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| 799 Roosevelt Road j/ | | 799 Roosevelt Road j/ |
| Clen ElLyn, Illinois 60137 4Y / | | Clen ElLyn, Illinois 60137 4Y / |
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| RE: Perry Nuclear Power Planc ) | | RE: Perry Nuclear Power Planc ) |
| Dockec Nos. 50-440; 50-441 > | | Dockec Nos. 50-440; 50-441 > |
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| I This letter serves as the Final Report as required by 10CFR50.55(e) concerning i lamination identifled in ASTM A36 gussec place hanger steel material. This was [ | | I This letter serves as the Final Report as required by 10CFR50.55(e) concerning i lamination identifled in ASTM A36 gussec place hanger steel material. This was [ |
| first reported by W. J. Racer of the Cleveland Electric Illuminating Company l to J. Nelsler of your office on December 19, 1980, and was followed up by the i Interim Report dated January 15, 1981. , | | first reported by W. J. Racer of the Cleveland Electric Illuminating Company l to J. Nelsler of your office on December 19, 1980, and was followed up by the i Interim Report dated January 15, 1981. , |
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| This Final Report includes a restacemenc of the description of the deficiency, l the corrective accion taken and overall conclusions. ; | | This Final Report includes a restacemenc of the description of the deficiency, l the corrective accion taken and overall conclusions. ; |
| Descripcion of Defielency [ | | Descripcion of Defielency [ |
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| showed that these indicacions were laminacions in the steel plate as received f rom the supplier. The place was cut from ASTM A36 macerial. This condicion l was documenced on L. K. Conscock Nonconformance Report EC-179. ! | | showed that these indicacions were laminacions in the steel plate as received f rom the supplier. The place was cut from ASTM A36 macerial. This condicion l was documenced on L. K. Conscock Nonconformance Report EC-179. ! |
| Corrective Accion Taken ! | | Corrective Accion Taken ! |
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| : 1. All gusset plate material of ASDi A36 held in field stock af ter February 1, [ | | : 1. All gusset plate material of ASDi A36 held in field stock af ter February 1, [ |
| 1980, was visually inspected for edge laminacions by the contractor (L. K. L Comstock) prior to ins tallation. Any place macerial exhibiting laminacion l was not used in any safecy-related hanger fabricacion. | | 1980, was visually inspected for edge laminacions by the contractor (L. K. L Comstock) prior to ins tallation. Any place macerial exhibiting laminacion l was not used in any safecy-related hanger fabricacion. |
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| U. S. Nuclear Regulatory Commission L 1 c/o Documenc Management Branch Washington, DC 20555 | | U. S. Nuclear Regulatory Commission L 1 c/o Documenc Management Branch Washington, DC 20555 |
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Similar Documents at Perry |
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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20217D5701998-03-20020 March 1998 Part 21 Rept 40 Re Governor Valve Stems Made of Inconel 718 Matl Which Caused Loss of Governor Control.Control Problems Have Been Traced to Valve Stems Mfg by Bw/Ip.Id of Carbon Spacer Should Be Increased to at Least .5005/.5010 ML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20137F3221997-03-26026 March 1997 Part 21 Rept Re Perry Nuclear Power Plant Experiencing False Trip of K600S K-Line Low Voltage Circuit Breaker w/SS-5 Solid State Trip Device.Breaker Removed from Svc & Returned to Abb for Analysis ML20133E8001997-01-0808 January 1997 Deficiency Rept Re Nonconformance Related to Masterflow 713 Grout,Which Master Builders,Inc Has Supplied as Nuclear SR Product to 18 Npps.Cause Unknown.Requests That Listed Info Be Provided to Gain Insight as to Scope & Possible Cause ML20134H3361996-11-0505 November 1996 Part 21 Rept Re Defective Inner Thrust Bearing 1801461-01 Used in PSA 35 Mechanical Shock Arrestor Used as Restraint on Piping Sys for Nuclear Generating Plant.Lot of Defective Parts Located & Isolated to Three Customers ML20115D2001996-07-0909 July 1996 Part 21 Rept Re Mfg Defect of Enterprise DSR-4 & DSRV-4 Edgs,Originally Mfg by Calcon Corp.Amot Control Corp Purchased Calcon Product Line & Maintains Design & Production.Valves Returned to Cooper Energy Svcs on 960131 