IR 05000440/2020004: Difference between revisions

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{{#Wiki_filter:February 12, 2021
{{#Wiki_filter:
 
==SUBJECT:==
PERRY NUCLEAR POWER PLANT - INTEGRATED INSPECTION REPORT 05000440/2020004
 
==Dear Mr. Penfield:==
On December 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Perry Nuclear Power Plant. On January 28, 2021, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.
 
One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
 
If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Perry Nuclear Power Plant.
 
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Perry Nuclear Power Plant. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
 
Sincerely,
/RA/
Billy C. Dickson, Jr., Chief Branch 2 Division of Reactor Projects Docket No. 05000440 License No. NPF-58
 
===Enclosure:===
As stated
 
==Inspection Report==
Docket Number: 05000440 License Number: NPF-58 Report Number: 05000440/2020004 Enterprise Identifier: I-2020-004-0031 Licensee: Energy Harbor Nuclear Corp.
 
Facility: Perry Nuclear Power Plant Location: Perry, OH Inspection Dates: October 01, 2020 to December 31, 2020 Inspectors: S. Bell, Health Physicist J. Nance, Operations Engineer T. Ospino, Resident Inspector G. Roach, Senior Operations Engineer J. Steffes, Senior Resident Inspector Approved By: Billy C. Dickson, Jr., Chief Branch 2 Division of Reactor Projects Enclosure
 
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Perry Nuclear Power Plant, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
 
===List of Findings and Violations===
 
Failure to Close Valve During Surveillance Procedure Causes Inoperability and Unavailability of the Standby Liquid Control System Cornerstone          Significance                                  Cross-Cutting      Report Aspect              Section Mitigating            Green                                        [H.12] - Avoid      71152 Systems              NCV 05000440/2020004-01                      Complacency Open A finding of very low safety significance (Green) and associated non-cited violation of Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the licensees failure to perform activities affecting quality in accordance with an approved procedure appropriate for the circumstances. Specifically, during performance of PTI-C41-P0001, Standby Liquid Control Transfer System Pump and Valve Operability Test,
Revision 10, operators failed to shut transfer line isolation valve, 1C41-F522, causing an unplanned eight-hour limiting condition for operation (LCO) entry and unavailability of both trains of the standby liquid control system.
 
===Additional Tracking Items===
None.
 
=PLANT STATUS=
 
The plant began the inspection period at rated thermal power. On October 31, 2020, reactor power was lowered to 66 percent to perform a rod sequence exchange and control rod scram time testing. The unit was returned to rated thermal power on November 11, 2020. On November 14, 2020, reactor power was lowered to 65 percent to perform a rod pattern adjustment. The unit was returned to rated thermal power the same day. On December 14, 2020, reactor power was lowered to 69 percent to perform turbine control valve testing. The unit was returned to rated thermal power on December 15, 2020. The unit remained at, or near, rated thermal power until December 23, 2020, when the unit entered into coastdown operations to refueling outage 1R18. The plant was at 97 percent power on December 31,
 
==INSPECTION SCOPES==
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
 
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.
 
==REACTOR SAFETY==
 
==71111.01 - Adverse Weather Protection==
 
===External Flooding Sample (IP Section 03.03) (1 Sample)===
: (1) External flooding walk down inspection Service Building on December 2, 2020
 
==71111.04 - Equipment Alignment==
 
===Partial Walkdown Sample (IP Section 03.01) (4 Samples)===
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
: (1) Emergency closed cooling system (ECCS) valve alignment October 18, 2020
: (2) Low pressure core spray venting and valve lineup October 22, 2020
: (3) A residual heat removal (RHR) system lineup verification on November 18, 2020 (4)  "A" standby liquid control (SLC) system alignment verification on December 3, 2020
 
===Complete Walkdown Sample (IP Section 03.02) (1 Sample)===
: (1) The inspectors evaluated system configurations during a complete walkdown of the          high-pressure core spray system on November 10 to 20, 2020.
 
==71111.05 - Fire Protection==
 
===Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)===
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
: (1) Intermediate building, elevation 620-foot, fire zone (FZ) 0IB-3 on November 7, 2020
: (2) Fuel handling building, elevation 620-foot, FZ 0FH-3 on November 7, 2020
: (3) Diesel generator building, 620- and 646-foot elevations, FZs 1DG-1C and DG-1D on November 7, 2020
: (4) Auxiliary building, 620- and 599-foot elevations on November 7 to 10, 2020
: (5) Unit 1 Division 3 Switchgear 620-6 FZ 1CC-3c on November 9, 2020
: (6) Emergency Service Water pumphouse FZ 0EW on November 10, 2020
 
==71111.06 - Flood Protection Measures==
 
===Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)===
The inspectors evaluated internal flooding mitigation protections in the:    (1)  "C" RHR system room on December 29, 2020
: (2) ECCS system on December 30, 2020
 
==71111.07A - Heat Sink Performance==
 
===Annual Review (IP Section 03.01) (1 Sample)===
The inspectors evaluated readiness and performance of:
: (1) Division 1 emergency diesel generator (EDG) jacket water heat exchanger review on December 7 to 17, 2020
 
==71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance==
 
===Requalification Examination Results (IP Section 03.03) (1 Sample)===
: (1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification program biennial written examination and annual operating test administered between October 26 and December 7, 2020.
 
==71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance==
 
Licensed Operator Requalification Program (IP Section 03.04) (1 Partial)
    (1)  (Partial)
Biennial Requalification Written Examinations The inspectors evaluated the quality of the licensed operator biennial requalification written examination administered on December 10, 2020.
 
Annual Requalification Operating Tests The inspectors evaluated the adequacy of the facility licensees annual requalification operating test.
 
Administration of an Annual Requalification Operating Test Due to the COVID-19 PHE, the inspectors could not by direct observation, evaluate the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives. Specifically, the inspectors did not observe the administration of simulator scenarios and Job Performance Measures (JPM) during the conduct of an annual requalification operating test required by 10 CFR 55.59(a)(2).
 
Requalification Examination Security The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.
 
