ML15188A532: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(7 intermediate revisions by the same user not shown)
Line 2: Line 2:
| number = ML15188A532
| number = ML15188A532
| issue date = 07/07/2015
| issue date = 07/07/2015
| title = IR 05000458/2015009; on 01/26/2015 - 06/29/2015; River Bend Station; Special Inspection for the Scram With Complications That Occurred on December 25, 2014
| title = IR 05000458/2015009; on 01/26/2015 - 06/29/2015; River Bend Station; Special Inspection for the Scram with Complications That Occurred on December 25, 2014
| author name = Pruett T W
| author name = Pruett T
| author affiliation = NRC/RGN-IV/DRP
| author affiliation = NRC/RGN-IV/DRP
| addressee name = Olson E W
| addressee name = Olson E
| addressee affiliation = Entergy Operations, Inc
| addressee affiliation = Entergy Operations, Inc
| docket = 05000458
| docket = 05000458
Line 15: Line 15:
| page count = 43
| page count = 43
}}
}}
See also: [[followed by::IR 05000458/2015009]]
See also: [[see also::IR 05000458/2015009]]


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:UNITED STATES
[[Issue date::July 7, 2015]]
                              NUCLEAR REGULATORY COMMISSION
                                                REGION IV
                                          1600 E. LAMAR BLVD
                                        ARLINGTON, TX 76011-4511
                                            July 7, 2015
EA-15-043
Mr. Eric W. Olson, Site Vice President
Entergy Operations, Inc.
River Bend Station
5485 U.S. Highway 61N
St. Francisville, LA 70775
SUBJECT: RIVER BEND STATION - NRC SPECIAL INSPECTION
              REPORT 05000458/2015009; PRELIMINARY WHITE FINDING
Dear Mr. Olson:
On June 29, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed a Special
Inspection at the River Bend Station to evaluate the facts and circumstances surrounding an
unplanned reactor trip. Based upon the risk and deterministic criteria specified in NRC
Management Directive 8.3, NRC Incident Investigation Program, the NRC initiated a Special
Inspection in accordance with Inspection Procedure 93812, Special Inspection. The basis for
initiating the special inspection and the focus areas for review are detailed in the Special
Inspection Charter (Attachment 2). The NRC determined the need to perform a Special
Inspection on January 15, 2015, and the onsite inspection started on January 26, 2015. The
enclosed report documents the inspection findings that were discussed on May 21 and
June 29, 2015, with you and members of your staff. The team documented the results of this
inspection in the enclosed inspection report.
The enclosed inspection report documents a finding that has preliminarily been determined to
be White, a finding with low to moderate safety significance that may require additional NRC
inspections, regulatory actions, and oversight. The team identified an apparent violation for
failure to maintain the simulator so it would accurately reproduce the operating characteristics of
the facility. Specifically, the River Bend Station simulator failed to accurately model feedwater
flow and reactor vessel level response following a scram, failed to provide the correct alarm
response for loss of a reactor protection system motor generator set, and failed to correctly
model the operation of the startup feedwater regulating valve. As a result of the simulator
deficiencies, operations personnel were presented with additional challenges to control the plant
and maintain plant parameters following a reactor scram on December 25, 2014. Because
actions have been taken to initiate discrepancy reports, to investigate and resolve the potential
fidelity issues and to provide training to operations personnel, the simulator deficiencies do not
represent a continuing safety concern. The NRC assessed this finding using the best available
information, and Manual Chapter 0609, Significance Determination Process. The basis for the
NRCs preliminary significance determination is described in the enclosed report. The finding is
also an apparent violation of NRC requirements and is being considered for escalated
enforcement action in accordance with the Enforcement Policy, which can be found on the


EA-15-043 Mr. Eric W. Olson, Site Vice President Entergy Operations, Inc. River Bend Station 5485 U.S. Highway 61N St. Francisville, LA 70775
E. Olson                                        -2-
NRCs website at http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html.
The NRC will inform you in writing when the final significance has been determined.
Before we make a final decision on this matter, we are providing you with an opportunity to
(1) attend a Regulatory Conference where you can present your perspective on the facts and
assumptions used to arrive at the finding and assess its significance, or (2) submit your position
on the finding to the NRC in writing. If you request a Regulatory Conference, it should be held
within 30 days of your receipt of this letter. We encourage you to submit supporting
documentation at least one week prior to the conference in an effort to make the conference
more efficient and effective. The focus of the Regulatory Conference is to discuss the
significance of the finding and not necessarily the root cause(s) or corrective action(s)
associated with the finding. If you choose to attend a Regulatory Conference, it will be open for
public observation. The NRC will issue a public meeting notice and press release to announce
the conference. If you decide to submit only a written response, it should be sent to the NRC
within 30 days of your receipt of this letter. If you decline to request a Regulatory Conference or
to submit a written response, you relinquish your right to appeal the NRCs final significance
determination, in that by not choosing an option, you fail to meet the appeal requirements stated
in the Prerequisites and Limitations sections of Attachment 2, Process for Appealing NRC
Characterization of Inspection Findings (SDP Appeal Process), of NRC Inspection Manual
Chapter 0609.
Please contact Greg Warnick at (817) 200-1144, and in writing, within 10 days from the issue
date of this letter to notify us of your intentions. If we have not heard from you within 10 days,
we will continue with our final significance determination and enforcement decision. The final
resolution of this matter will be conveyed in separate correspondence.
Because the NRC has not made a final determination in this matter, no Notice of Violation is
being issued for this inspection finding at this time. In addition, please be advised that the
number and characterization of the apparent violation described in the enclosed inspection
report may change based on further NRC review.
In addition, the NRC inspectors documented four findings of very low safety significance
(Green) in this report. Three of these findings were determined to involve violations of NRC
requirements. The NRC is treating these violations as non-cited violations consistent with
Section 2.3.2.a of the Enforcement Policy.
If you contest the violations or significance of these non-cited violations, you should provide a
response within 30 days of the date of this inspection report, with the basis for your denial, to
the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,
Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,
Washington, DC 20555-0001; and the NRC resident inspector at the River Bend Station.
If you disagree with a cross-cutting aspect assignment in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your
disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the
River Bend Station.


SUBJECT: RIVER BEND STATION - NRC SPECIAL INSPECTION REPORT 05000458/2015009; PRELIMINARY WHITE FINDING
E. Olson                                    -3-
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public
Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your
response (if any) will be available electronically for public inspection in the NRC's Public
Document Room or from the Publicly Available Records (PARS) component of the NRC's
Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible
from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic
Reading Room).
                                              Sincerely,
                                              /RA/
                                              Troy W. Pruett
                                              Director
                                              Division of Reactor Projects
Docket No. 50-458
License No. NPF-47
Enclosure:
Inspection Report 05000458/2015009
    w/ Attachments:
    1. Supplemental Information
    2. Special Inspection Charter


==Dear Mr. Olson:==
On June 29, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed a Special Inspection at the River Bend Station to evaluate the facts and circumstances surrounding an unplanned reactor trip. Based upon the risk and deterministic criteria specified in NRC Management Directive 8.3, "NRC Incident Investigation Program," the NRC initiated a Special Inspection in accordance with Inspection Procedure 93812, "Special Inspection." The basis for initiating the special inspection and the focus areas for review are detailed in the Special Inspection Charter (Attachment 2). The NRC determined the need to perform a Special Inspection on January 15, 2015, and the onsite inspection started on January 26, 2015. The enclosed report documents the inspection findings that were discussed on May 21 and June 29, 2015, with you and members of your staff. The team documented the results of this inspection in the enclosed inspection report. The enclosed inspection report documents a finding that has preliminarily been determined to be White, a finding with low to moderate safety significance that may require additional NRC inspections, regulatory actions, and oversight. The team identified an apparent violation for failure to maintain the simulator so it would accurately reproduce the operating characteristics of the facility. Specifically, the River Bend Station simulator failed to accurately model feedwater flow and reactor vessel level response following a scram, failed to provide the correct alarm response for loss of a reactor protection system motor generator set, and failed to correctly model the operation of the startup feedwater regulating valve. As a result of the simulator deficiencies, operations personnel were presented with additional challenges to control the plant and maintain plant parameters following a reactor scram on December 25, 2014. Because actions have been taken to initiate discrepancy reports, to investigate and resolve the potential fidelity issues and to provide training to operations personnel, the simulator deficiencies do not represent a continuing safety concern. The NRC assessed this finding using the best available information, and Manual Chapter 0609, "Significance Determination Process." The basis for the NRC's preliminary significance determination is described in the enclosed report. The finding is also an apparent violation of NRC requirements and is being considered for escalated enforcement action in accordance with the Enforcement Policy, which can be found on the NRC's website at http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html. The NRC will inform you in writing when the final significance has been determined. Before we make a final decision on this matter, we are providing you with an opportunity to (1) attend a Regulatory Conference where you can present your perspective on the facts and assumptions used to arrive at the finding and assess its significance, or (2) submit your position on the finding to the NRC in writing. If you request a Regulatory Conference, it should be held within 30 days of your receipt of this letter. We encourage you to submit supporting documentation at least one week prior to the conference in an effort to make the conference more efficient and effective. The focus of the Regulatory Conference is to discuss the significance of the finding and not necessarily the root cause(s) or corrective action(s)
associated with the finding. If you choose to attend a Regulatory Conference, it will be open for public observation. The NRC will issue a public meeting notice and press release to announce the conference. If you decide to submit only a written response, it should be sent to the NRC within 30 days of your receipt of this letter. If you decline to request a Regulatory Conference or to submit a written response, you relinquish your right to appeal the NRC's final significance determination, in that by not choosing an option, you fail to meet the appeal requirements stated in the Prerequisites and Limitations sections of Attachment 2, "Process for Appealing NRC Characterization of Inspection Findings (SDP Appeal Process)," of NRC Inspection Manual Chapter 0609. Please contact Greg Warnick at (817) 200-1144, and in writing, within 10 days from the issue date of this letter to notify us of your intentions. If we have not heard from you within 10 days, we will continue with our final significance determination and enforcement decision. The final resolution of this matter will be conveyed in separate correspondence. Because the NRC has not made a final determination in this matter, no Notice of Violation is being issued for this inspection finding at this time. In addition, please be advised that the number and characterization of the apparent violation described in the enclosed inspection report may change based on further NRC review. In addition, the NRC inspectors documented four findings of very low safety significance (Green) in this report. Three of these findings were determined to involve violations of NRC requirements. The NRC is treating these violations as non-cited violations consistent with Section 2.3.2.a of the Enforcement Policy. If you contest the violations or significance of these non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the River Bend Station. If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the River Bend Station. In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/ Troy W. Pruett Director Division of Reactor Projects Docket No. 50-458 License No. NPF-47


===Enclosure:===
  SUNSI Review          ADAMS            Non-Sensitive        Publicly Available
Inspection Report 05000458/2015009 w/  
  By: RVA                  Yes  No        Sensitive            Non-Publicly Available
  OFFICE      SRI:DRP/B SRI:DRS/PSB2 RI:DRP/A          BC:DRS/OB SES:ACES          TL:ACES  BC:DRP/C
  NAME        THartman    JDrake          DBradley    VGaddy      RBrowder      MHay    GWarnick
  SIGNATURE /RA/          /RA/            /RA/        /RA/        /RA/          /RA/    /RA/
  DATE        06/04/15    06/04/15        06/05/15    06/30/15    06/04/15      06/04/15 06/04/15
  OFFICE      D:DRP
  NAME        TPruett
  SIGNATURE /RA/
  DATE        7/7/15
                                     
Letter to Eric Olson from Troy Pruett dated July 7, 2015.
SUBJECT: RIVER BEND STATION - NRC SPECIAL INSPECTION
            REPORT 05000458/2015009; PRELIMINARY WHITE FINDING
DISTRIBUTION:
Regional Administrator (Marc.Dapas@nrc.gov)
Deputy Regional Administrator (Kriss.Kennedy@nrc.gov)
DRP Director (Troy.Pruett@nrc.gov)
DRP Deputy Director (Ryan.Lantz@nrc.gov)
DRS Director (Anton.Vegel@nrc.gov)
DRS Deputy Director (Jeff.Clark@nrc.gov)
Senior Resident Inspector (Jeffrey.Sowa@nrc.gov)
Resident Inspector (Andy.Barrett@nrc.gov)
RBS Administrative Assistant (Lisa.Day@nrc.gov)
Branch Chief, DRP/C (Greg.Warnick@nrc.gov)
Senior Project Engineer (Ray.Azua@nrc.gov)
Project Engineer (Michael.Stafford@nrc.gov)
Project Engineer (Paul.Nizov@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov)
Public Affairs Officer (Lara.Uselding@nrc.gov)
RIV RSLO (Bill.Maier@nrc.gov)
Project Manager (Alan.Wang@nrc.gov)
Team Leader, DRS/TSS (Don.Allen@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov)
ACES (R4Enforcement.Resource@nrc.gov)
Regional Counsel (Karla.Fuller@nrc.gov)
Technical Support Assistant (Loretta.Williams@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)
RIV/ETA: OEDO (Michael.Waters@nrc.gov)
Senior Staff Engineer, TSB (Kent.Howard@nrc.gov)
Enforcement Specialist, OE/EB (Robert.Carpenter@nrc.gov)
Senior Enforcement Specialist, OE/EB (John.Wray@nrc.gov)
Branch Chief, OE (Nick.Hilton@nrc.gov)
Enforcement Coordinator, NRR/DIRS/IPAB/IAET (Lauren.Casey@nrc.gov)
Branch Chief, Operations and Training Branch (Scott.Sloan@nrc.gov)
NRREnforcement.Resource@nrc.gov
RidsOEMailCenterResource
ROPreports
Electronic Distribution via Listserv for River Bend Station


===Attachments:===
            U.S. NUCLEAR REGULATORY COMMISSION
1. Supplemental Information 2. Special Inspection Charter
                              REGION IV
Docket:          05000458
License:        NPF-47
Report:         05000458/2015009
Licensee:        Entergy Operations, Inc.
Facility:        River Bend Station, Unit 1
Location:        5485 U.S. Highway 61N
                St. Francisville, LA 70775
Dates:          January 26 through June 29, 2015
Inspectors:      T. Hartman, Senior Resident Inspector
                D. Bradley, Resident Inspector
                J. Drake, Senior Reactor Inspector
Approved By:    T. Pruett, Director
                Division of Reactor Projects
                                                      Enclosure


=SUMMARY OF FINDINGS=
                                      SUMMARY OF FINDINGS
IR 05000458/2015009; 01/26/2015 - 06/29/2015; River Bend Station; Special inspection for the scram with complications that occurred on December 25, 2014. The report covered one week of onsite inspection and in-office review through June 29, 2015, by inspectors from the NRC's Region IV office. One preliminary White apparent violation, three Green non-cited violations, and one Green finding were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination Process.Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
IR 05000458/2015009; 01/26/2015 - 06/29/2015; River Bend Station; Special inspection for the
scram with complications that occurred on December 25, 2014.
The report covered one week of onsite inspection and in-office review through June 29, 2015,
by inspectors from the NRCs Region IV office. One preliminary White apparent violation, three
Green non-cited violations, and one Green finding were identified. The significance of most
findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual
Chapter 0609, Significance Determination Process. Findings for which the significance
determination process does not apply may be Green or be assigned a severity level after NRC
management review. The NRCs program for overseeing the safe operation of commercial
nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,
dated December 2006.
Cornerstone: Initiating Events
*  Green. The team reviewed a self-revealing, non-cited violation of Technical
    Specification 5.4.1.a for the licensees failure to establish adequate procedures to properly
    preplan and perform maintenance that affected the performance of the B reactor protection
    system motor generator set. Specifically, due to inadequate procedures for troubleshooting
    on the B reactor protection system motor generator set, the licensee failed to identify a
    degraded capacitor that caused the B reactor protection system motor generator set output
    breaker to trip, which resulted in a reactor scram. The licensee entered this issue into their
    corrective action program as Condition Report CR-RBS-2014-06605 and replaced the
    degraded field flash card capacitor.
    This performance deficiency is more than minor, and therefore a finding, because it is
    associated with the procedure quality attribute of the Initiating Events Cornerstone and
    adversely affected the cornerstone objective to limit the likelihood of events that upset plant
    stability and challenge critical safety functions during shutdown as well as power operations.
    Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination
    Process (SDP) for Findings At-Power, Exhibit 1, Initiating Event Screening Questions, this
    finding is determined to have a very low safety significance (Green) because the transient
    initiator did not contribute to both the likelihood of a reactor trip and the likelihood that
    mitigation equipment or functions would not have been available. This finding has an
    evaluation cross-cutting aspect within the problem identification and resolution area because
    the licensee failed to thoroughly evaluate this issue to ensure that the resolution addressed
    the cause commensurate with its safety significance. Specifically, the licensee failed to
    thoroughly evaluate the condition of the field flash card to ensure that the cause of the trip
    had been correctly identified and corrected prior to returning the B reactor protection system
    motor generator set to service [P.2]. (Section 2.7.a)
Cornerstone: Mitigating Systems
*  Green. The team reviewed a self-revealing, non-cited violation of Technical
    Specification 5.4.1.a for the licensees failure to establish, implement and maintain a
    procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
                                                    -2-


===Cornerstone: Initiating Events===
  Specifically, Procedure OSP-0053, Emergency and Transient Response Support
: '''Green.'''
  Procedure, Revision 22, which is required by Regulatory Guide 1.33, inappropriately
The team reviewed a self-revealing, non-cited violation of Technical Specification 5.4.1.a for the licensee's failure to establish adequate procedures to properly preplan and perform maintenance that affected the performance of the B reactor protection system motor generator set. Specifically, due to inadequate procedures for troubleshooting on the B reactor protection system motor generator set, the licensee failed to identify a degraded capacitor that caused the B reactor protection system motor generator set output breaker to trip, which resulted in a reactor scram. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2014-06605 and replaced the degraded field flash card capacitor. This performance deficiency is more than minor, and therefore a finding, because it is associated with the procedure quality attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Using Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," Exhibit 1, "Initiating Event Screening Questions," this finding is determined to have a very low safety significance (Green) because the transient initiator did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not have been available. This finding has an evaluation cross-cutting aspect within the problem identification and resolution area because the licensee failed to thoroughly evaluate this issue to ensure that the resolution addressed the cause commensurate with its safety significance. Specifically, the licensee failed to thoroughly evaluate the condition of the field flash card to ensure that the cause of the trip had been correctly identified and corrected prior to returning the B reactor protection system motor generator set to service [P.2]. (Section 2.7.a)
  directed operations personnel to establish feedwater flow to the reactor pressure vessel
  using the startup feedwater regulating valve as part of the post-scram actions. The startup
  feedwater regulating valve operator characteristics are non-linear and not designed to
  operate in the dynamic conditions immediately following a reactor scram. To correct the
  inadequate procedure, the licensee implemented a change to direct operations personnel to
  utilize one of the main feedwater regulating valves until the plant is stabilized. This issue
  was entered in the licensees corrective action program as Condition
  Report CR-RBS-2015-00657.
  This performance deficiency is more than minor, and therefore a finding, because it is
  associated with the procedure quality attribute of the Mitigating Systems Cornerstone and
  adversely affected the cornerstone objective to ensure the availability, reliability, and
  capability of systems that respond to initiating events to prevent undesirable consequences.
  Specifically, the procedure directed operations personnel to isolate the main feedwater
  regulating valves and control reactor pressure vessel level using the startup feedwater
  regulating valve, whose operator was not designed to function in the dynamic conditions
  associated with a post-scram event from high power, and this challenged the capability of
  the system. The team performed an initial screening of the finding in accordance with
  Inspection Manual Chapter 0609, Appendix A, The Significance Determination
  Process (SDP) for Findings At-Power. Using Inspection Manual Chapter 0609, Appendix A,
  Exhibit 2, Mitigating Systems Screening Questions, the team determined that the finding is
  of very low safety significance (Green) because it: (1) was not a deficiency affecting the
  design or qualification of a mitigating structure, system, or component, and did not result in a
  loss of operability or functionality; (2) did not represent a loss of system and/or function;
  (3) did not represent an actual loss of function of at least a single train for longer than its
  technical specification allowed outage time, or two separate safety systems out-of-service
  for longer than their technical specification allowed outage time; and (4) did not represent an
  actual loss of function of one or more non-technical specification trains of equipment
  designated as high safety-significant in accordance with the licensees maintenance rule
  program. This finding has an evaluation cross-cutting aspect within the problem
  identification and resolution area because the licensee failed to thoroughly evaluate this
  issue to ensure that the resolution addressed the cause commensurate with its safety
  significance. Specifically, the licensee failed to properly evaluate the design characteristics
  of the startup feedwater regulating valve operator before implementing the procedure to use
  the valve for post-scram recovery actions [P.2]. (Section 2.7.b)
* Green. The team identified a non-cited violation of 10 CFR Part 50, Appendix B,
  Criterion XVI, Corrective Action, for the licensees failure to assure a condition adverse to
  quality was promptly identified. Specifically, the licensee failed to identify, that reaching the
  reactor pressure vessel water Level 8 (high) setpoint, on December 25, 2014, was an
  adverse condition, and as a result, failed to enter it into the corrective action program. To
  restore compliance, the licensee entered this issue into their corrective action program as
  Condition Report CR-RBS-2015-00620 and commenced a causal analysis for Level 8 (high)
  trips.
                                                  -3-


===Cornerstone: Mitigating Systems===
  This performance deficiency is more than minor, and therefore a finding, because it is
: '''Green.'''
  associated with the equipment performance attribute of the Mitigating Systems Cornerstone
The team reviewed a self-revealing, non-cited violation of Technical Specification 5.4.1.a for the licensee's failure to establish, implement and maintain a procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
  and adversely affected the cornerstone objective to ensure the availability, reliability, and
  capability of systems that respond to initiating events to prevent undesirable consequences.
  Specifically, failure to identify Level 8 (high) conditions and unplanned automatic actuations
  as conditions adverse to quality, would continue to result in the undesired isolation of
  mitigating equipment including reactor feedwater pumps, the high pressure core spray
  pump, and the reactor core isolation cooling pump. The team performed an initial screening
  of the finding in accordance with Inspection Manual Chapter 0609, Appendix A, The
  Significance Determination Process (SDP) for Findings At-Power. Using Inspection Manual
  Chapter 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the team
  determined that the finding is of very low safety significance (Green) because it: (1) was not
  a deficiency affecting the design or qualification of a mitigating structure, system, or
  component, and did not result in a loss of operability or functionality; (2) did not represent a
  loss of system and/or function; (3) did not represent an actual loss of function of at least a
  single train for longer than its technical specification allowed outage time, or two separate
  safety systems out-of-service for longer than their technical specification allowed outage
  time; and (4) did not represent an actual loss of function of one or more non-technical
  specification trains of equipment designated as high safety-significant in accordance with
  the licensees maintenance rule program. This finding has an avoid complacency
  cross-cutting aspect within the human performance area because the licensee failed to
  recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while
  expecting successful outcomes. Specifically, the licensee tolerated leakage past the
  feedwater regulating valves, did not plan for further degradation, and the condition ultimately
  resulted in the Level 8 (high) trip of the running reactor feedwater pump on December 25,
  2014 [H.12]. (Section 2.7.c)
* TBD. The team identified an apparent violation of 10 CFR 55.46(c)(1), Plant-Referenced
  Simulators, for the licensees failure to maintain the simulator so it would demonstrate
  expected plant response to operator input and to normal, transient, and accident conditions
  to which the simulator has been designed to respond. As of January 30, 2015, the licensee
  failed to maintain the simulator consistent with actual plant response for normal and
  transient conditions related to feedwater flows, alarm response, and behavior of the startup
  feedwater regulating valve controller. Specifically, the River Bend Station simulator failed to
  correctly model feedwater flows and resulting reactor vessel level response following a
  scram, failed to provide the correct alarm response for a loss of a reactor protection system
  motor generator set, and failed to correctly model the behavior of the startup feedwater
  regulating valve controller. As a result, operations personnel were challenged in their
  control of the plant during a reactor scram that occurred on December 25, 2014. This issue
  has been entered into the corrective action program as Condition
  Report RBS-CR-2015-01261, which includes actions to initiate simulator discrepancy
  reports, investigate and resolve the potential fidelity issues, and provide training to
  operations personnel on simulator differences.
  This performance deficiency is more than minor, and therefore a finding, because it is
  associated with the human performance attribute of the Mitigating Systems Cornerstone and
  adversely affected the cornerstone objective of ensuring availability, reliability, and capability
                                                  -4-


Specifically, Procedure OSP-0053, "Emergency and Transient Response Support Procedure," Revision 22, which is required by Regulatory Guide 1.33, inappropriately directed operations personnel to establish feedwater flow to the reactor pressure vessel using the startup feedwater regulating valve as part of the post-scram actions. The startup feedwater regulating valve operator characteristics are non-linear and not designed to operate in the dynamic conditions immediately following a reactor scram. To correct the inadequate procedure, the licensee implemented a change to direct operations personnel to utilize one of the main feedwater regulating valves until the plant is stabilized. This issue was entered in the licensee's corrective action program as Condition Report CR-RBS-2015-00657. This performance deficiency is more than minor, and therefore a finding, because it is associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the procedure directed operations personnel to isolate the main feedwater regulating valves and control reactor pressure vessel level using the startup feedwater regulating valve, whose operator was not designed to function in the dynamic conditions associated with a post-scram event from high power, and this challenged the capability of the system. The team performed an initial screening of the finding in accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power.Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," the team determined that the finding is of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensee's maintenance rule program. This finding has an evaluation cross-cutting aspect within the problem identification and resolution area because the licensee failed to thoroughly evaluate this issue to ensure that the resolution addressed the cause commensurate with its safety significance. Specifically, the licensee failed to properly evaluate the design characteristics of the startup feedwater regulating valve operator before implementing the procedure to use the valve for post-scram recovery actions [P.2].  (Section 2.7.b)
  of systems needed to respond to initiating events to prevent undesired consequences.
: '''Green.'''
  Specifically, the incorrect simulator response adversely affected the operations personnels
The team identified a non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for the licensee's failure to assure a condition adverse to quality was promptly identified. Specifically, the licensee failed to identify, that reaching the reactor pressure vessel water Level 8 (high) setpoint, on December 25, 2014, was an adverse condition, and as a result, failed to enter it into the corrective action program. To restore compliance, the licensee entered this issue into their corrective action program as Condition Report CR-RBS-2015-00620 and commenced a causal analysis for Level 8 (high) trips.
  ability to assess plant conditions and take actions in accordance with approved procedures
  during the December 25, 2014, scram. The team performed an initial screening of the
  finding in accordance with inspection Manual Chapter 0609, Appendix A, The Significance
  Determination Process (SDP) for Findings At-Power, Attachment 4, Initial Characterization
  of Findings. Using Inspection Manual Chapter 0609, Attachment 4, Table 3, SDP
  Appendix Router, the team answered yes to the following question: Does the finding
  involve the operator licensing requalification program or simulator fidelity? As a result, the
  team used Inspection Manual Chapter 0609, Appendix I, Licensed Operator Requalification
  Significance Determination Process (SDP), and preliminarily determined the finding was of
  low to moderate safety significance (White) because the deficient simulator performance
  negatively impacted operations personnel performance in the actual plant during a
  reportable event (reactor scram). This finding has an evaluation cross-cutting aspect within
  the problem identification and resolution cross-cutting area because the licensee failed to
  thoroughly evaluate this issue to ensure that the resolution addressed the extent of condition
  commensurate with its safety significance. Specifically, the licensees evaluation of the
  fidelity issue identified by the NRC in March 2014, focused on other training areas that used
  simulation, rather than evaluating the simulator modelling for additional fidelity
  discrepancies [P.2]. (Section 2.7.d)
* Green. The team identified a finding for the licensees failure to follow written procedures for
  classifying deficient plant conditions as operator workarounds and providing compensatory
  measures or training in accordance with fleet Procedure EN-OP-117, Operations
  Assessment Resources, Revision 8. A misclassification of these conditions resulted in the
  failure of the operations department to fully assess the impact these conditions had during a
  plant transient. The failure to identify operator workarounds contributed to complications
  experienced during reactor scram recovery on December 25, 2014. The licensee entered
  this issue into their corrective action program as Condition Report CR-RBS-2015-00795.
  This performance deficiency is more than minor, and therefore a finding, because it had the
  potential to lead to a more significant safety concern if left uncorrected. Specifically, the
  performance deficiency contributed to complications experienced by the station when
  attempting to restore feedwater following a scram on December 25, 2014. The team
  performed an initial screening of the finding in accordance with Inspection Manual
  Chapter 0609, Appendix A, The Significance Determination Process (SDP) for
  Findings At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2,
  Mitigating Systems Screening Questions, the team determined this finding is of very low
  safety significance (Green) because it: (1) was not a deficiency affecting the design or
  qualification of a mitigating structure, system, or component, and did not result in a loss of
  operability or functionality; (2) did not represent a loss of system and/or function; (3) did not
  represent an actual loss of function of at least a single train for longer than its technical
  specification allowed outage time, or two separate safety systems out-of-service for longer
  than their technical specification allowed outage time; and (4) did not represent an actual
  loss of function of one or more non-technical specification trains of equipment designated as
  high safety-significant in accordance with the licensees maintenance rule program. This
  finding has a consistent process cross-cutting aspect in the area of human performance
                                                -5-


