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{{#Wiki_filter:CATEGORY 3y REGULA ORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9703070191 DOC.DATE: 97/03/03 NOTARIZED:
{{#Wiki_filter:CATEGORY 3y REGULA ORY INFORMATION DISTRIBUTION SYSTEM           (RIDS)
NO FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION VERRILLI,M.
ACCESSION NBR:9703070191           DOC.DATE: 97/03/03         NOTARIZED: NO         DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina                 05000400 AUTH. NAME           AUTHOR AFFILIATION VERRILLI,M.         Carolina Power & Light Co.
Carolina Power&Light Co.DONAHUE,J.iv.
DONAHUE,J.iv.       Carolina Power     &   Light Co.
Carolina Power&Light Co.RECIP.NAME RECIPIENT AFFILIATION DOCKET 05000400 E 05000400 NOTES:Application for permit renewal filed.
RECIP.NAME           RECIPIENT AFFILIATION


==SUBJECT:==
==SUBJECT:==
LER 97-001-00:on 970131,automatic reactor tripped resulting from SG low-low level.Caused by inadvertent closure of MFIV (1FW-159)&faulty hydraulic relays.Shuttle valves replaced, SG level discrepancy investigated.W/970303 ltr.DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.RECIPIENT ID CODE/NAME PD2-1 PD INTERNAL: ACRS AEOD/SPD/RRAB NRR/DE/ECGB NRR/DE/EMEB NRR/DRCH/HICB NRR/DRCH/HQMB NRR/DSSA/SPLB RES/DET/EIB EXTERNAL: L ST LOBBY WARD NOAC POORE,W.NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME~E(N AE/+PD/RAB ILE CENTE@N~RR" DE/EEI B NRR/DRCH/HHFB NRR/DRCH/HOLB NRR/DRPM/PECB NRR/DSSA/SRXB RGN2 FILE 01 LITCO BRYCE,J H NOAC QUEENER,DS NUDOCS FULL TXT COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 D E NOTE TO ALL"RIDS" RECIPIENTS:
LER   97-001-00:on 970131,automatic reactor tripped resulting from SG low-low level. Caused by inadvertent closure of MFIV (1FW-159) & faulty hydraulic relays. Shuttle valves replaced, SG level discrepancy       investigated.W/970303       ltr.
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL 25'
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR                   ENCL     SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.                           E NOTES:Application for permit renewal          filed.                              05000400 RECIPIENT          COPIES              RECIPIENT           COPIES ID CODE/NAME        LTTR ENCL          ID   CODE/NAME     LTTR ENCL PD2-1   PD               1    1      ~E(N                    1    1 INTERNAL: ACRS                       1    1      AE    /+PD/RAB          2    2 AEOD/SPD/RRAB             1    1        ILE CENTE@            1    1 NRR/DE/ECGB               1    1      N~RR" DE/EEI B          1    1 NRR/DE/EMEB               1    1      NRR/DRCH/HHFB          1    1 NRR/DRCH/HICB            1     1       NRR/DRCH/HOLB          1    1 NRR/DRCH/HQMB            1    1      NRR/DRPM/PECB           1    1 NRR/DSSA/SPLB            1     1       NRR/DSSA/SRXB          1     1 D
RES/DET/EIB              1     1       RGN2      FILE  01    1     1 EXTERNAL: L ST LOBBY WARD            1     1       LITCO BRYCE,J      H    1     1 NOAC POORE,W.            1     1       NOAC QUEENER,DS        1     1 NRC PDR                  1     1       NUDOCS FULL TXT        1     1 E
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED 25  '
TOTAL NUMBER OF COPIES REQUIRED: LTTR               25   ENCL