Remedial Training and Re-examinations The inspectors evaluated the effectiveness of remedial training conducted by the licensee and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.
 
Operator License Conditions The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.
 
Control Room Simulator The inspectors evaluated the adequacy of the facility licensees Control Room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.
 
Problem Identification and Resolution The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.
 
==71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance==
 
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)
(1 Sample)
: (1) The inspectors observed and evaluated licensed operator performance in the Control Room during down power for rod sequence exchange and scram time testing on October 31, 2020.
 
===Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)===
: (1) The inspectors observed and evaluated licensed operator performance in the simulator on October 28, 2020.
: (2) The inspectors observed and evaluated licensed operator performance in the simulator on November 4, 2020.
 
==71111.12 - Maintenance Effectiveness==
 
===Maintenance Effectiveness (IP Section 03.01) (6 Samples)===
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
: (1) SLC system unavailability due to dilution event on August 20, 2020
: (2) Emergency service water (ESW) radiation monitoring spiking on October 19 to 22, 2020
: (3) Work associated with "A" reactor protection system motor generator on November 12, 2020
: (4) Meteorological tower work after Quincy lane was down for weather-related event on November 17, 2020
: (5) Combustible gas mixing compressor "A" failure on December 22, 2020
: (6) Unit 2 startup transformer modification issues on December 22, 2020
 
==71111.13 - Maintenance Risk Assessments and Emergent Work Control==
 
===Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)===
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
: (1) Plant risk evaluation and assessment while "A" ESW, "A" ECCS system, and "A" RHR inoperable and unavailable for maintenance work window on October 20 to 22, 2020
: (2) Emergent work evaluation and risk assessment associated with reactor vessel level perturbation due to reactor feed pump "A" speed oscillations on November 5, 2020
: (3) Licensee response to feedwater system transient event on November 5, 2020
: (4) Emergent activities associated to the reactor protection system motor generator "A" work on November 12, 2020
 
==71111.15 - Operability Determinations and Functionality Assessments==
 
===Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)===
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
: (1) Division 1 EDG operability determination associated with CR 2020-08482 on November 9, 2020
: (2) Meteorological tower operability check following weather-related event on November 17, 2020
: (3) Functional test of the FLEX emergency service water pump B based on CR 2020-09317 on December 9, 2020
: (4) Unit 2 startup transformer disconnect failure on December 16 to 17, 2020
: (5) Division 1 EDG jacket water circulating pump failure due to a blown fuse on December 31, 2020
 
==71111.18 - Plant Modifications==
 
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)
(2 Samples)
The inspectors evaluated the following permanent modification:
: (1) Main steam line isolation valve nuclear steam supply shutoff system isolation logic "C" test jack modification on October 6, 2020
: (2) Unit 1 startup transformer modification implementation 19-0203-001 on November 12, 2020
 
==71111.19 - Post-Maintenance Testing==
 
===Post-Maintenance Test Sample (IP Section 03.01) (8 Samples)===
The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:
: (1) The replacement of filters on "A" hydraulic power unit recirculation system on September 17 to 21, 2020
: (2) The replacement of the cable on the A ESW radiation monitor on October 7, 2020
: (3) The replacement of "A" electro-hydraulic control pump discharge filter on October 8, 2020
: (4) The replacement of the ECCS pump room cooler AGASTAT E7000 TD relay on October 18, 2020 (5)    "A" ESW system loop flow and differential pressure test following maintenance work window on October 26, 2020 (6)    "A" low pressure core spray room cooler time delay relay replacement October 21, 2020 (7)    "A" RHR room cooler time delay relay replacement on October 28, 2020 (8)    "A" RHR surveillance following motor operated valve test and adjustment on October 29, 2020
==71111.22 - Surveillance Testing==
 
The inspectors evaluated the following surveillance tests:
 
===Surveillance Tests (other) (IP Section 03.01)===
{{IP sample|IP=IP 71111.22|count=4}}
: (1) Main steam line high flow C functional test on October 6, 2020
: (2) Main steam line low condenser vacuum channel A calibration on October 19, 2020 (3)    "A" ESW flow and differential pressure test on October 24, 2020
: (4) Channel "A" drywell high-pressure calibration for 1C71-N050A on
 
===September 21, 2020 Inservice Testing (IP Section 03.01) (1 Sample)===
: (1) High-pressure core spray pump and valve operability test, work order 200771908
 
===FLEX Testing (IP Section 03.02) (1 Sample)===
: (1) Test of the FLEX lake water pumps on June 6, 2020
 
==71114.04 - Emergency Action Level and Emergency Plan Changes==
 
===Inspection Review (IP Section 02.01-02.03) (1 Sample)===
: (1) The inspectors completed an evaluation of submitted Emergency Action Level and Emergency Plan changes on December 11, 2020. This evaluation does not constitute NRC approval.
 
==71114.06 - Drill Evaluation==
 
===Drill/Training Evolution Observation (IP Section 03.02) (2 Samples)===
The inspectors evaluated:
: (1) Inspectors observed and evaluated the emergency response organization tabletop drill on October 29, 2020.
: (2) Inspectors observed and evaluated simulator-based licensed operator requal training on November 4,
 