This performance deficiency is more than minor, and therefore a finding, because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to identify Level 8 (high) conditions and unplanned automatic actuations as conditions adverse to quality, would continue to result in the undesired isolation of mitigating equipment including reactor feedwater pumps, the high pressure core spray pump, and the reactor core isolation cooling pump. The team performed an initial screening of the finding in accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power."  Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," the team determined that the finding is of very low safety significance (Green) because it:  (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensee's maintenance rule program. This finding has an avoid complacency cross-cutting aspect within the human performance area because the licensee failed to recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee tolerated leakage past the feedwater regulating valves, did not plan for further degradation, and the condition ultimately resulted in the Level 8 (high) trip of the running reactor feedwater pump on December 25, 2014 [H.12].  (Section 2.7.c)  TBD. The team identified an apparent violation of 10 CFR 55.46(c)(1), "Plant-Referenced Simulators," for the licensee's failure to maintain the simulator so it would demonstrate expected plant response to operator input and to normal, transient, and accident conditions to which the simulator has been designed to respond. As of January 30, 2015, the licensee failed to maintain the simulator consistent with actual plant response for normal and transient conditions related to feedwater flows, alarm response, and behavior of the startup feedwater regulating valve controller. Specifically, the River Bend Station simulator failed to correctly model feedwater flows and resulting reactor vessel level response following a scram, failed to provide the correct alarm response for a loss of a reactor protection system motor generator set, and failed to correctly model the behavior of the startup feedwater regulating valve controller. As a result, operations personnel were challenged in their control of the plant during a reactor scram that occurred on December 25, 2014. This issue has been entered into the corrective action program as Condition Report RBS-CR-2015-01261, which includes actions to initiate simulator discrepancy reports, investigate and resolve the potential fidelity issues, and provide training to operations personnel on simulator differences. This performance deficiency is more than minor, and therefore a finding, because it is associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring availability, reliability, and capability of systems needed to respond to initiating events to prevent undesired consequences. Specifically, the incorrect simulator response adversely affected the operations personnel's ability to assess plant conditions and take actions in accordance with approved procedures during the December 25, 2014, scram. The team performed an initial screening of the finding in accordance with inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," Attachment 4, "Initial Characterization of Findings."  Using Inspection Manual Chapter 0609, Attachment 4, Table 3, "SDP Appendix Router," the team answered 'yes' to the following question:  "Does the finding involve the operator licensing requalification program or simulator fidelity?"  As a result, the team used Inspection Manual Chapter 0609, Appendix I, "Licensed Operator Requalification Significance Determination Process (SDP)," and preliminarily determined the finding was of low to moderate safety significance (White) because the deficient simulator performance negatively impacted operations personnel performance in the actual plant during a reportable event (reactor scram). This finding has an evaluation cross-cutting aspect within the problem identification and resolution cross-cutting area because the licensee failed to thoroughly evaluate this issue to ensure that the resolution addressed the extent of condition commensurate with its safety significance. Specifically, the licensee's evaluation of the fidelity issue identified by the NRC in March 2014, focused on other training areas that used simulation, rather than evaluating the simulator modelling for additional fidelity discrepancies [P.2]. (Section 2.7.d)
because the licensee failed to use a consistent, systematic approach to making decisions
: '''Green.'''
and failed to incorporate risk insights as appropriate. Specifically, no systematic approach
The team identified a finding for the licensee's failure to follow written procedures for classifying deficient plant conditions as operator workarounds and providing compensatory measures or training in accordance with fleet Procedure EN-OP-117, "Operations Assessment Resources," Revision 8. A misclassification of these conditions resulted in the failure of the operations department to fully assess the impact these conditions had during a plant transient. The failure to identify operator workarounds contributed to complications experienced during reactor scram recovery on December 25, 2014. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2015-00795.
was enacted in order to properly classify deficient conditions [H.8]. (Section 2.7.e)
                                            -6-


This performance deficiency is more than minor, and therefore a finding, because it had the potential to lead to a more significant safety concern if left uncorrected. Specifically, the performance deficiency contributed to complications experienced by the station when attempting to restore feedwater following a scram on December 25, 2014. The team performed an initial screening of the finding in accordance with Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power."  Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," the team determined this finding is of very low safety significance (Green) because it:  (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensee's maintenance rule program. This finding has a consistent process cross-cutting aspect in the area of human performance because the licensee failed to use a consistent, systematic approach to making decisions and failed to incorporate risk insights as appropriate. Specifically, no systematic approach was enacted in order to properly classify deficient conditions [H.8].  (Section 2.7.e)
                                      REPORT DETAILS
1. Basis for Special Inspection
  On December 25, 2014, at 8:37 a.m., River Bend Station scrammed from 85 percent
  power following a trip of the B reactor protection system (RPS) motor generator (MG)
  set. At the time of the MG set trip, a Division 1 half scram existed due to an unrelated
  equipment issue with a relay for the Number 2 turbine control valve fast closure RPS
  function. The combination of the B RPS MG set trip and the Division 1 half scram
  resulted in a scram of the reactor.
  The following equipment issues occurred during the initial scram response.
  *    An unexpected Level 8 (high) reactor water level signal at +51 was received which
        resulted in tripping the running reactor feedwater pumps (RFPs).
  *    Following reset of the Level 8 (high) reactor water level signal, operations personnel
        were unable to start RFP C. They responded by starting RFP A at a vessel level of
        +25. The licensee subsequently determined that the circuit breaker (Magne Blast
        type) for RFP C did not close.
  *    Following the start of RFP A, the licensee attempted to open the startup feedwater
        regulating valve (SFRV) but was unsuccessful prior to the Level 3 (low) reactor water
        level trip setpoint at +9.7. The licensee then opened main feedwater regulating
        valve (FRV) C to restore reactor vessel water level. The lowest level reached
        was +8.1. Subsequent troubleshooting revealed a faulty manual function control
        card. The card was replaced by the licensee and the SFRV was used on the
        subsequent plant startup.
  Following restoration of reactor vessel water level, the plant was stabilized in Mode 3. A
  plant startup was conducted on December 27, 2014, with RPS bus B being supplied by
  its alternate power source. During power ascension following startup, RFP B did not
  start. The licensee re-racked its associated circuit breaker and successfully started
  RFP B. The licensee did not investigate the cause of RFP B failing to start.
  Management Directive 8.3, NRC Incident Investigation Program, was used to evaluate
  the level of NRC response for this event. In evaluating the deterministic criteria of
  Management Directive 8.3, it was determined that the event: (1) included multiple
  failures in the feedwater system which is a short term decay heat removal mitigating
  system; (2) involved two Magne Blast circuit breaker issues which could possibly have
  generic implications regarding the licensees maintenance, testing, and operating
  practices for these components including safety-related breakers in the high pressure
  core spray system; and (3) involved several issues related to the ability of operations to
  control reactor vessel level between the Level 3 (low) and Level 8 (high) trip setpoints
  following a reactor scram. Since the deterministic criteria were met, the trip was
  evaluated for risk. The preliminary Estimated Conditional Core Damage Probability was
  determined to be 1.2E-6.
                                              -7-


=REPORT DETAILS=
      Based on the deterministic criteria and risk insights related to the multiple failures of the
1. Basis for Special Inspection On December 25, 2014, at 8:37 a.m., River Bend Station scrammed from 85 percent power following a trip of the B reactor protection system (RPS) motor generator (MG) set. At the time of the MG set trip, a Division 1 half scram existed due to an unrelated equipment issue with a relay for the Number 2 turbine control valve fast closure RPS function. The combination of the B RPS MG set trip and the Division 1 half scram resulted in a scram of the reactor.
      feedwater system, the potential generic concern with the Magne Blast circuit breakers,
      and the issues related to the licensees operations departments inability to control
      reactor vessel level between the Level 3 (low) and Level 8 (high) setpoints following a
      reactor scram, Region IV determined that the appropriate level of NRC response was to
      conduct a Special Inspection.
      This Special Inspection is chartered to identify the circumstances surrounding this event,
      determine if there are adverse generic implications, and review the licensees actions to
      address the causes of the event.
      The team used NRC Inspection Procedure 93812, Special Inspection Procedure, to
      conduct the inspection. The inspections included field walkdowns of equipment,
      interviews with station personnel, and reviews of procedures, corrective action
      documents, and design documentation. A list of documents reviewed is provided in
      Attachment 1 of this report; the Special Inspection Charter is included as Attachment 2.
2.   Inspection Results
2.1  Charter Item 2: Develop a complete sequence of events related to the reactor scram
      that occurred on December 25, 2014.
  a. Inspection Scope
      The team developed and evaluated a timeline of the events leading up to, during, and
      after the reactor scram. This includes troubleshooting activities and plant startup. The
      team developed the timeline, in part, through a review of work orders, action requests,
      station logs, and interviews with station personnel. The team created the following
      timeline during their review of the events related to the reactor trip that occurred on
      December 25, 2014.
                  Date/Time                                        Activity
            December 6, 2014
            10:12 a.m.                A Division 2 half-scram was received from loss of the
                                      B RPS MG set, licensee initiated Condition
                                      Report CR-RBS-2014-06233
            10:17 a.m.                The RPS bus B was transferred to the alternate power
                                      supply, Division 2 half-scram was reset
                                                -8-


The following equipment issues occurred during the initial scram response. An unexpected Level 8 (high) reactor water level signal at +51" was received which resulted in tripping the running reactor feedwater pumps (RFPs).
    Date/Time                                Activity
December 13, 2014
12:35 p.m.        The B RPS MG set was restored
December 16, 2014
9:30 p.m.        The RPS bus B was placed on B RPS MG set
December 23, 2014
7:59 a.m.        The licensee commenced a reactor downpower to
                  85 percent to support maintenance on RFP B
08:30 a.m.        The RFP B was secured to support maintenance
10:28 a.m.        A Division 1 half-scram signal from the turbine control
                  valve 2 fast closure relay was received, licensee initiated
                  Condition Report CR-RBS-2014-06581
2:21 p.m.        The Division 1 half-scram signal was reset by bypassing the
                  turbine control valve fast closure signal
10:00 p.m.        RPS channel A placed in trip condition to satisfy Technical
                  Specification 3.3.1.1
December 25, 2014
8:37 a.m.        Reactor scram due to loss of RPS bus B
8:39 a.m.        Feedwater master controller signal caused all FRVs to close,
                  feedwater continued injecting at 520,000 lbm/hr (leakby
                  through valves), reactor pressure vessel (RPV) water level at
                  27.8
8:40 a.m.        RFP A was secured per procedure, RPV water level ~ 43,
                  feedwater flow lowered to 426,400 lbm/hr (leakby through
                  valves)
                          -9-


Following reset of the Level 8 (high) reactor water level signal, operations personnel were unable to start RFP C. They responded by starting RFP A at a vessel level of +25". The licensee subsequently determined that the circuit breaker (Magne Blast type) for RFP C did not close.
    Date/Time                                Activity
8:41 a.m.        Reactor water level reached Level 8 (high) condition, RFP C
                  (only running RFP) trips
8:42 a.m.        All FRVs and associated isolation valves were closed by
                  operations personnel and the SFRV placed in AUTO with a
                  setpoint at 18 per procedure
8:45 a.m.        Reactor water level dropped below 51 allowing reset of
                  Level 8 (high) signal and restart of RFPs
8:50 a.m.        RFP C failed to start, no trip flags on RFP breaker, RPV
                  water level ~ 33 and lowering, licensee initiated Condition
                  Report CR-RBS-2014-06601
8:52 a.m.         Operations personnel started RFP A
8:54 a.m.        Operations personnel reset the reactor scram signal on
                  Division 2 of RPS only, RPV water level ~ 17 and lowering
8:54 a.m.         The SFRV did not respond as expected in the automatic
                  mode. Operations personnel attempted to control the SFRV
                  in Manual, however it did not respond. As a result,
                  operations personnel began placing the FRV C in service,
                  licensee initiated Condition Report CR-RBS-2014-06602
8:56 a.m.        Water level reached Level 3 (low) and actuated a second
                  reactor scram signal, RPV water level reached ~ 8.1,
                  operations personnel completed placing FRV C in service
                  and reactor water level began to rise
8:57 a.m.        RPV water level rose above 9.7, reactor scram signal clear
8:58 a.m.        Operations personnel reset the reactor scram signal on
                  Division 2 of RPS only, RPV water level ~ 15.7
December 27, 2014
12:53 a.m.       The plant entered Mode 2 and commenced a reactor startup
                          -10-


Following the start of RFP A, the licensee attempted to open the startup feedwater regulating valve (SFRV) but was unsuccessful prior to the Level 3 (low) reactor water level trip setpoint at +9.7". The licensee then opened main feedwater regulating valve (FRV) C to restore reactor vessel water level. The lowest level reached was +8.1". Subsequent troubleshooting revealed a faulty manual function control card. The card was replaced by the licensee and the SFRV was used on the subsequent plant startup.
              Date/Time                                        Activity
        10:00 a.m.                RFP C failed to start due to the associated minimum flow
                                    valve not fully opening, licensee initiated Condition
                                    Report CR-RBS-2014-06653
        10:18 a.m.                Operations personnel started RFP A
        5:41 p.m.                  The plant entered Mode 1
        December 28, 2014
        7:23 p.m.                  RFP B failed to start, licensee initiated Condition
                                    Report CR-RBS-2014-06649
        8:43 p.m.                  The RFP B breaker was racked out and then racked back in
        8:49 p.m.                  RFP B was successfully started
b. Findings and Observations
  In reviewing the sequence of events and developing the timeline, the team reviewed the
  licensees maintenance and troubleshooting activities associated with the B RPS MG set
  failure on December 6, 2014. Additionally, the team reviewed the operability
  determination to evaluate the licensees basis for returning the B RPS MG set to service.
  The licensees troubleshooting practices lacked the technical rigor and attention to detail
  necessary to identify and correct the deficient B RPS MG set conditions. On several
  occasions, the team noted that the licensee chose the expedient solution rather than
  complete an evaluation to determine that corrective actions resolved the deficient
  condition. Specifically, the licensee chose to restore the B RPS MG set to service
  without fully understanding the failure mechanism. Other examples included the
  licensees choice to have operations personnel rack in and out breakers, and have
  maintenance personnel manually operate a limit switch, on the makeup and start logic
  for the RFP C minimum flow valve, when the RFP did not start. As indicated above, the
  licensee performed these compensatory actions instead of evaluating and correcting the
  issue.
  Based upon a review of the events leading up to the reactor scram, the team determined
  the licensee failed to properly preplan and perform maintenance on the B RPS MG set
  after the failure that occurred on December 6, 2014. Further discussion involving the
  licensees failure to adequately troubleshoot, identify, and correct degraded components
  on the B RPS MG set, prior to returning it to service, is included in Section 2.7.a. of this
  report.
                                            -11-


Following restoration of reactor vessel water level, the plant was stabilized in Mode 3. A plant startup was conducted on December 27, 2014, with RPS bus B being supplied by its alternate power source. During power ascension following startup, RFP B did not start. The licensee re-racked its associated circuit breaker and successfully started RFP B. The licensee did not investigate the cause of RFP B failing to start. Management Directive 8.3, "NRC Incident Investigation Program," was used to evaluate the level of NRC response for this event. In evaluating the deterministic criteria of Management Directive 8.3, it was determined that the event:  (1) included multiple failures in the feedwater system which is a short term decay heat removal mitigating system; (2) involved two Magne Blast circuit breaker issues which could possibly have generic implications regarding the licensee's maintenance, testing, and operating practices for these components including safety-related breakers in the high pressure core spray system; and (3) involved several issues related to the ability of operations to control reactor vessel level between the Level 3 (low) and Level 8 (high) trip setpoints following a reactor scram. Since the deterministic criteria were met, the trip was evaluated for risk. The preliminary Estimated Conditional Core Damage Probability was determined to be 1.2E-6.
    Additionally, the team reviewed the procedures that operations personnel used to
    respond to the reactor scram and determined the licensee failed to provide adequate
    procedures to respond to a post-trip transient. Further discussion on the procedure
    prescribing activities affecting quality not being appropriate for the circumstances is
    included in Section 2.7.b. of this report.
2.2  Charter Items 3 and 8: Review the licensees root cause analysis and corrective actions
    from the current and previous scrams with complications.
  a. Inspection Scope
    At the time of the inspection, the root cause report for the December 25, 2014, scram
    had not been completed. To ensure the licensee was conducting the cause evaluation
    at a level of detail commensurate with the significance of the problem, the team
    reviewed corrective action procedures, met with members of the root cause team, and
    reviewed prior related corrective actions.
    The procedures reviewed by the team included quality related Procedure EN-LI-118,
    Cause Evaluation Process, Revision 21, and quality related Procedure EN-LI-102,
    Corrective Action Program, Revision 24.
    The licensees approach for the December 25, 2014, scram causal evaluation was to
    use several detailed evaluations as input to the overall root cause. Specifically, the
    licensee performed an apparent cause evaluation, under Condition
    Report CR-RBS-2014-06696, to understand the failure of Division 2 RPS equipment.
    The licensee performed an apparent cause evaluation under Condition
    Report CR-RBS-2014-06602, to review the conditions that resulted in the additional
    reactor water Level 3 (low) trip, after the initial scram. The licensee also performed an
    apparent cause evaluation, under Condition Report CR-RBS-2014-06581, to review the
    turbine control valve fast closure circuit failure that resulted in the Division 1 half-scram
    signal. All of these evaluations were reviewed under the parent root cause Condition
    Report CR-RBS-2014-06605.
    The licensee used multiple methods in their causal evaluations that included: event and
    causal factor charting, barrier analysis, and organizational and programmatic failure
    mode trees. The licensees charter for the root cause evaluation required several
    periodic meetings with the members of the different causal analysis teams. It also
    required a pre-corrective action review board update and review, a formal corrective
    action review board approval, and an external challenge review of the approved root
    cause report.
    The NRC team also reviewed corrective actions to address complications encountered
    during previous reactor scrams. Specifically, the following NRC inspection reports were
    reviewed and the related licensee corrective actions were assessed:
        *  05000458/2002002, Integrated Inspection Report, July 24, 2002, ML022050206
                                              -12-


Based on the deterministic criteria and risk insights related to the multiple failures of the feedwater system, the potential generic concern with the Magne Blast circuit breakers, and the issues related to the licensee's operations department's inability to control reactor vessel level between the Level 3 (low) and Level 8 (high) setpoints following a reactor scram, Region IV determined that the appropriate level of NRC response was to conduct a Special Inspection. This Special Inspection is chartered to identify the circumstances surrounding this event, determine if there are adverse generic implications, and review the licensee's actions to address the causes of the event. The team used NRC Inspection Procedure 93812, "Special Inspection Procedure," to conduct the inspection. The inspections included field walkdowns of equipment, interviews with station personnel, and reviews of procedures, corrective action documents, and design documentation. A list of documents reviewed is provided in Attachment 1 of this report; the Special Inspection Charter is included as Attachment 2. 2. Inspection Results 2.1 Charter Item 2:  Develop a complete sequence of events related to the reactor scram that occurred on December 25, 2014.
        *    05000458/2006013, Special Inspection Team Report, March 1, 2007,
              ML070640396
        *    05000458/2012009, Augmented Inspection Team Report, August 7, 2012,
              ML12221A233
        *    05000458/2012012, Supplemental Inspection Report, December 28, 2012,
              ML12363A170
  b. Findings and Observations
    The NRC team found the licensees root cause team members had met the
    organizational diversity and experience requirements of their procedures. The team
    reviewed the qualifications of the members of the root cause team and determined they
    were within the correct periodicity.
    At the time of the inspection, there were 4 root cause and 10 apparent cause evaluations
    in progress. The team determined the root cause analyses were conducted at a level of
    detail commensurate with the significance of the problems.
    In reviewing corrective actions for prior scrams, the team noted that there have been five
    unplanned reactor scrams in the past five years, including the December 25, 2014,
    event. Of those five scrams, two involved Level 8 (high) reactor water level signal trips
    of all running feedwater pumps. Based upon a review of prior scrams and associated
    corrective actions, the team determined that the licensee does not have an appropriately
    low threshold for recognizing Level 8 (high) reactor water level signal trips as an adverse
    condition, and entering that adverse condition into their corrective action program.
    Otherwise, the team determined that the licensees corrective actions to address
    complications, encountered during previous reactor scrams, were adequate. Further
    discussion involving the licensees failure to identify Level 8 (high) reactor water level
    signal trips as adverse conditions is included in Section 2.7.c of this report.
2.3  Charter Item 4: Determine the cause of the unexpected Level 8 (high) water level trip
    signal.
  a. Inspection Scope
    To determine the cause of the unexpected Level 8 (high) reactor water level trip on
    December 25, 2014, the NRC team reviewed control room logs and graphs of key
    reactor parameters to assess the plants response to transient conditions. This
    information was then compared to the actions taken by operations personnel in the
    control room per abnormal and emergency operating procedure requirements.
    Section 5.1 of Procedure AOP-0001, Reactor Scram, Revision 30, required operations
    personnel to verify that the feedwater system was operating to restore reactor water
    level. This was accomplished using an attachment of Procedure OSP-0053,
    Emergency and Transient Response Support Procedure, Revision 22. Specifically,
    Attachment 16, Post Scram Feedwater/Condensate Manipulations Below 5% Reactor
                                              -13-


====a. Inspection Scope====
  Power, required transferring reactor water level control to the startup feedwater system
The team developed and evaluated a timeline of the events leading up to, during, and after the reactor scram. This includes troubleshooting activities and plant startup. The team developed the timeline, in part, through a review of work orders, action requests, station logs, and interviews with station personnel. The team created the following timeline during their review of the events related to the reactor trip that occurred on December 25, 2014.
  after reactor water level had been stabilized in the prescribed band.
  Only four minutes elapsed from the time of the scram until the time the Level 8 (high)
  reactor water level isolation signal was reached. Consequently, operations personnel
  did not have sufficient time to gain control and stabilize reactor vessel level in the
  required band.
  To gain an understanding of issues affecting systems at the time of the scram, the NRC
  team met with system engineers for the feedwater system, feedwater level control
  system, and remotely operated valves. Discussions with engineering included system
  health reports, open corrective actions from condition reports, licensee event reports,
  design data for systems, startup testing and exceptions, post-trip reactor water level
  setpoint setdown parameters, open engineering change packages, and requirements for
  engineering to analyze post-transient plant data.
b. Findings and Observations
  Operations personnel responded to the events in accordance with procedure
  requirements. The NRC did not identify any performance deficiencies related to
  immediate or supplemental actions taken by control room staff during the transient.
  However, operations personnel stated that the plant did not respond in a manner
  consistent with their simulator training.
  Based on review of operations personnel response to the event and the training received
  from the simulator, the NRC team determined that the licensee did not maintain the
  simulator in a condition that accurately represented actual plant response. On April 10,
  2015, the licensee provided a white paper with additional information related to the
  modeling of the plant-referenced simulator. Further discussion involving the licensees
  failure to maintain the simulator is included in Section 2.7.d of this report.
  The NRC team determined that the plant did not respond per the design as described in
  the final safety analysis report. Specifically, the feedwater level control system and
  feedwater systems were designed to automatically control reactor water level in the
  programmed band post-scram. During the December 25, 2014 scram, reactor water
  level quickly (within 4 minutes) rose to a Level 8 (high) trip. By design, reactor water
  level should rapidly lower after the initial level transient from core void collapse, rise as
  feedwater compensates for the level change, and then return to the programed
  setpoint. A Level 8 (high) trip should not occur. The team determined that significant
  leakage past the feedwater isolation valves caused the rapid rise in reactor water level.
  Operations personnel were unable to compensate for the rapid change in reactor vessel
  level. The licensee initially discovered the adverse condition during startup testing in
  1986, and allowed the condition to degrade without effective corrective actions.
  The team noted that significant post-trip or post-transient plant performance data was
  available to system engineers, but review of this data was not prioritized by the licensee.
  The review of plant transient data was primarily driven by the licensees root cause team
                                            -14-


Date/Time Activity December 6, 2014  10:12 a.m. A Division 2 half-scram was received from loss of the B RPS MG set, licensee initiated Condition Report CR-RBS-2014-06233 10:17 a.m. The RPS bus B was transferred to the alternate power supply, Division 2 half-scram was reset Date/Time Activity December 13, 2014  12:35 p.m. The B RPS MG set was restored December 16, 2014  9:30 p.m. The RPS bus B was placed on B RPS MG set December 23, 2014  7:59 a.m. The licensee commenced a reactor downpower to 85 percent to support maintenance on RFP B 08:30 a.m. The RFP B was secured to support maintenance 10:28 a.m. A Division 1 half-scram signal from the turbine control valve 2 fast closure relay was received, licensee initiated Condition Report CR-RBS-2014-06581 2:21 p.m. The Division 1 half-scram signal was reset by bypassing the turbine control valve fast closure signal 10:00 p.m. RPS channel A placed in trip condition to satisfy Technical Specification 3.3.1.1 December 25, 2014  8:37 a.m. Reactor scram due to loss of RPS bus B 8:39 a.m. Feedwater master controller signal caused all FRVs to close, feedwater continued injecting at 520,000 lbm/hr (leakby through valves), reactor pressure vessel (RPV) water level at 27.8" 8:40 a.m. RFP A was secured per procedure, RPV water level ~ 43", feedwater flow lowered to 426,400 lbm/hr (leakby through valves)
    charter or by self-assigned good engineering practices. At the time of this inspection,
Date/Time Activity 8:41 a.m. Reactor water level reached Level 8 (high) condition, RFP C (only running RFP) trips 8:42 a.m. All FRV's and associated isolation valves were closed by operations personnel and the SFRV placed in AUTO with a setpoint at 18" per procedure 8:45 a.m. Reactor water level dropped below 51" allowing reset of Level 8 (high) signal and restart of RFPs 8:50 a.m. RFP C failed to start, no trip flags on RFP breaker, RPV water level ~ 33" and lowering, licensee initiated Condition Report CR-RBS-2014-06601 8:52 a.m. Operations personnel started RFP A 8:54 a.m. Operations personnel reset the reactor scram signal on Division 2 of RPS only, RPV water level ~ 17" and lowering 8:54 a.m. The SFRV did not respond as expected in the automatic mode. Operations personnel attempted to control the SFRV in Manual, however it did not respond. As a result, operations personnel began placing the FRV C in service, licensee initiated Condition Report CR-RBS-2014-06602 8:56 a.m. Water level reached Level 3 (low) and actuated a second reactor scram signal, RPV water level reached ~ 8.1", operations personnel completed placing FRV C in service and reactor water level began to rise 8:57 a.m. RPV water level rose above 9.7", reactor scram signal clear 8:58 a.m. Operations personnel reset the reactor scram signal on Division 2 of RPS only, RPV water level ~ 15.7" December 27, 2014  12:53 a.m. The plant entered Mode 2 and commenced a reactor startup Date/Time Activity 10:00 a.m. RFP C failed to start due to the associated minimum flow valve not fully opening, licensee initiated Condition Report CR-RBS-2014-06653 10:18 a.m. Operations personnel started RFP A 5:41 p.m. The plant entered Mode 1 December 28, 2014  7:23 p.m. RFP B failed to start, licensee initiated Condition Report CR-RBS-2014-06649 8:43 p.m. The RFP B breaker was racked out and then racked back in 8:49 p.m. RFP B was successfully started
    the licensee had not quantified the amount of leakage past the FRVs, although the
    scram and subsequent startup had occurred one month earlier. The NRC team
    observed that there was a potential to miss important trends in plant performance
    without a more timely review.
2.4  Charter Item 5: Review the effectiveness of licensee actions to address known
    equipment degradations that could complicate post-scram response by operations
    personnel.
  a. Inspection Scope
    The NRC team reviewed licensee procedures for classifying and addressing plant
    conditions that may challenge operations personnel while performing required actions
    per procedures during normal and off-normal conditions.
    The team reviewed the licensees current list of operator workarounds and operator
    burdens. Specifically, the team was looking for any known equipment issues that could
    complicate post-scram response by operations personnel.
  b. Findings and Observations
    The team determined the licensee did not properly classify several deficient plant
    conditions as operator workarounds in accordance with fleet Procedure EN-OP-117,
    Operations Assessment Resources, Revision 8. Further discussion related to the
    failure to classify plant deficiencies as operator workarounds is included in Section 2.7.e
    of this report.
2.5  Charter Items 6 and 7: Review the licensees maintenance, testing and operating
    practices for Magne Blast circuit breakers including the causes and corrective actions
    taken to address the failure of the RFPs to start.
  a. Inspection Scope
    The team reviewed the final safety analysis report, system description, the current
    system health report, selected drawings, maintenance and test procedures, and
    condition reports associated with Magne Blast breakers. The team also performed
    walkdowns and conducted interviews with system engineering and design engineering
    personnel to ensure circuit breakers were capable of performing their design basis
    safety functions. Specifically, the team reviewed:
          *  Vendor and plant single line, schematic, wiring, and layout drawings
          *  Circuit breaker preventive maintenance inspection and testing procedures
          *  Vendor installation and maintenance manuals
          *  Preventive maintenance and surveillance test procedures
          *  Completed surveillance test and preventive maintenance results
          *  Corrective actions and modifications
                                              -15-


====b. Findings and Observations====
  b. Findings and Observations
In reviewing the sequence of events and developing the timeline, the team reviewed the licensee's maintenance and troubleshooting activities associated with the B RPS MG set failure on December 6, 2014. Additionally, the team reviewed the operability determination to evaluate the licensee's basis for returning the B RPS MG set to service. The licensee's troubleshooting practices lacked the technical rigor and attention to detail necessary to identify and correct the deficient B RPS MG set conditions. On several occasions, the team noted that the licensee chose the expedient solution rather than complete an evaluation to determine that corrective actions resolved the deficient condition. Specifically, the licensee chose to restore the B RPS MG set to service without fully understanding the failure mechanism. Other examples included the licensee's choice to have operations personnel rack in and out breakers, and have maintenance personnel manually operate a limit switch, on the makeup and start logic for the RFP C minimum flow valve, when the RFP did not start. As indicated above, the licensee performed these compensatory actions instead of evaluating and correcting the issue.
    Unresolved Item (URI) - Vendor and Industry Recommended Testing Adequacy on
    Safety-related and Safety-significant Circuit Breakers
    Introduction. The team identified an unresolved item related to the licensees breaker
    maintenance and troubleshooting programs for safety-related and safety-significant
    circuit breakers. The charter tasked the team with inspecting the issues associated with
    Magne Blast breaker problems that occurred during and after the December 25, 2014,
    scram. The NRC team determined that breaker maintenance and troubleshooting
    practices extended beyond the Magne Blast breakers. The team identified that there
    were potential issues with safety-related Master Pact breakers and determined that
    maintenance procedures used to ensure that 4160 V and 13.8 kV safety-related and
    safety-significant breakers were being maintained and overhauled in a timely manner
    may not conform to industry recommended standards.
    Description. The team identified that the licensees maintenance programs for Division I,
    II, III, and non-safety 4160 V and 13.8 kV breakers installed in the plant may not meet
    the standards recommended by the vendor, corporate, or Electric Power Research
    Institute (EPRI) guidelines. The licensees programs were based on EPRI
    documents TR-106857-V2 and TR-106857-V3, which were preventive maintenance
    program bases for low and medium voltage switchgear. However, the licensee
    appeared to only implement portions of the recommended maintenance program, and
    were not able to provide the team with engineering analyses or technical bases to justify
    the changes. The EPRI guidance was developed specifically for Magne Blast breakers
    based on industry operating experience, NRC Information Notices, and General Electric
    SILs/SALs. The NRC team was concerned that the licensee may not have performed
    the entire vendor or EPRI recommended tests, inspections, and refurbishments on the
    breakers since they were installed. The aggregate impact of missing these preventive
    maintenance tasks needs to be evaluated to determine if the reliability of the affected
    breakers has been degraded.
    Pending further evaluation of the above issue by the licensee and subsequent review by
    NRC inspectors, this issue will be tracked as URI 05000458/2015009-01, Vendor and
    Industry Recommended Testing Adequacy on Safety-related and Safety-significant
    Circuit Breakers.
2.6  Charter Item 9: Evaluate pertinent industry operating experience and potential
    precursors to the event, including the effectiveness of any action taken in response to
    the operating experience.
  a. Inspection Scope
    The team evaluated the licensees application of industry operating experience related to
    this event. The team reviewed applicable operating experience and generic NRC
    communications with a specific emphasis on Magne Blast breaker maintenance
    practices, to assess whether the licensee had appropriately evaluated the notifications
                                            -16-