Carolina Power 8 light Company Harris NucIear Plant PO Box 165 New Hill NC 27562 MAR 8 1997 U.S.Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 Serial: HNP-97-033 10CFR50.73 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO.50-400 LICENSE NO.NPF-63 LICENSEE EVENT REPORT 97-001-00 Sir or Madam: In accordance with Title JO to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted.
Carolina Power 8 light Company Harris NucIear Plant PO Box 165 New Hill NC 27562 MAR     8 1997 U.S. Nuclear Regulatory Commission                                                         Serial: HNP-97-033 ATTN: NRC Document Control Desk                                                                     10CFR50.73 Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 97-001-00 Sir or Madam:
This report describes a reactor trip which occurred during routine surveillance testing when a main feedwater isolation valve unexpectedly stroked shut.Sincerely, J.W.Donahue Director of Site Operations Harris Plant MV Enclosure c: Mr.J.B.Brady (HNP Senior NRC Resident)Mr.L.A.Reyes (NRC Regional Administrator, Region II)Mr.N.B.Le (NRC-NRR Project Manager)/(p1 9703070191 970303 PDR ADOCK 05000400 S PDR IIIIIIIIIItllllll[lllltliilitllHllllllll State Road 1134 New Hill NC C
In accordance with Title JO to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted.     This report describes a reactor trip which occurred during routine surveillance testing when a main feedwater isolation valve unexpectedly stroked shut.
NRC FORM 366 H.95I U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)APPROVED BY OMB NO.3150.0104 EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY Wlnl THLV MANDATORY UIFORMATION COLLECTION REDUEST: 500 HRS.REPORTED LESSONS LEARNED ARE'ICORPORATEO UITO THE UCENSING PROCESS ANO FEO BACK TO UIDUSTRY.FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION ANO RECORDS MANAGEMENt BRANCH IT4I F331, US.NUCLEAR REGULATORY COMMISSION, WASHINGtON.
Sincerely, J. W. Donahue Director of Site Operations Harris Plant MV Enclosure c:       Mr. J. B. Brady (HNP Senior NRC Resident)
OC 20555OSI.ANO t0 THE PAPERWORK REDUCTION PROJECT l3150.DIOLL OFFICE OF MANAGEMENt ANO BUDGET, WASHUIGTON, OC 20503.FACIUTY NAME tll Harris Nuclear Plant Unit-1 DOCKET NUMBER I2I 50-400 PAGE I3)1 OF 2 TITLE I4I Reactor Trip on low-low S/G level due to inadvertent closure of a Main Feedwater Isolation Valve (1FW-159).
Mr. L. A. Reyes (NRC Regional Administrator, Region II)
EVENT DATE (5)LER NUMBER (6)REPORT DATE (7)OTHER FACILITIES INVOLVED (8)MONTH OAY 01 31 YEAR 97 SEQUENTIAL REVISION NUMBER NUMBER 97-001-0 MOIITH DAY YEAR 3 3 97 FACILITY NAME FACIUTY NAME DOCKET NUMBER DOCKET NUMBER 05000 OPERATING MODE (9)POWER LEVEL (10)97o SUANT TO THE REQUIREMENTS OF 10 CFR B: (Check one o THIS REPORT IS SUBMITTED PUR 50.73(a)(2)(i)50.73(a)(2)(ii)20.2203(a)(2)(v) 20.2203(a)
                                                                                                            /  (p1 Mr. N. B. Le (NRC - NRR Project Manager) 9703070191        970303 PDR     ADOCK     05000400 S                       PDR IIIIIIIIIItllllll[lllltliilitllHllllllll State Road 1134     New Hill NC
(3)(i)20.2201(b) 20.2203(a)
 