ML20083R9101995-04-26026 April 1995 Final Part 21 Rept Re Kepco,Inc Model RMX24-D-20804 Power Supplies in Which Transistors Q15 &/Or Q16 Failed to Open & R1 Was Open.Replacement of Transmitters w/XSIS-095 Along W/ Replacement of Electrolytic Capacitors Provides Solution ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20059A7181993-10-19019 October 1993 Part 21 Rept Re Defective Rocker Arms Supplied to TU & Clei. Rocker Arms Machined & Inspected to Incorrect Print & Discovered at Tu.Defective Rocker Arms Recalled from Nuclear Customers.No Corrective Action Required at Respective Utils ML20056D7071993-07-15015 July 1993 Part 21 Rept Re Reportable defect-75 PSIG Relief Check Valve 1 Npt,Emd 9521844,Kepner 416C-1-75 ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed PY-CEI-NRR-1518, Corrected Part 21 Rept Re Defects in MSIV Poppets Supplied by Atwood & Morrill Co,Inc,Originally Submitted Via .Corrects Info in Corrective Action Section to Indicate That Poppet S/N 4 Not S/N 3 Installed at Facility1992-07-0101 July 1992 Corrected Part 21 Rept Re Defects in MSIV Poppets Supplied by Atwood & Morrill Co,Inc,Originally Submitted Via .Corrects Info in Corrective Action Section to Indicate That Poppet S/N 4 Not S/N 3 Installed at Facility ML17289A6971992-06-26026 June 1992 Amend 1 to Part 21 Rept 158 Re gear-wear Induced Failures in engine-driven Jacket Water Pump in DSRV-16-4 Standby DG Sys. Initially Reported on 911029.Grand Gulf Station Observed Wear Characteristics in as Little as 500 Operating Hours ML20102B2071992-06-24024 June 1992 Part 21 Rept Re Cracking of Stellite 21 Hardfacing on Guide Nose of Poppets Supplied as Part of MSIV Leakage Improvement Mod.Initially Reported by Clei on 920522. 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Initially Reported on 860326.Next Rept Expected by 860414 ML20202F4601986-04-0303 April 1986 Interim Part 21 & Deficiency Rept (Rdc 145(86)) Re Kaman Instrumentation Co High Voltage Power Supply (P/N 450447) Found Oscillating Between 240 & 1,030 Volts at 100 Hz. Initially Reported on 860326.Investigation Continuing ML20141A1081986-03-31031 March 1986 Part 21 Rept 134 Re Potential Defect in K-1 Relay in Generator Voltage Regulator.Initially Reported on 860219. Corrective Action Must Take Into Account Equipment Operating Range of 100-137.5-volt Dc ML20154Q3141986-03-10010 March 1986 Final Part 21 Rept Re Possible Defect on Inflatable Door Seals for Personnel Air Locks Used in Plant Reactor Containment Sys.Program to Supply Environmentally Qualified Inflatable Seals Should Be Completed by mid-1986 ML20154N4361986-03-10010 March 1986 Part 21 Rept Re Defect on Inflatable Door Seals for Personnel Air Locks Used in Reactor Containment Sys of Nuclear Power Plants.Initially Reported on 830919.Environ Qualification Testing of New Seal Design Completed 1999-04-12
[Table view] Category:TEXT-SAFETY REPORT
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[Table view] |
Text
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. - s l
P o. Box 5000
- CLEVELANo. oHlo 44101 e TELEPHONE (216) 622-9800
- ILLUMINATING BLOG. e 55 POOLIC SoVARE ,
Serving The Best Location in the Nation r Dalwyn R. Davidson i vice *ResiotNr gd %
SYSTEM ENGWEERWG AND CONSTRUChoN ;
o March 2, 1981 Yv 'Q N i
Mr. Jactes C. Keppler b h
\fh E. l Director of Region III y g#S b j Office of Inspeccion and Enforcemenc .e t U. S. Nuclear Regulatory Commission ,5' \ ** -
799 Roosevelt Road j/
Clen ElLyn, Illinois 60137 4Y /
RE: Perry Nuclear Power Planc )
Dockec Nos. 50-440; 50-441 >
Final Report on Lamination ;
l Identified in A36 Cussec l Place Hanger Steel Material j
Dear Mr. Keppler:
I This letter serves as the Final Report as required by 10CFR50.55(e) concerning i lamination identifled in ASTM A36 gussec place hanger steel material. This was [
first reported by W. J. Racer of the Cleveland Electric Illuminating Company l to J. Nelsler of your office on December 19, 1980, and was followed up by the i Interim Report dated January 15, 1981. ,
This Final Report includes a restacemenc of the description of the deficiency, l the corrective accion taken and overall conclusions. ;
Descripcion of Defielency [
- Some 1/2" x 5" x 8" places used for gussets on Class 1 eleccrical c.able cray I
hangers were found to have linear indications along the edges. An inveselgacion ,
showed that these indicacions were laminacions in the steel plate as received f rom the supplier. The place was cut from ASTM A36 macerial. This condicion l was documenced on L. K. Conscock Nonconformance Report EC-179. !