Based upon a review of the events leading up to the reactor scram, the team determined the licensee failed to properly preplan and perform maintenance on the B RPS MG set after the failure that occurred on December 6, 2014. Further discussion involving the licensee's failure to adequately troubleshoot, identify, and correct degraded components on the B RPS MG set, prior to returning it to service, is included in Section 2.7.a. of this report.
    for relevance to the facility and incorporated applicable lessons learned into station
    programs and procedures.
  b. Findings and Observations
    Other than the URI described in Section 2.5, of this report, no additional findings or
    observations were identified.
2.7  Specific findings identified during this inspection.
  a. Failure to Establish Adequate Procedures to Perform Maintenance on Equipment that
    can Affect Safety-Related Equipment
    Introduction. The team reviewed a Green, self-revealing, non-cited violation of Technical
    Specification 5.4.1 for the licensees failure to establish adequate procedures to properly
    preplan and perform maintenance that affected the performance of the B RPS MG set.
    Specifically, due to inadequate procedures for troubleshooting on the B RPS MG set, the
    licensee failed to identify a degraded capacitor that caused the B RPS MG set output
    breaker to trip, which resulted in a reactor scram.
    Description. On December 6, 2014, during normal plant operations, RPS bus B
    unexpectedly lost power because of a B RPS MG set failure, which resulted in a
    Division 2 half scram and a containment isolation signal. The RPS system is designed
    to cause rapid insertion of control rods (scram) to shut down the reactor when specific
    variables exceed predetermined limits. The RPS power system, of which the B RPS MG
    set is a component, is designed to provide power to the logic system that is part of the
    reactor protection system.
    The licensees troubleshooting teams identified both the super spike suppressor card
    and the field flash card as the possible causes of the B RPS MG set failure. The
    licensee replaced the super spike suppressor card. While inspecting the field flash card,
    a strand of wire from one of the attached leads was found nearly touching a trace on the
    circuit board. A continuity test was performed while the field flash card was being
    tapped and no ground was observed. A ground was observed when forcibly pushing
    down on the wire. The licensee believed that the wire strand most likely caused the
    B RPS MG set trip. The licensee removed the wire strand and re-installed the field flash
    card without any further troubleshooting. Operations personnel returned the B RPS MG
    set to service on December 16, 2014.
    On December 25, 2014, while operating at 85 percent power, a reactor scram occurred
    due to a Division 2 RPS trip concurrent with a Division 1 RPS half-scram signal that was
    present at the time. The Division 1 half-scram signal was received on December 23,
    2014, because of a turbine control valve fast closure signal. Troubleshooting for the
    cause of the Division 1 half-scram was ongoing when the Division 2 RPS trip occurred.
    This resulted in a full RPS actuation and an automatic reactor scram. Electrical
    protection assembly breakers 3B/3D and the B RPS MG set output breaker were found
    tripped, similar to the conditions noted following the loss of the B RPS MG set on
    December 6, 2014. The subsequent failure modes analysis and troubleshooting teams
                                              -17-


Additionally, the team reviewed the procedures that operations personnel used to respond to the reactor scram and determined the licensee failed to provide adequate procedures to respond to a post-trip transient. Further discussion on the procedure prescribing activities affecting quality not being appropriate for the circumstances is included in Section 2.7.b. of this report. 2.2 Charter Items 3 and 8:  Review the licensee's root cause analysis and corrective actions from the current and previous scrams with complications.
identified the probable cause of the failure of the B RPS MG set output breaker was an
intermittent failure of the field flash card. A more detailed inspection of the field flash
card revealed that a 10 microfarad capacitor had been subjected to minor heating over a
long period of time. As a result, the degraded component contributed to a reactor
scram. The capacitor on the field flash card in the Division 2 RPS MG set was replaced.
Analysis. Failure to establish and implement procedures to perform maintenance to
correct adverse conditions on B RPS MG set equipment that can affect the performance
of the safety-related reactor protection system was a performance deficiency. This
performance deficiency is more than minor, and therefore a finding, because it is
associated with the procedure quality attribute of the Initiating Events Cornerstone and
adversely affected the cornerstone objective to limit the likelihood of events that upset
plant stability and challenge critical safety functions during shutdown as well as power
operations.
The team performed an initial screening of the finding in accordance with Inspection
Manual Chapter (IMC) 0609, Appendix A, The Significance Determination
Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 1,
Initiating Event Screening Questions, this finding is determined to have very low safety
significance because the transient initiator did not contribute to both the likelihood of a
reactor trip and the likelihood that mitigation equipment or functions would not have been
available. This finding has an evaluation cross-cutting aspect within the problem
identification and resolution area because the licensee failed to thoroughly evaluate the
failure of the B RPS MG set to ensure that the resolution addressed the cause
commensurate with its safety significance. Specifically, the licensee failed to thoroughly
evaluate the condition of the field flash card to ensure that the cause of the trip had been
correctly identified and corrected prior to returning the B MG set to service [P.2].
Enforcement. Technical Specification 5.4.1.a states, in part, that written procedures
shall be established, implemented, and maintained covering the applicable procedures
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
Regulatory Guide 1.33, Appendix A, Section 9.a., states, in part, that, maintenance that
can affect the performance of safety-related equipment should be properly preplanned
and performed in accordance with written procedures, documented instructions, or
drawings appropriate to the circumstances. Contrary to the above, on December 6,
2014, the licensee failed to establish adequate procedures to properly preplan and
perform maintenance on the B RPS MG set that ultimately affected the performance of
safety-related B RPS equipment. Specifically, due to inadequate procedures for
troubleshooting on the B RPS MG set, the licensee failed to identify a degraded
capacitor on the B RPS MG set that caused its output breaker to trip, prior to returning it
to service. On December 25, 2014, this degraded capacitor caused the B RPS MG set
breaker to trip causing a loss of power to the B RPS bus which resulted in a reactor
scram. The licensee entered this issue into their corrective action program as Condition
Report CR-RBS-2014-06605 and replaced the degraded field flash card capacitor.
Because this finding is determined to be of very low safety significance and has been
entered into the licensees corrective action program this violation is being treated as a
non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:
                                          -18-


====a. Inspection Scope====
  NCV 05000458/2015009-02, Failure to Establish Adequate Procedures to Perform
At the time of the inspection, the root cause report for the December 25, 2014, scram had not been completed. To ensure the licensee was conducting the cause evaluation at a level of detail commensurate with the significance of the problem, the team reviewed corrective action procedures, met with members of the root cause team, and reviewed prior related corrective actions.
  Maintenance on Equipment that can Affect Safety-Related Equipment.
b. Failure to Provide Adequate Procedures for Post-Scram Recovery
  Introduction. The team reviewed a Green, self-revealing, non-cited violation of Technical
  Specification 5.4.1.a for the licensees failure to establish, implement and maintain a
  procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
  Specifically, Procedure OSP-0053, Emergency and Transient Response Support
  Procedure, Revision 22, inappropriately directed operations personnel to establish
  feedwater flow to the reactor pressure vessel using the SFRV as part of the post-scram
  actions. The SFRV operator characteristics are non-linear and not designed to operate
  in the dynamic conditions immediately following a reactor scram from power.
  Description. On November 18, 2013, the licensee modified Procedure OSP-0053,
  Attachment 16, due to excessive leakage across the main FRVs and verified the
  adequacy of the change using the simulator. The licensee did not realize that the
  simulator incorrectly modeled the operating characteristics of the SFRV.
  On December 25, 2014, following a reactor scram, operations personnel attempted to
  implement Procedure OSP-0053, Attachment 16, Post Scram Feedwater/Condensate
  Manipulations Below 5% Reactor Power. When the SFRV did not begin to open as
  RPV level approached the level setpoint, operations personnel thought the SFRV had
  failed in automatic and placed the valve controller in manual. Unknown to operations
  personnel, the manual control of the valve was inoperable due to a faulty card. Unable
  to control the SFRV, operations personnel then began placing one of the main FRVs
  back in service. The isolation valves for the FRV are motor-operated and take
  approximately 90 seconds to reposition. Because of the delay in restoring feedwater to
  the RPV, a second Level 3 (low) water level reactor scram signal occurred.
  The NRC team determined that plant data indicated the SFRV does not open on a
  slowly decreasing RPV water level until the controller signal reaches approximately
  12.5 percent error or about 3 inches below the RPV water level setpoint on the
  controller. The SFRV in the simulator opens as soon as the controller open signal is
  greater than 0.0 percent error. When the licensee became aware of the SFRV design
  operating parameters, they determined that the SFRV was not designed to respond to
  the dynamic conditions that exist during post-scram recovery, and revised
  Procedure OSP-0053, Attachment 16, to continue using the main FRVs during
  post-scram recovery actions.
  Analysis. The licensees failure to provide adequate guidance in Procedure OSP-0053
  for post-scram recovery actions was a performance deficiency. This performance
  deficiency is more than minor, and therefore a finding, because it is associated with the
  procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected
  the cornerstone objective to ensure the availability, reliability, and capability of systems
  that respond to initiating events to prevent undesirable consequences. Specifically, the
  procedural guidance that directed operations personnel to establish feedwater flow to
                                            -19-


The procedures reviewed by the team included quality related Procedure EN-LI-118, "Cause Evaluation Process," Revision 21, and quality related Procedure EN-LI-102, "Corrective Action Program," Revision 24. The licensee's approach for the December 25, 2014, scram causal evaluation was to use several detailed evaluations as input to the overall root cause. Specifically, the licensee performed an apparent cause evaluation, under Condition Report CR-RBS-2014-06696, to understand the failure of Division 2 RPS equipment. The licensee performed an apparent cause evaluation under Condition Report CR-RBS-2014-06602, to review the conditions that resulted in the additional reactor water Level 3 (low) trip, after the initial scram. The licensee also performed an apparent cause evaluation, under Condition Report CR-RBS-2014-06581, to review the turbine control valve fast closure circuit failure that resulted in the Division 1 half-scram signal. All of these evaluations were reviewed under the parent root cause Condition Report CR-RBS-2014-06605.
the RPV using the SFRV as part of the post-scram actions adversely affected the
 
capability of the feedwater systems that respond to prevent undesirable consequences.
The licensee used multiple methods in their causal evaluations that included: event and causal factor charting, barrier analysis, and organizational and programmatic failure mode trees. The licensee's charter for the root cause evaluation required several periodic meetings with the members of the different causal analysis teams. It also required a pre-corrective action review board update and review, a formal corrective action review board approval, and an external challenge review of the approved root cause report.
The system capability was adversely affected since the valve operator characteristics
 
are non-linear and not designed to operate in the dynamic conditions immediately
The NRC team also reviewed corrective actions to address complications encountered during previous reactor scrams. Specifically, the following NRC inspection reports were reviewed and the related licensee corrective actions were assessed:    05000458/2002002, Integrated Inspection Report, July 24, 2002, ML022050206 05000458/2006013, Special Inspection Team Report, March 1, 2007, ML070640396  05000458/2012009, Augmented Inspection Team Report, August 7, 2012, ML12221A233  05000458/2012012, Supplemental Inspection Report, December 28, 2012, ML12363A170
following a reactor scram from high power levels.
 
The team performed an initial screening of the finding in accordance with IMC 0609,
====b. Findings and Observations====
Appendix A, The Significance Determination Process (SDP) for Findings At-Power.
The NRC team found the licensee's root cause team members had met the organizational diversity and experience requirements of their procedures. The team reviewed the qualifications of the members of the root cause team and determined they were within the correct periodicity.
Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the
 
finding was of very low safety significance (Green) because it: (1) was not a deficiency
At the time of the inspection, there were 4 root cause and 10 apparent cause evaluations in progress. The team determined the root cause analyses were conducted at a level of detail commensurate with the significance of the problems. In reviewing corrective actions for prior scrams, the team noted that there have been five unplanned reactor scrams in the past five years, including the December 25, 2014, event. Of those five scrams, two involved Level 8 (high) reactor water level signal trips of all running feedwater pumps. Based upon a review of prior scrams and associated corrective actions, the team determined that the licensee does not have an appropriately low threshold for recognizing Level 8 (high) reactor water level signal trips as an adverse condition, and entering that adverse condition into their corrective action program. Otherwise, the team determined that the licensee's corrective actions to address complications, encountered during previous reactor scrams, were adequate. Further discussion involving the licensee's failure to identify Level 8 (high) reactor water level signal trips as adverse conditions is included in Section 2.7.c of this report. 2.3 Charter Item 4:  Determine the cause of the unexpected Level 8 (high) water level trip signal.
affecting the design or qualification of a mitigating structure, system, or component, and
 
did not result in a loss of operability or functionality; (2) did not represent a loss of
====a. Inspection Scope====
system and/or function; (3) did not represent an actual loss of function of at least a single
To determine the cause of the unexpected Level 8 (high) reactor water level trip on December 25, 2014, the NRC team reviewed control room logs and graphs of key reactor parameters to assess the plant's response to transient conditions. This information was then compared to the actions taken by operations personnel in the control room per abnormal and emergency operating procedure requirements.
train for longer than its technical specification allowed outage time, or two separate
 
safety systems out-of-service for longer than their technical specification allowed outage
Section 5.1 of Procedure AOP-0001, "Reactor Scram," Revision 30, required operations personnel to verify that the feedwater system was operating to restore reactor water level. This was accomplished using an attachment of Procedure OSP-0053, "Emergency and Transient Response Support Procedure," Revision 22. Specifically, Attachment 16, "Post Scram Feedwater/Condensate Manipulations Below 5% Reactor Power," required transferring reactor water level control to the startup feedwater system after reactor water level had been stabilized in the prescribed band. Only four minutes elapsed from the time of the scram until the time the Level 8 (high) reactor water level isolation signal was reached. Consequently, operations personnel did not have sufficient time to gain control and stabilize reactor vessel level in the required band. To gain an understanding of issues affecting systems at the time of the scram, the NRC team met with system engineers for the feedwater system, feedwater level control system, and remotely operated valves. Discussions with engineering included system health reports, open corrective actions from condition reports, licensee event reports, design data for systems, startup testing and exceptions, post-trip reactor water level setpoint setdown parameters, open engineering change packages, and requirements for engineering to analyze post-transient plant data.
time; and (4) did not represent an actual loss of function of one or more non-technical
 
specification trains of equipment designated as high safety-significant in accordance with
====b. Findings and Observations====
the licensees maintenance rule program.
Operations personnel responded to the events in accordance with procedure requirements. The NRC did not identify any performance deficiencies related to immediate or supplemental actions taken by control room staff during the transient.
This finding has an evaluation cross-cutting aspect within the problem identification and
 
resolution area because the licensee failed to thoroughly evaluate this issue to ensure
However, operations personnel stated that the plant did not respond in a manner consistent with their simulator training. Based on review of operations personnel response to the event and the training received from the simulator, the NRC team determined that the licensee did not maintain the simulator in a condition that accurately represented actual plant response. On April 10, 2015, the licensee provided a white paper with additional information related to the modeling of the plant-referenced simulator. Further discussion involving the licensee's failure to maintain the simulator is included in Section 2.7.d of this report. The NRC team determined that the plant did not respond per the design as described in the final safety analysis report. Specifically, the feedwater level control system and feedwater systems were designed to automatically control reactor water level in the programmed band post-scram. During the December 25, 2014 scram, reactor water level quickly (within 4 minutes) rose to a Level 8 (high) trip. By design, reactor water level should rapidly lower after the initial level transient from core void collapse, rise as feedwater compensates for the level change, and then return to the programed setpoint. A Level 8 (high) trip should not occur. The team determined that significant leakage past the feedwater isolation valves caused the rapid rise in reactor water level. Operations personnel were unable to compensate for the rapid change in reactor vessel level. The licensee initially discovered the adverse condition during startup testing in 1986, and allowed the condition to degrade without effective corrective actions.
that the resolution addressed the cause commensurate with its safety significance.
 
Specifically, the licensee failed to properly evaluate the design characteristics of the
The team noted that significant post-trip or post-transient plant performance data was available to system engineers, but review of this data was not prioritized by the licensee. The review of plant transient data was primarily driven by the licensee's root cause team charter or by self-assigned good engineering practices. At the time of this inspection, the licensee had not quantified the amount of leakage past the FRVs, although the scram and subsequent startup had occurred one month earlier. The NRC team observed that there was a potential to miss important trends in plant performance without a more timely review. 2.4 Charter Item 5:  Review the effectiveness of licensee actions to address known equipment degradations that could complicate post-scram response by operations personnel.
SFRV operator before implementing procedural guidance for post-scram recovery
 
actions [P.2].
====a. Inspection Scope====
Enforcement. Technical Specification 5.4.1.a states, in part, that written procedures
The NRC team reviewed licensee procedures for classifying and addressing plant conditions that may challenge operations personnel while performing required actions per procedures during normal and off-normal conditions. The team reviewed the licensee's current list of operator workarounds and operator burdens. Specifically, the team was looking for any known equipment issues that could complicate post-scram response by operations personnel.
shall be established, implemented, and maintained covering the applicable procedures
 
recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.
====b. Findings and Observations====
Regulatory Guide 1.33, Appendix A, Section 6.u., identifies procedures for responding to
The team determined the licensee did not properly classify several deficient plant conditions as operator workarounds in accordance with fleet Procedure EN-OP-117, "Operations Assessment Resources," Revision 8. Further discussion related to the failure to classify plant deficiencies as operator workarounds is included in Section 2.7.e of this report. 2.5 Charter Items 6 and 7:  Review the licensee's maintenance, testing and operating practices for Magne Blast circuit breakers including the causes and corrective actions taken to address the failure of the RFPs to start.
a Reactor Trip as required procedures. Procedure OSP-0053, Attachment 16, Post
 
Scram Feedwater/Condensate Manipulations Below 5% Reactor Power, was a
====a. Inspection Scope====
procedure established by the licensee for responding to a reactor trip. Contrary to the
The team reviewed the final safety analysis report, system description, the current system health report, selected drawings, maintenance and test procedures, and condition reports associated with Magne Blast breakers. The team also performed walkdowns and conducted interviews with system engineering and design engineering personnel to ensure circuit breakers were capable of performing their design basis safety functions. Specifically, the team reviewed:  Vendor and plant single line, schematic, wiring, and layout drawings  Circuit breaker preventive maintenance inspection and testing procedures  Vendor installation and maintenance manuals  Preventive maintenance and surveillance test procedures  Completed surveillance test and preventive maintenance results  Corrective actions and modifications
above, from March 3, 2010, until January 30, 2015, the licensee failed to establish,
 
implement and maintain Procedure OSP-0053, which directs operator actions for a
====b. Findings and Observations====
reactor trip. Specifically, Procedure OSP-0053 inappropriately directed operations
Unresolved Item (URI) - Vendor and Industry Recommended Testing Adequacy on Safety-related and Safety-significant Circuit Breakers
personnel to establish feedwater flow to the reactor pressure vessel using the SFRV as
 
part of the post-scram actions. The SFRV operator characteristics are non-linear and
=====Introduction.=====
not designed to operate in the dynamic conditions immediately following a reactor scram
The team identified an unresolved item related to the licensee's breaker maintenance and troubleshooting programs for safety-related and safety-significant circuit breakers. The charter tasked the team with inspecting the issues associated with Magne Blast breaker problems that occurred during and after the December 25, 2014, scram. The NRC team determined that breaker maintenance and troubleshooting practices extended beyond the Magne Blast breakers. The team identified that there were potential issues with safety-related Master Pact breakers and determined that maintenance procedures used to ensure that 4160 V and 13.8 kV safety-related and safety-significant breakers were being maintained and overhauled in a timely manner may not conform to industry recommended standards.
from high power. Subsequent to the event, the licensee changed the procedure,
 
directing operations personnel to utilize one of the main FRVs until the plant was
=====Description.=====
stabilized. Because this finding is determined to be of very low safety significance and
The team identified that the licensee's maintenance programs for Division I, II, III, and non-safety 4160 V and 13.8 kV breakers installed in the plant may not meet the standards recommended by the vendor, corporate, or Electric Power Research Institute (EPRI) guidelines. The licensee's programs were based on EPRI documents TR-106857-V2 and TR-106857-V3, which were preventive maintenance program bases for low and medium voltage switchgear. However, the licensee appeared to only implement portions of the recommended maintenance program, and were not able to provide the team with engineering analyses or technical bases to justify the changes. The EPRI guidance was developed specifically for Magne Blast breakers based on industry operating experience, NRC Information Notices, and General Electric SILs/SALs. The NRC team was concerned that the licensee may not have performed the entire vendor or EPRI recommended tests, inspections, and refurbishments on the breakers since they were installed. The aggregate impact of missing these preventive maintenance tasks needs to be evaluated to determine if the reliability of the affected breakers has been degraded. Pending further evaluation of the above issue by the licensee and subsequent review by NRC inspectors, this issue will be tracked as URI 05000458/2015009-01, "Vendor and Industry Recommended Testing Adequacy on Safety-related and Safety-significant Circuit Breakers."  2.6 Charter Item 9:  Evaluate pertinent industry operating experience and potential precursors to the event, including the effectiveness of any action taken in response to the operating experience.
has been entered into the licensees corrective action program as Condition
 
Report CR-RBS-2015-00657, this violation is being treated as a non-cited violation
====a. Inspection Scope====
consistent with Section 2.3.2.a of the NRC Enforcement Policy:
The team evaluated the licensee's application of industry operating experience related to this event. The team reviewed applicable operating experience and generic NRC communications with a specific emphasis on Magne Blast breaker maintenance practices, to assess whether the licensee had appropriately evaluated the notifications for relevance to the facility and incorporated applicable lessons learned into station programs and procedures.
NCV 05000458/2015009-03, Failure to Provide Adequate Procedures for Post-scram
 
Recovery.
====b. Findings and Observations====
                                          -20-
Other than the URI described in Section 2.5, of this report, no additional findings or observations were identified. 2.7 Specific findings identified during this inspection. a. Failure to Establish Adequate Procedures to Perform Maintenance on Equipment that can Affect Safety-Related Equipment
 
=====Introduction.=====
The team reviewed a Green, self-revealing, non-cited violation of Technical Specification 5.4.1 for the licensee's failure to establish adequate procedures to properly preplan and perform maintenance that affected the performance of the B RPS MG set. Specifically, due to inadequate procedures for troubleshooting on the B RPS MG set, the licensee failed to identify a degraded capacitor that caused the B RPS MG set output breaker to trip, which resulted in a reactor scram.
 
=====Description.=====
On December 6, 2014, during normal plant operations, RPS bus B unexpectedly lost power because of a B RPS MG set failure, which resulted in a Division 2 half scram and a containment isolation signal. The RPS system is designed to cause rapid insertion of control rods (scram) to shut down the reactor when specific variables exceed predetermined limits. The RPS power system, of which the B RPS MG set is a component, is designed to provide power to the logic system that is part of the reactor protection system. The licensee's troubleshooting teams identified both the super spike suppressor card and the field flash card as the possible causes of the B RPS MG set failure. The licensee replaced the super spike suppressor card. While inspecting the field flash card, a strand of wire from one of the attached leads was found nearly touching a trace on the circuit board. A continuity test was performed while the field flash card was being tapped and no ground was observed. A ground was observed when forcibly pushing down on the wire. The licensee believed that the wire strand most likely caused the B RPS MG set trip. The licensee removed the wire strand and re-installed the field flash card without any further troubleshooting. Operations personnel returned the B RPS MG set to service on December 16, 2014. On December 25, 2014, while operating at 85 percent power, a reactor scram occurred due to a Division 2 RPS trip concurrent with a Division 1 RPS half-scram signal that was present at the time. The Division 1 half-scram signal was received on December 23, 2014, because of a turbine control valve fast closure signal. Troubleshooting for the cause of the Division 1 half-scram was ongoing when the Division 2 RPS trip occurred. This resulted in a full RPS actuation and an automatic reactor scram. Electrical protection assembly breakers 3B/3D and the B RPS MG set output breaker were found tripped, similar to the conditions noted following the loss of the B RPS MG set on December 6, 2014. The subsequent failure modes analysis and troubleshooting teams identified the probable cause of the failure of the B RPS MG set output breaker was an intermittent failure of the field flash card. A more detailed inspection of the field flash card revealed that a 10 microfarad capacitor had been subjected to minor heating over a long period of time. As a result, the degraded component contributed to a reactor scram. The capacitor on the field flash card in the Division 2 RPS MG set was replaced.
 
=====Analysis.=====
Failure to establish and implement procedures to perform maintenance to correct adverse conditions on B RPS MG set equipment that can affect the performance of the safety-related reactor protection system was a performance deficiency. This performance deficiency is more than minor, and therefore a finding, because it is associated with the procedure quality attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The team performed an initial screening of the finding in accordance with Inspection Manual Chapter (IMC) 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power."  Using IMC 0609, Appendix A, Exhibit 1, "Initiating Event Screening Questions," this finding is determined to have very low safety significance because the transient initiator did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not have been available. This finding has an evaluation cross-cutting aspect within the problem identification and resolution area because the licensee failed to thoroughly evaluate the failure of the B RPS MG set to ensure that the resolution addressed the cause commensurate with its safety significance. Specifically, the licensee failed to thoroughly evaluate the condition of the field flash card to ensure that the cause of the trip had been correctly identified and corrected prior to returning the B MG set to service [P.2]. 
 
=====Enforcement.=====
Technical Specification 5.4.1.a states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Appendix A, Section 9.a., states, in part, that, "maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances."  Contrary to the above, on December 6, 2014, the licensee failed to establish adequate procedures to properly preplan and perform maintenance on the B RPS MG set that ultimately affected the performance of safety-related B RPS equipment. Specifically, due to inadequate procedures for troubleshooting on the B RPS MG set, the licensee failed to identify a degraded capacitor on the B RPS MG set that caused its output breaker to trip, prior to returning it to service. On December 25, 2014, this degraded capacitor caused the B RPS MG set breaker to trip causing a loss of power to the B RPS bus which resulted in a reactor scram. The licensee entered this issue into their corrective action program as Condition Report CR-RBS-2014-06605 and replaced the degraded field flash card capacitor. Because this finding is determined to be of very low safety significance and has been entered into the licensee's corrective action program this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:
NCV 05000458/2015009-02, "Failure to Establish Adequate Procedures to Perform Maintenance on Equipment that can Affect Safety-Related Equipment."  b. Failure to Provide Adequate Procedures for Post-Scram Recovery
 
=====Introduction.=====
The team reviewed a Green, self-revealing, non-cited violation of Technical Specification 5.4.1.a for the licensee's failure to establish, implement and maintain a procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Specifically, Procedure OSP-0053, "Emergency and Transient Response Support Procedure," Revision 22, inappropriately directed operations personnel to establish feedwater flow to the reactor pressure vessel using the SFRV as part of the post-scram actions. The SFRV operator characteristics are non-linear and not designed to operate in the dynamic conditions immediately following a reactor scram from power.
 
=====Description.=====
On November 18, 2013, the licensee modified Procedure OSP-0053, Attachment 16, due to excessive leakage across the main FRVs and verified the adequacy of the change using the simulator. The licensee did not realize that the simulator incorrectly modeled the operating characteristics of the SFRV.
 
On December 25, 2014, following a reactor scram, operations personnel attempted to implement Procedure OSP-0053, Attachment 16, "Post Scram Feedwater/Condensate Manipulations Below 5% Reactor Power."  When the SFRV did not begin to open as RPV level approached the level setpoint, operations personnel thought the SFRV had failed in automatic and placed the valve controller in manual. Unknown to operations personnel, the manual control of the valve was inoperable due to a faulty card. Unable to control the SFRV, operations personnel then began placing one of the main FRVs back in service. The isolation valves for the FRV are motor-operated and take approximately 90 seconds to reposition. Because of the delay in restoring feedwater to the RPV, a second Level 3 (low) water level reactor scram signal occurred.
 
The NRC team determined that plant data indicated the SFRV does not open on a slowly decreasing RPV water level until the controller signal reaches approximately 12.5 percent error or about 3 inches below the RPV water level setpoint on the controller. The SFRV in the simulator opens as soon as the controller open signal is greater than 0.0 percent error. When the licensee became aware of the SFRV design operating parameters, they determined that the SFRV was not designed to respond to the dynamic conditions that exist during post-scram recovery, and revised Procedure OSP-0053, Attachment 16, to continue using the main FRVs during post-scram recovery actions.
 
=====Analysis.=====
The licensee's failure to provide adequate guidance in Procedure OSP-0053 for post-scram recovery actions was a performance deficiency. This performance deficiency is more than minor, and therefore a finding, because it is associated with the procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the procedural guidance that directed operations personnel to establish feedwater flow to the RPV using the SFRV as part of the post-scram actions adversely affected the capability of the feedwater systems that respond to prevent undesirable consequences. The system capability was adversely affected since the valve operator characteristics are non-linear and not designed to operate in the dynamic conditions immediately following a reactor scram from high power levels. The team performed an initial screening of the finding in accordance with IMC 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power."  Using IMC 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," the finding was of very low safety significance (Green) because it:  (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensee's maintenance rule program. This finding has an evaluation cross-cutting aspect within the problem identification and resolution area because the licensee failed to thoroughly evaluate this issue to ensure that the resolution addressed the cause commensurate with its safety significance. Specifically, the licensee failed to properly evaluate the design characteristics of the SFRV operator before implementing procedural guidance for post-scram recovery actions [P.2].
 