==RADIATION SAFETY==
 
==71124.05 - Radiation Monitoring Instrumentation==
 
===Calibration and Testing Program (IP Section 03.02) (11 Samples)===
: (1) Thermo Scientific PCM-3 personnel contamination monitor, serial number L70L004E, calibrated on December 13, 2019
: (2) JL Shepherd Model 89 Irradiator calibrated on January 10, 2020
: (3) Canberra Fastscan Whole Body Counter calibrated on February 5, 2020
: (4) Mirion telepole survey instrument, serial number L70L074A, calibrated on February 11, 2020
: (5) Ludlum model 12 survey instrument, serial number L70L096D, calibrated on February 26, 2020
: (6) Eberline model RM20 survey instrument, serial number L70L020K calibrated on April 1, 2020
: (7) Eberline R02 survey instrument, serial number L70L030H, calibrated on May 15, 2020
: (8) Eberline model SAC-4 survey instrument, serial number L70L003E, calibrated on July 16, 2020
: (9) Bicron RSO-50 survey instrument, serial number L70L0045Z, calibrated on August 24, 2020
: (10) Thermo Scientific SAM9 small article monitor, serial number L70L504L, calibrated on September 9, 2020
: (11) Thermo Scientific SPM-906 portal monitor, serial number L702009L calibrated on September 25, 2020 Effluent Monitoring Calibration and Testing Program Sample (IP Sample 03.03) (2 Samples)
The inspectors evaluated the calibration and maintenance of the following radioactive effluent monitoring and measurement instrumentation:
: (1) Unit 1 Off-Gas Vent Pipe Noble Gas Calibration for 1D17-K836
: (2) Unit 1 ESW Loop A Radiation Monitor Channel Calibration for 1D17-K604
 
==OTHER ACTIVITIES - BASELINE==
 
===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) ===
{{IP sample|IP=IP 71151|count=1}}
: (1) October 1, 2019 through September 30, 2020
 
===BI02: RCS Leak Rate Sample (IP Section 02.11) (1 Sample)===
: (1) July 1, 2019 through September 30, 2020
 
===OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)===
: (1) October 1, 2019 through September 30, 2020
 
==71152 - Problem Identification and Resolution==
 
===Semiannual Trend Review (IP Section 02.02) (1 Sample)===
: (1) Human performance trend June through December 2020
 
===Annual Follow-up of Selected Issues (IP Section 02.03) (3 Samples)===
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
: (1) CR 2020-06561, Standby Liquid Control Hi/Lo Level Alarm During SLC Transfer Pump and Valve"
: (2) CR 2020-06471, "Timeliness of General Emergency Classification During August 8, 2020, Dry Run Drill"
: (3) Loss of Feedwater Heating Results in Loss of Safety Function
 
===71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02) ===
{{IP sample|IP=IP 71153|count=1}}
The inspectors evaluated the following licensee event reports (LERs):
: (1) LER 2019-004 and LER 2019-004-001, Loss of Feedwater Heating results in Loss of Safety Function on August 6, 2019.
 
The inspectors determined that the cause of the condition described in the LER was not reasonably within the licensees ability to foresee and correct, and, therefore, was not reasonably preventable. No performance deficiency nor violation of NRC requirements was identified.
 
==INSPECTION RESULTS==
Failure to Close Valve During Surveillance Procedure Causes Inoperability and Unavailability of the Standby Liquid Control System Cornerstone            Significance                                Cross-Cutting      Report Aspect              Section Mitigating            Green                                      [H.12] - Avoid      71152 Systems                NCV 05000440/2020004-01                    Complacency Open A finding of very low safety significance (Green) and associated non-cited violation of Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed for the licensees failure to perform activities affecting quality in accordance with an approved procedure appropriate for the circumstances. Specifically, during performance of PTI-C41- P0001, Standby Liquid Control Transfer System Pump and Valve Operability Test, Revision 10, operators failed to shut transfer line isolation valve, 1C41-F522 causing an unplanned eight-hour limiting condition for operation (LCO) entry and unavailability of both trains of the SLC system.
 
=====Description:=====
On August 20, 2020, during the performance of PTI-C41-P0001, Standby Liquid Control Transfer System Pump and Valve Operability Test, Revision 10, the licensee received the SLC storage tank level HI/LO alarm shortly after starting the SLC transfer pump. The evolution resulted in the unintended addition of approximately 226 gallons of water to the SLC storage tank. The licensee reviewed system response, interviewed personnel, and reviewed procedure PTI-C41-P0001 and determined that the normally locked open transfer line isolation valve, 1C41-F522, had not been shut.
 
The licensee completed Surveillance Requirement 3.1.7.5 to sample SLC storage tank concentration within 24-hours following the inadvertent water addition. Based on boron concentration, the licensee determined that both the SLC system trains were inoperable and entered LCO 3.1.7 Condition B to restore one train to operable status within eight hours. The licensee returned SLC storage tank concentration to the correct specification about three hours after the initial tank solution test.
 
Corrective Actions: Immediate corrective actions included determination and correction of SLC storage tank concentration and restoring the SLC system to operable. Additionally, the licensee made procedural changes to add an independent verification step to the closure of the transfer line isolation valve, 1C41-F522.
 
Corrective Action References: CR 2020-06561, Standby Liquid Control Hi/Lo Level Alarm During SLC Transfer Pump and Valve, 08/20/2020; CR 2020-06563, Leakby Observed Through SLC Transfer Line Isolation Valve, 08/20/2020; and CR 2020-07110, Misposition Plant Status Control Event During SLC Transfer System Pump and Valve Operability Test, 09/11/2020.
 
=====Performance Assessment:=====
Performance Deficiency: The inspectors determined that the licensees failure to implement Section 5.1.3, Step 3, of PTI-C41-P0001, Standby Liquid Control Transfer System Pump and Valve Operability Test, Revision 10, was a performance deficiency. Specifically, the failure to close the transfer line isolation valve 1C41-F522 in accordance with the procedure directly led to the inoperability and unavailability of the SLC system.
 
Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The inspectors determined the performance deficiency was more than minor because it was associated with the Human Performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, an operator failed to close the transfer line isolation valve 1C41-F522, which allowed water to be added to the SLC storage tank, thus negatively impacting the availability of the SLC system.
 
Significance: The inspectors assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspector assessed the significance of the finding using Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors screened the finding against the Mitigating Systems screening questions in Exhibit 2 and answered NO to all screening questions. Therefore, the finding screened to very low safety significance (Green).
 
Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risks, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Specifically, the operator failed to implement error reduction tools to ensure both actions contained with the step were performed in accordance with written procedures.
 
=====Enforcement:=====
Violation: Title 10 CFR 50 Appendix B, Part V, Instructions, Procedures, and Drawings, states, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings.
 
