ML19319B785: Difference between revisions
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d | d LICENSE E E'." NT R EPORT v - | ||
CoNrnoietcCx L, L j i lj t G | CoNrnoietcCx L, L j i lj t G | ||
' ' f.'.' 't" t.CC~se~,-ot. '? '.T ' 5,''~.' | ' ' f.'.' 't" t.CC~se~,-ot. '? '.T ' 5,''~.' | ||
@]2IOIH I DlB 1 Silj i. | @]2IOIH I DlB 1 Silj i. | ||
Line 32: | Line 28: | ||
C a i t cc. ..,o.t s. .u C e noen ,~uo.e. e sc ~, naii . c .o . , o . . e | C a i t cc. ..,o.t s. .u C e noen ,~uo.e. e sc ~, naii . c .o . , o . . e | ||
[ Cowtgg g gg 15 ; 0 ; ._! 0; 3 ;4 i 6 10 i8 i l;5 ! 7 ;7 i i c ; 9: 0;9,77 1 (VEN T Of 5Cnip f EON gi On August 15, 1977, the Main Steam Line 2 Isolation Valve, MS100, closed , | [ Cowtgg g gg 15 ; 0 ; ._! 0; 3 ;4 i 6 10 i8 i l;5 ! 7 ;7 i i c ; 9: 0;9,77 1 (VEN T Of 5Cnip f EON gi On August 15, 1977, the Main Steam Line 2 Isolation Valve, MS100, closed , | ||
7 a2 gl due to a control air leak. This placed the station in the Action Stata "'; | 7 a2 gl due to a control air leak. This placed the station in the Action Stata "'; | ||
7 33 . | 7 33 . | ||
Line 39: | Line 34: | ||
7 99 EL 1 O | 7 99 EL 1 O | ||
CNE nNL Cr%*coar N T Conr 'aS"'* eow El CI D I ( Ej iV I AI L!Vi Oi ?I Sveh("a" ua7v"3;41""d'a 1q i v.o] | CNE nNL Cr%*coar N T Conr 'aS"'* eow El CI D I ( Ej iV I AI L!Vi Oi ?I Sveh("a" ua7v"3;41""d'a 1q i v.o] | ||
7 89 to in 12 i; 43 44 43 4, | 7 89 to in 12 i; 43 44 43 4, CAU5F DESCRIPTION | ||
CAU5F DESCRIPTION | |||
@[ The instrument air moisture trap bowl had failed at the threads. The ; | @[ The instrument air moisture trap bowl had failed at the threads. The ; | ||
i 9 .. | i 9 .. | ||
Line 47: | Line 40: | ||
P | P | ||
] | ] | ||
g | g k . I 7 6G g s i EI''s u % 'o e ' set e s t a t us pe5IENa v osscovt nv ca.se nirvic'e b I IIJ | ||
k . I 7 6G g s i EI''s u % 'o e ' set e s t a t us pe5IENa v osscovt nv ca.se nirvic'e b I IIJ | |||
'b I N '! I DJ ( ,', _] | 'b I N '! I DJ ( ,', _] | ||
7 0 7 to iJ 44 41 46 E3 Nt* s = court %s | 7 0 7 to iJ 44 41 46 E3 Nt* s = court %s | ||
Line 56: | Line 46: | ||
~3 3 3 l_ ZJ , lij 9 50 l | ~3 3 3 l_ ZJ , lij 9 50 l | ||
is NA me l l NA 43 oJ | is NA me l l NA 43 oJ | ||
*t nSoNNEL E XPOSUAt$ | *t nSoNNEL E XPOSUAt$ | ||
Nv** w9 * ' 1 * .C e s.f son | Nv** w9 * ' 1 * .C e s.f son | ||
* 3 1010! | * 3 1010! | ||
7 89 I'l lZ] | 7 89 I'l lZ] | ||
ti i2 | ti i2 OF.S5A iJ bJ rin50NNEL INJU8erE5 NUMO C 84 01 sc . s P f 'Of* | ||
OF.S5A iJ | |||
bJ | |||
rin50NNEL INJU8erE5 NUMO C 84 01 sc . s P f 'Of* | |||
$ 1,01 e, | $ 1,01 e, | ||
0! 01 ! NA [ | 0! 01 ! NA [ | ||
1 | 1 is ia m oF F 5 tit CONSE 0ttt NCES NA> ^ | ||
is ia m oF F 5 tit CONSE 0ttt NCES NA> ^ | |||
i LOSS oH Dauact to F ActLily | i LOSS oH Dauact to F ActLily | ||
] | ] | ||
Line 79: | Line 59: | ||
; @ | ; @ | ||
r a evetZ l NA w | r a evetZ l NA w | ||
I | I fueLICITY i | ||
fueLICITY i | |||
@le, NA - | @le, NA - | ||
m l | m l | ||
apostioNat s aCf ons | apostioNat s aCf ons 8 i NA l | ||
> e . | > e . | ||
tb j 4 | tb j 4 | ||
r ee n NAug Jacque Lingenfelter/ Stan 3atch (4197 259-5000, Ext. 251 PHONC 4 | |||
r ee n | DVR #105-1 8001270M3 | ||
NAug Jacque Lingenfelter/ Stan 3atch (4197 259-5000, Ext. 251 PHONC 4 | |||
DVR #105-1 | |||
8001270M3 | |||
l J | l J | ||
