ML18004B829: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(One intermediate revision by the same user not shown)
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:REGULATORY INFORMATION DISTR IBU N SYSTEM (R IDS)'%l'2a ,'ACCESSION NBR: 870605 252 DOC.DATk'//05/26 NOTA IZED: NO l FACIL: 50-400 Sheav on Harv is Nuclear Pover Planti Unit ii Carolina AUTH.NA~iE AUTHOR AFFILIATION SCHWABENBAUER Cav o 1 in a P over 8<L i g h+C o.WATSON R.A.Cav olina Power 8<Light Co.RECIP.NAME RECIPIENT AFFILIATIV'j DOCKET 05000400 SUB JECT: LER 87-027-00:
{{#Wiki_filter:REGULATORY INFORMATION DISTR IBU               N SYSTEM (R IDS)
on 870426'uv ing test>v'edundant transmitter pv'essuri zer pressuv e channels dec lav'ed inopev able.Caused bg t~o out of thv ee channels ou+of calibv 0 v eading low.Channels v ecalibv'k test corp leted.W/870526 ltv'.DISTRIBUTION CODE: IE22D, COPIES RFCF IVEU: LTR ENCL SI ZF: TITLE: 50.73 Licensee Event Repov t (L~H>i Incident Rpt>etc~NOTES: Application for pev mit v eneval f iled.05000400 RECIPIENT ID CODE/NAME PD2-1 LA BUCKLEY, B INTERNAL: ACRS MI CHELSON AEOD/DOA AEOD/DSP/TPAB NRR/DEST/ADE NRR/DEST/CEB NRR/DEBT/ICSB NRR/DEST/MTB NRR/DEST/RSB NRR/DLPG/HFB NRR/DOEA/EAB NRR/DREP/RPB NRR/PMAS/PTSB RES DEPY QI EXTERNAL: EQS(Q QROH, M LPDR NSIC-HARRIS, J COPIES LTTR ENCL 1 1 1 1 1 1 1 0 1 1 1 1 1 1 1 1 2'1 1 1 1 5 5 1 1 1 1'ECIPIENT ID CODE/MANE PD2-1 PD*CRS MOELLER AFOD/DSP/ROAB DEXTRO NwR/DEST/ADS NRR/DEST/ELB NRR/DEST/MEG NRR/DEST/PSB NRR/DEST/SGB NRR/DLPG/GAB
'%l   '2a
!'!RR/DREP/RAB NR.-ILRB REC FILE 02 CN2 FILE 01 H ST LOBBY WARD NHC PDR<!SIC MAYST Q COPIES LTTR ENCL 1 2 2 2 2 1 1 0 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 TOTAL NUMBER OF COPIES REQUIRED: LT1R 42 ENCL 40 NRC Form 355 (94)3)I~LICENSEE EVENT REPORT (LER)U.S.NUCLEAR REOULATORY COMMISSION APPROVED OMB NO.3)500104 EXPIRES: 5/31/SS FACILITY NAME (T)Shearon Harris Plant Unit 1 TITLE (4)Pressurizer Pressure Channels Inoperable DOCKET NUMBER (2)0 5 0 0 0 4 PA E 3 1OF02 EVENT DATE (5)DAY YEAR YEAR Pg MONTH LER NUMBER (5)REPORT DATE (7)SEQUENTtAL NUMBER REVN~MONTH?.Sse NUMBER DAY YEAR DOCKET NUMBER(S)0 5 0 0 0 FACILITY NAMES OTHER FACILITIES INVOLVED (5)0 4 26 878 7 2 7 00 05 2 687 0 5 0 0 0 OPERATINO MODE (9)POWER LEYEL 1 0 0 g''Rr.....y S.r'g;,4r 20A02(lr)20.405(e)(1)(I)20AOS(e)(1)
,'ACCESSION NBR: 870605 252             DOC. DATk'//05/26         NOTA IZED: NO             DOCKET l FACIL: 50-400     Sheav on Harv is Nuclear Pover Planti Unit             ii Carolina     05000400 AUTH. NA~iE           AUTHOR AFFILIATION SCHWABENBAUER                                 i Cav o 1 in a P over 8< L g h+ C o.