=====Enforcement.=====
Technical Specification 5.4.1.a states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Regulatory Guide 1.33, Appendix A, Section 6.u., identifies procedures for responding to a Reactor Trip as required procedures. Procedure OSP-0053, Attachment 16, "Post Scram Feedwater/Condensate Manipulations Below 5% Reactor Power," was a procedure established by the licensee for responding to a reactor trip. Contrary to the above, from March 3, 2010, until January 30, 2015, the licensee failed to establish, implement and maintain Procedure OSP-0053, which directs operator actions for a reactor trip. Specifically, Procedure OSP-0053 inappropriately directed operations personnel to establish feedwater flow to the reactor pressure vessel using the SFRV as part of the post-scram actions. The SFRV operator characteristics are non-linear and not designed to operate in the dynamic conditions immediately following a reactor scram from high power. Subsequent to the event, the licensee changed the procedure, directing operations personnel to utilize one of the main FRVs until the plant was stabilized. Because this finding is determined to be of very low safety significance and has been entered into the licensee's corrective action program as Condition Report CR-RBS-2015-00657, this violation is being treated as a non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:  NCV 05000458/2015009-03, "Failure to Provide Adequate Procedures for Post-scram Recovery."


c. Failure to Identify High Reactor Water Level as a Condition Adverse to Quality
c. Failure to Identify High Reactor Water Level as a Condition Adverse to Quality
  Introduction. The team identified a Green, non-cited violation of 10 CFR Part 50,
  Appendix B, Criterion XVI, Corrective Action, for the licensees failure to assure a
  condition adverse to quality was promptly identified. Specifically, the licensee failed to
  identify that reaching the reactor pressure vessel water Level 8 (high) setpoint, on
  December 25, 2014, was an adverse condition and enter it into the corrective action
  program.
  Description. On December 25, 2014, the licensee experienced a scram with
  complications. The team reviewed the post-scram report as documented in
  Procedure GOP-0003, Scram Recovery, Revision 24. During the scram, the licensee
  experienced a Level 8 (high) reactor water condition approximately four minutes after the
  scram. This high water level condition should not occur for a scram when main steam
  isolation valves remain open and safety relief valves do not actuate.
  The team noted that operations personnel followed their training and performed the
  required post-scram actions. Those actions did not prevent the overfeeding of the
  reactor vessel (which reached the Level 8 (high) setpoint), causing the RFPs to trip off
  and would have caused isolation of other emergency core cooling systems, if actuated,
  such as high pressure core spray and reactor core isolation cooling. The loss of all
  feedwater contributed to the RPV water level lowering to a Level 3 (low) condition that
  actuated a second reactor scram signal.
  The team interviewed control room operations personnel, system engineers, and
  corrective action staff regarding the plants response to the scram. Further, the team
  reviewed plant parameter graphs, control room logs, alarm logs, design history, and
  licensing basis documents, and determined that excessive leakage past the FRVs
  caused the Level 8 (high) trip of all RFPs.
  In reviewing the feedwater system data from the December 24, 2014, scram, the
  licensee estimated 500,000 lbm/hr leaked past the closed FRVs. This represents
  approximately 3 percent of the full-power feedwater flow and significantly exceeds the
  design specification for leakage of 135,000-150,000 lbm/hr.
  The licensee identified excessive leakage past the FRVs during testing in 1986. At the
  time of inspection, the licensee could not produce any corrective actions taken to identify
  or correct leakage past the FRVs. Further, the licensee had not quantified the amount of
  leakage past the FRVs prior to the December 24, 2014, event and NRC Special
  Inspection.
  Procedure GOP-0003 provided a post-scram checklist to operations personnel to help
  identify equipment and procedure problems that should be corrected prior to the reactor
  startup. This document was then reviewed by the Offsite Safety Review Committee in
  order to understand and confirm that the plant was safe to restart. Step 1.1 stated the
  following:
                                            -21-


=====Introduction.=====
        Following a reactor scram from high power levels, there is an initial RPV level
The team identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," for the licensee's failure to assure a condition adverse to quality was promptly identified. Specifically, the licensee failed to identify that reaching the reactor pressure vessel water Level 8 (high) setpoint, on December 25, 2014, was an adverse condition and enter it into the corrective action program.
        Shrink of 20 to 40 inches followed by a Swell of approximately 10 to 20 inches.
 
        The Feedwater Level Control System is programmed to ride out this shrink and
=====Description.=====
        swell without overfilling the RPV.
On December 25, 2014, the licensee experienced a scram with complications. The team reviewed the post-scram report as documented in Procedure GOP-0003, "Scram Recovery," Revision 24. During the scram, the licensee experienced a Level 8 (high) reactor water condition approximately four minutes after the scram. This high water level condition should not occur for a scram when main steam isolation valves remain open and safety relief valves do not actuate.
In section 6.7 of Procedure GOP-003, the licensee documented that there was a control
 
system trip of RFPs due to reaching Level 8 (high). In section 6.12, however, the
The team noted that operations personnel followed their training and performed the required post-scram actions. Those actions did not prevent the overfeeding of the reactor vessel (which reached the Level 8 (high) setpoint), causing the RFPs to trip off and would have caused isolation of other emergency core cooling systems, if actuated, such as high pressure core spray and reactor core isolation cooling. The loss of all feedwater contributed to the RPV water level lowering to a Level 3 (low) condition that actuated a second reactor scram signal.
licensee failed to document any off-normal trips (Level 8 (high) feed pump trips). In
 
Attachment 3 of GOP-003 Procedure, Analysis and Evaluations, Level 8 (high) was
The team interviewed control room operations personnel, system engineers, and corrective action staff regarding the plant's response to the scram. Further, the team reviewed plant parameter graphs, control room logs, alarm logs, design history, and licensing basis documents, and determined that excessive leakage past the FRVs caused the Level 8 (high) trip of all RFPs.
mentioned as part of a timeline discussion but was not listed in the final section labeled
 
Corrective Actions Required Prior to Returning Unit to Service. This final section was
In reviewing the feedwater system data from the December 24, 2014, scram, the licensee estimated 500,000 lbm/hr leaked past the closed FRVs. This represents approximately 3 percent of the full-power feedwater flow and significantly exceeds the design specification for leakage of 135,000-150,000 lbm/hr.
where condition reports were required for all items listed. By omitting Level 8 (high) from
 
the discussion, no corrective action document was generated for that condition.
The licensee identified excessive leakage past the FRVs during testing in 1986. At the time of inspection, the licensee could not produce any corrective actions taken to identify or correct leakage past the FRVs. Further, the licensee had not quantified the amount of leakage past the FRVs prior to the December 24, 2014, event and NRC Special Inspection.
The licensee did not identify that reaching reactor water Level 8 (high) was an adverse
 
condition. Therefore, the unexpected Level 8 (high) trip was not addressed prior to
Procedure GOP-0003 provided a post-scram checklist to operations personnel to help identify equipment and procedure problems that should be corrected prior to the reactor startup. This document was then reviewed by the Offsite Safety Review Committee in order to understand and confirm that the plant was safe to restart. Step 1.1 stated the following:
startup on December 28, 2014.
Following a reactor scram from high power levels, there is an initial RPV level "Shrink" of 20 to 40 inches followed by a "Swell" of approximately 10 to 20 inches. The Feedwater Level Control System is programmed to "ride out" this shrink and swell without overfilling the RPV. In section 6.7 of Procedure GOP-003, the licensee documented that there was a control system trip of RFPs due to reaching Level 8 (high). In section 6.12, however, the licensee failed to document any off-normal trips (Level 8 (high) feed pump trips). In Attachment 3 of GOP-003 Procedure, "Analysis and Evaluations," Level 8 (high) was mentioned as part of a timeline discussion but was not listed in the final section labeled "Corrective Actions Required Prior to Returning Unit to Service.This final section was where condition reports were required for all items listed. By omitting Level 8 (high) from the discussion, no corrective action document was generated for that condition. The licensee did not identify that reaching reactor water Level 8 (high) was an adverse condition. Therefore, the unexpected Level 8 (high) trip was not addressed prior to startup on December 28, 2014. The team reviewed the history of Level 8 (high) RFP trips and noted that similar issues of concern were raised by the NRC in 2012. Specifically, a Supplemental Inspection, performed in 2012, for a White performance indicator associated with reactor scrams with complications documented the failure to recognize a Level 8 (high) trip as an adverse condition and enter it into the corrective action program. This non-cited violation was documented in NRC Inspection Report 05000458/2012012.
The team reviewed the history of Level 8 (high) RFP trips and noted that similar issues
 
of concern were raised by the NRC in 2012. Specifically, a Supplemental Inspection,
The team determined that the licensee did not have a sufficiently low threshold for entering issues into their corrective action program for reactor water level transients.
performed in 2012, for a White performance indicator associated with reactor scrams
 
with complications documented the failure to recognize a Level 8 (high) trip as an
Specifically, long-standing equipment issues associated with FRV leakage has led to the licensee reaching reactor water Level 8 (high) during two reactor scrams in a three-year period.
adverse condition and enter it into the corrective action program. This non-cited
 
violation was documented in NRC Inspection Report 05000458/2012012.
=====Analysis.=====
The team determined that the licensee did not have a sufficiently low threshold for
The failure to identify Level 8 (high) reactor water level trips as adverse conditions was a performance deficiency. This performance deficiency is more than minor, and therefore a finding, because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, failure to identify Level 8 (high) conditions and resulting actuations as conditions adverse to quality, would continue to result in the undesired isolation of mitigating equipment including RFPs, the high pressure core spray pump, and the reactor core isolation cooling pump.
entering issues into their corrective action program for reactor water level transients.
 
Specifically, long-standing equipment issues associated with FRV leakage has led to the
The team performed an initial screening of the finding in accordance with IMC 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power.Using IMC 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," the finding was of very low safety significance (Green) because it: (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensee's maintenance rule program.
licensee reaching reactor water Level 8 (high) during two reactor scrams in a three-year
 
period.
This finding has an avoid complacency cross-cutting aspect within the human performance area because the licensee failed to recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Specifically, the licensee tolerated excessive leakage past the FRVs, did not plan for further degradation, and the condition ultimately resulted in the Level 8 (high) trip of the running RFP on December 25, 2014 [H.12].
Analysis. The failure to identify Level 8 (high) reactor water level trips as adverse
 
conditions was a performance deficiency. This performance deficiency is more than
=====Enforcement.=====
minor, and therefore a finding, because it is associated with the equipment performance
Title 10 of the Code of Federal Regulations, Part 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and non-conformances are promptly identified and corrected. Contrary to the above, from December 25, 2014, to January 29, 2015, the licensee failed to assure that a condition adverse to quality was promptly identified. Specifically, the licensee failed to identify that reaching the reactor pressure vessel water Level 8 (high) setpoint, on December 25, 2014, was an adverse condition and enter it into the corrective action program. To restore compliance, the licensee entered this issue into their corrective action program as Condition Report CR-RBS-2015-00620 to perform a causal analysis for Level 8 (high) trips. Since the violation was of very low safety significance (Green), this violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy:  NCV 05000458/2015009-04, "Failure to Identify High Reactor Water Level as a Condition Adverse to Quality."  d. Failure of the Plant-Referenced Simulator to Demonstrate Expected Plant Response
attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone
 
objective to ensure the availability, reliability, and capability of systems that respond to
=====Introduction.=====
initiating events to prevent undesirable consequences. Specifically, failure to identify
The team identified an apparent violation of 10 CFR 55.46(c)(1), "Plant-Referenced Simulators," for the licensee's failure to maintain the simulator so it would demonstrate expected plant response to operator input and to normal, transient, and accident conditions to which the simulator has been designed to respond. As of January 30, 2015, the licensee failed to maintain the simulator consistent with actual plant response for normal and transient conditions related to feedwater flows, alarm response, and behavior of the SFRV controller. As a result, operations personnel were challenged in their control of the plant during a reactor scram that occurred on December 25, 2014.
Level 8 (high) conditions and resulting actuations as conditions adverse to quality, would
 
continue to result in the undesired isolation of mitigating equipment including RFPs, the
=====Description.=====
high pressure core spray pump, and the reactor core isolation cooling pump.
On December 25, 2014, River Bend Station was operating at 85 percent power when a reactor scram occurred. On January 26, 2015, a Special Inspection was initiated in response to this event. The Special Inspection team reviewed the event and identified several simulator fidelity issues. Licensee Procedure EN-TQ-202, "Simulator Configuration Control," Revision 9, provided the process requirements necessary to satisfy the guidelines for simulator testing, performance, and configuration control specified by ANSI/ANS-3.5-2009. Standard ANSI/ANS-3.5-2009, "Nuclear Power Plant Simulators for Use in Operator Training and Examination," provides the simulator testing requirements, as well as simulator configuration management to ensure simulator fidelity. Specifically, as of January 30, 2015, the River Bend Station simulator failed to model feedwater accurately and failed to model resulting reactor vessel level response following a scram, failed to provide the correct alarm response for a loss of a RPS MG set, and failed to correctly model the behavior of the SFRV controller. The simulator modeling discrepancies and how these discrepancies affected plant response during the plant trip are discussed below:  The licensee stated their simulator modeled zero leakage across the FRV rather than the actual leakage in the plant. General Electric record 0247.230-000-016, "Feedwater Control Valve Assembly - Purchase Specification," described the total design leakage across all the FRVs was approximately 135,000 lbm/hr. This is equal to approximately 1.1 percent full feedwater flow. The flow rate across the FRVs measured in the plant on December 25, 2014, was approximately 500,000 lbm/hr, which is approximately 3 percent full feedwater flow. The rate of level change of the reactor vessel in the plant was larger than operations personnel anticipated based on training received in the simulator. ANSI/ANS-3.5-2009, Section 4.1.4(3), states, "The simulator shall not fail to cause an alarm or automatic action if the reference unit would have caused an alarm or automatic action under identical circumstances."  In this case, the simulator under similar conditions did not reach the RPV water Level 8 (high) condition and trip the RFPs, when the actual plant did.
The team performed an initial screening of the finding in accordance with IMC 0609,
 
Appendix A, The Significance Determination Process (SDP) for Findings At-Power.
The licensee's simulator did not correctly model all alarms that would be received on a loss of power to the RPS. ANSI/ANS-3.5-2009, Section 4.1.4(3), states, "The simulator shall not fail to cause an alarm or automatic action if the reference unit would have caused an alarm or automatic action under identical circumstances."  Although the licensee had identified this discrepancy on December 11, 2014, and implemented a correction in the simulator model, operations personnel had not received training nor were they notified of the discrepancy. As a result, during the plant scram on December 25, 2014, the alarms for drywell high pressure and RPV high pressure annunciated per the facility design, operations personnel were not expecting the alarms because they did not alarm in the simulator during training.
Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the
 
finding was of very low safety significance (Green) because it: (1) was not a deficiency
The simulator SFRV responded differently than the actual SFRV in the reference plant. ANSI/ANS-3.5-2009, Section 4.1.4(2) [for malfunctions], stated, "Any observable change in simulated parameters corresponds in direction to the change expected from actual or best estimate response of the reference unit to the malfunction."  Plant data indicated the SFRV does not open on a slowly decreasing RPV water level until the controller signal reaches approximately 12.5 percent or about 3 inches below the RPV water level setpoint of the controller. The SFRV in the simulator opens as soon as the controller open signal is greater than 0.0. Because the SFRV did not respond as expected, operations personnel incorrectly believed the SFRV had failed in automatic operation and placed the controller in manual. Due to an unrelated issue, the manual function of the SFRV was unavailable. Collectively, these modeling discrepancies negatively impacted licensed operations personnel performance in the actual control room, during the event of December 25, 2014. Specifically, operations personnel were not able to control reactor vessel water level during the reactor scram.
affecting the design or qualification of a mitigating structure, system, or component, and
 
did not result in a loss of operability or functionality; (2) did not represent a loss of
The team noted that the licensee similarly stated in Condition Report CR-RBS-2015-00641 that, "During an investigation into the report at the OSRC (Onsite Safety Review Committee) for the SCRAM on December 25, 2014, that feed regulating valve leakage (FRV) contributed to the Level 8 received reactor vessel, it was determined by analysis that there is sufficient evidence that leakage by the Feedwater Regulating Valves presents a significant challenge to Operations during a scram event."  On April 10, 2015, the licensee provided a white paper with additional information related to the modeling of the plant-referenced simulator. Specifically, it provided the licensee's perspective with regard to the following issues raised by the NRC:  1. Two unexpected alarms on loss of Division II Reactor Protection System Power 2. Main Feedwater Regulating Valve Seat Leakage 3. Start-up Feedwater Regulating Valve Response  The licensee concluded that although they perceived that there were differences between the simulator and the actual plant, they were considered to be minor. For each of the items in question, the paper summarized that operator performance was not impacted by simulator modeling. The team considered the information in the white paper, and disagreed with the licensee's conclusions. Some of the information provided, however, did improve the team's understanding of the modeling deficiencies.
                                          -22-
 
=====Analysis.=====
The failure to maintain the plant-referenced simulator so that it would demonstrate expected plant response to operator input and to normal and transient conditions was a performance deficiency. This performance deficiency is more than minor, and therefore a finding, because it is associated with the human performance attribute of the Mitigating Systems Cornerstone and adversely affected the objective of ensuring availability, reliability, and capability of systems needed to respond to initiating events to prevent undesired consequences. Specifically, the incorrect simulator response adversely affected the operating crew's ability to assess plant conditions and take actions in accordance with approved procedures during the December 25, 2014, scram.
 
The team performed an initial screening of the finding in accordance with IMC 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," Attachment 4, "Initial Characterization of Findings."  Using IMC 0609, Attachment 4, Table 3, "SDP Appendix Router," the team answered 'yes' to the following question:  "Does the finding involve the operator licensing requalification program or simulator fidelity?"  As a result, the team used IMC 0609, Appendix I, "Licensed Operator Requalification Significance Determination Process (SDP)," and preliminarily determined the finding was of low to moderate safety significance (White) because the deficient simulator performance negatively impacted operations personnel performance in the actual plant during a reportable event. This modeling deficiency resulted in actual impact on operations personnel performance during response to a reactor scram that occurred on December 25, 2014.
 
The NRC recently issued a non-cited violation related to simulator fidelity in March 2014 documented in Inspection Report 05000458/2014301. Since the licensee recently verified simulator fidelity, this issue is indicative of current plant performance and has an evaluation cross-cutting aspect within the problem identification and resolution area because the licensee failed to thoroughly evaluate this issue to ensure that the resolution addressed the extent of condition commensurate with its safety significance. Specifically, the licensee's evaluation of the fidelity issue focused on other training areas that used simulation, rather than evaluating the simulator modelling for additional fidelity discrepancies [P.2].
 
=====Enforcement.=====
Title 10 of the Code of Federal Regulations, Part 55.46(c)(1), "Plant-Referenced Simulators," requires in part, that a simulator "must demonstrate expected plant response to operator input and to normal, transient, and accident conditions to which the simulator has been designed to respond."
 
Contrary to the above, as of January 30, 2015, the simulator failed to demonstrate expected plant response to operator input and to normal, transient, and accident conditions to which the simulator has been designed to respond. Specifically, the River Bend Station simulator failed to correctly model leakage flow rates across the FRVs; failed to provide the correct alarm response for a loss of a RPS MG set; and failed to correctly model the behavior of the SFRV controller. These simulator modeling issues led to negative training of operators. This subsequently complicated the operator's response to a reactor scram in the actual plant on December 25, 2014. This issue has been entered into the corrective action program as Condition Report CR-RBS-2015-01261. The licensee's condition report included actions to initiate simulator discrepancy reports, to investigate and resolve the potential fidelity issues, and to provide training to operations personnel on simulator differences. This is a violation of 10 CFR 55.46(c)(1), "Plant-Referenced Simulators":  AV 05000458/2015009-05, "Failure of the Plant-Referenced Simulator to Demonstrate Expected Plant Response."  e. Failure to Identify and Classify Operator Workarounds that Impacted Scram Recovery Actions
 
=====Introduction.=====
The team identified a Green finding for the licensee's failure to follow written procedures for classifying deficient plant conditions as operator workarounds and providing compensatory measures or training in accordance with fleet Procedure EN-OP-117. A misclassification of these conditions resulted in the failure of the operations department to fully assess the impact these conditions had during a plant transient. The failure to identify operator workarounds contributed to complications experienced during reactor scram recovery on December 25, 2014.
 
=====Description.=====
The team reviewed the recovery actions taken by the main control room staff following the reactor scram on December 25, 2014, from 85 percent power. During the review, the team observed the station had zero conditions identified as operator workarounds. The team reviewed fleet Procedure EN-FAP-OP-006, "Operator Aggregate Impact Index Performance Indicator," Revision 2. This procedure defined an operator workaround as:  Any plant condition (equipment or other) that would require compensatory operator actions in the execution of normal operating procedures, abnormal operating procedures, emergency operating procedures, or annunciator response procedures during off-normal conditions. This indicator provided a measure of plant safety. It provided a measure of the likelihood that a plant transient may be complicated by equipment and human performance problems.


During their review, the team identified the following three conditions which met the definition of an operator workaround as described in Procedure EN-FAP-OP-006, and which were in effect prior to the December 25, 2014, event:  Work Order WO-RBS-00404323:  RFP B supply breaker repetitive failures to close potentially reduces the number of feedwater pumps available to operations personnel during a transient following reactor pressure vessel water Level 8 (high). Operations personnel would rack out and then rack the breaker back in until the breaker would function properly. This work order was initiated on February 3, 2015, following discussions with the NRC inspection team.
  system and/or function; (3) did not represent an actual loss of function of at least a single
  train for longer than its technical specification allowed outage time, or two separate
  safety systems out-of-service for longer than their technical specification allowed outage
  time; and (4) did not represent an actual loss of function of one or more non-technical
  specification trains of equipment designated as high safety-significant in accordance with
  the licensees maintenance rule program.
  This finding has an avoid complacency cross-cutting aspect within the human
  performance area because the licensee failed to recognize and plan for the possibility of
  mistakes, latent issues, and inherent risk, even while expecting successful outcomes.
  Specifically, the licensee tolerated excessive leakage past the FRVs, did not plan for
  further degradation, and the condition ultimately resulted in the Level 8 (high) trip of the
  running RFP on December 25, 2014 [H.12].
  Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,
  Criterion XVI, Corrective Action, requires, in part, that measures shall be established to
  assure that conditions adverse to quality, such as failures, malfunctions, deficiencies,
  deviations, defective material and equipment, and non-conformances are promptly
  identified and corrected. Contrary to the above, from December 25, 2014, to
  January 29, 2015, the licensee failed to assure that a condition adverse to quality was
  promptly identified. Specifically, the licensee failed to identify that reaching the reactor
  pressure vessel water Level 8 (high) setpoint, on December 25, 2014, was an adverse
  condition and enter it into the corrective action program. To restore compliance, the
  licensee entered this issue into their corrective action program as Condition
  Report CR-RBS-2015-00620 to perform a causal analysis for Level 8 (high) trips. Since
  the violation was of very low safety significance (Green), this violation is being treated as
  a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy:
  NCV 05000458/2015009-04, Failure to Identify High Reactor Water Level as a
  Condition Adverse to Quality.
d. Failure of the Plant-Referenced Simulator to Demonstrate Expected Plant Response
  Introduction. The team identified an apparent violation of 10 CFR 55.46(c)(1), Plant-
  Referenced Simulators, for the licensees failure to maintain the simulator so it would
  demonstrate expected plant response to operator input and to normal, transient, and
  accident conditions to which the simulator has been designed to respond. As of
  January 30, 2015, the licensee failed to maintain the simulator consistent with actual
  plant response for normal and transient conditions related to feedwater flows, alarm
  response, and behavior of the SFRV controller. As a result, operations personnel were
  challenged in their control of the plant during a reactor scram that occurred on
  December 25, 2014.
  Description. On December 25, 2014, River Bend Station was operating at 85 percent
  power when a reactor scram occurred. On January 26, 2015, a Special Inspection was
  initiated in response to this event. The Special Inspection team reviewed the event and
  identified several simulator fidelity issues. Licensee Procedure EN-TQ-202, Simulator
  Configuration Control, Revision 9, provided the process requirements necessary to
                                            -23-


Work Order WO-RBS-00396449: RFP C minimum flow valve does not stroke fully open which prevents starting the C feed pump. Maintenance personnel would manually operate a limit switch on the valve to make up the start logic for the RFP. This work order was initiated on October 10, 2014.
satisfy the guidelines for simulator testing, performance, and configuration control
specified by ANSI/ANS-3.5-2009. Standard ANSI/ANS-3.5-2009, Nuclear Power Plant
Simulators for Use in Operator Training and Examination, provides the simulator testing
requirements, as well as simulator configuration management to ensure simulator
fidelity. Specifically, as of January 30, 2015, the River Bend Station simulator failed to
model feedwater accurately and failed to model resulting reactor vessel level response
following a scram, failed to provide the correct alarm response for a loss of a RPS MG
set, and failed to correctly model the behavior of the SFRV controller. The simulator
modeling discrepancies and how these discrepancies affected plant response during the
plant trip are discussed below:
    *  The licensee stated their simulator modeled zero leakage across the FRV rather
        than the actual leakage in the plant. General Electric record 0247.230-000-016,
        Feedwater Control Valve Assembly - Purchase Specification, described the
        total design leakage across all the FRVs was approximately 135,000 lbm/hr.
        This is equal to approximately 1.1 percent full feedwater flow. The flow rate
        across the FRVs measured in the plant on December 25, 2014, was
        approximately 500,000 lbm/hr, which is approximately 3 percent full feedwater
        flow. The rate of level change of the reactor vessel in the plant was larger than
        operations personnel anticipated based on training received in the simulator.
        ANSI/ANS-3.5-2009, Section 4.1.4(3), states, The simulator shall not fail to
        cause an alarm or automatic action if the reference unit would have caused an
        alarm or automatic action under identical circumstances. In this case, the
        simulator under similar conditions did not reach the RPV water Level 8 (high)
        condition and trip the RFPs, when the actual plant did.
    *  The licensees simulator did not correctly model all alarms that would be received
        on a loss of power to the RPS. ANSI/ANS-3.5-2009, Section 4.1.4(3),
        states, The simulator shall not fail to cause an alarm or automatic action if the
        reference unit would have caused an alarm or automatic action under identical
        circumstances. Although the licensee had identified this discrepancy on
        December 11, 2014, and implemented a correction in the simulator model,
        operations personnel had not received training nor were they notified of the
        discrepancy. As a result, during the plant scram on December 25, 2014, the
        alarms for drywell high pressure and RPV high pressure annunciated per the
        facility design, operations personnel were not expecting the alarms because they
        did not alarm in the simulator during training.
    *  The simulator SFRV responded differently than the actual SFRV in the reference
        plant. ANSI/ANS-3.5-2009, Section 4.1.4(2) [for malfunctions], stated, Any
        observable change in simulated parameters corresponds in direction to the
        change expected from actual or best estimate response of the reference unit to
        the malfunction. Plant data indicated the SFRV does not open on a slowly
        decreasing RPV water level until the controller signal reaches approximately
        12.5 percent or about 3 inches below the RPV water level setpoint of the
        controller. The SFRV in the simulator opens as soon as the controller open
        signal is greater than 0.0. Because the SFRV did not respond as expected,
                                          -24-


Work Order WO-RBS-00346642:  leakage past FRVs when closed complicated post-scram reactor water level control. Operations personnel proceduralized the closure of the main feedwater isolation valves to stop the effect of the leakage. This work order was initiated on March 27, 2013.
        operations personnel incorrectly believed the SFRV had failed in automatic
        operation and placed the controller in manual. Due to an unrelated issue, the
        manual function of the SFRV was unavailable.
Collectively, these modeling discrepancies negatively impacted licensed operations
personnel performance in the actual control room, during the event of December 25,
2014. Specifically, operations personnel were not able to control reactor vessel water
level during the reactor scram.
The team noted that the licensee similarly stated in Condition Report
CR-RBS-2015-00641 that, During an investigation into the report at the OSRC (Onsite
Safety Review Committee) for the SCRAM on December 25, 2014, that feed regulating
valve leakage (FRV) contributed to the Level 8 received reactor vessel, it was
determined by analysis that there is sufficient evidence that leakage by the Feedwater
Regulating Valves presents a significant challenge to Operations during a scram event.
On April 10, 2015, the licensee provided a white paper with additional information related
to the modeling of the plant-referenced simulator. Specifically, it provided the licensees
perspective with regard to the following issues raised by the NRC:
    1. Two unexpected alarms on loss of Division II Reactor Protection System Power
    2. Main Feedwater Regulating Valve Seat Leakage
    3. Start-up Feedwater Regulating Valve Response
The licensee concluded that although they perceived that there were differences
between the simulator and the actual plant, they were considered to be minor. For each
of the items in question, the paper summarized that operator performance was not
impacted by simulator modeling. The team considered the information in the white
paper, and disagreed with the licensees conclusions. Some of the information provided,
however, did improve the teams understanding of the modeling deficiencies.
Analysis. The failure to maintain the plant-referenced simulator so that it would
demonstrate expected plant response to operator input and to normal and transient
conditions was a performance deficiency. This performance deficiency is more than
minor, and therefore a finding, because it is associated with the human performance
attribute of the Mitigating Systems Cornerstone and adversely affected the objective of
ensuring availability, reliability, and capability of systems needed to respond to initiating
events to prevent undesired consequences. Specifically, the incorrect simulator
response adversely affected the operating crews ability to assess plant conditions and
take actions in accordance with approved procedures during the December 25, 2014,
scram.
The team performed an initial screening of the finding in accordance with IMC 0609,
Appendix A, The Significance Determination Process (SDP) for Findings At-Power,
Attachment 4, Initial Characterization of Findings. Using IMC 0609, Attachment 4,
Table 3, SDP Appendix Router, the team answered yes to the following question:
Does the finding involve the operator licensing requalification program or simulator
                                          -25-


The deficient conditions in WO-RBS-00346642 and WO-RBS-00396449 contributed to complications experienced by the station when attempting to restore feedwater following a scram and loss of all feedwater pumps on a reactor pressure vessel water Level 8 (high).
  fidelity? As a result, the team used IMC 0609, Appendix I, Licensed Operator
  Requalification Significance Determination Process (SDP), and preliminarily determined
  the finding was of low to moderate safety significance (White) because the deficient
  simulator performance negatively impacted operations personnel performance in the
  actual plant during a reportable event. This modeling deficiency resulted in actual
  impact on operations personnel performance during response to a reactor scram that
  occurred on December 25, 2014.
  The NRC recently issued a non-cited violation related to simulator fidelity in March 2014
  documented in Inspection Report 05000458/2014301. Since the licensee recently
  verified simulator fidelity, this issue is indicative of current plant performance and has an
  evaluation cross-cutting aspect within the problem identification and resolution area
  because the licensee failed to thoroughly evaluate this issue to ensure that the
  resolution addressed the extent of condition commensurate with its safety significance.
  Specifically, the licensees evaluation of the fidelity issue focused on other training areas
  that used simulation, rather than evaluating the simulator modelling for additional fidelity
  discrepancies [P.2].
  Enforcement. Title 10 of the Code of Federal Regulations, Part 55.46(c)(1), Plant-
  Referenced Simulators, requires in part, that a simulator must demonstrate expected
  plant response to operator input and to normal, transient, and accident conditions to
  which the simulator has been designed to respond.
  Contrary to the above, as of January 30, 2015, the simulator failed to demonstrate
  expected plant response to operator input and to normal, transient, and accident
  conditions to which the simulator has been designed to respond. Specifically, the River
  Bend Station simulator failed to correctly model leakage flow rates across the FRVs;
  failed to provide the correct alarm response for a loss of a RPS MG set; and failed to
  correctly model the behavior of the SFRV controller. These simulator modeling issues
  led to negative training of operators. This subsequently complicated the operators
  response to a reactor scram in the actual plant on December 25, 2014. This issue has
  been entered into the corrective action program as Condition Report
  CR-RBS-2015-01261. The licensees condition report included actions to initiate
  simulator discrepancy reports, to investigate and resolve the potential fidelity issues, and
  to provide training to operations personnel on simulator differences. This is a violation of
  10 CFR 55.46(c)(1), Plant-Referenced Simulators: AV 05000458/2015009-05, Failure
  of the Plant-Referenced Simulator to Demonstrate Expected Plant Response.
e. Failure to Identify and Classify Operator Workarounds that Impacted Scram Recovery
  Actions
  Introduction. The team identified a Green finding for the licensees failure to follow
  written procedures for classifying deficient plant conditions as operator workarounds and
  providing compensatory measures or training in accordance with fleet
  Procedure EN-OP-117. A misclassification of these conditions resulted in the failure of
  the operations department to fully assess the impact these conditions had during a plant
                                              -26-