(1)20.2203la)(2)(i)20.2203(a)(2)(ii)20.2203(a)(2)(iii) 20.2203(a)
C NRC FORM 366                                 U.S. NUCLEAR REGULATORY COMMISSION                               APPROVED BY OMB NO. 3150.0104 H.95I                                                                                                                      EXPIRES     04/30/98 ESTIMATED BURDEN PER RESPONSE           TO COMPLY Wlnl THLV MANDATORY UIFORMATION COLLECTION REDUEST: 500 HRS. REPORTED LESSONS LEARNED LICENSEE EVENT REPORT                        (LER)                                        UITO THE UCENSING PROCESS ANO FEO BACK TO UIDUSTRY.
(2)(iv)20.2203(a)
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION ANO ARE'ICORPORATEO RECORDS MANAGEMENt BRANCH IT4I F331, US. NUCLEAR REGULATORY COMMISSION, (See reverse for required number of                                    WASHINGtON. OC 20555OSI. ANO t0 THE PAPERWORK REDUCTION PROJECT l3150.
(3)(ii)20.2203(a)(4) 50.36(c)(l) 50.36(c)(2) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii)r more)(11)50.73(a)(2)(viii) 50.73(a)(2)(x) 73.71 OTHER Specify in Abstrect below or in NRC Form 306A NAME LICENSEE CONTACT FOR THIS LER (12)TELEPHONE NUM 8 FR (Iridvde Ares Code)Michael Vettilli Sr.Analyst-Licensing (919)362-2303 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TQ NPROS:::4+k;Q.Ke CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS SJ ISV B350 Y ris YS SUPPLEMENTAL REPORT EXPECTED (14)YES (If yes, complete EXPECTED SUBMISSION DATE).X NO EXPECTED SUBMISSION DATE (15)MONTH QAY YEAR ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single.spaced typewritten lines)(16)On January 31, 1997, with the plant operating in Mode 1 at 97%power, an automatic reactor trip resulted from steam generator low-low level in the"A" Steam Generator (S/G).This trip occurred while performing quarterly surveillance testing on the Main Feedwater and Main Steam Isolation Valves (Operations Surveillance Test, OST-1018).
digits/characters for each block)                                  DIOLL OFFICE OF MANAGEMENt ANO BUDGET, WASHUIGTON, OC 20503.
During this testing, the Main Feedwater Isolation valve to the"A" S/G (1FW-159)was taken to the TEST position which should have caused the valve to stroke in the closed direction to the 90%open position.However, 1FW-159 stroked fully shut causing a decrease in feed flow and S/G level.The reactor operator performing the surveillance test in the main control room recognized that 1FW-159 had fully shut and attempted to restore feedwater flow the S/G by taking the control switch for 1FW-159 to the SHUT/RESET position and then holding the control switch in the OPEN position.The"A" feedwater regulating valve was also fully opened to increase feed flow.1FW-159 would not re-open, thus resulting in a continued decrease m"A" S/G level.A locally stationed auxiliary operator reported that 1FW-159 opened approximately 2-3 inches then re-shut several times.Based on these conditions, the Unit Semor Control Operator commenced a load reduction to reduce steam demand and made plans to manually trip the reactor if S/G level decreased to 40%.(S/G low low level reactor trip setpoint is 38.5%)At 0438 hours, with lowest main control board indicated S/G level at approximately 44%, an automatic S/G low-low level reactor trip occurred.Due to the shrink in S/G levels, The Auxiliary Feedwater system started as required.All support systems functioned as required except for the pressurizer bank-A backup heater supply breaker, which tripped open after approximately ten minutes of operation.
FACIUTY NAME   tll                                                                             DOCKET NUMBER I2I                                        PAGE I3)
The plant was then stabilized in Mode-3 (Hot Standby).This event was caused by faulty hydraulic relays (solenoid operated shuttle valves)that control the position of IFW-159.Investigation revealed that the shuttle valve's o-ring seals were leaking by which prevented proper hydraulic operation.
Harris Nuclear Plant Unit-1                                                                           50-400                               1 OF 2 TITLE I4I Reactor Trip on low-low S/G level due to inadvertent closure of a Main Feedwater Isolation Valve (1FW-159).
I Corrective actions included replacing the shuttle valves and satisfactorily testing 1FW-159, troubleshooting the pressurizer heater su 1 breaker and investi attn the a arent steam encrator level discre anc.
EVENT DATE (5)                     LER NUMBER (6)               REPORT DATE (7)                             OTHER FACILITIES INVOLVED (8)
NRC FORM 366A I4 95I LICENSEE EVENT REPORT (LEB)TEXT CONTINUATION U.S.NUCLEAR REGUUITORY COMMISSION FACILITY NAME (II Shearon Harris Nuclear Plant~Unit rII1 TEXT AY mort spooo it roOoirsd.oso oddiIFoool oopios of iVRC Form 3664I IITI OOCKET 50400 LER NUMBER (6I YEAR SEOUENTIAL REVISION NUMBER NUMBER 97-001-00 PAGE LT)2 OF 2 EVENT DESCRIPTION:
FACILITY NAME                                  DOCKET NUMBER SEQUENTIAL    REVISION MONTH       OAY       YEAR                                         MOIITH     DAY     YEAR NUMBER      NUMBER FACIUTY NAME                                    DOCKET NUMBER 01        31        97        97      001              0        3         3       97                                                             05000 OPERATING                   THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR B: (Check one o r more) (11)