(9)20AOS(~I(1)I III I 20.405(e)(I)(lv)20.405(e)(I)(v)20.405(c)50M(c)(I)50.35(c)(2)50.73(e)(2)(I)*50.73(e)(2)(9)50.73(c)(2)(ill l LICENSEE CONTACT FOR THIS LER (12)50,73(s)(2)(iv)50.73(e)(2)(v) 50.73(c)(2)(vii)50.73(e)(2)(vill)(A)50.73(e)(2)(vill)(5)50.73(~)(2)(x)THIS REPORT IS SUBMITTED PURSUANT T 0 THE REQUIREMENTS OF 10 CFR gr (Check one or more of the folios(lop)
WATSON R. A.         Cav olina Power 8< Light Co.
(11 73.71(II)73.71(c)OTHER (Specify In Ahstrect INlovr end ln Text, HRC Form 388AI NAME Richard Schwabenbauer
RECIP. NAME           RECIPIENT AFFILIATIV'j SUB JECT: LER   87-027-00: on 870426'uv ing test> v'edundant transmitter pv'essuri zer pressuv e channels dec lav'ed inopev able. Caused           bg t~o out of thv ee channels ou+ of calibv 0 v eading low.
-Regulatory Compliance TELEPHONE NUMBER AREA CODE 9 19 362-2 69 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFAC.TURER'" y~CpScy.REPORTABLE rc~TO NPRDS.:.r.CAUSE SYSTEM COMPONENT MANUFAC.TURER EPORTABLE TO NPRDS wm SUPPLEMENTAL REPORT EXPECTED (14)EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR YES (If yes, complere EXPECTED SII84tISSIOH DA TEI NO ABSTRACT (Limit to f400 sprees, I e., epproxlmetely fifteen slnple-specs typevrritten linNI (15)ABSTRACT On April 26, 1987 the plant was operating at 100 percent power in Node 1.Pressurizer Pressure Channel PT-455 was being tested.It was thought to be out of calibration (reading high), but was found to be correct.At 0930 hours, as a result of conducting the test on PT-455, two other channels, PT-456 and PT-457 were found to oe out, of calibration, reading low, and declared inoperable.
Channels v ecalibv'k test corp leted. W/870526 ltv'.
All three channels are redundant transmitters for Pressurizer pressure.Technical Specifications permit only one channel to be inoperable at a time.Therefore, at 1008 hours, actions were commenced to satisfy the prerequisites of GP-006, Normal Plant Shutdown for Power Operation to Hot Standby (Mode 1 to Mode 3), to satisfy Technical Specification Action 3.0.3.Priority 1 work requests were immediately initiated to recalibrate the two inoperable channels per the appropriate Maintenance Surveillance Tests (MST).MST-I0120 was successfully completed at 1140 hours and Channel PT-456 was declared operable.With two operable channels, Technical Specifications allowed continued plant operation under Table 3.3-3, Action 15.MST-I0121 was successfully completed at 1615 hours and Channel PT-457 was declared