recurrence No further actions are required.
10:I2}}
10:I2}}

Revision as of 14:42, 19 October 2019

LER 79-108/03L-0:on 790904,motor-driven Auxiliary Feedwater Pump 1-FW-P-3A Inoperable.Caused by Removal of Strainer for Maint.Strainer Was Reinstalled
ML19209B701
Person / Time
Site: North Anna Dominion icon.png
Issue date: 10/04/1979
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209B689 List:
References
LER-79-108-03L, LER-79-108-3L, NUDOCS 7910100337
Download: ML19209B701 (2)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION wm .

LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l l (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 O o i VAlN lA S 1 l@lIS 0 l0 l- 0 l0 14 l0 l0 l0 -l 0 023l@l426 1LICEN5E LIL E N5E NU*.'d E H l1 11T YPE l1 30l@lSi LAIS3 l@

l 8 9 LICENSEE CODE CON'T

"

o i 5C i t i@l 01 51 01DOCK o fE T01 31 31 81@] (.3 01 fra I 01417 ] 91@l5 1 l 0 EVENT OATE 14

] ol a l 71 809@

REPORT D ATE l 6 t. 0 f> l N U'.* 3 E R EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 21 l On September 4, 1979, durino Mode 1 operation. the motor driven auxiliarv co n +.. u n ,- I o 3 l pump 1-FW-P-3A became inoperable when the pump's lube oil strainer was removed for 1 o 4 l maintenance after a lower than usual lube oil pressure was Observed. Tha hnalth and I o s j safety of the general public were not af fec+ed by this incident because the redundant I o c l auxiliary feedwater pumps 1-FW-P-3B and 1-FW-P-2 remained available for naaratio if l 0 7 l required. Reportable pursuant to T.S. 6.o.l.9.b. l 0 a l l

80 7 8 9 SYSTE\1 CAUSE CAUSE COYP VALVE CODE CODE SUSCODE COVPONENT CODE SU8 CODE SUSCODE 1

o 9 8

l Hl H @ l E h l X l@ l Fl ll L Tl E R h l z lh [_Z_j h 9 10 11 12 73 18 19 20 SEQUEN TI AL OCCURRENCE REFORT REVISION EVENT YE AR RE POR T NO. CODE TYPE N o.

@ "LE ugR RO t

l-l l1 l0 l8 l I/l l 0'. 3 [L_j l-l 0l

_ l217 22l9 l 23 24 26 2/ 28 29 30 31 31 ACTION FUTURE EFFECT SHU T Do c.N ATT ACHV ENT N P R D-4 PHIVE COM; COYPONENT TAKEN ACTION ON PLANT METHOD HOURS SUSVITTED FORM Suts. SUPP LI E R MAN UF AC TUR EFs IDI@lzig 33 34 35 zg l zig 36 10 l010 3/ 40 l [vjg 41 lNg 42 43 Al@ lCl714l5l@

44 4; CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O The decrease in the pu r.p's lube oil pressure was caused by a partially cloaced lobe 1

[i li l l oil strainer. After bei.: removed and disassembled, the strainer was cleaned. adjm t-

, 7 i ed, and reinsta led. I IiI3I L I

i g 7 8 9 80 STA S  % PO/JER OTHER STATUS blSC V RY DISCOVERY DESCRIPTION i 5 l E @ l 0l ol2l@l NA l B l@l Surveillance Test l AC TIVI TY CO TENT RELEASED OF RELE ASE AVOUNT OF ACTIVITY LOCATION OF RELE ASE 7

i c 8 9

@@l Zl@l 10 11 NA 44 l l 45 NA 80 l

PERSONNE L E XPOSURES 1 7 l0 0 0 l@TQl [ l 7 8 9 11 12 13 80 PERSONNE L INJURIES NUMHER DESCF, N f h 'l h C-li p l l 0l 0 0l@l NA 80 l

7 8 9 11 12 LOSS OF OR D AVAGE TO FACILITY TYPE DESCHIPTION i o Lzjgj NA -) ) ~7 l

, s 9 ISSUEn m

Pus t iCi TY DtSCR'PTION 7 910100 W / NHC USE ONLY

[219 ] [Njhl NA T l 68 69 llllllll lll l}

I d 9 10 80 5 NAMF OF PREPARER . . Ca ght pggyg; 703-894-5151 2

Virginia Electric and Power Company North Anna Power Station, Unit #1

Attachment:

Page 1 of 1 Doc ke t No . 50-338 Report No. LER 79-103/03tc0 Description of Event On September 4,1979, during the performance of the monthly surveillance test, the lube oil pressure for the motor driven auxiliary feedwater pump 1-FW-P-3A was observed to be lower than usual. The pump's lube oil strainer was removed for maintenance rendering 1-FW-P-3A inoperable. This event is contrary to T.S. 3.7.1.2.a. .

Probable Consequences of Occurrence The consequences of this event were limited because the redundant motor driven auxiliary feedwater pump as well as the steam driven auxiliary feedwater pump were both available for operation if required. As a result, the public health and safety were not af fected by this event. There are no generic implications associated with this occurrence.

Cause of Occurrence The low lube oil pressure was caused by the lube oil strainer being partially clogged.

Immediate Corrective Action The lube oil strainer was removed and disassembled to allow for cleaning.

Af ter being thoroughly cleaned, the strainer was adjusted and reinstalled.

Scheduled Corrective Action No scheduled corrective action required.

Actions Taken to Prevent Recurrence No further actions are required.

10:I2