On January 31, 1997, with the plant operating in Mode 1 at 97%power, an automatic reactor trip resulted from Steam Generator low-low level in the"A" Steam Generator (S/G).This trip occurred while performing quarterly surveillance testing on the Main Feedwater and Main Steam Isolation Valves (Operations Surveillance Test, OST-1018).During this testing, the Main Feedwater Isolation valve to the"A" S/G (1FW-159, EIIS Code:SJ-ISV) was taken to the TEST position which should have caused the valve to stroke in the closed direction to the 90%open position.However, 1FW-159 stroked fully shut causing a decrease in feed flow and S/G level.The reactor operator performing the surveillance test in the main control room recognized that 1FW-159 had fully shut and attempted to restore feedwater flow the S/G by taking the control switch for 1FW-159 to the SHUT/RESET position and then holding the control switch in the OPEN position.The"A" feedwater regulating valve was also fully opened to increase feed flow.1FW-159 would not re-open, thus resulting in a continued decrease in"A" S/G level.A locally stationed auxiliary operator reported that 1FW-159 opened approximately 2-3 inches then re-shut several times.Based on these conditions, the Unit Senior Control Operator commenced a load reduction to reduce steam demand and made plans to manually trip the reactor if S/G level decreased to 40%.(S/G low low level reactor trip setpoint is 38.5%)At 0438 hours, with lowest main control board indicated S/G level at approximately 44%, an automatic S/G low-low level reactor trip occurred.The turbine tripped as expected on Turbine Trip/Reactor Trip P4 and due to the shrink in S/G levels, both motor-driven Auxiliary Feedwater (AFW)pumps and the turbine-driven AFW pump started as required.All support systems functioned as required.The pressurizer bank-A backup heater supply breaker tripped open after approximately ten minutes of operation, but the remaining banks of pressurizer heaters restored pressurizer pressure to its normal band.The plant was then stabilized and maintained in Mode-3 (Hot Standby)to allow investigation into the reactor trip.CAUSE: This event was caused by faulty hydraulic relays (solenoid operated shuttle valves)that control the position of 1FW-159.Investigation revealed that the shuttle valve's o-ring seals were leaking by which prevented proper hydraulic operation.
MODE (9)                       20.2201(b)                     20.2203(a)(2)(v)                         50.73(a) (2) (i)                       50.73(a)(2)(viii)
POWER                        20.2203(a) (1)                 20.2203(a) (3) (i)                       50.73(a)(2) (ii)                       50.73(a)(2)(x)
LEVEL (10) 97o          20.2203la)(2) (i)             20.2203(a) (3) (ii)                     50.73(a)(2)(iii)                       73.71 20.2203(a)(2) (ii)             20.2203(a)(4)                           50.73(a)(2)(iv)                         OTHER 20.2203(a)(2)(iii)             50.36(c)(l)                             50.73(a)(2)(v)                     Specify in Abstrect below or in NRC Form 306A 20.2203(a) (2)(iv)             50.36(c)(2)                             50. 73(a) (2) (vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME                                                                                                  TELEPHONE  NUM 8 FR (Iridvde Ares Code)
Michael Vettilli Sr. Analyst - Licensing                                                                        (919) 362-2303 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
REPORTABLE                                                                                    REPORTABLE CAUSE         SYSTEM       COMPONENT       MANUFACTURER                               CAUSE        SYSTEM        COMPONENT        MANUFACTURER TQ NPROS                                                                                      TO NPROS
:::4+k;Q. Ke SJ             ISV             B350           Y       ris YS SUPPLEMENTAL REPORT EXPECTED (14)                                                                             MONTH        QAY        YEAR EXPECTED YES                                                                                                       SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE).                             X     NO                           DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single. spaced typewritten lines) (16)
On January 31, 1997, with the plant operating in Mode 1 at 97% power, an automatic reactor trip resulted from steam generator low-low level in the "A" Steam Generator (S/G). This trip occurred while performing quarterly surveillance testing on the Main Feedwater and Main Steam Isolation Valves (Operations Surveillance Test, OST-1018). During this testing, the Main Feedwater Isolation valve to the "A" S/G (1FW-159) was taken to the TEST position which should have caused the valve to stroke in the closed direction to the 90% open position. However, 1FW-159 stroked fully shut causing a decrease in feed flow and S/G level. The reactor operator performing the surveillance test in the main control room recognized that 1FW-159 had fully shut and attempted to restore feedwater flow the S/G by taking the control switch for 1FW-159 to the SHUT/RESET position and then holding the control switch in the OPEN position. The "A" feedwater regulating valve was also fully opened to increase feed flow. 1FW-159 would not re-open, thus resulting in a continued decrease m "A" S/G level. A locally stationed auxiliary operator reported that 1FW-159 opened approximately 2-3 inches then re-shut several times. Based on these conditions, the Unit Semor Control Operator commenced a load reduction to reduce steam demand and made plans to manually trip the reactor if S/G level decreased to 40%. (S/G low low level reactor trip setpoint is 38.5%) At 0438 hours, with lowest main control board indicated S/G level at approximately 44%,
an automatic S/G low-low level reactor trip occurred. Due to the shrink in S/G levels, The Auxiliary Feedwater system started as required. All support systems functioned as required except for the pressurizer bank-A backup heater supply breaker, which tripped open after approximately ten minutes of operation. The plant was then stabilized in Mode-3 (Hot Standby).
This event was caused by faulty hydraulic relays (solenoid operated shuttle valves) that control the position of IFW-159.
Investigation revealed that the shuttle valve's o-ring seals were leaking by which prevented proper hydraulic operation.
I Corrective actions included replacing the shuttle valves and satisfactorily testing 1FW-159, troubleshooting the pressurizer heater su       1   breaker and investi attn the a arent steam encrator level discre anc .
 