Corrective Accion Taken !
- 1. All gusset plate material of ASDi A36 held in field stock af ter February 1, [
1980, was visually inspected for edge laminacions by the contractor (L. K. L Comstock) prior to ins tallation. Any place macerial exhibiting laminacion l was not used in any safecy-related hanger fabricacion.
- 2. Concurrent with icem (1) above, hanger place material was changed via !
Engineering Change Nocice No. 3862-33-545 from ASTM A36 to ASTM A36 with i supplementary requirement S1 or ASDi A516 grade 70 with supplementary ,
requirement S8. This change was incended to improve place quality and
~
minimize the potencial for laminacions. Since che depletion of remaining field stock of A36 place material from item (1) above, all material has conformed to che new macerial requirements.
I
< s i J
8103 09 e ss; ID f i
, a =- -m - ,
- 4r. James G. Keppler March 2, 1981
- 3. For A36 gusset places installed prior to February 1,1530, a random sampling inspeccion program was conducted by L. K. Comscock Qualici Control Inspectors per guidelines as specified by the Project Organiza tion Nucicar Denign Section.
Based upon installation records, L. K. Conscock has identified .:.ac 498 hangers wich A36 gussec places were installed prior to February 1, 1980.
Thirty-chree (33) of chose gusset places were chosen on a random sample basis and inspec ced pe r che follovin6:
- a. The selected gussecs were ground on both 5" long place edges to remove existing painc. Exposed edges were visually inspected in accordance with the fn11owing acceptance criteria:
- 1. Laminar type edge discontinuities were not to exceed 1" in length.
- 2. Discontinuicies were considered to be continuous when separated by a distance less chan the length of the smaller of the two adjacent discontinuities.
- b. If the above acceptance criteria were violated, che place edges were re-ground and re-inspected per che above criteria, with the limitacion that the cocal amount of place material to be removed by grinding should not exceed 1/8" on each edge. If the acceptance criteria were still not satisfied af ter grinding 1/8", che gussec place was to be reported to the Project Organizacion as a violacion.
Results of the above inspeccion program have shown that all of the selected gussec places have me t the specified acceptance criteria. All inspeccions have been docu-menced by L. K. Comstock QC inspectors.
Analysis of Safecy Implicacion
- 1. '4ork installed prior co February 1,1980:
Since che gusset places selected for inspeccion are representative of all places installed prior to February 1,1980 and rul acceptance criteria vio-lacions were found, ic is concludc5 that work installed previous to this date is acceptable "as is". The originally documenced deficiency (L. K.
Comscock Nonconformance Report EC-179) involved cwo grossly laminated places which were pro 1 ably caused by improper billet cropping at the steel mill.
Per disposicio t of NR No. EC-179, these two plates were removed and replaced.
- 2. Jork installed after February 1, 1980:
As mencioned earlier, all remaining field stock of A36 gusset place was visually inspected for edge laminations. This insures no laminated A36 places have been used in hanger fabrication af *sr this date. Also, the change to different macerial types (ASTM A36 a ad ASTM A516, grade 70 with supplemencary requriements S1 and 3 8, respectively) should insure improved place quality. In addition, L. K. Comstock is doing on-going random in-speccion of this material for edge laminations. Material with laminacions will not be used in any hanger fabricacion.
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.- -Mr. J,ames C. Koppler March 2 1981 l 1 !
l Conclusion f
In summary, chis report concludes chac the originally documenced deficiency (NR {
No. EC-179) was an isolated case which was routinely identified because of the !
- gross nature of the laminacions. Appropriate corrective accion has been caken [
co correct chac specific deficiency as well as to insure previously inacalled i I
and fuctire hanger installations are free of significanc place laminacions.
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Very cruly yours, jf i
- Dalwy R. Davids j
! Vice residenc !*
! System Engineering and Construccion
! I I ksz !
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l cc: J. Hughes l i U. S. NRC -- Site !
i i -Mr. Victor Stello, Director [
Office of Inspe:cion and Enforcemenc !
U. S. Nuclear Regulatory Commission {
Washington, DC 20555 ;
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U. S. Nuclear Regulatory Commission L 1 c/o Documenc Management Branch Washington, DC 20555
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