Contrary to the above, on August 20, 2020, while performing an activity affecting quality, operators did not accomplish a surveillance procedure in accordance with the procedure and incorrectly performed a step in surveillance procedure PTI-C41-P0001, and failed to close a valve. Specifically, operators failed to close the transfer line isolation valve 1C41-F522, resulting in an unplanned entry into Technical Specification 3.1.7, Condition B, and adversely affected the availability of the SLC system.
 
Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.
 
Observation: Human Performance Trend June to December 2020                              71152 During the second half of 2020, while performing reviews associated with the daily corrective action program, the inspectors identified 17 corrective action documents with human performance-related issues. Examples of human performance issues were spread across different working groups and resulted in various consequential outcomes. These examples included, but were not limited to, a chemistry department individual loss of attention to detail and dropped a glass vial containing a source resulting in a spill, electrician personal not implementing human performance tools (peer check) resulting in the miswiring during modification to the Unit 2 startup transformer and an increase in the out of service time, and the failure to close a valve between the SLC and standby liquid control transfer systems resulting in the inoperability and unavailability of the SLC system. Following their review, the inspectors concluded that the Human Performance attributes associated with the issues were associated with a lack of attention to detail, supervisors' failure to challenge performance and enforce standards and requirements, and individuals not following their processes and procedures. The inspectors engaged the licensee and expressed their observations through meetings and other methods. The inspectors expressed their concern with the upward negative trend in licensee performance and its impacts to plant safety.
 
Due in part to previous inspector observations, the licensee developed a "critical coaching initiative" to analyze performance gaps and perform training for the site supervisors as documented in CR 2019-09164, "2019 INPO E&A AFI LF.1: Leadership." Following the critical coaching initiative institution, the inspectors observed a temporary reduction in human performance issues. However, considering the most recent human performance issues, the inspectors have concerns about the licensee's corrective actions' effectiveness and longevity.
 
Additionally, the inspectors noted as a consequence of the most recent supervisor coaching; the licensee wrote five condition reports for supervisors failing the "critical coaching lab in site supervisor training," as documented in CR 2020-08703, CR 2020-08696, CR 2020-08008, CR 2020-08007, and CR2020-07767. The inspectors concluded that while the licensee had begun to address human performance gaps site-wide, but as demonstrated by the most recent supervisor failures of the critical coaching lab, more work was required to ensure performance improvement.
 
The inspectors did not identify any findings or violations of NRC requirements in the course of their review.
 
Observation: Emergency Preparedness Drill General Emergency Classification              71152 Timeliness Review The inspectors performed a detailed review of CR 2020-06471, "ERO-Drill: Timeliness of General Emergency Classification During August 8, 2020, Dry Run Drill." The purpose of emergency preparedness drill performance and evaluation, in part, is to determine the licensee's ability to identify and classify events based on plant conditions and communicate emergency action level declarations promptly to state and local authorities. Title 10 CFR 50 Appendix E requires, in part, that "licensees shall establish and maintain the capability to assess, classify, and declare an emergency condition within 15-minutes after the availability of indications to plant operators that an emergency action level has been exceeded and shall promptly declare the emergency conditions as soon as possible following the identification of the appropriate emergency classification level." To assess the timeliness of licensee notification, a "time zero" is identified in drill scenarios when plant conditions change, which should be recognized by plant staff followed by event classification.
 
The inspectors noted that CR 2020-06471 documented a drill controller issue that the scenario "time zero" was different than what occurred during drill execution. Specifically, the scenario guide stated, "time zero" was 11:35 am, and "time zero" during drill debrief was determined to be 11:40 am. The inspectors noted this distinction to be important because event classification occurred at 11:54 am. The inspectors noted that "Perry Emergency Response Organization Integrated Drill Scenario Guide," Revision 1, stated that at 11:35 am a catastrophic body-to-bonnet failure of the "B" main steam line isolation valve occurred resulting in the rapid increase in steam tunnel temperatures, as well as turbine building/heater bay and Unit 1 plant vent radiation monitor readings. The Perry Emergency Response Organization Integrated Drill Scenario Guide controller notes stated that, "this is the indication for a General Emergency FG 1.1, loss of any two fission product barriers and the loss or potential loss of the third barrier." For this Problem Identification and Resolution sample, the inspectors focused on the licensee's evaluation and assessment of event classification timeliness and associated corrective actions.
 
The inspectors noted through review of licensee evaluation that upon insertion of the body-to-bonnet failure, the simulator errantly showed flow through the off-gas system.
 
The Perry Nuclear Power Plant construction is such that both outboard main steam isolation valves and main steam stops are contained in the steam tunnel. Therefore, an indication of off-gas flow in conjunction with the rise in steam tunnel temperatures and vent radiation monitor readings led the operations crew to believe the failure and steam leak had occurred downstream of the main steam stops. The operations crew shut the main steam stops and noted no change in steam tunnel temperature trend or turbine building/heater bay and Unit 1 plant vent radiation monitor readings. The operations crew determined that the leak was unisolable and constituted a loss of a fission product barrier. This information was not promptly communicated to the Emergency Director in the Emergency Operations Facility (EOF) due to conference bridge communications issues. The inspectors challenged the licensee as to why 11:40 am was "time zero" and not 11:35 am, as stated in the drill guide and when plant conditions first presented themselves. The inspectors reviewed PSI-0019, "Emergency Action Level (EAL) Bases Document," Revision 21, Attachment 2 fission product barrier loss/potential loss matrix and bases for an unisolable direct downstream pathway to the environment exists after containment isolation signal guidance. The inspectors noted that the threshold is considered met if the breach is not isolable from the Control Room or an attempt for isolation from the Control Room has been made and was unsuccessful. The licensee stated that based on the off-gas flow indications, even though erroneous and emergency action level basis guidance, it was reasonable for the operations crew to attempt to shut the main steam stops before declaring an unisolable leak.
 
The inspectors noted three contributors to the event classification almost exceeding the regulatory time frame:
1. Communication issues between the Control Room and EOF Emergency Director delayed recognition of the leak in the final fission product barrier and a General Emergency declaration. The licensee changed its process to require the Control Room and Emergency Director to maintain an open communication line rather than connecting to the bridge to relay information.
 