operable.870b050252 87052b PDR ADOCK 05000400 9 PDR NRC rerm erro NRC Form~(84(31 LICE SEE ENT REPORT (LER)TEXT CONTINUA ION U.S.NUCLEAR REGULATORY COMMISSION APPROVED OMS NO.3150&(04 EXPIRES: 8/31/88 FACILITY NAME l'll Sheyron Harris Plant Unit 1 DOCKET NUMBER (2)LER NUMBER (61 YEAR>X j SEGVENTIAL Na: REVISION CWX>NVMSER I/PS NUMBER PAGE (31 TEXT/Hm<<o<<>>co/I roEvie4 I>>o ER/E/<<>>/HRC F<<IR 36843/(ill DESCRIPTION 0 5 0 0 0 4 0 0 8 7 027-00 0 2 0 2 On April 26, 1987 the plant was operating at 100 percent power in Mode 1.Pressurizer Pressure Channel PT-455 was being tested.It was thought to be out of calibration, (reading high)but was found to be correct.At 0930 hours, as a result of this test, it was found the other two Channels, PT-456 and PT-457, were out of calibration reading low, and were declared inoperable.
DISTRIBUTION CODE: IE22D, COPIES RFCF IVEU: LTR                   ENCL     SI ZF:
TITLE: 50. 73 Licensee Event Repov t (L~H >i Incident Rpt> etc               ~
NOTES: Application for       pev mit v eneval   f iled.                                 05000400 RECIPIENT             COPIES                                  COPIES ID CODE/NAME           LTTR ENCL          ID CODE/MANE        LTTR ENCL PD2-1 LA                   1    1      PD2-1 PD                1 BUCKLEY, B                       1 INTERNAL: ACRS MICHELSON 1'ECIPIENT 1      *CRS MOELLER            2      2 AEOD/DOA                   1            AFOD/DSP/ROAB            2      2 AEOD/DSP/TPAB               1    1      DEXTRO                  1 NRR/DEST/ADE                     0      NwR/DEST/ADS            1      0 NRR/DEST/CEB               1    1      NRR/DEST/ELB            1      1 NRR/DEBT/ICSB              1    1      NRR/DEST/MEG            1      1 NRR/DEST/MTB                      1      NRR/DEST/PSB            1      1 NRR/DEST/RSB                      1      NRR/DEST/SGB            1      1 NRR/DLPG/HFB                      1       NRR/DLPG/GAB            1     1 NRR/DOEA/EAB                      1       !'!RR/DREP/RAB          1     1 NRR/DREP/RPB                2'           NR - .      ILRB        1     1 NRR/PMAS/PTSB              1     1       REC    FILE      02      1     1 RES DEPY QI                1     1         CN2    FILE 01        1      1 EXTERNAL:      EQS(Q QROH, M              5    5      H ST LOBBY WARD          1      1 LPDR                        1    1      NHC PDR                  1      1 NSIC -HARRIS, J            1            <!SIC MAYST Q TOTAL NUMBER OF COPIES REQUIRED:            LT1R      42    ENCL   40
 