NRC FORM 366A                                                                                                                           U.S. NUCLEAR REGUUITORY COMMISSION I4 95I LICENSEE EVENT REPORT (LEB)
TEXT CONTINUATION FACILITY NAME     (II                                 OOCKET                  LER NUMBER (6I                    PAGE LT)
SEOUENTIAL        REVISION YEAR NUMBER          NUMBER Shearon Harris Nuclear Plant              ~
Unit rII1                   50400                                                2    OF    2 97  -      001      -      00 TEXT AY mort spooo it roOoirsd. oso oddiIFoool oopios of iVRC Form 3664I IITI EVENT DESCRIPTION:
On January 31, 1997, with the plant operating in Mode 1 at 97% power, an automatic reactor trip resulted from Steam Generator low-low level in the "A" Steam Generator (S/G). This trip occurred while performing quarterly surveillance testing on the Main Feedwater and Main Steam Isolation Valves (Operations Surveillance Test, OST-1018). During this testing, the Main Feedwater Isolation valve to the "A" S/G (1FW-159, EIIS Code:SJ-ISV) was taken to the TEST position which should have caused the valve to stroke in the closed direction to the 90% open position. However, 1FW-159 stroked fully shut causing a decrease in feed flow and S/G level. The reactor operator performing the surveillance test in the main control room recognized that 1FW-159 had fully shut and attempted to restore feedwater flow the S/G by taking the control switch for 1FW-159 to the SHUT/RESET position and then holding the control switch in the OPEN position. The "A" feedwater regulating valve was also fully opened to increase feed flow. 1FW-159 would not re-open, thus resulting in a continued decrease in "A" S/G level. A locally stationed auxiliary operator reported that 1FW-159 opened approximately                                       2-3 inches then     re-shut     several times. Based on these conditions, the Unit Senior Control Operator commenced a load                                       reduction   to reduce   steam     demand and made plans to manually trip the reactor if                             S/G   level decreased to 40%. (S/G   low low level reactor   trip   setpoint   is 38.5%)
At 0438 hours, with lowest main control board indicated S/G level at approximately 44%, an automatic S/G low-low level reactor trip occurred. The turbine tripped as expected on Turbine Trip/Reactor Trip P4 and due to the shrink in S/G levels, both motor-driven Auxiliary Feedwater (AFW) pumps and the turbine-driven AFW pump started as required. All support systems functioned as required. The pressurizer bank-A backup heater supply breaker tripped open after approximately ten minutes of operation, but the remaining banks of pressurizer heaters restored pressurizer pressure to its normal band. The plant was then stabilized and maintained in Mode-3 (Hot Standby) to allow investigation into the reactor trip.
CAUSE:
This event was caused by faulty hydraulic relays (solenoid operated shuttle valves) that control the position of 1FW-159. Investigation revealed that the shuttle valve's o-ring seals were leaking by which prevented proper hydraulic operation.
SAFETY SIGNIFICANCE:
SAFETY SIGNIFICANCE:
There were no adverse safety consequences associated with this event.With the exception of the pressurizer bank A backup heater supply breaker trip described above, all systems functioned as required to stabilize the reactor in Hot Standby.This is being reported per 10CFR50.73.a.2.iv as an unplanned Reactor Protection System/Engineered Safety Feature actuation.
There were no adverse safety consequences associated with this event. With the exception of the pressurizer bank A backup heater supply breaker trip described above, all systems functioned as required to stabilize the reactor in Hot Standby.
PREVIOUS SIMILAR EVENTS: There have been no previous reactor trips reported that were caused by faulty Main Feedwater Isolation valve solenoid operated shuttle valves.CORRECTIVE ACTIONS COMPLETED:
This is being reported per 10CFR50.73.a.2.iv                                     as an unplanned Reactor Protection System         / Engineered Safety Feature actuation.
1.The solenoid operated shuttle valves for 1FW-159 were replaced and 1FW-159 was satisfactorily tested on February 1, 1997.2.Troubleshooting was performed to determine the cause of the pressurizer bank-A backup heater supply breaker trip, but was inconclusive.
PREVIOUS SIMILAR EVENTS:
A malfunctioning test switch was found and was replaced on February 1, 1997.3.A review of archived plant process computer data was performed to investigate the apparent discrepancy between S/G levels last olserved in the main control room and the low-low S/G level reactor trip setpoint of 38.5%.However, due to the computer data point 10 second update rate, an accurate level value at the time of the reactor trip could not be verified.The"A" S/G level channels were checked to determine if,a calibration problem existed.No abnormalities were found and each of the channels were within the expected tolerance.
There have been no previous reactor trips reported that were caused by faulty Main Feedwater Isolation valve solenoid operated shuttle valves.
CORRECTIVE ACTIONS COMPLETED:
: 1.         The solenoid operated shuttle valves for 1FW-159 were replaced and 1FW-159 was satisfactorily tested on February 1, 1997.
: 2.           Troubleshooting was performed to determine the cause of the pressurizer bank-A backup heater supply breaker trip, but was inconclusive. A malfunctioning test switch was found and was replaced on February 1, 1997.
: 3.           A review of archived plant process computer data was performed to investigate the apparent discrepancy between S/G levels last olserved in the main control room and the low-low S/G level reactor trip setpoint of 38.5%. However, due to the computer data point 10 second update rate, an accurate level value at the time of the reactor trip could not be verified. The "A" S/G level channels were checked to determine if,a calibration problem existed. No abnormalities were found and each of the channels were within the expected tolerance.
These actions were completed on January 31, 1997.}}
These actions were completed on January 31, 1997.}}