Fleet Procedure EN-OP-117, Attachment 9.4, "Operator Aggregate Assessment of Plant Deficiencies," provides a method to assess and document the impact of plant deficiencies on operations personnel response during off-normal and emergency conditions. In order to assess the cumulative impact of outstanding operator aggregate impact deficiencies, several deficiency types were evaluated, including operator workarounds. Following assessment of deficiencies, Attachment 9.4, step 5, directed the station to provide compensatory measures or training as appropriate until the deficiencies could be corrected.
transient. The failure to identify operator workarounds contributed to complications
experienced during reactor scram recovery on December 25, 2014.
Description. The team reviewed the recovery actions taken by the main control room
staff following the reactor scram on December 25, 2014, from 85 percent power. During
the review, the team observed the station had zero conditions identified as operator
workarounds. The team reviewed fleet Procedure EN-FAP-OP-006, Operator
Aggregate Impact Index Performance Indicator, Revision 2. This procedure defined an
operator workaround as:
        Any plant condition (equipment or other) that would require compensatory
        operator actions in the execution of normal operating procedures, abnormal
        operating procedures, emergency operating procedures, or annunciator
        response procedures during off-normal conditions. This indicator provided a
        measure of plant safety. It provided a measure of the likelihood that a plant
        transient may be complicated by equipment and human performance problems.
During their review, the team identified the following three conditions which met the
definition of an operator workaround as described in Procedure EN-FAP-OP-006, and
which were in effect prior to the December 25, 2014, event:
    *    Work Order WO-RBS-00404323: RFP B supply breaker repetitive failures to
        close potentially reduces the number of feedwater pumps available to operations
        personnel during a transient following reactor pressure vessel water
        Level 8 (high). Operations personnel would rack out and then rack the breaker
        back in until the breaker would function properly. This work order was initiated
        on February 3, 2015, following discussions with the NRC inspection team.
    *    Work Order WO-RBS-00396449: RFP C minimum flow valve does not stroke
        fully open which prevents starting the C feed pump. Maintenance personnel
        would manually operate a limit switch on the valve to make up the start logic for
        the RFP. This work order was initiated on October 10, 2014.
    *    Work Order WO-RBS-00346642: leakage past FRVs when closed complicated
        post-scram reactor water level control. Operations personnel proceduralized the
        closure of the main feedwater isolation valves to stop the effect of the leakage.
        This work order was initiated on March 27, 2013.
The deficient conditions in WO-RBS-00346642 and WO-RBS-00396449 contributed to
complications experienced by the station when attempting to restore feedwater following
a scram and loss of all feedwater pumps on a reactor pressure vessel water
Level 8 (high).
Fleet Procedure EN-OP-117, Attachment 9.4, Operator Aggregate Assessment of Plant
Deficiencies, provides a method to assess and document the impact of plant
deficiencies on operations personnel response during off-normal and emergency
conditions. In order to assess the cumulative impact of outstanding operator aggregate
                                        -27-


The resident inspectors engaged operations department management in January 2015, and informed the licensee that the three conditions appeared to meet the definition of an operator workaround as described in Procedure EN-FAP-OP-006. Upon learning of the misclassification of these issues, the station revised their operator aggregate index on February 6, 2015, to account for the three operator workaround conditions and the indicator turned red. As a result, the station issued guidance for post-scram reactor water level control and required operating crews to attend simulator training on vessel level control and feedwater system recovery following a Level 8 (high) trip of feedwater pumps. Additionally, the station wrote Condition Report CR-RBS-2015-00795 to document the issue.
impact deficiencies, several deficiency types were evaluated, including operator
workarounds. Following assessment of deficiencies, Attachment 9.4, step 5, directed
the station to provide compensatory measures or training as appropriate until the
deficiencies could be corrected.
The resident inspectors engaged operations department management in January 2015,
and informed the licensee that the three conditions appeared to meet the definition of an
operator workaround as described in Procedure EN-FAP-OP-006. Upon learning of the
misclassification of these issues, the station revised their operator aggregate index on
February 6, 2015, to account for the three operator workaround conditions and the
indicator turned red. As a result, the station issued guidance for post-scram reactor
water level control and required operating crews to attend simulator training on vessel
level control and feedwater system recovery following a Level 8 (high) trip of feedwater
pumps. Additionally, the station wrote Condition Report CR-RBS-2015-00795 to
document the issue.
Analysis. The failure to follow written procedures for classifying deficient plant
conditions as operator workarounds and providing compensatory measures or training in
accordance with fleet Procedure EN-OP-117 was a performance deficiency. This
performance deficiency is more than minor, and therefore a finding, because it had the
potential to lead to a more significant safety concern if left uncorrected. Specifically, the
performance deficiency contributed to complications experienced by the station when
attempting to restore feedwater following a scram on December 25, 2014.
The team performed an initial screening of the finding in accordance with IMC 0609,
Appendix A, The Significance Determination Process (SDP) for Findings At-Power.
Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the
finding was of very low safety significance (Green) because it: (1) was not a deficiency
affecting the design or qualification of a mitigating structure, system, or component, and
did not result in a loss of operability or functionality; (2) did not represent a loss of
system and/or function; (3) did not represent an actual loss of function of at least a single
train for longer than its technical specification allowed outage time, or two separate
safety systems out-of-service for longer than their technical specification allowed outage
time; and (4) did not represent an actual loss of function of one or more non-technical
specification trains of equipment designated as high safety-significant in accordance with
the licensees maintenance rule program.
This finding has a consistent process cross-cutting aspect within the human
performance area because the licensee failed to use a consistent, systematic approach
to making decisions and incorporate risk insights as appropriate. Specifically, no
systematic approach was enacted in order to properly classify deficient conditions [H.8].
Enforcement. Enforcement action does not apply because the performance deficiency
did not involve a violation of regulatory requirements. Because this finding does not
involve a violation and is of very low safety significance, this issue was entered into the
licensees corrective action program as Condition Report CR-RBS-2015-00795: FIN
                                          -28-


=====Analysis.=====
        05000458/2015001-06, Failure to Identify and Classify Operator Workarounds That
The failure to follow written procedures for classifying deficient plant conditions as operator workarounds and providing compensatory measures or training in accordance with fleet Procedure EN-OP-117 was a performance deficiency. This performance deficiency is more than minor, and therefore a finding, because it had the potential to lead to a more significant safety concern if left uncorrected. Specifically, the performance deficiency contributed to complications experienced by the station when attempting to restore feedwater following a scram on December 25, 2014.
        Impacted Scram Recovery Actions.
4OA6 Meetings, Including Exit
Exit Meeting Summary
On January 20, 2015, the team initially debriefed Mr. E. Olson, Site Vice President, and other
members of the licensee's staff. The licensee representatives acknowledged the findings
presented.
On June 29, 2015, the team conducted an exit briefing with Mr. E. Olson, Site Vice President,
and other members of the licensees staff. The licensee representatives acknowledged the
findings presented.
                                              -29-


The team performed an initial screening of the finding in accordance with IMC 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power."  Using IMC 0609, Appendix A, Exhibit 2, "Mitigating Systems Screening Questions," the finding was of very low safety significance (Green) because it:  (1) was not a deficiency affecting the design or qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) did not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant in accordance with the licensee's maintenance rule program.
                                SUPPLEMENTAL INFORMATION
                                  KEY POINTS OF CONTACT
Licensee Personnel
E. Olson, Site Vice President
D. Bergstrom, Senior Operations Instructor
M. Browning, Senior Operations Instructor
T. Brumfield, Director, Regulatory & Performance Improvement
S. Carter, Manager, Shift Operations
M. Chase, Manager, Training
J. Clark, Manager, Regulatory Assurance
F. Corley, Manager, Design & Program Engineering
T. Creekbaum, Engineer
G. Degraw, Manager, Training
G. Dempsey, Senior Operations Instructor
S. Durbin, Superintendent, Operations Training
R. Gadbois, General Manager, Plant Operations
T. Gates, Manager, Operations Support
J. Henderson, Assistant Manager, Operations
K. Huffstatler, Senior Licensing Specialist, Licensing
K. Jelks, Engineering Supervisor
G. Krause, Assistant Manager, Operations
T. Laporte, Senior Staff Operations Instructor
R. Leasure, Superintendent, Radiation Protection
P. Lucky, Manager, Performance Improvement
J. Maher, Manager, Systems & Components Engineering
W. Mashburn, Director, Engineering
W. Renz, Director, Emergency Planning, Entergy South
J. Reynolds, Senior Manager, Maintenance
T. Shenk, Manager, Operations
T. Schenk, Manager, Operations
S. Vazquez, Director, Engineering
D. Williamson, Senior Licensing Specialist
D. Yoes, Manager, Quality Assurance
NRC Personnel
G. Warnick, Branch Chief
J. Sowa, Senior Resident Inspector
R. Deese, Senior Reactor Analyst
                                                A1-1        Attachment 1


This finding has a consistent process cross-cutting aspect within the human performance area because the licensee failed to use a consistent, systematic approach to making decisions and incorporate risk insights as appropriate. Specifically, no systematic approach was enacted in order to properly classify deficient conditions [H.8].
                LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000458/2015009-01  URI    Vendor and Industry Recommended Testing Adequacy on
                              Safety-related and Safety-significant Circuit Breakers
                              (Section 2.5.b)
Opened and Closed
05000458/2015009-02  NCV    Failure to Establish Adequate Procedures to Perform
                              Maintenance on Equipment that can Affect Safety-Related
                              Equipment (Section 2.7.a)
05000458/2015009-03  NCV    Failure to Provide Adequate Procedures for Post-scram
                              Recovery (Section 2.7.b)
05000458/2015009-04  NCV    Failure to Identify High Reactor Water Level as a Condition
                              Adverse to Quality (Section 2.7.c)
05000458/2015009-05  AV      Failure of the Plant-Referenced Simulator to Demonstrate
                              Expected Plant Response (Section 2.7.d)
05000458/2015009-06  FIN    Failure to Identify and Classify Operator Workarounds that
                              Impacted Scram Recovery Actions (Section 2.7.e)
                        LIST OF DOCUMENTS REVIEWED
DRAWINGS
NUMBER          TITLE                                                          REVISION
GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System        34
Sheet 7
GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System        33
Sheet 8
GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System        31
Sheet 10
GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System        30
Sheet 11
GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System        30
Sheet 12
GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System        37
Sheet 15
GE-944E981      Elementary Diagram - RPS MG Set Control System                11
                                        A1-2


=====Enforcement.=====
DRAWINGS
Enforcement action does not apply because the performance deficiency did not involve a violation of regulatory requirements. Because this finding does not involve a violation and is of very low safety significance, this issue was entered into the licensee's corrective action program as Condition Report CR-RBS-2015-00795: FIN 05000458/2015001-06, "Failure to Identify and Classify Operator Workarounds That Impacted Scram Recovery Actions."
NUMBER        TITLE                                                  REVISION
{{a|4OA6}}
PID-25-01A    Engineering P&I Diagram - System 051, Nuclear Boiling  19
==4OA6 Meetings, Including Exit Exit Meeting Summary On January 20, 2015, the team initially debriefed Mr. E. Olson, Site Vice President, and other members of the licensee's staff.==
              Instrumentation
The licensee representatives acknowledged the findings presented. On June 29, 2015, the team conducted an exit briefing with Mr. E. Olson, Site Vice President, and other members of the licensee's staff. The licensee representatives acknowledged the findings presented.
PID-25-01B    Engineering P&I Diagram - System 051, Nuclear Boiling  7
              Instrumentation
828E531AA,   Elementary Diagram - Reactor Protection System        25
Sheet 4
828E531AA,   Elementary Diagram - Reactor Protection System        22
Sheet 4A
828E531AA,   Elementary Diagram - Reactor Protection System        27
Sheet 6
PROCEDURES
NUMBER        TITLE                                                  REVISION
AOP-0001      Reactor Scram                                          30
AOP-0003      Automatic Isolations                                    33
AOP-0006      Condensate/Feedwater Failures                          19
AOP-0010      Loss of One RPS Bus                                    19
EN-FAP-OM-004  Fleet and Site Business Plan Process                    0
EN-FAP-OM-012  Prompt Investigation, Notifications and Duty Manager    6
              Responsibilities
EN-FAP-OP-006  Operator Aggregate Impact Index Performance Indicator  2
EN-LI-102      Corrective Action Program                              24
EN-LI-118      Cause Evaluation Process                                21
EN-MA-125      Troubleshooting Control of Maintenance Activities      17
EN-OP-104      Operability Determination Process                      7
EN-OP-115      Conduct of Operations                                  15
EN-OP-117      Operations Assessment Resources                        8
EN-OP-115-09  Log Keeping                                            1
EN-TQ-202      Simulator Configuration Control                        9
EOP-0001      RPV Control                                            26
EOP-0003      Secondary Containment and Radioactive Release Control  16
                                        A1-3


A1-
PROCEDURES
NUMBER          TITLE                                                      REVISION
EPSTG-0001      Emergency Operating and Severe Accident Procedures - Plant 16
                Specific Technical Guidelines (PSTG)
EPSTG-0002      EPGs/SAGs to PSTG to EOP/SAP Flowcharts Comparison        16
EPSTG-0002,    Emergency Operating and Severe Accident Procedures -      16
Appendix B      Bases
GOP-0001        Plant Startup                                              83
GOP-0002        Plant Shutdown                                            70
GOP-0003        Scram Recovery for December 27, 2014                      24
OSP-0001        Control of Operator Aids                                  13
OSP-0053        Emergency and Transient Response Support Procedure        22
CONDITION REPORTS
CR-RBS-1998-00384  CR-RBS-2002-00672        CR-RBS-2002-00688  CR-RBS-2006-04078
CR-RBS-2011-02209  CR-RBS-2011-09053        CR-RBS-2012-02249  CR-RBS-2012-03434
CR-RBS-2012-03439  CR-RBS-2012-03440        CR-RBS-2012-03665  CR-RBS-2012-03739
CR-RBS-2012-03816  CR-RBS-2012-03817        CR-RBS-2012-05894  CR-RBS-2012-06015
CR-RBS-2012-07249  CR-RBS-2012-07250        CR-RBS-2012-07251  CR-RBS-2012-07253
CR-RBS-2012-07254  CR-RBS-2013-04419        CR-RBS-2014-05200  CR-RBS-2014-05209
CR-RBS-2014-06233  CR-RBS-2014-06357        CR-RBS-2014-06561  CR-RBS-2014-06581
CR-RBS-2014-06602  CR-RBS-2014-06605        CR-RBS-2014-06649  CR-RBS-2014-06696
CR-RBS-2015-00030  CR-RBS-2015-00043        CR-RBS-2015-00153  CR-RBS-2015-00318
CR-RBS-2015-00365  CR-RBS-2015-00480        CR-RBS-2015-00482  CR-RBS-2015-00483
CR-RBS-2015-00484  CR-RBS-2015-00486        CR-RBS-2015-00487  CR-RBS-2015-00579
CR-RBS-2015-00620  CR-RBS-2015-00626        CR-RBS-2015-00641  CR-RBS-2015-00657
CR-RBS-2015-00795  CR-RBS-2015-01261        CR-RBS-2015-02810
WORK ORDERS
WO-RBS-00346642    WO-RBS-00396449          WO-RBS-00401085    WO-RBS-00404323
                                        A1-4


=SUPPLEMENTAL INFORMATION=
MISCELLANEOUS DOCUMENT
NUMBER          TITLE                                                      REVISION /
                                                                          DATE
EC 50374        Engineering Change - Feedwater Level Control Setpoint      0
                Setdown Modification
EN-LI-100-ATT-  Process Applicability Determination Form for AOP-0001,    August 6,
9.1            Reactor Scram, Revision 24                                2007
LI-101          50.59 Review Form for GOP-0002, Power Decrease/Plant      August 26,
                Shutdown, Revision 30                                      2004
GE-22A3778      Feedwater Control System (Motor Driven Feed Pumps)        4
                Design Specification
GE-22A3778AB    Feedwater Control System (Motor Driven Feed Pumps)        7
                Design Specification Data Sheet
RLP-LOP-0511    Licensed Operator Requalification - Industry              August 1,
                Events/Operating Experience and Plant Modifications        2002
1-ST-27-TC6    Startup Procedure and Results - Turbine Trip and Generator June 27,
                Load Reject                                                1986
107-Feedwater  System Health Report - Feedwater                          Q2 2014
0247.230-000-16 Feedwater Control Valve Assembly - Purchase Specifications 301
                List of Actuations/Isolations That Occur From Loss of RPS  January 29,
                Bus B                                                      2015
                Main Control Room Log                                      December 6,
                                                                          2014
                Main Control Room Log                                      December 13,
                                                                          2014
                Main Control Room Log                                      December 16,
                                                                          2014
                Main Control Room Log                                      December 27,
                                                                          2014
                Main Control Room Log                                      December 28,
                                                                          2014
                                            A1-5


==KEY POINTS OF CONTACT==
                                            UNITED STATES
                              NUCLEAR REGULATORY COMMISSION
                                                REGION IV
                                            1600 E LAMAR BLVD
                                        ARLINGTON, TX 76011-4511
                                          January 15, 2015
MEMORANDUM TO: Tom Hartman, Senior Resident Inspector
                          Reactor Projects Branch B
                          Division of Reactor Projects
FROM:                    Troy Pruett, Director /RA/
                          Division of Reactor Projects
SUBJECT:                  SPECIAL INSPECTION CHARTER TO EVALUATE CAUSES OF THE
                          UNPLANNED REACTOR TRIP WITH COMPLICATIONS AT THE
                          RIVER BEND STATION
In response to the unplanned reactor trip with complications at the River Bend Station, a special
inspection will be performed. You are hereby designated as the special inspection team leader.
The following members are assigned to your team:
    *  Jim Drake, Senior Reactor Inspector, Division of Reactor Safety
    *  Dan Bradley, Resident Inspector, Division of Reactor Projects
A.      Basis
        On December 25, 2014, at 8:37 AM, River Bend Station scrammed from 85 percent power
        following a trip of the B reactor protection system (RPS) motor generator (MG) set. At the
        time of the MG set trip, a Division 1 half scram existed due to an unrelated equipment
        issue with a relay for the No. 2 turbine control valve fast closure RPS function. The
        combination of the B RPS MG set trip and the Division 1 half scram resulted in a scram of
        the reactor.
        The following equipment issues occurred during the initial scram response.
        *    An unexpected Level 8 (high) reactor water level signal was received which resulted in
            tripping of all RFPs.
        *    Following reset of the Level 8 high reactor water level signal, plant operators were
            unable to start RFP C. Plant operators responded by starting RFP A at a vessel level
            of 25. The licensee subsequently determined that the circuit breaker (Magne Blast
            type) for RFP C did not close because an interlock lever for a microswitch that controls
            the breaker close permissive was not fully engaged in the cubicle.
        *    Following the start of RFP A, the licensee attempted to open the startup feed
            regulating valve but was unsuccessful prior the Level 3 low reactor water level trip
            setpoint at +9.7. The licensee then opened the C main feedwater regulating valve to
                                                  A2-1                                Attachment 2


===Licensee Personnel===
        restore reactor vessel water level. The lowest level reached was +7.5. Subsequent
: [[contact::E. Olson]], Site Vice President
        troubleshooting revealed a faulty manual function control card. The card was
: [[contact::D. Bergstrom]], Senior Operations Instructor
        replaced by the licensee and the startup feedwater regulating valve was used on the
: [[contact::M. Browning]], Senior Operations Instructor
        subsequent plant startup.
: [[contact::T. Brumfield]], Director, Regulatory & Performance Improvement
  Following restoration of reactor vessel water level, the plant was stabilized in Mode 3. A
: [[contact::S. Carter]], Manager, Shift Operations
  plant startup was conducted on December 27, 2014 with RPS bus B being supplied by
: [[contact::M. Chase]], Manager, Training
  its alternate power source. During power ascension following startup, RFP B did not
: [[contact::J. Clark]], Manager, Regulatory Assurance
  start. The licensee re-racked its associated circuit breaker and successfully started
: [[contact::F. Corley]], Manager, Design & Program Engineering
  RFP B.
: [[contact::T. Creekbaum]], Engineer
  Management Directive 8.3, NRC Incident Investigation Program, was used to evaluate
: [[contact::G. Degraw]], Manager, Training 
  the level of NRC response for this event. In evaluating the deterministic criteria of
: [[contact::G. Dempsey]], Senior Operations Instructor
  MD 8.3, it was determined that: (1) The event included multiple failures in the feedwater
: [[contact::S. Durbin]], Superintendent, Operations Training
  system which is a short term decay heat removal mitigating system; (2) involved two
: [[contact::R. Gadbois]], General Manager, Plant Operations
  Magna Blast circuit breaker issues which could possibly have generic implications
: [[contact::T. Gates]], Manager, Operations Support
  regarding the licensees maintenance, testing, and operating practices for these
: [[contact::J. Henderson]], Assistant Manager, Operations
  components including safety-related breakers in the high pressure core spray system;
: [[contact::K. Huffstatler]], Senior Licensing Specialist, Licensing
  and, (3) involved several issues related to the ability of operations to control reactor vessel
: [[contact::K. Jelks]], Engineering Supervisor
  level between the Level 3 low and Level 8 high trip set points following a reactor scram.
: [[contact::G. Krause]], Assistant Manager, Operations
  Since the deterministic criteria was met, the trip was evaluated for risk. The preliminary
: [[contact::T. Laporte]], Senior Staff Operations Instructor
  Estimated Conditional Core Damage Probability was determined to be 1.2E-6.
: [[contact::R. Leasure]], Superintendent, Radiation Protection
  Based on the deterministic criteria and risk insights related to the multiple failures of the
: [[contact::P. Lucky]], Manager, Performance Improvement
  feedwater system, the potential generic concern with the Magna Blast circuit breakers,
: [[contact::J. Maher]], Manager, Systems & Components Engineering
  and the issues related to the licensees Operations departments inability to control reactor
: [[contact::W. Mashburn]], Director, Engineering
  vessel level between the Level 3 and Level 8 setpoints following a reactor scram, Region
: [[contact::W. Renz]], Director, Emergency Planning, Entergy South
  IV determined that the appropriate level of NRC response was to conduct a Special
: [[contact::J. Reynolds]], Senior Manager, Maintenance
  Inspection.
: [[contact::T. Shenk]], Manager, Operations
  This Special Inspection is chartered to identify the circumstances surrounding this event,
: [[contact::T. Schenk]], Manager, Operations
  determine if there are adverse generic implications, and review the licensees actions to
: [[contact::S. Vazquez]], Director, Engineering
  address the causes of the event.
: [[contact::D. Williamson]], Senior Licensing Specialist
B. Scope
: [[contact::D. Yoes]], Manager, Quality Assurance 
  The inspection is expected to perform data gathering and fact-finding in order to address
===NRC Personnel===
  the following:
: [[contact::G. Warnick]], Branch Chief
  1.       Provide a recommendation to Region IV management as to whether the
: [[contact::J. Sowa]], Senior Resident Inspector
            inspection should be upgraded to an augmented inspection team response. This
: [[contact::R. Deese]], Senior Reactor Analyst   
            recommendation should be provided by the end of the first day on site.
  2.       Develop a complete sequence of events related to the reactor scram that
            occurred on December 25, 2014. The chronology should include the events
            leading to the reactor scram, the licensees immediate scram response and the
            licensees post-scram recovery actions including troubleshooting and reactor
            startup.
                                            A2-2


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
  3.    Review the licensees root cause analysis and determine if it is being conducted
          at a level of detail commensurate with the significance of the problem.
  4.    Determine the causes for the unexpected Level 8 high water level trip signal that
          was experienced following the reactor scram.
  5.    Review the effectiveness of licensee actions to address known equipment
          degradations that could complicate post scram operator response.
  6.    Review the causes and corrective actions taken to address the failure of RFP C
          to start during the initial scram response and RFP B during the subsequent
          reactor startup. For issues related to Magne Blast circuit breakers, verify that the
          licensees corrective actions have addressed extent of condition and extent of
          cause.
  7.    Review the licensees maintenance, testing and operating practices for Magne
          Blast circuit breakers. Promptly communicate any potential generic issues to
          regional management.
  8.    Review the licensees corrective actions to address complications encountered
          during previous reactor scrams. Reference previously docketed correspondence
          regarding complicated reactor scrams in NRC inspection reports
          05000458/2002002, 05000458/2006013, 05000458/2012009 and
          05000458/2012012.
  9.    Evaluate pertinent industry operating experience and potential precursors to the
          event, including the effectiveness of any action taken in response to the
          operating experience.
  10.    Collect data necessary to support completion of the significance determination
          process.
C. Guidance
  Inspection Procedure 93812, "Special Inspection," provides additional guidance to be
  used by the Special Inspection Team. Your duties will be as described in Inspection
  Procedure 93812. The inspection should emphasize fact-finding in its review of the
  circumstances surrounding the event. It is not the responsibility of the team to examine
                                            A2-3