2. The EOF Emergency Director had noted and focused solely on rising Unit 1 plant vent radiation levels as the indicator to determine a General Emergency had occurred.
 
The Director was slow to recognize the unisolable leak condition in the Emergency Action Level matrix also applied until prompted by the Control Room.
 
3. Recent simulator software upgrades resulted in the unintended off-gas flow indications encountered during the drill. The licensee had validated the scenario before the software upgrades going into effect and had not revalidated before the licensee performing the drill. The licensee changed its process to ensure simulator fidelity before drill execution following software upgrades.
 
The inspectors did not identify any findings or violations of NRC requirements in the course of their review.
 
Observation: Loss of Feedwater Heating results in Loss of Safety Function                71152 The inspectors reviewed the associated causal evaluation and corrective actions associated with loss of feedwater heating due to heater 5B isolation during heater alignment. The inspectors noted that the apparent cause was inadequate communication within the Perry organization associated with heater tuning strategies and implications to operating procedures. Specifically, the licensee tuned the heater normal controller for steady-state operations to dampen heater level oscillations at 100 percent power. This strategy restricts the ability to transfer level control from alternate to normal at power levels greater than 62 percent power. The inspectors noted that the operations procedure did not include mitigating actions to reduce power based on the tuning strategy and resulted in heater isolation. Corrective actions included, but were not limited to, revising IOI-0003, "Power Changes," to provide a caution note to operations about heater drain control based on power level, which would incorporate level control restrictions based on tuning strategy. The inspectors did not identify any findings or violations of NRC requirements in the course of their review.
 
==EXIT MEETINGS AND DEBRIEFS==
The inspectors verified no proprietary information was retained or documented in this report.
* On January 28, 2021, the inspectors presented the integrated inspection results to Mr. R. Penfield, Site Vice President, and other members of the licensee staff.
* On December 10, 2020, the inspectors presented the radiation protection baseline inspection results to Mr. R. Penfield, Site Vice President, and other members of the licensee staff.
* On December 11, 2020, the inspectors presented the Perry Biennial Licensed Operator Requalification Program Inspection Results inspection results to Mr. R. Penfield, Site Vice President, and other members of the licensee staff.
* On December 11, 2020, the inspectors presented the emergency action level and emergency plan changes inspection results to Mr. R. Penfield, Site Vice President, and other members of the licensee staff.
* On January 28, 2021, the inspectors presented the integrated inspection results to Mr. R. Penfield, Site Vice President, and other members of the licensee staff.
 