Latest revision as of 04:55, 22 October 2019

LER 97-001-00:on 970131,automatic Reactor Tripped Resulting from SG low-low Level.Caused by Inadvertent Closure of Mfiv (1FW-159) & Faulty Hydraulic Relays.Shuttle Valves Replaced, SG Level Discrepancy investigated.W/970303 Ltr
ML18012A543
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 03/03/1997
From: Donahue J, Verrilli M
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
HNP-97-033, HNP-97-33, LER-97-001-01, LER-97-1-1, NUDOCS 9703070191
Download: ML18012A543 (6)


Text

CATEGORY 3y REGULA ORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9703070191 DOC.DATE: 97/03/03 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME AUTHOR AFFILIATION VERRILLI,M. Carolina Power & Light Co.

DONAHUE,J.iv. Carolina Power & Light Co.

RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

LER 97-001-00:on 970131,automatic reactor tripped resulting from SG low-low level. Caused by inadvertent closure of MFIV (1FW-159) & faulty hydraulic relays. Shuttle valves replaced, SG level discrepancy investigated.W/970303 ltr.

DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:

TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc. E NOTES:Application for permit renewal filed. 05000400 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-1 PD 1 1 ~E(N 1 1 INTERNAL: ACRS 1 1 AE /+PD/RAB 2 2 AEOD/SPD/RRAB 1 1 ILE CENTE@ 1 1 NRR/DE/ECGB 1 1 N~RR" DE/EEI B 1 1 NRR/DE/EMEB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRCH/HQMB 1 1 NRR/DRPM/PECB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 D

RES/DET/EIB 1 1 RGN2 FILE 01 1 1 EXTERNAL: L ST LOBBY WARD 1 1 LITCO BRYCE,J H 1 1 NOAC POORE,W. 1 1 NOAC QUEENER,DS 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 E

NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN SD-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

FULL TEXT CONVERSION REQUIRED 25 '

TOTAL NUMBER OF COPIES REQUIRED: LTTR 25 ENCL

Carolina Power 8 light Company Harris NucIear Plant PO Box 165 New Hill NC 27562 MAR 8 1997 U.S. Nuclear Regulatory Commission Serial: HNP-97-033 ATTN: NRC Document Control Desk 10CFR50.73 Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 97-001-00 Sir or Madam:

In accordance with Title JO to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report describes a reactor trip which occurred during routine surveillance testing when a main feedwater isolation valve unexpectedly stroked shut.

Sincerely, J. W. Donahue Director of Site Operations Harris Plant MV Enclosure c: Mr. J. B. Brady (HNP Senior NRC Resident)

Mr. L. A. Reyes (NRC Regional Administrator, Region II)

/ (p1 Mr. N. B. Le (NRC - NRR Project Manager) 9703070191 970303 PDR ADOCK 05000400 S PDR IIIIIIIIIItllllll[lllltliilitllHllllllll State Road 1134 New Hill NC

C NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150.0104 H.95I EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY Wlnl THLV MANDATORY UIFORMATION COLLECTION REDUEST: 500 HRS. REPORTED LESSONS LEARNED LICENSEE EVENT REPORT (LER) UITO THE UCENSING PROCESS ANO FEO BACK TO UIDUSTRY.

FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION ANO ARE'ICORPORATEO RECORDS MANAGEMENt BRANCH IT4I F331, US. NUCLEAR REGULATORY COMMISSION, (See reverse for required number of WASHINGtON. OC 20555OSI. ANO t0 THE PAPERWORK REDUCTION PROJECT l3150.

digits/characters for each block) DIOLL OFFICE OF MANAGEMENt ANO BUDGET, WASHUIGTON, OC 20503.

FACIUTY NAME tll DOCKET NUMBER I2I PAGE I3)

Harris Nuclear Plant Unit-1 50-400 1 OF 2 TITLE I4I Reactor Trip on low-low S/G level due to inadvertent closure of a Main Feedwater Isolation Valve (1FW-159).

EVENT DATE (5) LER NUMBER (6) REPORT DATE (7) OTHER FACILITIES INVOLVED (8)

FACILITY NAME DOCKET NUMBER SEQUENTIAL REVISION MONTH OAY YEAR MOIITH DAY YEAR NUMBER NUMBER FACIUTY NAME DOCKET NUMBER 01 31 97 97 001 0 3 3 97 05000 OPERATING THIS REPORT IS SUBMITTED PUR SUANT TO THE REQUIREMENTS OF 10 CFR B: (Check one o r more) (11)

MODE (9) 20.2201(b) 20.2203(a)(2)(v) 50.73(a) (2) (i) 50.73(a)(2)(viii)

POWER 20.2203(a) (1) 20.2203(a) (3) (i) 50.73(a)(2) (ii) 50.73(a)(2)(x)

LEVEL (10) 97o 20.2203la)(2) (i) 20.2203(a) (3) (ii) 50.73(a)(2)(iii) 73.71 20.2203(a)(2) (ii) 20.2203(a)(4) 50.73(a)(2)(iv) OTHER 20.2203(a)(2)(iii) 50.36(c)(l) 50.73(a)(2)(v) Specify in Abstrect below or in NRC Form 306A 20.2203(a) (2)(iv) 50.36(c)(2) 50. 73(a) (2) (vii)

LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUM 8 FR (Iridvde Ares Code)

Michael Vettilli Sr. Analyst - Licensing (919) 362-2303 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

REPORTABLE REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER CAUSE SYSTEM COMPONENT MANUFACTURER TQ NPROS TO NPROS

4+k;Q. Ke SJ ISV B350 Y ris YS SUPPLEMENTAL REPORT EXPECTED (14) MONTH QAY YEAR EXPECTED YES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). X NO DATE (15)

ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single. spaced typewritten lines) (16)

On January 31, 1997, with the plant operating in Mode 1 at 97% power, an automatic reactor trip resulted from steam generator low-low level in the "A" Steam Generator (S/G). This trip occurred while performing quarterly surveillance testing on the Main Feedwater and Main Steam Isolation Valves (Operations Surveillance Test, OST-1018). During this testing, the Main Feedwater Isolation valve to the "A" S/G (1FW-159) was taken to the TEST position which should have caused the valve to stroke in the closed direction to the 90% open position. However, 1FW-159 stroked fully shut causing a decrease in feed flow and S/G level. The reactor operator performing the surveillance test in the main control room recognized that 1FW-159 had fully shut and attempted to restore feedwater flow the S/G by taking the control switch for 1FW-159 to the SHUT/RESET position and then holding the control switch in the OPEN position. The "A" feedwater regulating valve was also fully opened to increase feed flow. 1FW-159 would not re-open, thus resulting in a continued decrease m "A" S/G level. A locally stationed auxiliary operator reported that 1FW-159 opened approximately 2-3 inches then re-shut several times. Based on these conditions, the Unit Semor Control Operator commenced a load reduction to reduce steam demand and made plans to manually trip the reactor if S/G level decreased to 40%. (S/G low low level reactor trip setpoint is 38.5%) At 0438 hours0.00507 days <br />0.122 hours <br />7.242063e-4 weeks <br />1.66659e-4 months <br />, with lowest main control board indicated S/G level at approximately 44%,

an automatic S/G low-low level reactor trip occurred. Due to the shrink in S/G levels, The Auxiliary Feedwater system started as required. All support systems functioned as required except for the pressurizer bank-A backup heater supply breaker, which tripped open after approximately ten minutes of operation. The plant was then stabilized in Mode-3 (Hot Standby).

This event was caused by faulty hydraulic relays (solenoid operated shuttle valves) that control the position of IFW-159.