NRC Form 355 (94)3)
I~                                U.S. NUCLEAR REOULATORY COMMISSION APPROVED OMB NO. 3)500104 EXPIRES: 5/31/SS LICENSEE EVENT REPORT (LER)
FACILITY NAME (T)                                                                                                                           DOCKET NUMBER (2)                              PA E  3 Shearon Harris Plant Unit                                   1                                                                       0    5      0    0      0 4              1OF02 TITLE (4)
Pressurizer Pressure Channels Inoperable EVENT DATE (5)                       LER NUMBER (5)                               REPORT DATE (7)                         OTHER FACILITIES INVOLVED (5)
MONTH      DAY        YEAR    YEAR          SEQUENTtAL                REVN~ MONTH DAY                 YEAR           FACILITYNAMES                              DOCKET NUMBER(S)
Pg NUMBER ?.Sse NUMBER 0   5   0     0 0 0 4        26 878                   7                   2 7             00 05               2         687                                                         0   5   0     0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT T 0 THE REQUIREMENTS OF 10 CFR gr (Check one or more                        of the folios(lop) (11 MODE (9)                     20A02(lr)                                       20.405(c)                          50,73(s) (2) (iv)                                73.71(II)
POWER                            20.405(e)(1) (I)                                 50M(c) (I)                         50.73(e)(2)(v)                                   73.71(c)
LEYEL 1    0 0          20AOS(e)(1) (9)                                  50.35(c) (2)                       50.73(c) (2) (vii)                               OTHER (Specify In Ahstrect INlovrend ln Text, HRC Form g'      '
20AOS( ~ I(1) I IIII                            50.73(e) (2) (I)                   50.73(e) (2) (vill)(A)                          388AI Rr.....y S. r'g;,4r 20.405(e ) (I ) (lv) 20.405(e) (I ) (v) 50.73(e) (2) (9) 50.73(c) (2) (illl 50.73(e) (2) (vill)(5) 50.73( ~ )(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
NAME                                                                                                                                                                TELEPHONE NUMBER AREA CODE Richard Schwabenbauer                              Regulatory                  Compliance                                                9    19          362 -2                    69 MANUFAC.             REPORTABLE COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) y~CpScy.
rc ~                                                  MANUFAC.            EPORTABLE CAUSE    SYSTEM      COMPONENT                                    TO NPRDS                              CAUSE SYSTEM  COMPONENT TURER                                                                                                TURER              TO NPRDS wm
                                                                                                    .r.
SUPPLEMENTAL REPORT EXPECTED (14)                                                                                         MONTH    DAY      YEAR EXPECTED SUBMISSION DATE (15)
YES (If yes, complere EXPECTED SII84tISSIOH DA TEI                                            NO ABSTRACT (Limit to f400 sprees,  I e., epproxlmetely    fifteen slnple-specs typevrritten linNI (15)
ABSTRACT On    April 26, 1987 the plant was operating at 100 percent power in Node 1.
Pressurizer Pressure Channel PT-455 was being tested. It was thought to be out of calibration (reading high), but was found to be correct. At 0930 hours, as a result of conducting the test on PT-455, two other channels, PT-456 and PT-457 were found to oe out, of calibration, reading low, and declared inoperable. All three channels are redundant transmitters for Pressurizer pressure.
Technical Specifications permit only one channel to be inoperable at a time.
Therefore, at 1008 hours, actions were commenced to satisfy the prerequisites of GP-006, Normal Plant Shutdown for Power Operation to Hot Standby (Mode 1 to Mode 3), to satisfy Technical Specification Action 3.0.3.                                                                         Priority 1 work requests were immediately initiated to recalibrate the two inoperable channels per the appropriate Maintenance Surveillance Tests (MST).
MST-I0120 was                 successfully completed at                                     1140 hours and Channel                         PT-456 was declared operable. With two operable channels, Technical Specifications allowed continued plant operation under Table 3.3-3, Action 15.
MST-I0121 was                 successfully completed at                                     1615 hours and Channel                         PT-457 was declared operable.
870b050252 87052b PDR           ADOCK 05000400 9                                         PDR NRC rerm erro
 