=DOCUMENTS REVIEWED=
 
Inspection Type              Designation    Description or Title                                        Revision or
Procedure                                                                                                Date
71111.01  Engineering                      FENOC Perry Flood Hazard Reevaluation Report                12/4/2020
Evaluations
71111.04  Drawings          302-0701-00000  High-Pressure Core Spray System                            KK
Procedures        SVI-C41-T2001-A Standby Liquid Control                                      22
SVI-P42-T5326  Emergency Closed Cooling System Valve Position Check        9
VLI-E22A        High-Pressure Core Spray                                    10
Work Orders      200753720      SVI-E12-T1182A RHR A PLCI Vlv L/U (31D) RHR A LPCI          11/18/2020
Valve Lineup Verification and System Venting
200754601      SVI-P42-T5326 ECCS Vlv Position Check (31D) Emergency      10/18/2020
Closed Cooling System Valve Position Check
200754975      SVI-E21-T11 LPCS Venting and Vlv L/U (31D) LPCS            10/22/2020
Venting and Valve Lineup Verification
71111.05  Fire Plans        FPI-0FH        Fuel Handling Building                                      6
FPI-0IB        Intermediate Building                                      10
FPI-1AB        Auxiliary Building Unit 1                                  4
FPI-1DG        Diesel Generator Building                                  9
Procedures        FPI-0CC        Unit 1- Division 3 Switchgear 620 - 6 Elevation Fire Zone 12
1CC-3c
FPI-0EW        Emergency Service Water Pumphouse                          7
71111.06  Calculations      JL-083          Flooding Analysis of Control Complex Building, Intermediate 3
Building, and Fuel Handling Building - Floor Elevation 574
Feet - 10 Inches
Corrective Action 2013-05625      Corrective Action Generated to Track Closure of Prompt      10/23/2015
Documents                        Functionability Assessment for CR 2013-05625
71111.07A  Calculations      R46-023        Division 1 Diesel Generator Jacket Water Heat Exchanger    4
Performance Testing Results
71111.11A  Miscellaneous                    Perry Nuclear Power Plant Annual LORT Exam Information      12/14/2020
71111.11B  Corrective Action CR 2019-08949  Recombiner A/B TEMP HI / LOW Alarm in the Control Room      10/26/2019
Documents                        Label Does Not Match the Alarm Response Instruction or
Simulator Alarm Window
CR 2019-10283  Simulator Hardware Failure During Annual Exam Job          12/10/2019
Performance Measures
Inspection Type              Designation        Description or Title                                      Revision or
Procedure                                                                                                  Date
CR 2020-02702      Simulator Hardware Issue Caused Short Training Delay      03/27/2020
Corrective Action CR 2020-09365      Inaccurate Information Provided to the NRC                12/07/2020
Documents
Resulting from
Inspection
Miscellaneous                        2019 LORT Attendance Records
20 LORT Attendance Records
100% Simulator Steady-State Test                          08/28/2020
75% Simulator Steady-State Test                            07/27/2019
75% Simulator Steady-State Test                            08/28/2020
43% Simulator Steady-State Test                            07/27/2019
43% Simulator Steady-State Test                            08/28/2020
Operator Remediation Plan; Various Operators              12/31/2019
100% Simulator Steady-State Test                          07/27/2019
2019 01-05          Requalification Training Schedule                          12/31/2019
20 06-10          Requalification Training Schedule                          12/01/2020
20-13            RO Written Exam                                            Week 7
20-14            SRO Written Exam                                          Week 7
B2.2.1.1            Transient Testing, Manual SCRAM                            03/27/2019
B2.2.1.10          Transient Testing, Main Steam Isolation Valve Closure with 07/24/2020
One Safety Relief Valve Stuck Open
B2.2.1.2            Transient Testing, Trip All Reactor Feed Pump Turbines    03/27/2019
B2.2.1.3            Transient Testing, Main Steam Isolation Valve Closure      07/23/2020
B2.2.1.4            Transient Testing, Simultaneous Trip of All B33 Recirc    03/27/2019
Pumps
B2.2.1.5            Transient Testing, Trip Single B33 Recirc Pump            07/24/2020
B2.2.1.7            Transient Testing, Maximum Rate Power Ramp (100% to        07/24/2020
75% to 100%) Using Flow Control Valves
B2.2.1.9            Transient Testing, Main Steam Line Rupture in Drywell      03/27/2019
Credit for Position BOP Operator                                              12/31/2019
Report
Credit for Position ATC Operator                                              12/31/2019
Report
Inspection Type          Designation        Description or Title                    Revision or
Procedure                                                                            Date
Credit for Position Shift Manager                          12/31/2019
Report
Credit for Position Unit Supervisor                        12/31/2019
Report
Credit for Position BOP Operator                            12/01/2020
Report
Credit for Position ATC Operator                            12/01/2020
Report
Credit for Position Unit Supervisor                        12/01/2020
Report
Credit for Position Shift Manager                          12/01/2020
Report
Cycle 18            Real Time Annual Testing                03/26/2019
OT-3070-PC1E        Simulator Scenario Guide PC1E          0
OT-3070-001-        Simulator Scenario Guide PC5D          0
PC5D
OT-3070-005-        Simulator Scenario Guide RP2A          0
RP2A
OT-3070-RP1D        Simulator Scenario Guide RP1D          0
OT-3701-ADM-        SRO Admin JPM                          Week 4
25SRO
OT-3701-ADM-        SRO Admin Job Performance Measure (JPM) Week 2
24SRO
OT-3701C11-        Simulator JPM                          Week 7
514RO
OT-3701C41-        In Plant JPM                            Week 7
008RO
OT-3701C61-        In Plant JPM                            Week 7
501RO
OT-3701C71-        Simulator JPM                          Week 7
003RO
OT-3701G43-        RO Admin JPM                            Week 7
001RO
71111.11B  Miscellaneous OT-3701P57-        In Plant JPM                            Week 4
Inspection Type            Designation      Description or Title                                    Revision or
Procedure                                                                                            Date
001RO
OT-3701R10-      In Plant JPM                                            Week 4
2RO
OT-3701R43-      Simulator JPM                                          Week 6
501RO
OTLC-            Scenario Based Testing                                  0
3058202006-PY-
SGA
OTLC-            Scenario Based Testing                                  0
3058202006-PY-
SGB
OTLC-            Scenario Based Testing                                  0
3058202006-PY-
SGC1
OTLC-            Scenario Based Testing                                  0
3058202007-PY-
SGA
OTLC-            Scenario Based Testing                                  0
3058202008-PY-
SGA-HIT
Simulator Post  Turbine Valve Closure                                  05/28/2019
Event Testing
Simulator Post  Loss of Two Circulating Water Pumps                    02/17/2020