===Opened===
        the regulatory process. Safety concerns identified that are not directly related to the
: 05000458/2015009-01 URI Vendor and Industry Recommended Testing Adequacy on Safety-related and Safety-significant Circuit Breakers (Section 2.5.b) 
        event should be reported to the Region IV office for appropriate action.
===Opened and Closed===
        You will formally begin the special inspection with an entrance meeting to be conducted
: 05000458/2015009-02 NCV Failure to Establish Adequate Procedures to Perform Maintenance on Equipment that can Affect Safety-Related Equipment (Section 2.7.a)
        no later than January 26, 2015. You should provide a daily briefing to Region IV
: 05000458/2015009-03 NCV Failure to Provide Adequate Procedures for Post-scram Recovery (Section 2.7.b)
        management during the course of your inspections and prior to your exit meeting. A
: 05000458/2015009-04 NCV Failure to Identify High Reactor Water Level as a Condition Adverse to Quality (Section 2.7.c)
        report documenting the results of the inspection should be issued within 45 days of the
: 05000458/2015009-05 AV Failure of the Plant-Referenced Simulator to Demonstrate Expected Plant Response (Section 2.7.d)
        completion of the inspection.
: 05000458/2015009-06 FIN Failure to Identify and Classify Operator Workarounds that Impacted Scram Recovery Actions (Section 2.7.e) 
        This Charter may be modified should you develop significant new information that
==LIST OF DOCUMENTS REVIEWED==
        warrants review. Should you have any questions concerning this Charter, contact
DRAWINGS NUMBER TITLE REVISION
        Jeremy Groom at (817) 200-1144.
: GE-828E445AA, Sheet 7 Elementary Diagram - Nuclear Steam Supply Shutoff System 34
cc via E-mail:
: GE-828E445AA, Sheet 8 Elementary Diagram - Nuclear Steam Supply Shutoff System 33
M. Dapas
: GE-828E445AA, Sheet 10 Elementary Diagram - Nuclear Steam Supply Shutoff System 31
K. Kennedy
: GE-828E445AA, Sheet 11 Elementary Diagram - Nuclear Steam Supply Shutoff System 30
T. Pruett
: GE-828E445AA, Sheet 12 Elementary Diagram - Nuclear Steam Supply Shutoff System 30
A. Vegel
: GE-828E445AA, Sheet 15 Elementary Diagram - Nuclear Steam Supply Shutoff System 37
J. Clark
: GE-944E981 Elementary Diagram - RPS MG Set Control System 11 
V. Dricks
: DRAWINGS NUMBER TITLE REVISION
W. Maier
: PID-25-01A Engineering P&I Diagram - System 051, Nuclear Boiling Instrumentation 19
J. Groom
: PID-25-01B Engineering P&I Diagram - System 051, Nuclear Boiling Instrumentation 7 828E531AA, Sheet 4 Elementary Diagram - Reactor Protection System 25 828E531AA, Sheet 4A Elementary Diagram - Reactor Protection System 22 828E531AA, Sheet 6 Elementary Diagram - Reactor Protection System 27
J. Sowa
: PROCEDURES NUMBER TITLE REVISION
R. Azua
: AOP-0001 Reactor Scram 30
N. Taylor
: AOP-0003 Automatic Isolations 33
T. Hartman
: AOP-0006 Condensate/Feedwater Failures 19
J. Drake
: AOP-0010 Loss of One RPS Bus 19
D. Bradley
: EN-FAP-OM-004 Fleet and Site Business Plan Process 0
ADAMS ACCESSION NUMBER ML15015A634
: EN-FAP-OM-012 Prompt Investigation, Notifications and Duty Manager Responsibilities 6
  SUNSI Rev Compl. Yes No ADAMS                   Yes No       Reviewer Initials     JRG
: EN-FAP-OP-006 Operator Aggregate Impact Index Performance Indicator 2
  Publicly Avail         Yes No Sensitive         Yes No       Sens. Type Initials     JRG
: EN-LI-102 Corrective Action Program 24
  Keyword               MD 3.4/A.7
: EN-LI-118 Cause Evaluation Process 21
  RIV/DRP: BC         RIV/DRP: DIR
: EN-MA-125 Troubleshooting Control of Maintenance Activities 17
      JRGroom             TWPruett
: EN-OP-104 Operability Determination Process 7
    /RA/RAzua for             /RA/
: EN-OP-115 Conduct of Operations 15
        1/15/15             1/15/15
: EN-OP-117 Operations Assessment Resources 8
                                      OFFICIAL RECORD
: EN-OP-115-09 Log Keeping 1
                                                A2-4
: EN-TQ-202 Simulator Configuration Control 9
: EOP-0001 RPV Control 26
: EOP-0003 Secondary Containment and Radioactive Release Control 16 
: PROCEDURES NUMBER TITLE REVISION
: EPSTG-0001 Emergency Operating and Severe Accident Procedures - Plant Specific Technical Guidelines (PSTG) 16
: EPSTG-0002 EPGs/SAGs to PSTG to EOP/SAP Flowcharts Comparison 16
: EPSTG-0002, Appendix B Emergency Operating and Severe Accident Procedures - Bases 16
: GOP-0001 Plant Startup 83
: GOP-0002 Plant Shutdown 70
: GOP-0003 Scram Recovery for December 27, 2014 24
: OSP-0001 Control of Operator Aids 13
: OSP-0053 Emergency and Transient Response Support Procedure 22
: CONDITION REPORTS
: CR-RBS-1998-00384
: CR-RBS-2002-00672
: CR-RBS-2002-00688
: CR-RBS-2006-04078
: CR-RBS-2011-02209
: CR-RBS-2011-09053
: CR-RBS-2012-02249
: CR-RBS-2012-03434
: CR-RBS-2012-03439
: CR-RBS-2012-03440
: CR-RBS-2012-03665
: CR-RBS-2012-03739
: CR-RBS-2012-03816
: CR-RBS-2012-03817
: CR-RBS-2012-05894
: CR-RBS-2012-06015
: CR-RBS-2012-07249
: CR-RBS-2012-07250
: CR-RBS-2012-07251
: CR-RBS-2012-07253
: CR-RBS-2012-07254
: CR-RBS-2013-04419
: CR-RBS-2014-05200
: CR-RBS-2014-05209
: CR-RBS-2014-06233
: CR-RBS-2014-06357
: CR-RBS-2014-06561
: CR-RBS-2014-06581
: CR-RBS-2014-06602
: CR-RBS-2014-06605
: CR-RBS-2014-06649
: CR-RBS-2014-06696
: CR-RBS-2015-00030
: CR-RBS-2015-00043
: CR-RBS-2015-00153
: CR-RBS-2015-00318
: CR-RBS-2015-00365
: CR-RBS-2015-00480
: CR-RBS-2015-00482
: CR-RBS-2015-00483
: CR-RBS-2015-00484
: CR-RBS-2015-00486
: CR-RBS-2015-00487
: CR-RBS-2015-00579
: CR-RBS-2015-00620
: CR-RBS-2015-00626
: CR-RBS-2015-00641
: CR-RBS-2015-00657
: CR-RBS-2015-00795
: CR-RBS-2015-01261
: CR-RBS-2015-02810 
: WORK ORDERS
: WO-RBS-00346642
: WO-RBS-00396449
: WO-RBS-00401085
: WO-RBS-00404323 
: MISCELLANEOUS DOCUMENT NUMBER TITLE REVISION / DATE
: EC 50374 Engineering Change - Feedwater Level Control Setpoint Setdown Modification 0
: EN-LI-100-ATT-9.1 Process Applicability Determination Form for
: AOP-0001, Reactor Scram, Revision 24 August 6, 2007
: LI-101 50.59 Review Form for
: GOP-0002, Power Decrease/Plant Shutdown, Revision 30 August 26, 2004
: GE-22A3778 Feedwater Control System (Motor Driven Feed Pumps) Design Specification 4
: GE-22A3778AB Feedwater Control System (Motor Driven Feed Pumps) Design Specification Data Sheet 7
: RLP-LOP-0511 Licensed Operator Requalification - Industry Events/Operating Experience and Plant Modifications August 1, 2002 1-ST-27-TC6 Startup Procedure and Results - Turbine Trip and Generator Load Reject June 27, 1986 107-Feedwater System Health Report - Feedwater Q2 2014 0247.230-000-16 Feedwater Control Valve Assembly - Purchase Specifications 301
: List of Actuations/Isolations That Occur From Loss of RPS Bus B January 29, 2015
: Main Control Room Log December 6, 2014
: Main Control Room Log December 13, 2014
: Main Control Room Log December 16, 2014
: Main Control Room Log December 27, 2014
: Main Control Room Log December 28, 2014 
: Attachment 2
: January 15, 2015
: MEMORANDUM TO: Tom Hartman, Senior Resident Inspector Reactor Projects Branch B Division of Reactor Projects
: FROM: Troy Pruett, Director /RA/ Division of Reactor Projects
: SUBJECT:
: SPECIAL INSPECTION CHARTER TO EVALUATE CAUSES OF THE UNPLANNED REACTOR TRIP WITH COMPLICATIONS AT THE RIVER BEND STATION
: In response to the unplanned reactor trip with complications at the River Bend Station, a special inspection will be performed.
: You are hereby designated as the special inspection team leader.
: The following members are assigned to your team:
: Jim Drake, Senior Reactor Inspector, Division of Reactor Safety
: Dan Bradley, Resident Inspector, Division of Reactor Projects
: A. Basis
: On December 25, 2014, at 8:37 AM, River Bend Station scrammed from 85 percent power following a trip of the B reactor protection system (RPS) motor generator (MG) set.
: At the time of the MG set trip, a Division 1 half scram existed due to an unrelated equipment issue with a relay for the No. 2 turbine control valve fast closure RPS function.
: The combination of the B RPS MG set trip and the Division 1 half scram resulted in a scram of the reactor.
: The following equipment issues occurred during the initial scram response.
: An unexpected Level 8 (high) reactor water level signal was received which resulted in tripping of all RFPs.
: Following reset of the Level 8 high reactor water level signal, plant operators were unable to start RFP C.
: Plant operators responded by starting RFP A at a vessel level of 25".
: The licensee subsequently determined that the circuit breaker (Magne Blast type) for RFP C did not close because an interlock lever for a microswitch that controls the breaker close permissive was not fully engaged in the cubicle.
: Following the start of RFP A, the licensee attempted to open the startup feed regulating valve but was unsuccessful prior the Level 3 low reactor water level trip setpoint at +9.7".
: The licensee then opened the C main feedwater regulating valve to
: UNITED STATES NUCLEAR REGULATORY COMMISSION REGION
: IV 1600 E LAMAR BLVD ARLINGTON,
: TX 76011-4511
restore reactor vessel water level.
: The lowest level reached was +7.5".
: Subsequent troubleshooting revealed a faulty manual function control card.
: The card was replaced by the licensee and the startup feedwater regulating valve was used on the subsequent plant startup.
: Following restoration of reactor vessel water level, the plant was stabilized in Mode 3.
: A plant startup was conducted on December 27, 2014 with RPS bus B being supplied by its alternate power source.
: During power ascension following startup, RFP B did not start.
: The licensee re-racked its associated circuit breaker and successfully started RFP B.
: Management Directive 8.3, "NRC Incident Investigation Program," was used to evaluate the level of NRC response for this event.
: In evaluating the deterministic criteria of
: MD 8.3, it was determined that: (1) The event included multiple failures in the feedwater system which is a short term decay heat removal mitigating system; (2) involved two Magna Blast circuit breaker issues which could possibly have generic implications regarding the licensee's maintenance, testing, and operating practices for these components including safety-related breakers in the high pressure core spray system; and, (3) involved several issues related to the ability of operations to control reactor vessel level between the Level 3 low and Level 8 high trip set points following a reactor scram.
: Since the deterministic criteria was met, the trip was evaluated for risk.
: The preliminary Estimated Conditional Core Damage Probability was determined to be 1.2E-6.
: Based on the deterministic criteria and risk insights related to the multiple failures of the feedwater system, the potential generic concern with the Magna Blast circuit breakers,  and the issues related to the licensee's Operations department's inability to control reactor vessel level between the Level 3 and Level 8 setpoints following a reactor scram, Region
: IV determined that the appropriate level of NRC response was to conduct a Special Inspection.
: This Special Inspection is chartered to identify the circumstances surrounding this event, determine if there are adverse generic implications, and review the licensee's actions to address the causes of the event.
: B. Scope
: The inspection is expected to perform data gathering and fact-finding in order to address the following:
: 1. Provide a recommendation to Region IV management as to whether the inspection should be upgraded to an augmented inspection team response.
: This recommendation should be provided by the end of the first day on site.
: 2. Develop a complete sequence of events related to the reactor scram that occurred on December 25, 2014.
: The chronology should include the events leading to the reactor scram, the licensee's immediate scram response and the licensee's post-scram recovery actions including troubleshooting and reactor startup.
: 3. Review the licensee's root cause analysis and determine if it is being conducted at a level of detail commensurate with the significance of the problem.
: 4. Determine the causes for the unexpected Level 8 high water level trip signal that was experienced following the reactor scram.
: 5. Review the effectiveness of licensee actions to address known equipment degradations that could complicate post scram operator response.
: 6. Review the causes and corrective actions taken to address the failure of RFP C to start during the initial scram response and RFP B during the subsequent reactor startup.
: For issues related to Magne Blast circuit breakers, verify that the licensee's corrective actions have addressed extent of condition and extent of cause.
: 7. Review the licensee's maintenance, testing and operating practices for Magne Blast circuit breakers.
: Promptly communicate any potential generic issues to regional management.
: 8. Review the licensee's corrective actions to address complications encountered during previous reactor scrams.
: Reference previously docketed correspondence regarding complicated reactor scrams in NRC inspection reports 05000458/2002002, 05000458/2006013, 05000458/2012009 and 05000458/2012012.
: 9. Evaluate pertinent industry operating experience and potential precursors to the event, including the effectiveness of any action taken in response to the operating experience.
: 10. Collect data necessary to support completion of the significance determination process.
: C. Guidance
: Inspection Procedure 93812, "Special Inspection," provides additional guidance to be used by the Special Inspection Team.
: Your duties will be as described in Inspection 
===Procedure===
: 93812.
: The inspection should emphasize fact-finding in its review of the circumstances surrounding the event.
: It is not the responsibility of the team to examine the regulatory process.
: Safety concerns identified that are not directly related to the event should be reported to the Region IV office for appropriate action.
: You will formally begin the special inspection with an entrance meeting to be conducted no later than January 26, 2015.
: You should provide a daily briefing to Region IV management during the course of your inspections and prior to your exit meeting.
: A report documenting the results of the inspection should be issued within 45 days of the completion of the inspection.
: This Charter may be modified should you develop significant new information that warrants review.
: Should you have any questions concerning this Charter, contact Jeremy Groom at (817) 200-1144.
cc via E-mail: M. Dapas K. Kennedy T. Pruett A. Vegel J. Clark V. Dricks W. Maier J. Groom J. Sowa R. Azua N. Taylor T. Hartman J. Drake D. Bradley
: ADAMS ACCESSION NUMBER
: ML15015A634 SUNSI Rev Compl.
: Yes
: No ADAMS Yes
: No Reviewer Initials JRG Publicly Avail
: Yes
: No Sensitive
: Yes No Sens. Type Initials
: JRG Keyword MD 3.4/A.7
: RIV/DRP: BC RIV/DRP: DIR
: JRGroom TWPruett   /RA/RAzua for /RA/
: 1/15/15 1/15/15
: OFFICIAL RECORD
}}
}}

Latest revision as of 09:22, 31 October 2019

IR 05000458/2015009; on 01/26/2015 - 06/29/2015; River Bend Station; Special Inspection for the Scram with Complications That Occurred on December 25, 2014
ML15188A532
Person / Time
Site: River Bend Entergy icon.png
Issue date: 07/07/2015
From: Troy Pruett
NRC/RGN-IV/DRP
To: Olson E
Entergy Operations
Greg Warnick
References
EA-15-043 EA-15-043, IR 2015009
Download: ML15188A532 (43)


See also: IR 05000458/2015009

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

1600 E. LAMAR BLVD

ARLINGTON, TX 76011-4511

July 7, 2015

EA-15-043

Mr. Eric W. Olson, Site Vice President

Entergy Operations, Inc.

River Bend Station

5485 U.S. Highway 61N

St. Francisville, LA 70775

SUBJECT: RIVER BEND STATION - NRC SPECIAL INSPECTION

REPORT 05000458/2015009; PRELIMINARY WHITE FINDING

Dear Mr. Olson:

On June 29, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed a Special

Inspection at the River Bend Station to evaluate the facts and circumstances surrounding an

unplanned reactor trip. Based upon the risk and deterministic criteria specified in NRC

Management Directive 8.3, NRC Incident Investigation Program, the NRC initiated a Special

Inspection in accordance with Inspection Procedure 93812, Special Inspection. The basis for

initiating the special inspection and the focus areas for review are detailed in the Special

Inspection Charter (Attachment 2). The NRC determined the need to perform a Special

Inspection on January 15, 2015, and the onsite inspection started on January 26, 2015. The

enclosed report documents the inspection findings that were discussed on May 21 and

June 29, 2015, with you and members of your staff. The team documented the results of this

inspection in the enclosed inspection report.

The enclosed inspection report documents a finding that has preliminarily been determined to

be White, a finding with low to moderate safety significance that may require additional NRC

inspections, regulatory actions, and oversight. The team identified an apparent violation for

failure to maintain the simulator so it would accurately reproduce the operating characteristics of

the facility. Specifically, the River Bend Station simulator failed to accurately model feedwater

flow and reactor vessel level response following a scram, failed to provide the correct alarm

response for loss of a reactor protection system motor generator set, and failed to correctly

model the operation of the startup feedwater regulating valve. As a result of the simulator

deficiencies, operations personnel were presented with additional challenges to control the plant

and maintain plant parameters following a reactor scram on December 25, 2014. Because

actions have been taken to initiate discrepancy reports, to investigate and resolve the potential

fidelity issues and to provide training to operations personnel, the simulator deficiencies do not

represent a continuing safety concern. The NRC assessed this finding using the best available

information, and Manual Chapter 0609, Significance Determination Process. The basis for the

NRCs preliminary significance determination is described in the enclosed report. The finding is

also an apparent violation of NRC requirements and is being considered for escalated

enforcement action in accordance with the Enforcement Policy, which can be found on the

E. Olson -2-

NRCs website at http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html.

The NRC will inform you in writing when the final significance has been determined.

Before we make a final decision on this matter, we are providing you with an opportunity to

(1) attend a Regulatory Conference where you can present your perspective on the facts and

assumptions used to arrive at the finding and assess its significance, or (2) submit your position

on the finding to the NRC in writing. If you request a Regulatory Conference, it should be held

within 30 days of your receipt of this letter. We encourage you to submit supporting

documentation at least one week prior to the conference in an effort to make the conference

more efficient and effective. The focus of the Regulatory Conference is to discuss the

significance of the finding and not necessarily the root cause(s) or corrective action(s)

associated with the finding. If you choose to attend a Regulatory Conference, it will be open for

public observation. The NRC will issue a public meeting notice and press release to announce

the conference. If you decide to submit only a written response, it should be sent to the NRC

within 30 days of your receipt of this letter. If you decline to request a Regulatory Conference or

to submit a written response, you relinquish your right to appeal the NRCs final significance

determination, in that by not choosing an option, you fail to meet the appeal requirements stated

in the Prerequisites and Limitations sections of Attachment 2, Process for Appealing NRC

Characterization of Inspection Findings (SDP Appeal Process), of NRC Inspection Manual

Chapter 0609.

Please contact Greg Warnick at (817) 200-1144, and in writing, within 10 days from the issue

date of this letter to notify us of your intentions. If we have not heard from you within 10 days,

we will continue with our final significance determination and enforcement decision. The final

resolution of this matter will be conveyed in separate correspondence.

Because the NRC has not made a final determination in this matter, no Notice of Violation is

being issued for this inspection finding at this time. In addition, please be advised that the

number and characterization of the apparent violation described in the enclosed inspection

report may change based on further NRC review.

In addition, the NRC inspectors documented four findings of very low safety significance

(Green) in this report. Three of these findings were determined to involve violations of NRC

requirements. The NRC is treating these violations as non-cited violations consistent with

Section 2.3.2.a of the Enforcement Policy.

If you contest the violations or significance of these non-cited violations, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the

Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington, DC 20555-0001; and the NRC resident inspector at the River Bend Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the

River Bend Station.

E. Olson -3-

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your

response (if any) will be available electronically for public inspection in the NRC's Public

Document Room or from the Publicly Available Records (PARS) component of the NRC's

Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic

Reading Room).

Sincerely,

/RA/

Troy W. Pruett

Director

Division of Reactor Projects

Docket No. 50-458

License No. NPF-47

Enclosure:

Inspection Report 05000458/2015009

w/ Attachments:

1. Supplemental Information

2. Special Inspection Charter

SUNSI Review ADAMS Non-Sensitive Publicly Available

By: RVA Yes No Sensitive Non-Publicly Available

OFFICE SRI:DRP/B SRI:DRS/PSB2 RI:DRP/A BC:DRS/OB SES:ACES TL:ACES BC:DRP/C

NAME THartman JDrake DBradley VGaddy RBrowder MHay GWarnick

SIGNATURE /RA/ /RA/ /RA/ /RA/ /RA/ /RA/ /RA/

DATE 06/04/15 06/04/15 06/05/15 06/30/15 06/04/15 06/04/15 06/04/15

OFFICE D:DRP

NAME TPruett

SIGNATURE /RA/

DATE 7/7/15

Letter to Eric Olson from Troy Pruett dated July 7, 2015.

SUBJECT: RIVER BEND STATION - NRC SPECIAL INSPECTION

REPORT 05000458/2015009; PRELIMINARY WHITE FINDING

DISTRIBUTION:

Regional Administrator (Marc.Dapas@nrc.gov)

Deputy Regional Administrator (Kriss.Kennedy@nrc.gov)

DRP Director (Troy.Pruett@nrc.gov)

DRP Deputy Director (Ryan.Lantz@nrc.gov)

DRS Director (Anton.Vegel@nrc.gov)

DRS Deputy Director (Jeff.Clark@nrc.gov)

Senior Resident Inspector (Jeffrey.Sowa@nrc.gov)

Resident Inspector (Andy.Barrett@nrc.gov)

RBS Administrative Assistant (Lisa.Day@nrc.gov)

Branch Chief, DRP/C (Greg.Warnick@nrc.gov)

Senior Project Engineer (Ray.Azua@nrc.gov)

Project Engineer (Michael.Stafford@nrc.gov)

Project Engineer (Paul.Nizov@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

RIV RSLO (Bill.Maier@nrc.gov)

Project Manager (Alan.Wang@nrc.gov)

Team Leader, DRS/TSS (Don.Allen@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

ACES (R4Enforcement.Resource@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Technical Support Assistant (Loretta.Williams@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

RIV Congressional Affairs Officer (Angel.Moreno@nrc.gov)

RIV/ETA: OEDO (Michael.Waters@nrc.gov)

Senior Staff Engineer, TSB (Kent.Howard@nrc.gov)

Enforcement Specialist, OE/EB (Robert.Carpenter@nrc.gov)

Senior Enforcement Specialist, OE/EB (John.Wray@nrc.gov)

Branch Chief, OE (Nick.Hilton@nrc.gov)

Enforcement Coordinator, NRR/DIRS/IPAB/IAET (Lauren.Casey@nrc.gov)

Branch Chief, Operations and Training Branch (Scott.Sloan@nrc.gov)

NRREnforcement.Resource@nrc.gov

RidsOEMailCenterResource

ROPreports

Electronic Distribution via Listserv for River Bend Station

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000458

License: NPF-47

Report: 05000458/2015009

Licensee: Entergy Operations, Inc.

Facility: River Bend Station, Unit 1

Location: 5485 U.S. Highway 61N

St. Francisville, LA 70775

Dates: January 26 through June 29, 2015

Inspectors: T. Hartman, Senior Resident Inspector

D. Bradley, Resident Inspector

J. Drake, Senior Reactor Inspector

Approved By: T. Pruett, Director

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000458/2015009; 01/26/2015 - 06/29/2015; River Bend Station; Special inspection for the

scram with complications that occurred on December 25, 2014.

The report covered one week of onsite inspection and in-office review through June 29, 2015,

by inspectors from the NRCs Region IV office. One preliminary White apparent violation, three

Green non-cited violations, and one Green finding were identified. The significance of most

findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual

Chapter 0609, Significance Determination Process. Findings for which the significance

determination process does not apply may be Green or be assigned a severity level after NRC

management review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4,

dated December 2006.

Cornerstone: Initiating Events

  • Green. The team reviewed a self-revealing, non-cited violation of Technical

Specification 5.4.1.a for the licensees failure to establish adequate procedures to properly

preplan and perform maintenance that affected the performance of the B reactor protection

system motor generator set. Specifically, due to inadequate procedures for troubleshooting

on the B reactor protection system motor generator set, the licensee failed to identify a

degraded capacitor that caused the B reactor protection system motor generator set output

breaker to trip, which resulted in a reactor scram. The licensee entered this issue into their

corrective action program as Condition Report CR-RBS-2014-06605 and replaced the

degraded field flash card capacitor.

This performance deficiency is more than minor, and therefore a finding, because it is

associated with the procedure quality attribute of the Initiating Events Cornerstone and

adversely affected the cornerstone objective to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power operations.

Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination

Process (SDP) for Findings At-Power, Exhibit 1, Initiating Event Screening Questions, this

finding is determined to have a very low safety significance (Green) because the transient

initiator did not contribute to both the likelihood of a reactor trip and the likelihood that

mitigation equipment or functions would not have been available. This finding has an

evaluation cross-cutting aspect within the problem identification and resolution area because

the licensee failed to thoroughly evaluate this issue to ensure that the resolution addressed

the cause commensurate with its safety significance. Specifically, the licensee failed to

thoroughly evaluate the condition of the field flash card to ensure that the cause of the trip

had been correctly identified and corrected prior to returning the B reactor protection system

motor generator set to service [P.2]. (Section 2.7.a)

Cornerstone: Mitigating Systems

  • Green. The team reviewed a self-revealing, non-cited violation of Technical

Specification 5.4.1.a for the licensees failure to establish, implement and maintain a

procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

-2-

Specifically, Procedure OSP-0053, Emergency and Transient Response Support

Procedure, Revision 22, which is required by Regulatory Guide 1.33, inappropriately

directed operations personnel to establish feedwater flow to the reactor pressure vessel

using the startup feedwater regulating valve as part of the post-scram actions. The startup

feedwater regulating valve operator characteristics are non-linear and not designed to

operate in the dynamic conditions immediately following a reactor scram. To correct the

inadequate procedure, the licensee implemented a change to direct operations personnel to

utilize one of the main feedwater regulating valves until the plant is stabilized. This issue

was entered in the licensees corrective action program as Condition

Report CR-RBS-2015-00657.

This performance deficiency is more than minor, and therefore a finding, because it is

associated with the procedure quality attribute of the Mitigating Systems Cornerstone and

adversely affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, the procedure directed operations personnel to isolate the main feedwater

regulating valves and control reactor pressure vessel level using the startup feedwater

regulating valve, whose operator was not designed to function in the dynamic conditions

associated with a post-scram event from high power, and this challenged the capability of

the system. The team performed an initial screening of the finding in accordance with

Inspection Manual Chapter 0609, Appendix A, The Significance Determination

Process (SDP) for Findings At-Power. Using Inspection Manual Chapter 0609, Appendix A,

Exhibit 2, Mitigating Systems Screening Questions, the team determined that the finding is

of very low safety significance (Green) because it: (1) was not a deficiency affecting the

design or qualification of a mitigating structure, system, or component, and did not result in a

loss of operability or functionality; (2) did not represent a loss of system and/or function;

(3) did not represent an actual loss of function of at least a single train for longer than its

technical specification allowed outage time, or two separate safety systems out-of-service

for longer than their technical specification allowed outage time; and (4) did not represent an

actual loss of function of one or more non-technical specification trains of equipment

designated as high safety-significant in accordance with the licensees maintenance rule

program. This finding has an evaluation cross-cutting aspect within the problem

identification and resolution area because the licensee failed to thoroughly evaluate this

issue to ensure that the resolution addressed the cause commensurate with its safety

significance. Specifically, the licensee failed to properly evaluate the design characteristics

of the startup feedwater regulating valve operator before implementing the procedure to use

the valve for post-scram recovery actions [P.2]. (Section 2.7.b)

Criterion XVI, Corrective Action, for the licensees failure to assure a condition adverse to

quality was promptly identified. Specifically, the licensee failed to identify, that reaching the

reactor pressure vessel water Level 8 (high) setpoint, on December 25, 2014, was an

adverse condition, and as a result, failed to enter it into the corrective action program. To

restore compliance, the licensee entered this issue into their corrective action program as

Condition Report CR-RBS-2015-00620 and commenced a causal analysis for Level 8 (high)

trips.

-3-

This performance deficiency is more than minor, and therefore a finding, because it is

associated with the equipment performance attribute of the Mitigating Systems Cornerstone

and adversely affected the cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable consequences.

Specifically, failure to identify Level 8 (high) conditions and unplanned automatic actuations

as conditions adverse to quality, would continue to result in the undesired isolation of

mitigating equipment including reactor feedwater pumps, the high pressure core spray

pump, and the reactor core isolation cooling pump. The team performed an initial screening

of the finding in accordance with Inspection Manual Chapter 0609, Appendix A, The

Significance Determination Process (SDP) for Findings At-Power. Using Inspection Manual

Chapter 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the team

determined that the finding is of very low safety significance (Green) because it: (1) was not

a deficiency affecting the design or qualification of a mitigating structure, system, or

component, and did not result in a loss of operability or functionality; (2) did not represent a

loss of system and/or function; (3) did not represent an actual loss of function of at least a

single train for longer than its technical specification allowed outage time, or two separate

safety systems out-of-service for longer than their technical specification allowed outage

time; and (4) did not represent an actual loss of function of one or more non-technical

specification trains of equipment designated as high safety-significant in accordance with

the licensees maintenance rule program. This finding has an avoid complacency

cross-cutting aspect within the human performance area because the licensee failed to

recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while

expecting successful outcomes. Specifically, the licensee tolerated leakage past the

feedwater regulating valves, did not plan for further degradation, and the condition ultimately

resulted in the Level 8 (high) trip of the running reactor feedwater pump on December 25,

2014 [H.12]. (Section 2.7.c)

Simulators, for the licensees failure to maintain the simulator so it would demonstrate

expected plant response to operator input and to normal, transient, and accident conditions

to which the simulator has been designed to respond. As of January 30, 2015, the licensee

failed to maintain the simulator consistent with actual plant response for normal and

transient conditions related to feedwater flows, alarm response, and behavior of the startup

feedwater regulating valve controller. Specifically, the River Bend Station simulator failed to

correctly model feedwater flows and resulting reactor vessel level response following a

scram, failed to provide the correct alarm response for a loss of a reactor protection system

motor generator set, and failed to correctly model the behavior of the startup feedwater

regulating valve controller. As a result, operations personnel were challenged in their

control of the plant during a reactor scram that occurred on December 25, 2014. This issue

has been entered into the corrective action program as Condition

Report RBS-CR-2015-01261, which includes actions to initiate simulator discrepancy

reports, investigate and resolve the potential fidelity issues, and provide training to

operations personnel on simulator differences.

This performance deficiency is more than minor, and therefore a finding, because it is

associated with the human performance attribute of the Mitigating Systems Cornerstone and

adversely affected the cornerstone objective of ensuring availability, reliability, and capability

-4-

of systems needed to respond to initiating events to prevent undesired consequences.

Specifically, the incorrect simulator response adversely affected the operations personnels

ability to assess plant conditions and take actions in accordance with approved procedures

during the December 25, 2014, scram. The team performed an initial screening of the

finding in accordance with inspection Manual Chapter 0609, Appendix A, The Significance

Determination Process (SDP) for Findings At-Power, Attachment 4, Initial Characterization

of Findings. Using Inspection Manual Chapter 0609, Attachment 4, Table 3, SDP

Appendix Router, the team answered yes to the following question: Does the finding

involve the operator licensing requalification program or simulator fidelity? As a result, the

team used Inspection Manual Chapter 0609, Appendix I, Licensed Operator Requalification

Significance Determination Process (SDP), and preliminarily determined the finding was of

low to moderate safety significance (White) because the deficient simulator performance

negatively impacted operations personnel performance in the actual plant during a

reportable event (reactor scram). This finding has an evaluation cross-cutting aspect within

the problem identification and resolution cross-cutting area because the licensee failed to

thoroughly evaluate this issue to ensure that the resolution addressed the extent of condition

commensurate with its safety significance. Specifically, the licensees evaluation of the

fidelity issue identified by the NRC in March 2014, focused on other training areas that used

simulation, rather than evaluating the simulator modelling for additional fidelity

discrepancies [P.2]. (Section 2.7.d)

  • Green. The team identified a finding for the licensees failure to follow written procedures for

classifying deficient plant conditions as operator workarounds and providing compensatory

measures or training in accordance with fleet Procedure EN-OP-117, Operations

Assessment Resources, Revision 8. A misclassification of these conditions resulted in the

failure of the operations department to fully assess the impact these conditions had during a

plant transient. The failure to identify operator workarounds contributed to complications

experienced during reactor scram recovery on December 25, 2014. The licensee entered

this issue into their corrective action program as Condition Report CR-RBS-2015-00795.

This performance deficiency is more than minor, and therefore a finding, because it had the

potential to lead to a more significant safety concern if left uncorrected. Specifically, the

performance deficiency contributed to complications experienced by the station when

attempting to restore feedwater following a scram on December 25, 2014. The team

performed an initial screening of the finding in accordance with Inspection Manual

Chapter 0609, Appendix A, The Significance Determination Process (SDP) for

Findings At-Power. Using Inspection Manual Chapter 0609, Appendix A, Exhibit 2,

Mitigating Systems Screening Questions, the team determined this finding is of very low

safety significance (Green) because it: (1) was not a deficiency affecting the design or

qualification of a mitigating structure, system, or component, and did not result in a loss of

operability or functionality; (2) did not represent a loss of system and/or function; (3) did not

represent an actual loss of function of at least a single train for longer than its technical

specification allowed outage time, or two separate safety systems out-of-service for longer

than their technical specification allowed outage time; and (4) did not represent an actual

loss of function of one or more non-technical specification trains of equipment designated as

high safety-significant in accordance with the licensees maintenance rule program. This

finding has a consistent process cross-cutting aspect in the area of human performance

-5-

because the licensee failed to use a consistent, systematic approach to making decisions

and failed to incorporate risk insights as appropriate. Specifically, no systematic approach

was enacted in order to properly classify deficient conditions [H.8]. (Section 2.7.e)

-6-

REPORT DETAILS

1. Basis for Special Inspection

On December 25, 2014, at 8:37 a.m., River Bend Station scrammed from 85 percent

power following a trip of the B reactor protection system (RPS) motor generator (MG)

set. At the time of the MG set trip, a Division 1 half scram existed due to an unrelated

equipment issue with a relay for the Number 2 turbine control valve fast closure RPS

function. The combination of the B RPS MG set trip and the Division 1 half scram

resulted in a scram of the reactor.

The following equipment issues occurred during the initial scram response.

  • An unexpected Level 8 (high) reactor water level signal at +51 was received which

resulted in tripping the running reactor feedwater pumps (RFPs).

  • Following reset of the Level 8 (high) reactor water level signal, operations personnel

were unable to start RFP C. They responded by starting RFP A at a vessel level of

+25. The licensee subsequently determined that the circuit breaker (Magne Blast

type) for RFP C did not close.

  • Following the start of RFP A, the licensee attempted to open the startup feedwater

regulating valve (SFRV) but was unsuccessful prior to the Level 3 (low) reactor water

level trip setpoint at +9.7. The licensee then opened main feedwater regulating

valve (FRV) C to restore reactor vessel water level. The lowest level reached

was +8.1. Subsequent troubleshooting revealed a faulty manual function control

card. The card was replaced by the licensee and the SFRV was used on the

subsequent plant startup.

Following restoration of reactor vessel water level, the plant was stabilized in Mode 3. A

plant startup was conducted on December 27, 2014, with RPS bus B being supplied by

its alternate power source. During power ascension following startup, RFP B did not

start. The licensee re-racked its associated circuit breaker and successfully started

RFP B. The licensee did not investigate the cause of RFP B failing to start.

Management Directive 8.3, NRC Incident Investigation Program, was used to evaluate

the level of NRC response for this event. In evaluating the deterministic criteria of

Management Directive 8.3, it was determined that the event: (1) included multiple

failures in the feedwater system which is a short term decay heat removal mitigating

system; (2) involved two Magne Blast circuit breaker issues which could possibly have

generic implications regarding the licensees maintenance, testing, and operating

practices for these components including safety-related breakers in the high pressure

core spray system; and (3) involved several issues related to the ability of operations to

control reactor vessel level between the Level 3 (low) and Level 8 (high) trip setpoints

following a reactor scram. Since the deterministic criteria were met, the trip was

evaluated for risk. The preliminary Estimated Conditional Core Damage Probability was

determined to be 1.2E-6.