NRC Form (84(31
        ~                        LICE SEE             ENT REPORT (LER) TEXT CONTINUA ION U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO. 3150&(04 EXPIRES: 8/31/88 FACILITYNAME l'll                                                   DOCKET NUMBER (2)               LER NUMBER (61                     PAGE (31 YEAR >X j SEGVENTIAL Na: REVISION Sheyron Harris Plant                                                                    CWX>   NVMSER   I/PS NUMBER Unit 027 00 1
0  5  0  0    0 4 0 0 8 7                                    0 2        0    2 TEXT /Hm<<o <<>>co /I roEvie4 I>>o ER/E/<<>>/HRC F<<IR 36843/ (ill DESCRIPTION On   April 26, 1987 the plant was operating at 100 percent power in Mode 1.
Pressurizer Pressure Channel PT-455 was being tested. It was thought to be out of calibration, (reading high) but was found to be correct. At 0930 hours, as a result of this test,                       it was found the other two Channels, PT-456 and PT-457, were out of calibration reading low, and were declared inoperable.
All three channels are redundant transmitters for Pressurizer pressure and have bistables for the following trips and interlock:
All three channels are redundant transmitters for Pressurizer pressure and have bistables for the following trips and interlock:
g 2,385 psig Reactor Trip-High Pressure Q 2,000 psig P-11 Interlock g 1,960 psig Reactor Trip-Low Pressure Q 1,850 psig Safety Injection Signal For continued plant operation, Technical Specifications permit only one channel to be inoperable at a time.Therefore, at 1008 hours, actions were commenced to satisfy the prerequisites of GP-006 Normal Plant Shutdown from Power Operation to Hot Standby (Mode 1 to Mode 3)in compliance with Technical Specification Action 3.0.3.Priority 1 Work Requests to run the applicable Maintenance Surveillance Tests (MST)to recalibrate the inoperable channels were immediately initiated.
g 2,385       psig Reactor Trip High Pressure Q   2,000 psig P-11 Interlock g 1,960 psig Reactor Trip Low Pressure Q 1,850 psig Safety Injection Signal For continued plant operation, Technical Specifications permit                                 only one channel to be inoperable at a time. Therefore, at 1008 hours,                                   actions were commenced to satisfy the prerequisites of GP-006 Normal Plant                                   Shutdown from Power Operation to Hot Standby (Mode 1 to Mode 3) in compliance                                 with Technical Specification Action 3.0.3.
At 1140 hours, MST-I0120 was successfully completed for Channel PT-456 and declared operable.With two operable channels, Technical Specifications allowed continued plant operation under Table 3.3-3, Action 15.At 1615 hours, MST-I0121 was successfully completed for Channel PT-457 and declared operable.CAUSE The cause of the event was that two out of the three channels for the Pressurizer Pressure drifted low.The transmitters were recalibrated successfully.
Priority         1 Work Requests               to run the applicable Maintenance Surveillance Tests (MST)       to recalibrate the inoperable channels were immediately initiated.
ANALYSIS This event is reportable under 10CFR50.73(a)(2)(i)(B) because the plant entered Technical Specification Action 3.0.3.CORRECTIVE ACTION: 1)Channel PT-456 was correctly calibrated via WR&A 88-DYD174.
At 1140 hours, MST-I0120 was successfully completed for Channel PT-456 and declared operable. With two operable channels, Technical Specifications allowed continued plant operation under Table 3.3-3, Action 15.
2)Channel PT"457 was correctly calibrated via WR&A 88-JOR237.
At 1615 hours, MST-I0121 was successfully completed                             for Channel PT-457 and declared operable.
NRC FORM 366A (SELT I*U.S.GPO/I QSO-0-624 538/455 Carolina Power&Light Company HARRIS NUCLEAR PROJECT P.O.Box 165 New Hill, NC 27562 MAY 26 198T File Number'SHF/10-13510C Letter Number: HO-870441 (0)U.S.Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO.50-400 LICENSE NO.NPF-63 LICENSEE EVENT REPORT 87-027-00 Gentlemen'.
CAUSE The cause           of the event was that two out of the three channels for the Pressurizer Pressure drifted low. The transmitters were recalibrated successfully.
In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted.
ANALYSIS This event is reportable under 10CFR50.73(a)(2)(i)(B) because the plant entered Technical Specification Action 3.0.3.
This report fulfills the requirement for a written report within thirty (30)days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September, 1983.Very truly yours, RAW:sdg Enclosure R.A.Watson Vice President Harris Nuclear Project cc: Dr.J.Nelson Grace (NRC-RII)Mr.B.Buckley (NRR)Mr.G.Maxwell (NRC-SHNPP)MEM/HO-8704410/PAGE 1/Osl}}
CORRECTIVE ACTION:
: 1)       Channel PT-456 was             correctly calibrated via     WR&A   88-DYD174.
: 2)       Channel PT"457 was             correctly calibrated via     WR&A   88-JOR237.
NRC FORM 366A                                                                                                             *U.S.GPO/I QSO-0-624 538/455 (SELT I
 