Investigation revealed that the shuttle valve's o-ring seals were leaking by which prevented proper hydraulic operation.

I Corrective actions included replacing the shuttle valves and satisfactorily testing 1FW-159, troubleshooting the pressurizer heater su 1 breaker and investi attn the a arent steam encrator level discre anc .

NRC FORM 366A U.S. NUCLEAR REGUUITORY COMMISSION I4 95I LICENSEE EVENT REPORT (LEB)

TEXT CONTINUATION FACILITY NAME (II OOCKET LER NUMBER (6I PAGE LT)

SEOUENTIAL REVISION YEAR NUMBER NUMBER Shearon Harris Nuclear Plant ~

Unit rII1 50400 2 OF 2 97 - 001 - 00 TEXT AY mort spooo it roOoirsd. oso oddiIFoool oopios of iVRC Form 3664I IITI EVENT DESCRIPTION:

On January 31, 1997, with the plant operating in Mode 1 at 97% power, an automatic reactor trip resulted from Steam Generator low-low level in the "A" Steam Generator (S/G). This trip occurred while performing quarterly surveillance testing on the Main Feedwater and Main Steam Isolation Valves (Operations Surveillance Test, OST-1018). During this testing, the Main Feedwater Isolation valve to the "A" S/G (1FW-159, EIIS Code:SJ-ISV) was taken to the TEST position which should have caused the valve to stroke in the closed direction to the 90% open position. However, 1FW-159 stroked fully shut causing a decrease in feed flow and S/G level. The reactor operator performing the surveillance test in the main control room recognized that 1FW-159 had fully shut and attempted to restore feedwater flow the S/G by taking the control switch for 1FW-159 to the SHUT/RESET position and then holding the control switch in the OPEN position. The "A" feedwater regulating valve was also fully opened to increase feed flow. 1FW-159 would not re-open, thus resulting in a continued decrease in "A" S/G level. A locally stationed auxiliary operator reported that 1FW-159 opened approximately 2-3 inches then re-shut several times. Based on these conditions, the Unit Senior Control Operator commenced a load reduction to reduce steam demand and made plans to manually trip the reactor if S/G level decreased to 40%. (S/G low low level reactor trip setpoint is 38.5%)

At 0438 hours0.00507 days <br />0.122 hours <br />7.242063e-4 weeks <br />1.66659e-4 months <br />, with lowest main control board indicated S/G level at approximately 44%, an automatic S/G low-low level reactor trip occurred. The turbine tripped as expected on Turbine Trip/Reactor Trip P4 and due to the shrink in S/G levels, both motor-driven Auxiliary Feedwater (AFW) pumps and the turbine-driven AFW pump started as required. All support systems functioned as required. The pressurizer bank-A backup heater supply breaker tripped open after approximately ten minutes of operation, but the remaining banks of pressurizer heaters restored pressurizer pressure to its normal band. The plant was then stabilized and maintained in Mode-3 (Hot Standby) to allow investigation into the reactor trip.

CAUSE:

This event was caused by faulty hydraulic relays (solenoid operated shuttle valves) that control the position of 1FW-159. Investigation revealed that the shuttle valve's o-ring seals were leaking by which prevented proper hydraulic operation.

SAFETY SIGNIFICANCE:

There were no adverse safety consequences associated with this event. With the exception of the pressurizer bank A backup heater supply breaker trip described above, all systems functioned as required to stabilize the reactor in Hot Standby.

This is being reported per 10CFR50.73.a.2.iv as an unplanned Reactor Protection System / Engineered Safety Feature actuation.

PREVIOUS SIMILAR EVENTS:

There have been no previous reactor trips reported that were caused by faulty Main Feedwater Isolation valve solenoid operated shuttle valves.

CORRECTIVE ACTIONS COMPLETED:

1. The solenoid operated shuttle valves for 1FW-159 were replaced and 1FW-159 was satisfactorily tested on February 1, 1997.
2. Troubleshooting was performed to determine the cause of the pressurizer bank-A backup heater supply breaker trip, but was inconclusive. A malfunctioning test switch was found and was replaced on February 1, 1997.
3. A review of archived plant process computer data was performed to investigate the apparent discrepancy between S/G levels last olserved in the main control room and the low-low S/G level reactor trip setpoint of 38.5%. However, due to the computer data point 10 second update rate, an accurate level value at the time of the reactor trip could not be verified. The "A" S/G level channels were checked to determine if,a calibration problem existed. No abnormalities were found and each of the channels were within the expected tolerance.

These actions were completed on January 31, 1997.