Event Testing
Procedures      NOBP-TR-1271,    Inactive License Retraining Program Records; Various    11
Operators
NOP-OP-1013-04  Time Critical Operator Actions Tracking Sheet          0
NOP-TR-1240-06  Remediation Training                                    0
NOP-TR-1280      Simulator Configuration Management                      2
Self-Assessments                  2020 Nuclear Oversight Quality Assessment of Operations 03/31/2020
Department
2019 Nuclear Oversight Quality Assessment of Training  02/27/2020
Department
Simulator Review Meeting Minutes                                        02/20/2019
Inspection Type              Designation        Description or Title                                      Revision or
Procedure                                                                                                Date
Committee
Simulator Review  Meeting Minutes                                          04/17/2019
Committee
Simulator Review  Meeting Minutes                                          01/30/2020
Committee
Simulator Review  Meeting Minutes                                          04/16/2020
Committee
Simulator Review  Meeting Minutes                                          08/17/2020
Committee
Work Orders      19-0002            DFWCS Reactor Feed Pump Trip and Swap to Single          05/02/2019
Element
19-0003            ECP 04-0145 RFP Min Flow Controller Modification          02/21/2019
19-0004            ECP 18-0081 Implement Stroke Time Changes for            02/21/2019
1G33F0039 & 1G33F0040
19-0006            Implement Cycle 18 Core Files for All Three Exposures    03/05/2019
                                                (BOL, MOL, EOL)
19-0007            Implement ECP 18-0274 to Eliminate Automatic High Shaft  03/12/2019
Vibration Trip from Main Turbine Protection System
19-0012            Div 2 EH12 Undervoltage ECP 16-0336-002                  03/18/2019
19-0019            Install ECP 04-0113-001 Fire Computer in Control Room    08/28/2019
19-0030            Install ECP 12-0238 Diesel Fire Pump Switch on P970      10/01/2019
20-0015            Install Div 3 DG RM Vent CO2 Injection Bypass Switch on  02/24/2020
P800
20-0044            Implement ECP 17-0220 in the Simulator (MSIV Bypass      10/20/2020
Jacks)
20-0045            Implement ECP 15-0517 for Div 3 in the Simulator          08/17/2020
71111.11Q Miscellaneous      Evolution Specific Perry Nuclear Power Plant October 2020 Pattern Adjustment 0
Reactivity Plan
OT-3070-003-      Scenario Guide                                            0
RP1C
OT-3070-PC1B      Scenario Guide                                            1
OT-3070-RP5A      Scenario Guide                                            5
71111.12  Corrective Action 2020-06482        Emergency Service Water Radiation Monitor Spiking        08/17/2020
Documents        2020-08558        Reactor Protection System (RPS) MG SET a Tripped During  11/04/2020
Inspection Type              Designation    Description or Title                                        Revision or
Procedure                                                                                              Date
PMT
20-08868    MET Tower Instrumentation Not Restored Upon Restoration    11/17/2020
of Quincy Power
20-09476    Unit 2 Startup Transformer Manual Disconnect Stuck Open    12/15/2020
20-09635    Combustible Gas Mixing Compressor Suction Valve Would      12/22/2020
Not Reopen Following Compressor Start
Work Orders      200840084      Replace Power Supply CR 2020-08986                          11/23/2020
71111.13  Corrective Action 2020-08567    Uncertainty of Proper Motor starter Overload Settings for  11/04/2020
Documents                        Reactor Protection System (RPS) Motor Generator (MG) Set
A
20-08575    Feedback System Transient - Steamflow/Feedflow              11/05/2020
Mismatch
Procedures        NOP-ER-3001-03 Simple Troubleshooting Plan                                4
NOP-OP-1007    Risk Management                                            33
PAP-1924      Risk-Informed Safety Assessment and Risk Management        9
Work Orders      200093606      Replace Relays in RPS "A" MG set                            11/27/2020
200835639      ECP 20-0179-001 Disable LS6/7 Linkage TM                    11/18/2020
71111.15  Corrective Action 2008-50767    Less Than Adequate Documentation for USAR Technical        12/12/2008
Documents                        Basis
2014-10996    60dpm Leak Shaft Div 2 Jacket Water Circ Pump Prompt        06/27/2014
Operability Determination Test
20-08868    MET Tower Instrumentation not Restored upon Restoration    11/17/2020
of Quincy Power
20-09317    Rheostat on FLEX Lake Pump for ESW "B" Doesnt Work        12/09/2020
Correctly Acts as On Off Switch
20-09535    As Found Condition of the Unit 2 Startup Transformer        12/17/2020
Manual Disconnect 2S11-S290 Gearing
20-09640    Division 1 Diesel Generator Jacket Water Circulation Pump  12/22/2020
Blown Fuse
Operability      2020-07870    Plan for Actions for Operation Challenge, Degraded Division 10/16/2020
Evaluations                      1 D/G Circulating Jacket Water Pump/Motor
Procedures        R45-025        Division 1 and 2 Emergency Diesel Generator Jacket Water    03/09/2010
Available Net Positive Suction Head
Work Orders      200841352      Unit 2 Main Transformer Troubleshooting for Unexpected      12/18/2020
Inspection Type              Designation    Description or Title                                    Revision or
Procedure                                                                                            Date
Results Upon Installation of a Modification
71111.18  Corrective Action 2020-06562      During Development of the Open Phase Modification      08/20/2020
Documents                        ECP-19-203, an Engineer Walkdown of the Startup
Transformer Relay Panel (1H13P0809) was Not Performed
20-08701      Failed PMT Unit 1 Startup OPPS Modification            11/10/2020
Engineering      ECP 17-0220-003 Main Steam Line Isolation Valve Nuclear Steam Supply    0
Changes                          Shutoff System Isolation Logic C Test Jack Installation
ECP 17-0220-003 Main Steam Line Isolation Valve Nuclear Steam Supply    1
Shutoff System Isolation Logic C Test Jack Installation
Engineering      601293470      Engineering Evaluation Request                          11/11/2020
Evaluations
Procedures        IP-ENG-001 Form 19-0203-000 Dedicated Open Phase Control Room          0
Annunciators - Unit-1
NOP-WM-1001-0  Addendum # A-4 TEST Functional WO 200803505            3
SVI-E31-T0074-C MSL High Flow Channel "C" Functional for 1E31-N686C and 8
1E31-N688C
Work Orders      200737101      Implement ECP 17-0220-003                              05/10/2020
200751207      SVI-E31-T0074C (92D) MSL High Flow Channel "C"          06/10/2020
Functional for 1E31-N686C and 1E31-N688C
71111.19  Corrective Action 2020-07809      Steam Bypass and Pressure Regulating Pump A          10/08/2020
Documents                        Discharge Filter Failed Post-Maintenance Testing
Work Orders      200750868      Emergency Service Water Loop "A" Flow and Differential  10/24/2020
Pressure Test
200752301      Replace 3.0 Micron Filter                              10/08/2020
200752959      Replace Fullers Earth Filters                          09/12/2020
200762832      Replace High-Pressure Filter, HPU A                  09/17/2020
200773294      SVI-D17-T8041 ESW Loop A Radiation Monitor Channel    10/07/2020