Carolina Power & Light Company HARRIS NUCLEAR PROJECT P.O. Box 165 New   Hill,   NC   27562 MAY 26   198T File Number'SHF/10-13510C Letter Number: HO-870441 (0)
U.S. Nuclear Regulatory Commission ATTN:   NRC Document Control Desk Washington, DC   20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 87-027-00 Gentlemen'.
In accordance with Title     10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report fulfills the requirement for a written report within thirty (30) days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September, 1983.
Very   truly yours, R. A. Watson Vice President Harris Nuclear Project RAW:sdg Enclosure cc: Dr. J. Nelson Grace (NRC       RII)
Mr. B. Buckley (NRR)
Mr. G. Maxwell (NRC SHNPP)
MEM/HO-8704410/PAGE   1/Osl}}

Latest revision as of 21:29, 3 February 2020

LER 87-027-00:on 870426,during Test,Redundant Transmitter Pressurizer Pressure Channels Declared Inoperable.Caused by Two Out of Three Channels Out of Calibr & Reading Low. Channels Recalibr & Test completed.W/870526 Ltr
ML18004B829
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 05/26/1987
From: Schwabenbauer, Watson R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
HO-870441-(O), LER-87-027, LER-87-27, NUDOCS 8706050252
Download: ML18004B829 (4)


Text

REGULATORY INFORMATION DISTR IBU N SYSTEM (R IDS)

'%l '2a

,'ACCESSION NBR: 870605 252 DOC. DATk'//05/26 NOTA IZED: NO DOCKET l FACIL: 50-400 Sheav on Harv is Nuclear Pover Planti Unit ii Carolina 05000400 AUTH. NA~iE AUTHOR AFFILIATION SCHWABENBAUER i Cav o 1 in a P over 8< L g h+ C o.

WATSON R. A. Cav olina Power 8< Light Co.

RECIP. NAME RECIPIENT AFFILIATIV'j SUB JECT: LER 87-027-00: on 870426'uv ing test> v'edundant transmitter pv'essuri zer pressuv e channels dec lav'ed inopev able. Caused bg t~o out of thv ee channels ou+ of calibv 0 v eading low.

Channels v ecalibv'k test corp leted. W/870526 ltv'.

DISTRIBUTION CODE: IE22D, COPIES RFCF IVEU: LTR ENCL SI ZF:

TITLE: 50. 73 Licensee Event Repov t (L~H >i Incident Rpt> etc ~

NOTES: Application for pev mit v eneval f iled. 05000400 RECIPIENT COPIES COPIES ID CODE/NAME LTTR ENCL ID CODE/MANE LTTR ENCL PD2-1 LA 1 1 PD2-1 PD 1 BUCKLEY, B 1 INTERNAL: ACRS MICHELSON 1'ECIPIENT 1 *CRS MOELLER 2 2 AEOD/DOA 1 AFOD/DSP/ROAB 2 2 AEOD/DSP/TPAB 1 1 DEXTRO 1 NRR/DEST/ADE 0 NwR/DEST/ADS 1 0 NRR/DEST/CEB 1 1 NRR/DEST/ELB 1 1 NRR/DEBT/ICSB 1 1 NRR/DEST/MEG 1 1 NRR/DEST/MTB 1 NRR/DEST/PSB 1 1 NRR/DEST/RSB 1 NRR/DEST/SGB 1 1 NRR/DLPG/HFB 1 NRR/DLPG/GAB 1 1 NRR/DOEA/EAB 1  !'!RR/DREP/RAB 1 1 NRR/DREP/RPB 2' NR - . ILRB 1 1 NRR/PMAS/PTSB 1 1 REC FILE 02 1 1 RES DEPY QI 1 1 CN2 FILE 01 1 1 EXTERNAL: EQS(Q QROH, M 5 5 H ST LOBBY WARD 1 1 LPDR 1 1 NHC PDR 1 1 NSIC -HARRIS, J 1 <!SIC MAYST Q TOTAL NUMBER OF COPIES REQUIRED: LT1R 42 ENCL 40