-7-

Based on the deterministic criteria and risk insights related to the multiple failures of the

feedwater system, the potential generic concern with the Magne Blast circuit breakers,

and the issues related to the licensees operations departments inability to control

reactor vessel level between the Level 3 (low) and Level 8 (high) setpoints following a

reactor scram, Region IV determined that the appropriate level of NRC response was to

conduct a Special Inspection.

This Special Inspection is chartered to identify the circumstances surrounding this event,

determine if there are adverse generic implications, and review the licensees actions to

address the causes of the event.

The team used NRC Inspection Procedure 93812, Special Inspection Procedure, to

conduct the inspection. The inspections included field walkdowns of equipment,

interviews with station personnel, and reviews of procedures, corrective action

documents, and design documentation. A list of documents reviewed is provided in

Attachment 1 of this report; the Special Inspection Charter is included as Attachment 2.

2. Inspection Results

2.1 Charter Item 2: Develop a complete sequence of events related to the reactor scram

that occurred on December 25, 2014.

a. Inspection Scope

The team developed and evaluated a timeline of the events leading up to, during, and

after the reactor scram. This includes troubleshooting activities and plant startup. The

team developed the timeline, in part, through a review of work orders, action requests,

station logs, and interviews with station personnel. The team created the following

timeline during their review of the events related to the reactor trip that occurred on

December 25, 2014.

Date/Time Activity

December 6, 2014

10:12 a.m. A Division 2 half-scram was received from loss of the

B RPS MG set, licensee initiated Condition

Report CR-RBS-2014-06233

10:17 a.m. The RPS bus B was transferred to the alternate power

supply, Division 2 half-scram was reset

-8-

Date/Time Activity

December 13, 2014

12:35 p.m. The B RPS MG set was restored

December 16, 2014

9:30 p.m. The RPS bus B was placed on B RPS MG set

December 23, 2014

7:59 a.m. The licensee commenced a reactor downpower to

85 percent to support maintenance on RFP B

08:30 a.m. The RFP B was secured to support maintenance

10:28 a.m. A Division 1 half-scram signal from the turbine control

valve 2 fast closure relay was received, licensee initiated

Condition Report CR-RBS-2014-06581

2:21 p.m. The Division 1 half-scram signal was reset by bypassing the

turbine control valve fast closure signal

10:00 p.m. RPS channel A placed in trip condition to satisfy Technical

Specification 3.3.1.1

December 25, 2014

8:37 a.m. Reactor scram due to loss of RPS bus B

8:39 a.m. Feedwater master controller signal caused all FRVs to close,

feedwater continued injecting at 520,000 lbm/hr (leakby

through valves), reactor pressure vessel (RPV) water level at

27.8

8:40 a.m. RFP A was secured per procedure, RPV water level ~ 43,

feedwater flow lowered to 426,400 lbm/hr (leakby through

valves)

-9-

Date/Time Activity

8:41 a.m. Reactor water level reached Level 8 (high) condition, RFP C

(only running RFP) trips

8:42 a.m. All FRVs and associated isolation valves were closed by

operations personnel and the SFRV placed in AUTO with a

setpoint at 18 per procedure

8:45 a.m. Reactor water level dropped below 51 allowing reset of

Level 8 (high) signal and restart of RFPs

8:50 a.m. RFP C failed to start, no trip flags on RFP breaker, RPV

water level ~ 33 and lowering, licensee initiated Condition

Report CR-RBS-2014-06601

8:52 a.m. Operations personnel started RFP A

8:54 a.m. Operations personnel reset the reactor scram signal on

Division 2 of RPS only, RPV water level ~ 17 and lowering

8:54 a.m. The SFRV did not respond as expected in the automatic

mode. Operations personnel attempted to control the SFRV

in Manual, however it did not respond. As a result,

operations personnel began placing the FRV C in service,

licensee initiated Condition Report CR-RBS-2014-06602

8:56 a.m. Water level reached Level 3 (low) and actuated a second

reactor scram signal, RPV water level reached ~ 8.1,

operations personnel completed placing FRV C in service

and reactor water level began to rise

8:57 a.m. RPV water level rose above 9.7, reactor scram signal clear

8:58 a.m. Operations personnel reset the reactor scram signal on

Division 2 of RPS only, RPV water level ~ 15.7

December 27, 2014

12:53 a.m. The plant entered Mode 2 and commenced a reactor startup

-10-

Date/Time Activity

10:00 a.m. RFP C failed to start due to the associated minimum flow

valve not fully opening, licensee initiated Condition

Report CR-RBS-2014-06653

10:18 a.m. Operations personnel started RFP A

5:41 p.m. The plant entered Mode 1

December 28, 2014

7:23 p.m. RFP B failed to start, licensee initiated Condition

Report CR-RBS-2014-06649

8:43 p.m. The RFP B breaker was racked out and then racked back in

8:49 p.m. RFP B was successfully started

b. Findings and Observations

In reviewing the sequence of events and developing the timeline, the team reviewed the

licensees maintenance and troubleshooting activities associated with the B RPS MG set

failure on December 6, 2014. Additionally, the team reviewed the operability

determination to evaluate the licensees basis for returning the B RPS MG set to service.

The licensees troubleshooting practices lacked the technical rigor and attention to detail

necessary to identify and correct the deficient B RPS MG set conditions. On several

occasions, the team noted that the licensee chose the expedient solution rather than

complete an evaluation to determine that corrective actions resolved the deficient

condition. Specifically, the licensee chose to restore the B RPS MG set to service

without fully understanding the failure mechanism. Other examples included the

licensees choice to have operations personnel rack in and out breakers, and have

maintenance personnel manually operate a limit switch, on the makeup and start logic

for the RFP C minimum flow valve, when the RFP did not start. As indicated above, the

licensee performed these compensatory actions instead of evaluating and correcting the

issue.

Based upon a review of the events leading up to the reactor scram, the team determined

the licensee failed to properly preplan and perform maintenance on the B RPS MG set

after the failure that occurred on December 6, 2014. Further discussion involving the

licensees failure to adequately troubleshoot, identify, and correct degraded components

on the B RPS MG set, prior to returning it to service, is included in Section 2.7.a. of this

report.

-11-

Additionally, the team reviewed the procedures that operations personnel used to

respond to the reactor scram and determined the licensee failed to provide adequate

procedures to respond to a post-trip transient. Further discussion on the procedure

prescribing activities affecting quality not being appropriate for the circumstances is

included in Section 2.7.b. of this report.

2.2 Charter Items 3 and 8: Review the licensees root cause analysis and corrective actions

from the current and previous scrams with complications.

a. Inspection Scope

At the time of the inspection, the root cause report for the December 25, 2014, scram

had not been completed. To ensure the licensee was conducting the cause evaluation

at a level of detail commensurate with the significance of the problem, the team

reviewed corrective action procedures, met with members of the root cause team, and

reviewed prior related corrective actions.

The procedures reviewed by the team included quality related Procedure EN-LI-118,

Cause Evaluation Process, Revision 21, and quality related Procedure EN-LI-102,

Corrective Action Program, Revision 24.

The licensees approach for the December 25, 2014, scram causal evaluation was to

use several detailed evaluations as input to the overall root cause. Specifically, the

licensee performed an apparent cause evaluation, under Condition

Report CR-RBS-2014-06696, to understand the failure of Division 2 RPS equipment.

The licensee performed an apparent cause evaluation under Condition

Report CR-RBS-2014-06602, to review the conditions that resulted in the additional

reactor water Level 3 (low) trip, after the initial scram. The licensee also performed an

apparent cause evaluation, under Condition Report CR-RBS-2014-06581, to review the

turbine control valve fast closure circuit failure that resulted in the Division 1 half-scram

signal. All of these evaluations were reviewed under the parent root cause Condition

Report CR-RBS-2014-06605.

The licensee used multiple methods in their causal evaluations that included: event and

causal factor charting, barrier analysis, and organizational and programmatic failure

mode trees. The licensees charter for the root cause evaluation required several

periodic meetings with the members of the different causal analysis teams. It also

required a pre-corrective action review board update and review, a formal corrective

action review board approval, and an external challenge review of the approved root

cause report.

The NRC team also reviewed corrective actions to address complications encountered

during previous reactor scrams. Specifically, the following NRC inspection reports were

reviewed and the related licensee corrective actions were assessed:

-12-

ML070640396

ML12221A233

ML12363A170

b. Findings and Observations

The NRC team found the licensees root cause team members had met the

organizational diversity and experience requirements of their procedures. The team

reviewed the qualifications of the members of the root cause team and determined they

were within the correct periodicity.

At the time of the inspection, there were 4 root cause and 10 apparent cause evaluations

in progress. The team determined the root cause analyses were conducted at a level of

detail commensurate with the significance of the problems.

In reviewing corrective actions for prior scrams, the team noted that there have been five

unplanned reactor scrams in the past five years, including the December 25, 2014,

event. Of those five scrams, two involved Level 8 (high) reactor water level signal trips

of all running feedwater pumps. Based upon a review of prior scrams and associated

corrective actions, the team determined that the licensee does not have an appropriately

low threshold for recognizing Level 8 (high) reactor water level signal trips as an adverse

condition, and entering that adverse condition into their corrective action program.

Otherwise, the team determined that the licensees corrective actions to address

complications, encountered during previous reactor scrams, were adequate. Further

discussion involving the licensees failure to identify Level 8 (high) reactor water level

signal trips as adverse conditions is included in Section 2.7.c of this report.

2.3 Charter Item 4: Determine the cause of the unexpected Level 8 (high) water level trip

signal.

a. Inspection Scope

To determine the cause of the unexpected Level 8 (high) reactor water level trip on

December 25, 2014, the NRC team reviewed control room logs and graphs of key

reactor parameters to assess the plants response to transient conditions. This

information was then compared to the actions taken by operations personnel in the

control room per abnormal and emergency operating procedure requirements.

Section 5.1 of Procedure AOP-0001, Reactor Scram, Revision 30, required operations

personnel to verify that the feedwater system was operating to restore reactor water

level. This was accomplished using an attachment of Procedure OSP-0053,

Emergency and Transient Response Support Procedure, Revision 22. Specifically,

Attachment 16, Post Scram Feedwater/Condensate Manipulations Below 5% Reactor

-13-

Power, required transferring reactor water level control to the startup feedwater system

after reactor water level had been stabilized in the prescribed band.

Only four minutes elapsed from the time of the scram until the time the Level 8 (high)

reactor water level isolation signal was reached. Consequently, operations personnel

did not have sufficient time to gain control and stabilize reactor vessel level in the

required band.

To gain an understanding of issues affecting systems at the time of the scram, the NRC

team met with system engineers for the feedwater system, feedwater level control

system, and remotely operated valves. Discussions with engineering included system

health reports, open corrective actions from condition reports, licensee event reports,

design data for systems, startup testing and exceptions, post-trip reactor water level

setpoint setdown parameters, open engineering change packages, and requirements for

engineering to analyze post-transient plant data.

b. Findings and Observations

Operations personnel responded to the events in accordance with procedure

requirements. The NRC did not identify any performance deficiencies related to

immediate or supplemental actions taken by control room staff during the transient.

However, operations personnel stated that the plant did not respond in a manner

consistent with their simulator training.

Based on review of operations personnel response to the event and the training received

from the simulator, the NRC team determined that the licensee did not maintain the

simulator in a condition that accurately represented actual plant response. On April 10,

2015, the licensee provided a white paper with additional information related to the

modeling of the plant-referenced simulator. Further discussion involving the licensees

failure to maintain the simulator is included in Section 2.7.d of this report.

The NRC team determined that the plant did not respond per the design as described in

the final safety analysis report. Specifically, the feedwater level control system and

feedwater systems were designed to automatically control reactor water level in the

programmed band post-scram. During the December 25, 2014 scram, reactor water

level quickly (within 4 minutes) rose to a Level 8 (high) trip. By design, reactor water

level should rapidly lower after the initial level transient from core void collapse, rise as

feedwater compensates for the level change, and then return to the programed

setpoint. A Level 8 (high) trip should not occur. The team determined that significant

leakage past the feedwater isolation valves caused the rapid rise in reactor water level.

Operations personnel were unable to compensate for the rapid change in reactor vessel

level. The licensee initially discovered the adverse condition during startup testing in

1986, and allowed the condition to degrade without effective corrective actions.

The team noted that significant post-trip or post-transient plant performance data was

available to system engineers, but review of this data was not prioritized by the licensee.

The review of plant transient data was primarily driven by the licensees root cause team

-14-

charter or by self-assigned good engineering practices. At the time of this inspection,

the licensee had not quantified the amount of leakage past the FRVs, although the

scram and subsequent startup had occurred one month earlier. The NRC team

observed that there was a potential to miss important trends in plant performance

without a more timely review.

2.4 Charter Item 5: Review the effectiveness of licensee actions to address known

equipment degradations that could complicate post-scram response by operations

personnel.

a. Inspection Scope

The NRC team reviewed licensee procedures for classifying and addressing plant

conditions that may challenge operations personnel while performing required actions

per procedures during normal and off-normal conditions.

The team reviewed the licensees current list of operator workarounds and operator

burdens. Specifically, the team was looking for any known equipment issues that could

complicate post-scram response by operations personnel.

b. Findings and Observations

The team determined the licensee did not properly classify several deficient plant

conditions as operator workarounds in accordance with fleet Procedure EN-OP-117,

Operations Assessment Resources, Revision 8. Further discussion related to the

failure to classify plant deficiencies as operator workarounds is included in Section 2.7.e

of this report.

2.5 Charter Items 6 and 7: Review the licensees maintenance, testing and operating

practices for Magne Blast circuit breakers including the causes and corrective actions

taken to address the failure of the RFPs to start.

a. Inspection Scope

The team reviewed the final safety analysis report, system description, the current

system health report, selected drawings, maintenance and test procedures, and

condition reports associated with Magne Blast breakers. The team also performed

walkdowns and conducted interviews with system engineering and design engineering

personnel to ensure circuit breakers were capable of performing their design basis

safety functions. Specifically, the team reviewed:

  • Vendor and plant single line, schematic, wiring, and layout drawings
  • Circuit breaker preventive maintenance inspection and testing procedures
  • Vendor installation and maintenance manuals
  • Preventive maintenance and surveillance test procedures
  • Completed surveillance test and preventive maintenance results
  • Corrective actions and modifications

-15-

b. Findings and Observations

Unresolved Item (URI) - Vendor and Industry Recommended Testing Adequacy on

Safety-related and Safety-significant Circuit Breakers

Introduction. The team identified an unresolved item related to the licensees breaker

maintenance and troubleshooting programs for safety-related and safety-significant

circuit breakers. The charter tasked the team with inspecting the issues associated with

Magne Blast breaker problems that occurred during and after the December 25, 2014,

scram. The NRC team determined that breaker maintenance and troubleshooting

practices extended beyond the Magne Blast breakers. The team identified that there

were potential issues with safety-related Master Pact breakers and determined that

maintenance procedures used to ensure that 4160 V and 13.8 kV safety-related and

safety-significant breakers were being maintained and overhauled in a timely manner

may not conform to industry recommended standards.

Description. The team identified that the licensees maintenance programs for Division I,

II, III, and non-safety 4160 V and 13.8 kV breakers installed in the plant may not meet

the standards recommended by the vendor, corporate, or Electric Power Research

Institute (EPRI) guidelines. The licensees programs were based on EPRI

documents TR-106857-V2 and TR-106857-V3, which were preventive maintenance

program bases for low and medium voltage switchgear. However, the licensee

appeared to only implement portions of the recommended maintenance program, and

were not able to provide the team with engineering analyses or technical bases to justify

the changes. The EPRI guidance was developed specifically for Magne Blast breakers

based on industry operating experience, NRC Information Notices, and General Electric

SILs/SALs. The NRC team was concerned that the licensee may not have performed

the entire vendor or EPRI recommended tests, inspections, and refurbishments on the

breakers since they were installed. The aggregate impact of missing these preventive

maintenance tasks needs to be evaluated to determine if the reliability of the affected

breakers has been degraded.

Pending further evaluation of the above issue by the licensee and subsequent review by

NRC inspectors, this issue will be tracked as URI 05000458/2015009-01, Vendor and

Industry Recommended Testing Adequacy on Safety-related and Safety-significant

Circuit Breakers.

2.6 Charter Item 9: Evaluate pertinent industry operating experience and potential

precursors to the event, including the effectiveness of any action taken in response to

the operating experience.

a. Inspection Scope

The team evaluated the licensees application of industry operating experience related to

this event. The team reviewed applicable operating experience and generic NRC

communications with a specific emphasis on Magne Blast breaker maintenance

practices, to assess whether the licensee had appropriately evaluated the notifications

-16-

for relevance to the facility and incorporated applicable lessons learned into station

programs and procedures.

b. Findings and Observations

Other than the URI described in Section 2.5, of this report, no additional findings or

observations were identified.

2.7 Specific findings identified during this inspection.

a. Failure to Establish Adequate Procedures to Perform Maintenance on Equipment that

can Affect Safety-Related Equipment

Introduction. The team reviewed a Green, self-revealing, non-cited violation of Technical

Specification 5.4.1 for the licensees failure to establish adequate procedures to properly

preplan and perform maintenance that affected the performance of the B RPS MG set.

Specifically, due to inadequate procedures for troubleshooting on the B RPS MG set, the

licensee failed to identify a degraded capacitor that caused the B RPS MG set output

breaker to trip, which resulted in a reactor scram.

Description. On December 6, 2014, during normal plant operations, RPS bus B

unexpectedly lost power because of a B RPS MG set failure, which resulted in a

Division 2 half scram and a containment isolation signal. The RPS system is designed

to cause rapid insertion of control rods (scram) to shut down the reactor when specific

variables exceed predetermined limits. The RPS power system, of which the B RPS MG

set is a component, is designed to provide power to the logic system that is part of the

reactor protection system.

The licensees troubleshooting teams identified both the super spike suppressor card

and the field flash card as the possible causes of the B RPS MG set failure. The

licensee replaced the super spike suppressor card. While inspecting the field flash card,

a strand of wire from one of the attached leads was found nearly touching a trace on the

circuit board. A continuity test was performed while the field flash card was being

tapped and no ground was observed. A ground was observed when forcibly pushing

down on the wire. The licensee believed that the wire strand most likely caused the

B RPS MG set trip. The licensee removed the wire strand and re-installed the field flash

card without any further troubleshooting. Operations personnel returned the B RPS MG

set to service on December 16, 2014.

On December 25, 2014, while operating at 85 percent power, a reactor scram occurred

due to a Division 2 RPS trip concurrent with a Division 1 RPS half-scram signal that was

present at the time. The Division 1 half-scram signal was received on December 23,

2014, because of a turbine control valve fast closure signal. Troubleshooting for the

cause of the Division 1 half-scram was ongoing when the Division 2 RPS trip occurred.

This resulted in a full RPS actuation and an automatic reactor scram. Electrical

protection assembly breakers 3B/3D and the B RPS MG set output breaker were found

tripped, similar to the conditions noted following the loss of the B RPS MG set on

December 6, 2014. The subsequent failure modes analysis and troubleshooting teams

-17-

identified the probable cause of the failure of the B RPS MG set output breaker was an

intermittent failure of the field flash card. A more detailed inspection of the field flash

card revealed that a 10 microfarad capacitor had been subjected to minor heating over a

long period of time. As a result, the degraded component contributed to a reactor

scram. The capacitor on the field flash card in the Division 2 RPS MG set was replaced.

Analysis. Failure to establish and implement procedures to perform maintenance to

correct adverse conditions on B RPS MG set equipment that can affect the performance

of the safety-related reactor protection system was a performance deficiency. This

performance deficiency is more than minor, and therefore a finding, because it is

associated with the procedure quality attribute of the Initiating Events Cornerstone and

adversely affected the cornerstone objective to limit the likelihood of events that upset

plant stability and challenge critical safety functions during shutdown as well as power

operations.

The team performed an initial screening of the finding in accordance with Inspection

Manual Chapter (IMC) 0609, Appendix A, The Significance Determination

Process (SDP) for Findings At-Power. Using IMC 0609, Appendix A, Exhibit 1,

Initiating Event Screening Questions, this finding is determined to have very low safety

significance because the transient initiator did not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment or functions would not have been

available. This finding has an evaluation cross-cutting aspect within the problem

identification and resolution area because the licensee failed to thoroughly evaluate the

failure of the B RPS MG set to ensure that the resolution addressed the cause

commensurate with its safety significance. Specifically, the licensee failed to thoroughly

evaluate the condition of the field flash card to ensure that the cause of the trip had been

correctly identified and corrected prior to returning the B MG set to service [P.2].

Enforcement. Technical Specification 5.4.1.a states, in part, that written procedures

shall be established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Regulatory Guide 1.33, Appendix A, Section 9.a., states, in part, that, maintenance that

can affect the performance of safety-related equipment should be properly preplanned

and performed in accordance with written procedures, documented instructions, or

drawings appropriate to the circumstances. Contrary to the above, on December 6,

2014, the licensee failed to establish adequate procedures to properly preplan and

perform maintenance on the B RPS MG set that ultimately affected the performance of

safety-related B RPS equipment. Specifically, due to inadequate procedures for

troubleshooting on the B RPS MG set, the licensee failed to identify a degraded

capacitor on the B RPS MG set that caused its output breaker to trip, prior to returning it

to service. On December 25, 2014, this degraded capacitor caused the B RPS MG set

breaker to trip causing a loss of power to the B RPS bus which resulted in a reactor

scram. The licensee entered this issue into their corrective action program as Condition

Report CR-RBS-2014-06605 and replaced the degraded field flash card capacitor.

Because this finding is determined to be of very low safety significance and has been

entered into the licensees corrective action program this violation is being treated as a

non-cited violation consistent with Section 2.3.2.a of the NRC Enforcement Policy:

-18-

NCV 05000458/2015009-02, Failure to Establish Adequate Procedures to Perform

Maintenance on Equipment that can Affect Safety-Related Equipment.

b. Failure to Provide Adequate Procedures for Post-Scram Recovery

Introduction. The team reviewed a Green, self-revealing, non-cited violation of Technical

Specification 5.4.1.a for the licensees failure to establish, implement and maintain a

procedure required by Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Specifically, Procedure OSP-0053, Emergency and Transient Response Support

Procedure, Revision 22, inappropriately directed operations personnel to establish

feedwater flow to the reactor pressure vessel using the SFRV as part of the post-scram

actions. The SFRV operator characteristics are non-linear and not designed to operate

in the dynamic conditions immediately following a reactor scram from power.

Description. On November 18, 2013, the licensee modified Procedure OSP-0053,

Attachment 16, due to excessive leakage across the main FRVs and verified the

adequacy of the change using the simulator. The licensee did not realize that the

simulator incorrectly modeled the operating characteristics of the SFRV.

On December 25, 2014, following a reactor scram, operations personnel attempted to

implement Procedure OSP-0053, Attachment 16, Post Scram Feedwater/Condensate

Manipulations Below 5% Reactor Power. When the SFRV did not begin to open as

RPV level approached the level setpoint, operations personnel thought the SFRV had

failed in automatic and placed the valve controller in manual. Unknown to operations

personnel, the manual control of the valve was inoperable due to a faulty card. Unable

to control the SFRV, operations personnel then began placing one of the main FRVs

back in service. The isolation valves for the FRV are motor-operated and take

approximately 90 seconds to reposition. Because of the delay in restoring feedwater to

the RPV, a second Level 3 (low) water level reactor scram signal occurred.

The NRC team determined that plant data indicated the SFRV does not open on a

slowly decreasing RPV water level until the controller signal reaches approximately

12.5 percent error or about 3 inches below the RPV water level setpoint on the

controller. The SFRV in the simulator opens as soon as the controller open signal is

greater than 0.0 percent error. When the licensee became aware of the SFRV design

operating parameters, they determined that the SFRV was not designed to respond to

the dynamic conditions that exist during post-scram recovery, and revised

Procedure OSP-0053, Attachment 16, to continue using the main FRVs during

post-scram recovery actions.

Analysis. The licensees failure to provide adequate guidance in Procedure OSP-0053

for post-scram recovery actions was a performance deficiency. This performance

deficiency is more than minor, and therefore a finding, because it is associated with the

procedure quality attribute of the Mitigating Systems Cornerstone and adversely affected

the cornerstone objective to ensure the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Specifically, the

procedural guidance that directed operations personnel to establish feedwater flow to

-19-

the RPV using the SFRV as part of the post-scram actions adversely affected the

capability of the feedwater systems that respond to prevent undesirable consequences.

The system capability was adversely affected since the valve operator characteristics

are non-linear and not designed to operate in the dynamic conditions immediately

following a reactor scram from high power levels.

The team performed an initial screening of the finding in accordance with IMC 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power.

Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the

finding was of very low safety significance (Green) because it: (1) was not a deficiency

affecting the design or qualification of a mitigating structure, system, or component, and

did not result in a loss of operability or functionality; (2) did not represent a loss of

system and/or function; (3) did not represent an actual loss of function of at least a single

train for longer than its technical specification allowed outage time, or two separate

safety systems out-of-service for longer than their technical specification allowed outage

time; and (4) did not represent an actual loss of function of one or more non-technical

specification trains of equipment designated as high safety-significant in accordance with

the licensees maintenance rule program.

This finding has an evaluation cross-cutting aspect within the problem identification and

resolution area because the licensee failed to thoroughly evaluate this issue to ensure

that the resolution addressed the cause commensurate with its safety significance.

Specifically, the licensee failed to properly evaluate the design characteristics of the

SFRV operator before implementing procedural guidance for post-scram recovery

actions [P.2].

Enforcement. Technical Specification 5.4.1.a states, in part, that written procedures

shall be established, implemented, and maintained covering the applicable procedures

recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978.

Regulatory Guide 1.33, Appendix A, Section 6.u., identifies procedures for responding to

a Reactor Trip as required procedures. Procedure OSP-0053, Attachment 16, Post

Scram Feedwater/Condensate Manipulations Below 5% Reactor Power, was a

procedure established by the licensee for responding to a reactor trip. Contrary to the

above, from March 3, 2010, until January 30, 2015, the licensee failed to establish,

implement and maintain Procedure OSP-0053, which directs operator actions for a

reactor trip. Specifically, Procedure OSP-0053 inappropriately directed operations

personnel to establish feedwater flow to the reactor pressure vessel using the SFRV as

part of the post-scram actions. The SFRV operator characteristics are non-linear and

not designed to operate in the dynamic conditions immediately following a reactor scram

from high power. Subsequent to the event, the licensee changed the procedure,

directing operations personnel to utilize one of the main FRVs until the plant was

stabilized. Because this finding is determined to be of very low safety significance and

has been entered into the licensees corrective action program as Condition

Report CR-RBS-2015-00657, this violation is being treated as a non-cited violation

consistent with Section 2.3.2.a of the NRC Enforcement Policy:

NCV 05000458/2015009-03, Failure to Provide Adequate Procedures for Post-scram

Recovery.

-20-

c. Failure to Identify High Reactor Water Level as a Condition Adverse to Quality

Introduction. The team identified a Green, non-cited violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, for the licensees failure to assure a

condition adverse to quality was promptly identified. Specifically, the licensee failed to

identify that reaching the reactor pressure vessel water Level 8 (high) setpoint, on

December 25, 2014, was an adverse condition and enter it into the corrective action

program.

Description. On December 25, 2014, the licensee experienced a scram with

complications. The team reviewed the post-scram report as documented in

Procedure GOP-0003, Scram Recovery, Revision 24. During the scram, the licensee

experienced a Level 8 (high) reactor water condition approximately four minutes after the

scram. This high water level condition should not occur for a scram when main steam

isolation valves remain open and safety relief valves do not actuate.

The team noted that operations personnel followed their training and performed the

required post-scram actions. Those actions did not prevent the overfeeding of the

reactor vessel (which reached the Level 8 (high) setpoint), causing the RFPs to trip off

and would have caused isolation of other emergency core cooling systems, if actuated,

such as high pressure core spray and reactor core isolation cooling. The loss of all

feedwater contributed to the RPV water level lowering to a Level 3 (low) condition that

actuated a second reactor scram signal.

The team interviewed control room operations personnel, system engineers, and

corrective action staff regarding the plants response to the scram. Further, the team

reviewed plant parameter graphs, control room logs, alarm logs, design history, and

licensing basis documents, and determined that excessive leakage past the FRVs

caused the Level 8 (high) trip of all RFPs.

In reviewing the feedwater system data from the December 24, 2014, scram, the

licensee estimated 500,000 lbm/hr leaked past the closed FRVs. This represents

approximately 3 percent of the full-power feedwater flow and significantly exceeds the

design specification for leakage of 135,000-150,000 lbm/hr.

The licensee identified excessive leakage past the FRVs during testing in 1986. At the

time of inspection, the licensee could not produce any corrective actions taken to identify

or correct leakage past the FRVs. Further, the licensee had not quantified the amount of

leakage past the FRVs prior to the December 24, 2014, event and NRC Special

Inspection.

Procedure GOP-0003 provided a post-scram checklist to operations personnel to help

identify equipment and procedure problems that should be corrected prior to the reactor

startup. This document was then reviewed by the Offsite Safety Review Committee in

order to understand and confirm that the plant was safe to restart. Step 1.1 stated the

following:

-21-

Following a reactor scram from high power levels, there is an initial RPV level

Shrink of 20 to 40 inches followed by a Swell of approximately 10 to 20 inches.

The Feedwater Level Control System is programmed to ride out this shrink and

swell without overfilling the RPV.

In section 6.7 of Procedure GOP-003, the licensee documented that there was a control

system trip of RFPs due to reaching Level 8 (high). In section 6.12, however, the

licensee failed to document any off-normal trips (Level 8 (high) feed pump trips). In

Attachment 3 of GOP-003 Procedure, Analysis and Evaluations, Level 8 (high) was

mentioned as part of a timeline discussion but was not listed in the final section labeled

Corrective Actions Required Prior to Returning Unit to Service. This final section was

where condition reports were required for all items listed. By omitting Level 8 (high) from

the discussion, no corrective action document was generated for that condition.

The licensee did not identify that reaching reactor water Level 8 (high) was an adverse

condition. Therefore, the unexpected Level 8 (high) trip was not addressed prior to

startup on December 28, 2014.

The team reviewed the history of Level 8 (high) RFP trips and noted that similar issues

of concern were raised by the NRC in 2012. Specifically, a Supplemental Inspection,

performed in 2012, for a White performance indicator associated with reactor scrams

with complications documented the failure to recognize a Level 8 (high) trip as an

adverse condition and enter it into the corrective action program. This non-cited

violation was documented in NRC Inspection Report 05000458/2012012.

The team determined that the licensee did not have a sufficiently low threshold for

entering issues into their corrective action program for reactor water level transients.

Specifically, long-standing equipment issues associated with FRV leakage has led to the

licensee reaching reactor water Level 8 (high) during two reactor scrams in a three-year

period.