Calibration For 1D17-K604
200778768      Replace Time Delay Relay 1M39Q7004                      10/21/2020
200778768      Replace Time Delay Relay 1M39Q7004                      10/22/2020
200778769      Replace Time Delay Relay 1M39Q7008                      10/22/2020
200791518      Inspect/Replacement Filters, LPCS Room A              10/21/2020
200794100      Perform Static Motor Operated Valve Test                10/22/2020
200832456      A Rad Monitor Cable Replacement                      09/23/2020
Inspection Type          Designation    Description or Title                                      Revision or
Procedure                                                                                          Date
71111.22  Miscellaneous NEI 12-06      Diverse and Flexible Coping Strategies (FLEX)            4
Implementation Guide
Procedures    FSG 60.1        Supply ESW A Header from a FLEX Pump at the ESW          0
PTI-P45-P0001  ESW System Loop A Flow Differential Pressure Test      18
SVI-B21T0077A  MSL Low Condenser Vacuum Channel "A" Calibration For      11
1B21-N075A
SVI-C71-T0043-A Drywell High-Pressure Channel A Calibration For        9
1C71-NN050A
SVI-R43-T1317  Diesel Generator Start and Load Division 1                25
Work Orders  200737101      IMPLEMENT ECP 17-0220-003                                10/05/2020
200750868      PTI-P45P0001 1 (92D) EWS System Loop A Flow and        10/24/2020
Differential Pressure Test on
200751027      SVI-E31T0074C-1 (92D) MSL High Flow Channel "C"          10/06/2020
Functional for 1E31-N668C and 1E31-N688C
200752684      FLEX Water Pump Functional Testing                        06/15/2020
200770447      SVI-B21-T0077-A MSL Low Condenser Vacuum "A"              10/19/2020
Calibration For 1B21-N0
200773288      SVI-C71-T0043-A Drywell High-Pressure Channel A        09/21/2020
Calibration
71114.04  Miscellaneous                Perry Station 10 CFR 50.54(q) Evaluator Qualification and 05/19/2020
Training Records Spreadsheet
NRC Letter      Subj: Perry Nuclear Power Plant, Unit No. 1 - Issuance of 08/14/2019
ML19163A023    Amendment No. 186 Concerning Changes to Emergency
Response Organization Staff
PY-2019-017-00  10 CFR 50.54(q)2 Analysis for Perry Nuclear Power Plant  08/07/2019
Emergency Plan Revision
PY-2019-017-00  10 CFR 50.54(q)3 Evaluation for Perry Nuclear Power Plant 09/06/2019
Emergency Plan Revision
PY-2019-039-00  10 CFR 50.54(q)2 Analysis for Perry Nuclear Power Plant  11/04/2019
Emergency Plan Revision
PY-2019-039-00  10 CFR 50.54(q)3 Evaluation for Perry Nuclear Power Plant 11/06/2019
Emergency Plan Revision
PY-2019-044-00  10 CFR 50.54(q)2 Analysis for Perry Nuclear Power Plant  12/17/2019
Emergency Plan Revision
Inspection Type              Designation    Description or Title                                      Revision or
Procedure                                                                                            Date
PY-2019-044-00 10 CFR 50.54(q)3 Evaluation for Perry Nuclear Power Plant 01/06/2020
Emergency Plan Revision
Procedures                      Emergency Plan for Perry Nuclear Power Plant              54
Emergency Plan for Perry Nuclear Power Plant              55
Emergency Plan for Perry Nuclear Power Plant              56
Emergency Plan for Perry Nuclear Power Plant              57
NOP-LP-5002    Evaluation of Changes to Emergency Plans and Supporting  7
Documents 10 CFR 50.54(q)
71114.06  Miscellaneous                    2020 4th Quarter ERO Tabletop Drill TSC-EOF              0
71124.05  Calibration                      Abacos 2000 Whole Body Counter Calibration                02/05/2020
Records                          JL Shepherd Irradiator Calibration and Verification      01/10/2020
L702009L      Thermo Scientific SPM-906 Portal Monitor                  09/25/2020
L70L003E      Eberline SAC-4 Survey Instrument                          07/16/2020
L70L0045Z      Bicron RSO-50 Survey Instrument                          08/24/2020
L70L004E      Thermo Scientific PCM-2                                  12/13/2019
L70L020K      Eberline RM-20 Survey Instrument                          04/01/2020
L70L030H      Eberline RO2 Survey Instrument                            05/16/2020
L70L074A      Mirion Telepole Survey Instrument                        02/11/2020
L70L096D      Ludlum Model 12 Survey Instrument                        02/26/2020
L70L504L      Thermo Scientific Small Article Monitor                  09/22/2020
WO 200773294  ESW Loop A Radiation Monitor Channel Calibration for      10/07/2020
1D17-K604
Corrective Action CR-2020-05336  Procedure Adherence During WBC Calibration                06/29/2020
Documents        CR-2020-05337  Input Error in Creating WBC Calibration File              06/29/2020
CR-2020-05376  Pre NRC Assessment SA-BN-2020-1920 Identified            06/30/2020
Deficiency: Incorrect Source Information Contained in
SVI-D19-T1356A
Engineering                      D19 Containment Hi Range Radiation Monitor Evaluation    4
Evaluations
Procedures        HPI-J0054      Calibration of the Abacos 2000 Whole Body Counting        4, 6
System
NOP-OP-4401    Radiation Protection Instrumentation Program              3
Work Orders      200767227      Off-Gas Vent Pipe Noble Gas Radiation Monitor Calibration 09/17/2020
Inspection Type              Designation    Description or Title                                    Revision or
Procedure                                                                                            Date
200773294      ESW Loop A Radiation Monitor Channel Calibration for    10/07/2020
1D17-K604
71151      Corrective Action CR-2020-06028  NRC ID: Door 1P54X0202A High-Pressure Core Spray        07/29/2020
Documents                        Pump Room Found Unsecured
Miscellaneous                    Reactor Coolant System Dose Equivalent Iodine            Various
Determination Summary Data from 10/01/2019 Through
09/30/2020
Procedures        TSR Modes      Technical Specification Rounds Modes 1, 2, and 3        10/01/2019 -
1,2&3-19                                                                01/19/2020
TSR Modes      Technical Specification Rounds Modes 1, 2, and 3        01/20/2020 -
1,2&3-20                                                                09/30/2020
71152      Corrective Action 2019-06618      Entered ONI-N36 Loss of Feedwater Heating and ONI-C51    08/16/2019
Documents                        due to Heater 5B Isolation during Startup while Aligning
Heater Normal Drains Unplanned Limiting Condition of
Operation Entry
Drawings          302-0691-00000  Standby Liquid Control System                            AA
2-0692-00000  Standby Liquid Control Transfer System                  V
Miscellaneous    LER 2019-004    Loss of Feedwater Heating Results in Loss of Safety      06/08/2019
Function
Procedures        PTI-C41-P0001  Standby Liquid Control Transfer System Valve Test        11
71153      Miscellaneous    LER 2019-004    Loss of Feedwater Heating Results in Loss of Safety      06/08/2019
Function
LER 2019-004-01 Loss of Feedwater Heating Results in Loss of Safety      11/06/2019
Function
25
}}
}}

Revision as of 06:01, 18 January 2022

Integrated Inspection Report 05000440/2020004
ML21043A176
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 02/12/2021
From: Billy Dickson
NRC/RGN-III
To: Penfield R
Energy Harbor Nuclear Corp
References
IR 2020004
Download: ML21043A176 (28)


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