NRC Form 355 (94)3)

I~ U.S. NUCLEAR REOULATORY COMMISSION APPROVED OMB NO. 3)500104 EXPIRES: 5/31/SS LICENSEE EVENT REPORT (LER)

FACILITY NAME (T) DOCKET NUMBER (2) PA E 3 Shearon Harris Plant Unit 1 0 5 0 0 0 4 1OF02 TITLE (4)

Pressurizer Pressure Channels Inoperable EVENT DATE (5) LER NUMBER (5) REPORT DATE (7) OTHER FACILITIES INVOLVED (5)

MONTH DAY YEAR YEAR SEQUENTtAL REVN~ MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(S)

Pg NUMBER ?.Sse NUMBER 0 5 0 0 0 0 4 26 878 7 2 7 00 05 2 687 0 5 0 0 0 OPERATINO THIS REPORT IS SUBMITTED PURSUANT T 0 THE REQUIREMENTS OF 10 CFR gr (Check one or more of the folios(lop) (11 MODE (9) 20A02(lr) 20.405(c) 50,73(s) (2) (iv) 73.71(II)

POWER 20.405(e)(1) (I) 50M(c) (I) 50.73(e)(2)(v) 73.71(c)

LEYEL 1 0 0 20AOS(e)(1) (9) 50.35(c) (2) 50.73(c) (2) (vii) OTHER (Specify In Ahstrect INlovrend ln Text, HRC Form g' '

20AOS( ~ I(1) I IIII 50.73(e) (2) (I) 50.73(e) (2) (vill)(A) 388AI Rr.....y S. r'g;,4r 20.405(e ) (I ) (lv) 20.405(e) (I ) (v) 50.73(e) (2) (9) 50.73(c) (2) (illl 50.73(e) (2) (vill)(5) 50.73( ~ )(2)(x)

LICENSEE CONTACT FOR THIS LER (12)

NAME TELEPHONE NUMBER AREA CODE Richard Schwabenbauer Regulatory Compliance 9 19 362 -2 69 MANUFAC. REPORTABLE COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) y~CpScy.

rc ~ MANUFAC. EPORTABLE CAUSE SYSTEM COMPONENT TO NPRDS CAUSE SYSTEM COMPONENT TURER TURER TO NPRDS wm

.r.

SUPPLEMENTAL REPORT EXPECTED (14) MONTH DAY YEAR EXPECTED SUBMISSION DATE (15)

YES (If yes, complere EXPECTED SII84tISSIOH DA TEI NO ABSTRACT (Limit to f400 sprees, I e., epproxlmetely fifteen slnple-specs typevrritten linNI (15)

ABSTRACT On April 26, 1987 the plant was operating at 100 percent power in Node 1.

Pressurizer Pressure Channel PT-455 was being tested. It was thought to be out of calibration (reading high), but was found to be correct. At 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, as a result of conducting the test on PT-455, two other channels, PT-456 and PT-457 were found to oe out, of calibration, reading low, and declared inoperable. All three channels are redundant transmitters for Pressurizer pressure.

Technical Specifications permit only one channel to be inoperable at a time.

Therefore, at 1008 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.83544e-4 months <br />, actions were commenced to satisfy the prerequisites of GP-006, Normal Plant Shutdown for Power Operation to Hot Standby (Mode 1 to Mode 3), to satisfy Technical Specification Action 3.0.3. Priority 1 work requests were immediately initiated to recalibrate the two inoperable channels per the appropriate Maintenance Surveillance Tests (MST).

MST-I0120 was successfully completed at 1140 hours0.0132 days <br />0.317 hours <br />0.00188 weeks <br />4.3377e-4 months <br /> and Channel PT-456 was declared operable. With two operable channels, Technical Specifications allowed continued plant operation under Table 3.3-3, Action 15.