Analysis. The failure to identify Level 8 (high) reactor water level trips as adverse

conditions was a performance deficiency. This performance deficiency is more than

minor, and therefore a finding, because it is associated with the equipment performance

attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, failure to identify

Level 8 (high) conditions and resulting actuations as conditions adverse to quality, would

continue to result in the undesired isolation of mitigating equipment including RFPs, the

high pressure core spray pump, and the reactor core isolation cooling pump.

The team performed an initial screening of the finding in accordance with IMC 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power.

Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the

finding was of very low safety significance (Green) because it: (1) was not a deficiency

affecting the design or qualification of a mitigating structure, system, or component, and

did not result in a loss of operability or functionality; (2) did not represent a loss of

-22-

system and/or function; (3) did not represent an actual loss of function of at least a single

train for longer than its technical specification allowed outage time, or two separate

safety systems out-of-service for longer than their technical specification allowed outage

time; and (4) did not represent an actual loss of function of one or more non-technical

specification trains of equipment designated as high safety-significant in accordance with

the licensees maintenance rule program.

This finding has an avoid complacency cross-cutting aspect within the human

performance area because the licensee failed to recognize and plan for the possibility of

mistakes, latent issues, and inherent risk, even while expecting successful outcomes.

Specifically, the licensee tolerated excessive leakage past the FRVs, did not plan for

further degradation, and the condition ultimately resulted in the Level 8 (high) trip of the

running RFP on December 25, 2014 [H.12].

Enforcement. Title 10 of the Code of Federal Regulations, Part 50, Appendix B,

Criterion XVI, Corrective Action, requires, in part, that measures shall be established to

assure that conditions adverse to quality, such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and non-conformances are promptly

identified and corrected. Contrary to the above, from December 25, 2014, to

January 29, 2015, the licensee failed to assure that a condition adverse to quality was

promptly identified. Specifically, the licensee failed to identify that reaching the reactor

pressure vessel water Level 8 (high) setpoint, on December 25, 2014, was an adverse

condition and enter it into the corrective action program. To restore compliance, the

licensee entered this issue into their corrective action program as Condition

Report CR-RBS-2015-00620 to perform a causal analysis for Level 8 (high) trips. Since

the violation was of very low safety significance (Green), this violation is being treated as

a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy:

NCV 05000458/2015009-04, Failure to Identify High Reactor Water Level as a

Condition Adverse to Quality.

d. Failure of the Plant-Referenced Simulator to Demonstrate Expected Plant Response

Introduction. The team identified an apparent violation of 10 CFR 55.46(c)(1), Plant-

Referenced Simulators, for the licensees failure to maintain the simulator so it would

demonstrate expected plant response to operator input and to normal, transient, and

accident conditions to which the simulator has been designed to respond. As of

January 30, 2015, the licensee failed to maintain the simulator consistent with actual

plant response for normal and transient conditions related to feedwater flows, alarm

response, and behavior of the SFRV controller. As a result, operations personnel were

challenged in their control of the plant during a reactor scram that occurred on

December 25, 2014.

Description. On December 25, 2014, River Bend Station was operating at 85 percent

power when a reactor scram occurred. On January 26, 2015, a Special Inspection was

initiated in response to this event. The Special Inspection team reviewed the event and

identified several simulator fidelity issues. Licensee Procedure EN-TQ-202, Simulator

Configuration Control, Revision 9, provided the process requirements necessary to

-23-

satisfy the guidelines for simulator testing, performance, and configuration control

specified by ANSI/ANS-3.5-2009. Standard ANSI/ANS-3.5-2009, Nuclear Power Plant

Simulators for Use in Operator Training and Examination, provides the simulator testing

requirements, as well as simulator configuration management to ensure simulator

fidelity. Specifically, as of January 30, 2015, the River Bend Station simulator failed to

model feedwater accurately and failed to model resulting reactor vessel level response

following a scram, failed to provide the correct alarm response for a loss of a RPS MG

set, and failed to correctly model the behavior of the SFRV controller. The simulator

modeling discrepancies and how these discrepancies affected plant response during the

plant trip are discussed below:

  • The licensee stated their simulator modeled zero leakage across the FRV rather

than the actual leakage in the plant. General Electric record 0247.230-000-016,

Feedwater Control Valve Assembly - Purchase Specification, described the

total design leakage across all the FRVs was approximately 135,000 lbm/hr.

This is equal to approximately 1.1 percent full feedwater flow. The flow rate

across the FRVs measured in the plant on December 25, 2014, was

approximately 500,000 lbm/hr, which is approximately 3 percent full feedwater

flow. The rate of level change of the reactor vessel in the plant was larger than

operations personnel anticipated based on training received in the simulator.

ANSI/ANS-3.5-2009, Section 4.1.4(3), states, The simulator shall not fail to

cause an alarm or automatic action if the reference unit would have caused an

alarm or automatic action under identical circumstances. In this case, the

simulator under similar conditions did not reach the RPV water Level 8 (high)

condition and trip the RFPs, when the actual plant did.

  • The licensees simulator did not correctly model all alarms that would be received

on a loss of power to the RPS. ANSI/ANS-3.5-2009, Section 4.1.4(3),

states, The simulator shall not fail to cause an alarm or automatic action if the

reference unit would have caused an alarm or automatic action under identical

circumstances. Although the licensee had identified this discrepancy on

December 11, 2014, and implemented a correction in the simulator model,

operations personnel had not received training nor were they notified of the

discrepancy. As a result, during the plant scram on December 25, 2014, the

alarms for drywell high pressure and RPV high pressure annunciated per the

facility design, operations personnel were not expecting the alarms because they

did not alarm in the simulator during training.

  • The simulator SFRV responded differently than the actual SFRV in the reference

plant. ANSI/ANS-3.5-2009, Section 4.1.4(2) [for malfunctions], stated, Any

observable change in simulated parameters corresponds in direction to the

change expected from actual or best estimate response of the reference unit to

the malfunction. Plant data indicated the SFRV does not open on a slowly

decreasing RPV water level until the controller signal reaches approximately

12.5 percent or about 3 inches below the RPV water level setpoint of the

controller. The SFRV in the simulator opens as soon as the controller open

signal is greater than 0.0. Because the SFRV did not respond as expected,

-24-

operations personnel incorrectly believed the SFRV had failed in automatic

operation and placed the controller in manual. Due to an unrelated issue, the

manual function of the SFRV was unavailable.

Collectively, these modeling discrepancies negatively impacted licensed operations

personnel performance in the actual control room, during the event of December 25,

2014. Specifically, operations personnel were not able to control reactor vessel water

level during the reactor scram.

The team noted that the licensee similarly stated in Condition Report

CR-RBS-2015-00641 that, During an investigation into the report at the OSRC (Onsite

Safety Review Committee) for the SCRAM on December 25, 2014, that feed regulating

valve leakage (FRV) contributed to the Level 8 received reactor vessel, it was

determined by analysis that there is sufficient evidence that leakage by the Feedwater

Regulating Valves presents a significant challenge to Operations during a scram event.

On April 10, 2015, the licensee provided a white paper with additional information related

to the modeling of the plant-referenced simulator. Specifically, it provided the licensees

perspective with regard to the following issues raised by the NRC:

1. Two unexpected alarms on loss of Division II Reactor Protection System Power

2. Main Feedwater Regulating Valve Seat Leakage

3. Start-up Feedwater Regulating Valve Response

The licensee concluded that although they perceived that there were differences

between the simulator and the actual plant, they were considered to be minor. For each

of the items in question, the paper summarized that operator performance was not

impacted by simulator modeling. The team considered the information in the white

paper, and disagreed with the licensees conclusions. Some of the information provided,

however, did improve the teams understanding of the modeling deficiencies.

Analysis. The failure to maintain the plant-referenced simulator so that it would

demonstrate expected plant response to operator input and to normal and transient

conditions was a performance deficiency. This performance deficiency is more than

minor, and therefore a finding, because it is associated with the human performance

attribute of the Mitigating Systems Cornerstone and adversely affected the objective of

ensuring availability, reliability, and capability of systems needed to respond to initiating

events to prevent undesired consequences. Specifically, the incorrect simulator

response adversely affected the operating crews ability to assess plant conditions and

take actions in accordance with approved procedures during the December 25, 2014,

scram.

The team performed an initial screening of the finding in accordance with IMC 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power,

Attachment 4, Initial Characterization of Findings. Using IMC 0609, Attachment 4,

Table 3, SDP Appendix Router, the team answered yes to the following question:

Does the finding involve the operator licensing requalification program or simulator

-25-

fidelity? As a result, the team used IMC 0609, Appendix I, Licensed Operator

Requalification Significance Determination Process (SDP), and preliminarily determined

the finding was of low to moderate safety significance (White) because the deficient

simulator performance negatively impacted operations personnel performance in the

actual plant during a reportable event. This modeling deficiency resulted in actual

impact on operations personnel performance during response to a reactor scram that

occurred on December 25, 2014.

The NRC recently issued a non-cited violation related to simulator fidelity in March 2014

documented in Inspection Report 05000458/2014301. Since the licensee recently

verified simulator fidelity, this issue is indicative of current plant performance and has an

evaluation cross-cutting aspect within the problem identification and resolution area

because the licensee failed to thoroughly evaluate this issue to ensure that the

resolution addressed the extent of condition commensurate with its safety significance.

Specifically, the licensees evaluation of the fidelity issue focused on other training areas

that used simulation, rather than evaluating the simulator modelling for additional fidelity

discrepancies [P.2].

Enforcement. Title 10 of the Code of Federal Regulations, Part 55.46(c)(1), Plant-

Referenced Simulators, requires in part, that a simulator must demonstrate expected

plant response to operator input and to normal, transient, and accident conditions to

which the simulator has been designed to respond.

Contrary to the above, as of January 30, 2015, the simulator failed to demonstrate

expected plant response to operator input and to normal, transient, and accident

conditions to which the simulator has been designed to respond. Specifically, the River

Bend Station simulator failed to correctly model leakage flow rates across the FRVs;

failed to provide the correct alarm response for a loss of a RPS MG set; and failed to

correctly model the behavior of the SFRV controller. These simulator modeling issues

led to negative training of operators. This subsequently complicated the operators

response to a reactor scram in the actual plant on December 25, 2014. This issue has

been entered into the corrective action program as Condition Report

CR-RBS-2015-01261. The licensees condition report included actions to initiate

simulator discrepancy reports, to investigate and resolve the potential fidelity issues, and

to provide training to operations personnel on simulator differences. This is a violation of

10 CFR 55.46(c)(1), Plant-Referenced Simulators: AV 05000458/2015009-05, Failure

of the Plant-Referenced Simulator to Demonstrate Expected Plant Response.

e. Failure to Identify and Classify Operator Workarounds that Impacted Scram Recovery

Actions

Introduction. The team identified a Green finding for the licensees failure to follow

written procedures for classifying deficient plant conditions as operator workarounds and

providing compensatory measures or training in accordance with fleet

Procedure EN-OP-117. A misclassification of these conditions resulted in the failure of

the operations department to fully assess the impact these conditions had during a plant

-26-

transient. The failure to identify operator workarounds contributed to complications

experienced during reactor scram recovery on December 25, 2014.

Description. The team reviewed the recovery actions taken by the main control room

staff following the reactor scram on December 25, 2014, from 85 percent power. During

the review, the team observed the station had zero conditions identified as operator

workarounds. The team reviewed fleet Procedure EN-FAP-OP-006, Operator

Aggregate Impact Index Performance Indicator, Revision 2. This procedure defined an

operator workaround as:

Any plant condition (equipment or other) that would require compensatory

operator actions in the execution of normal operating procedures, abnormal

operating procedures, emergency operating procedures, or annunciator

response procedures during off-normal conditions. This indicator provided a

measure of plant safety. It provided a measure of the likelihood that a plant

transient may be complicated by equipment and human performance problems.

During their review, the team identified the following three conditions which met the

definition of an operator workaround as described in Procedure EN-FAP-OP-006, and

which were in effect prior to the December 25, 2014, event:

  • Work Order WO-RBS-00404323: RFP B supply breaker repetitive failures to

close potentially reduces the number of feedwater pumps available to operations

personnel during a transient following reactor pressure vessel water

Level 8 (high). Operations personnel would rack out and then rack the breaker

back in until the breaker would function properly. This work order was initiated

on February 3, 2015, following discussions with the NRC inspection team.

  • Work Order WO-RBS-00396449: RFP C minimum flow valve does not stroke

fully open which prevents starting the C feed pump. Maintenance personnel

would manually operate a limit switch on the valve to make up the start logic for

the RFP. This work order was initiated on October 10, 2014.

  • Work Order WO-RBS-00346642: leakage past FRVs when closed complicated

post-scram reactor water level control. Operations personnel proceduralized the

closure of the main feedwater isolation valves to stop the effect of the leakage.

This work order was initiated on March 27, 2013.

The deficient conditions in WO-RBS-00346642 and WO-RBS-00396449 contributed to

complications experienced by the station when attempting to restore feedwater following

a scram and loss of all feedwater pumps on a reactor pressure vessel water

Level 8 (high).

Fleet Procedure EN-OP-117, Attachment 9.4, Operator Aggregate Assessment of Plant

Deficiencies, provides a method to assess and document the impact of plant

deficiencies on operations personnel response during off-normal and emergency

conditions. In order to assess the cumulative impact of outstanding operator aggregate

-27-

impact deficiencies, several deficiency types were evaluated, including operator

workarounds. Following assessment of deficiencies, Attachment 9.4, step 5, directed

the station to provide compensatory measures or training as appropriate until the

deficiencies could be corrected.

The resident inspectors engaged operations department management in January 2015,

and informed the licensee that the three conditions appeared to meet the definition of an

operator workaround as described in Procedure EN-FAP-OP-006. Upon learning of the

misclassification of these issues, the station revised their operator aggregate index on

February 6, 2015, to account for the three operator workaround conditions and the

indicator turned red. As a result, the station issued guidance for post-scram reactor

water level control and required operating crews to attend simulator training on vessel

level control and feedwater system recovery following a Level 8 (high) trip of feedwater

pumps. Additionally, the station wrote Condition Report CR-RBS-2015-00795 to

document the issue.

Analysis. The failure to follow written procedures for classifying deficient plant

conditions as operator workarounds and providing compensatory measures or training in

accordance with fleet Procedure EN-OP-117 was a performance deficiency. This

performance deficiency is more than minor, and therefore a finding, because it had the

potential to lead to a more significant safety concern if left uncorrected. Specifically, the

performance deficiency contributed to complications experienced by the station when

attempting to restore feedwater following a scram on December 25, 2014.

The team performed an initial screening of the finding in accordance with IMC 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power.

Using IMC 0609, Appendix A, Exhibit 2, Mitigating Systems Screening Questions, the

finding was of very low safety significance (Green) because it: (1) was not a deficiency

affecting the design or qualification of a mitigating structure, system, or component, and

did not result in a loss of operability or functionality; (2) did not represent a loss of

system and/or function; (3) did not represent an actual loss of function of at least a single

train for longer than its technical specification allowed outage time, or two separate

safety systems out-of-service for longer than their technical specification allowed outage

time; and (4) did not represent an actual loss of function of one or more non-technical

specification trains of equipment designated as high safety-significant in accordance with

the licensees maintenance rule program.

This finding has a consistent process cross-cutting aspect within the human

performance area because the licensee failed to use a consistent, systematic approach

to making decisions and incorporate risk insights as appropriate. Specifically, no

systematic approach was enacted in order to properly classify deficient conditions [H.8].

Enforcement. Enforcement action does not apply because the performance deficiency

did not involve a violation of regulatory requirements. Because this finding does not

involve a violation and is of very low safety significance, this issue was entered into the

licensees corrective action program as Condition Report CR-RBS-2015-00795: FIN

-28-

05000458/2015001-06, Failure to Identify and Classify Operator Workarounds That

Impacted Scram Recovery Actions.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On January 20, 2015, the team initially debriefed Mr. E. Olson, Site Vice President, and other

members of the licensee's staff. The licensee representatives acknowledged the findings

presented.

On June 29, 2015, the team conducted an exit briefing with Mr. E. Olson, Site Vice President,

and other members of the licensees staff. The licensee representatives acknowledged the

findings presented.

-29-

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

E. Olson, Site Vice President

D. Bergstrom, Senior Operations Instructor

M. Browning, Senior Operations Instructor

T. Brumfield, Director, Regulatory & Performance Improvement

S. Carter, Manager, Shift Operations

M. Chase, Manager, Training

J. Clark, Manager, Regulatory Assurance

F. Corley, Manager, Design & Program Engineering

T. Creekbaum, Engineer

G. Degraw, Manager, Training

G. Dempsey, Senior Operations Instructor

S. Durbin, Superintendent, Operations Training

R. Gadbois, General Manager, Plant Operations

T. Gates, Manager, Operations Support

J. Henderson, Assistant Manager, Operations

K. Huffstatler, Senior Licensing Specialist, Licensing

K. Jelks, Engineering Supervisor

G. Krause, Assistant Manager, Operations

T. Laporte, Senior Staff Operations Instructor

R. Leasure, Superintendent, Radiation Protection

P. Lucky, Manager, Performance Improvement

J. Maher, Manager, Systems & Components Engineering

W. Mashburn, Director, Engineering

W. Renz, Director, Emergency Planning, Entergy South

J. Reynolds, Senior Manager, Maintenance

T. Shenk, Manager, Operations

T. Schenk, Manager, Operations

S. Vazquez, Director, Engineering

D. Williamson, Senior Licensing Specialist

D. Yoes, Manager, Quality Assurance

NRC Personnel

G. Warnick, Branch Chief

J. Sowa, Senior Resident Inspector

R. Deese, Senior Reactor Analyst

A1-1 Attachment 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000458/2015009-01 URI Vendor and Industry Recommended Testing Adequacy on

Safety-related and Safety-significant Circuit Breakers

(Section 2.5.b)

Opened and Closed

05000458/2015009-02 NCV Failure to Establish Adequate Procedures to Perform

Maintenance on Equipment that can Affect Safety-Related

Equipment (Section 2.7.a)05000458/2015009-03 NCV Failure to Provide Adequate Procedures for Post-scram

Recovery (Section 2.7.b)05000458/2015009-04 NCV Failure to Identify High Reactor Water Level as a Condition

Adverse to Quality (Section 2.7.c)05000458/2015009-05 AV Failure of the Plant-Referenced Simulator to Demonstrate

Expected Plant Response (Section 2.7.d)05000458/2015009-06 FIN Failure to Identify and Classify Operator Workarounds that

Impacted Scram Recovery Actions (Section 2.7.e)

LIST OF DOCUMENTS REVIEWED

DRAWINGS

NUMBER TITLE REVISION

GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System 34

Sheet 7

GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System 33

Sheet 8

GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System 31

Sheet 10

GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System 30

Sheet 11

GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System 30

Sheet 12

GE-828E445AA, Elementary Diagram - Nuclear Steam Supply Shutoff System 37

Sheet 15

GE-944E981 Elementary Diagram - RPS MG Set Control System 11

A1-2

DRAWINGS

NUMBER TITLE REVISION

PID-25-01A Engineering P&I Diagram - System 051, Nuclear Boiling 19

Instrumentation

PID-25-01B Engineering P&I Diagram - System 051, Nuclear Boiling 7

Instrumentation

828E531AA, Elementary Diagram - Reactor Protection System 25

Sheet 4

828E531AA, Elementary Diagram - Reactor Protection System 22

Sheet 4A

828E531AA, Elementary Diagram - Reactor Protection System 27

Sheet 6

PROCEDURES

NUMBER TITLE REVISION

AOP-0001 Reactor Scram 30

AOP-0003 Automatic Isolations 33

AOP-0006 Condensate/Feedwater Failures 19

AOP-0010 Loss of One RPS Bus 19

EN-FAP-OM-004 Fleet and Site Business Plan Process 0

EN-FAP-OM-012 Prompt Investigation, Notifications and Duty Manager 6

Responsibilities

EN-FAP-OP-006 Operator Aggregate Impact Index Performance Indicator 2

EN-LI-102 Corrective Action Program 24

EN-LI-118 Cause Evaluation Process 21

EN-MA-125 Troubleshooting Control of Maintenance Activities 17

EN-OP-104 Operability Determination Process 7

EN-OP-115 Conduct of Operations 15

EN-OP-117 Operations Assessment Resources 8

EN-OP-115-09 Log Keeping 1

EN-TQ-202 Simulator Configuration Control 9

EOP-0001 RPV Control 26

EOP-0003 Secondary Containment and Radioactive Release Control 16

A1-3

PROCEDURES

NUMBER TITLE REVISION

EPSTG-0001 Emergency Operating and Severe Accident Procedures - Plant 16

Specific Technical Guidelines (PSTG)

EPSTG-0002 EPGs/SAGs to PSTG to EOP/SAP Flowcharts Comparison 16

EPSTG-0002, Emergency Operating and Severe Accident Procedures - 16

Appendix B Bases

GOP-0001 Plant Startup 83

GOP-0002 Plant Shutdown 70

GOP-0003 Scram Recovery for December 27, 2014 24

OSP-0001 Control of Operator Aids 13

OSP-0053 Emergency and Transient Response Support Procedure 22

CONDITION REPORTS

CR-RBS-1998-00384 CR-RBS-2002-00672 CR-RBS-2002-00688 CR-RBS-2006-04078

CR-RBS-2011-02209 CR-RBS-2011-09053 CR-RBS-2012-02249 CR-RBS-2012-03434

CR-RBS-2012-03439 CR-RBS-2012-03440 CR-RBS-2012-03665 CR-RBS-2012-03739

CR-RBS-2012-03816 CR-RBS-2012-03817 CR-RBS-2012-05894 CR-RBS-2012-06015

CR-RBS-2012-07249 CR-RBS-2012-07250 CR-RBS-2012-07251 CR-RBS-2012-07253

CR-RBS-2012-07254 CR-RBS-2013-04419 CR-RBS-2014-05200 CR-RBS-2014-05209

CR-RBS-2014-06233 CR-RBS-2014-06357 CR-RBS-2014-06561 CR-RBS-2014-06581

CR-RBS-2014-06602 CR-RBS-2014-06605 CR-RBS-2014-06649 CR-RBS-2014-06696

CR-RBS-2015-00030 CR-RBS-2015-00043 CR-RBS-2015-00153 CR-RBS-2015-00318

CR-RBS-2015-00365 CR-RBS-2015-00480 CR-RBS-2015-00482 CR-RBS-2015-00483

CR-RBS-2015-00484 CR-RBS-2015-00486 CR-RBS-2015-00487 CR-RBS-2015-00579

CR-RBS-2015-00620 CR-RBS-2015-00626 CR-RBS-2015-00641 CR-RBS-2015-00657

CR-RBS-2015-00795 CR-RBS-2015-01261 CR-RBS-2015-02810

WORK ORDERS

WO-RBS-00346642 WO-RBS-00396449 WO-RBS-00401085 WO-RBS-00404323

A1-4

MISCELLANEOUS DOCUMENT

NUMBER TITLE REVISION /

DATE

EC 50374 Engineering Change - Feedwater Level Control Setpoint 0

Setdown Modification

EN-LI-100-ATT- Process Applicability Determination Form for AOP-0001, August 6,

9.1 Reactor Scram, Revision 24 2007

LI-101 50.59 Review Form for GOP-0002, Power Decrease/Plant August 26,

Shutdown, Revision 30 2004

GE-22A3778 Feedwater Control System (Motor Driven Feed Pumps) 4

Design Specification

GE-22A3778AB Feedwater Control System (Motor Driven Feed Pumps) 7

Design Specification Data Sheet

RLP-LOP-0511 Licensed Operator Requalification - Industry August 1,

Events/Operating Experience and Plant Modifications 2002

1-ST-27-TC6 Startup Procedure and Results - Turbine Trip and Generator June 27,

Load Reject 1986

107-Feedwater System Health Report - Feedwater Q2 2014

0247.230-000-16 Feedwater Control Valve Assembly - Purchase Specifications 301

List of Actuations/Isolations That Occur From Loss of RPS January 29,

Bus B 2015

Main Control Room Log December 6,

2014

Main Control Room Log December 13,

2014

Main Control Room Log December 16,

2014

Main Control Room Log December 27,

2014

Main Control Room Log December 28,

2014

A1-5

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION IV

1600 E LAMAR BLVD

ARLINGTON, TX 76011-4511

January 15, 2015

MEMORANDUM TO: Tom Hartman, Senior Resident Inspector

Reactor Projects Branch B

Division of Reactor Projects

FROM: Troy Pruett, Director /RA/

Division of Reactor Projects

SUBJECT: SPECIAL INSPECTION CHARTER TO EVALUATE CAUSES OF THE

UNPLANNED REACTOR TRIP WITH COMPLICATIONS AT THE

RIVER BEND STATION

In response to the unplanned reactor trip with complications at the River Bend Station, a special

inspection will be performed. You are hereby designated as the special inspection team leader.

The following members are assigned to your team:

  • Jim Drake, Senior Reactor Inspector, Division of Reactor Safety
  • Dan Bradley, Resident Inspector, Division of Reactor Projects

A. Basis

On December 25, 2014, at 8:37 AM, River Bend Station scrammed from 85 percent power

following a trip of the B reactor protection system (RPS) motor generator (MG) set. At the

time of the MG set trip, a Division 1 half scram existed due to an unrelated equipment

issue with a relay for the No. 2 turbine control valve fast closure RPS function. The

combination of the B RPS MG set trip and the Division 1 half scram resulted in a scram of

the reactor.

The following equipment issues occurred during the initial scram response.

  • An unexpected Level 8 (high) reactor water level signal was received which resulted in

tripping of all RFPs.

  • Following reset of the Level 8 high reactor water level signal, plant operators were

unable to start RFP C. Plant operators responded by starting RFP A at a vessel level

of 25. The licensee subsequently determined that the circuit breaker (Magne Blast

type) for RFP C did not close because an interlock lever for a microswitch that controls

the breaker close permissive was not fully engaged in the cubicle.

  • Following the start of RFP A, the licensee attempted to open the startup feed

regulating valve but was unsuccessful prior the Level 3 low reactor water level trip

setpoint at +9.7. The licensee then opened the C main feedwater regulating valve to

A2-1 Attachment 2

restore reactor vessel water level. The lowest level reached was +7.5. Subsequent

troubleshooting revealed a faulty manual function control card. The card was

replaced by the licensee and the startup feedwater regulating valve was used on the

subsequent plant startup.

Following restoration of reactor vessel water level, the plant was stabilized in Mode 3. A

plant startup was conducted on December 27, 2014 with RPS bus B being supplied by

its alternate power source. During power ascension following startup, RFP B did not

start. The licensee re-racked its associated circuit breaker and successfully started

RFP B.

Management Directive 8.3, NRC Incident Investigation Program, was used to evaluate

the level of NRC response for this event. In evaluating the deterministic criteria of

MD 8.3, it was determined that: (1) The event included multiple failures in the feedwater

system which is a short term decay heat removal mitigating system; (2) involved two

Magna Blast circuit breaker issues which could possibly have generic implications

regarding the licensees maintenance, testing, and operating practices for these

components including safety-related breakers in the high pressure core spray system;

and, (3) involved several issues related to the ability of operations to control reactor vessel

level between the Level 3 low and Level 8 high trip set points following a reactor scram.

Since the deterministic criteria was met, the trip was evaluated for risk. The preliminary

Estimated Conditional Core Damage Probability was determined to be 1.2E-6.

Based on the deterministic criteria and risk insights related to the multiple failures of the

feedwater system, the potential generic concern with the Magna Blast circuit breakers,

and the issues related to the licensees Operations departments inability to control reactor

vessel level between the Level 3 and Level 8 setpoints following a reactor scram, Region

IV determined that the appropriate level of NRC response was to conduct a Special

Inspection.

This Special Inspection is chartered to identify the circumstances surrounding this event,

determine if there are adverse generic implications, and review the licensees actions to

address the causes of the event.

B. Scope

The inspection is expected to perform data gathering and fact-finding in order to address

the following:

1. Provide a recommendation to Region IV management as to whether the

inspection should be upgraded to an augmented inspection team response. This

recommendation should be provided by the end of the first day on site.

2. Develop a complete sequence of events related to the reactor scram that

occurred on December 25, 2014. The chronology should include the events

leading to the reactor scram, the licensees immediate scram response and the

licensees post-scram recovery actions including troubleshooting and reactor

startup.

A2-2

3. Review the licensees root cause analysis and determine if it is being conducted

at a level of detail commensurate with the significance of the problem.

4. Determine the causes for the unexpected Level 8 high water level trip signal that

was experienced following the reactor scram.

5. Review the effectiveness of licensee actions to address known equipment

degradations that could complicate post scram operator response.

6. Review the causes and corrective actions taken to address the failure of RFP C

to start during the initial scram response and RFP B during the subsequent

reactor startup. For issues related to Magne Blast circuit breakers, verify that the

licensees corrective actions have addressed extent of condition and extent of

cause.

7. Review the licensees maintenance, testing and operating practices for Magne

Blast circuit breakers. Promptly communicate any potential generic issues to

regional management.

8. Review the licensees corrective actions to address complications encountered

during previous reactor scrams. Reference previously docketed correspondence

regarding complicated reactor scrams in NRC inspection reports

05000458/2002002, 05000458/2006013, 05000458/2012009 and

05000458/2012012.

9. Evaluate pertinent industry operating experience and potential precursors to the

event, including the effectiveness of any action taken in response to the

operating experience.

10. Collect data necessary to support completion of the significance determination

process.

C. Guidance

Inspection Procedure 93812, "Special Inspection," provides additional guidance to be

used by the Special Inspection Team. Your duties will be as described in Inspection

Procedure 93812. The inspection should emphasize fact-finding in its review of the

circumstances surrounding the event. It is not the responsibility of the team to examine

A2-3

the regulatory process. Safety concerns identified that are not directly related to the

event should be reported to the Region IV office for appropriate action.

You will formally begin the special inspection with an entrance meeting to be conducted

no later than January 26, 2015. You should provide a daily briefing to Region IV

management during the course of your inspections and prior to your exit meeting. A

report documenting the results of the inspection should be issued within 45 days of the

completion of the inspection.

This Charter may be modified should you develop significant new information that

warrants review. Should you have any questions concerning this Charter, contact

Jeremy Groom at (817) 200-1144.

cc via E-mail:

M. Dapas

K. Kennedy

T. Pruett

A. Vegel

J. Clark

V. Dricks

W. Maier

J. Groom

J. Sowa

R. Azua

N. Taylor

T. Hartman

J. Drake

D. Bradley

ADAMS ACCESSION NUMBER ML15015A634

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials JRG

Publicly Avail Yes No Sensitive Yes No Sens. Type Initials JRG

Keyword MD 3.4/A.7

RIV/DRP: BC RIV/DRP: DIR

JRGroom TWPruett

/RA/RAzua for /RA/

1/15/15 1/15/15

OFFICIAL RECORD

A2-4