MST-I0121 was successfully completed at 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br /> and Channel PT-457 was declared operable.

870b050252 87052b PDR ADOCK 05000400 9 PDR NRC rerm erro

NRC Form (84(31

~ LICE SEE ENT REPORT (LER) TEXT CONTINUA ION U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS NO. 3150&(04 EXPIRES: 8/31/88 FACILITYNAME l'll DOCKET NUMBER (2) LER NUMBER (61 PAGE (31 YEAR >X j SEGVENTIAL Na: REVISION Sheyron Harris Plant CWX> NVMSER I/PS NUMBER Unit 027 00 1

0 5 0 0 0 4 0 0 8 7 0 2 0 2 TEXT /Hm<<o <<>>co /I roEvie4 I>>o ER/E/<<>>/HRC F<<IR 36843/ (ill DESCRIPTION On April 26, 1987 the plant was operating at 100 percent power in Mode 1.

Pressurizer Pressure Channel PT-455 was being tested. It was thought to be out of calibration, (reading high) but was found to be correct. At 0930 hours0.0108 days <br />0.258 hours <br />0.00154 weeks <br />3.53865e-4 months <br />, as a result of this test, it was found the other two Channels, PT-456 and PT-457, were out of calibration reading low, and were declared inoperable.

All three channels are redundant transmitters for Pressurizer pressure and have bistables for the following trips and interlock:

g 2,385 psig Reactor Trip High Pressure Q 2,000 psig P-11 Interlock g 1,960 psig Reactor Trip Low Pressure Q 1,850 psig Safety Injection Signal For continued plant operation, Technical Specifications permit only one channel to be inoperable at a time. Therefore, at 1008 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.83544e-4 months <br />, actions were commenced to satisfy the prerequisites of GP-006 Normal Plant Shutdown from Power Operation to Hot Standby (Mode 1 to Mode 3) in compliance with Technical Specification Action 3.0.3.

Priority 1 Work Requests to run the applicable Maintenance Surveillance Tests (MST) to recalibrate the inoperable channels were immediately initiated.

At 1140 hours0.0132 days <br />0.317 hours <br />0.00188 weeks <br />4.3377e-4 months <br />, MST-I0120 was successfully completed for Channel PT-456 and declared operable. With two operable channels, Technical Specifications allowed continued plant operation under Table 3.3-3, Action 15.

At 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br />, MST-I0121 was successfully completed for Channel PT-457 and declared operable.

CAUSE The cause of the event was that two out of the three channels for the Pressurizer Pressure drifted low. The transmitters were recalibrated successfully.

ANALYSIS This event is reportable under 10CFR50.73(a)(2)(i)(B) because the plant entered Technical Specification Action 3.0.3.

CORRECTIVE ACTION:

1) Channel PT-456 was correctly calibrated via WR&A 88-DYD174.
2) Channel PT"457 was correctly calibrated via WR&A 88-JOR237.

NRC FORM 366A *U.S.GPO/I QSO-0-624 538/455 (SELT I

Carolina Power & Light Company HARRIS NUCLEAR PROJECT P.O. Box 165 New Hill, NC 27562 MAY 26 198T File Number'SHF/10-13510C Letter Number: HO-870441 (0)

U.S. Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 LICENSEE EVENT REPORT 87-027-00 Gentlemen'.

In accordance with Title 10 to the Code of Federal Regulations, the enclosed Licensee Event Report is submitted. This report fulfills the requirement for a written report within thirty (30) days of a reportable occurrence and is in accordance with the format set forth in NUREG-1022, September, 1983.

Very truly yours, R. A. Watson Vice President Harris Nuclear Project RAW:sdg Enclosure cc: Dr. J. Nelson Grace (NRC RII)

Mr. B. Buckley (NRR)

Mr. G. Maxwell (NRC SHNPP)

MEM/HO-8704410/PAGE 1/Osl