. TOLEDO EDISCN COMPANY C/ DAVIS-3 ESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-55 DATE OF EVENT: August 15, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Main Steam Isolation Valve MS100 failing closed due to control air leak. | . TOLEDO EDISCN COMPANY C/ DAVIS-3 ESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-55 DATE OF EVENT: August 15, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Main Steam Isolation Valve MS100 failing closed due to control air leak. | ||
Conditions Prior to Occurrence: The plant was in Mode 3, with Power (MWT) = 0 and Load (MWE) = 0. | Conditions Prior to Occurrence: The plant was in Mode 3, with Power (MWT) = 0 and Load (MWE) = 0. | ||
Line 114: | Line 75: | ||
(~') | (~') | ||
'' Desiunation of Apoarent Cause of Occurrence: The investigation by Instrument and Control personnel found that the valve operator instrument air coisture trap had f ailed it the plastic bowl threads. This component failure caused a loss of instru-ment air to the valve-which closes (fails safe) without air pressure acting on the operator. | '' Desiunation of Apoarent Cause of Occurrence: The investigation by Instrument and Control personnel found that the valve operator instrument air coisture trap had f ailed it the plastic bowl threads. This component failure caused a loss of instru-ment air to the valve-which closes (fails safe) without air pressure acting on the operator. | ||
Analysis of Occurrence: The purpose of the Main Steam Isolation Valves is to iso-late the affected steam generator in the event of a main steam line break down-stream of the isolation valve. Since the main steam isolation valve failed closed and remained closed, no threat to the health ande. safety of the public or to station personnel occurred. | Analysis of Occurrence: The purpose of the Main Steam Isolation Valves is to iso-late the affected steam generator in the event of a main steam line break down-stream of the isolation valve. Since the main steam isolation valve failed closed and remained closed, no threat to the health ande. safety of the public or to station personnel occurred. | ||
Corrective Action: Maintenance Work Order 77-1695 wa_s writ, ten to investigate the main steam isolation valve closure and repair as needed. It was decided the moisture traps were not needed and should be removed on both main steam isolation e.. es. | Corrective Action: Maintenance Work Order 77-1695 wa_s writ, ten to investigate the main steam isolation valve closure and repair as needed. It was decided the moisture traps were not needed and should be removed on both main steam isolation e.. es. | ||
This work was completed on August 17, 1977. Facility Change Request 77-231 was initiated for written approval of the moisture trap. | This work was completed on August 17, 1977. Facility Change Request 77-231 was initiated for written approval of the moisture trap. | ||
G | G | ||
'/- Failure Data: No previous similar events have occurred. | '/- Failure Data: No previous similar events have occurred. | ||
1 - | 1 - | ||
l}} | l}} |
Revision as of 05:31, 1 February 2020
ML19319B785 | |
Person / Time | |
---|---|
Site: | Davis Besse |
Issue date: | 09/09/1977 |
From: | Batch S, Lingenfelter J TOLEDO EDISON CO. |
To: | |
Shared Package | |
ML19319B687 | List: |
References | |
NUDOCS 8001270253 | |
Download: ML19319B785 (2) | |
Text
_
d LICENSE E E'." NT R EPORT v -
CoNrnoietcCx L, L j i lj t G
' ' f.'.' 't" t.CC~se~,-ot. '? '.T ' 5,~.'
@]2IOIH I DlB 1 Silj i.
[0 l 0[ j 0l 01 "! ?!?I-101a 3l is m
]4 ! 1[lj l l!j2 id lyA i
l
! ... .o..
C a i t cc. ..,o.t s. .u C e noen ,~uo.e. e sc ~, naii . c .o . , o . . e
[ Cowtgg g gg 15 ; 0 ; ._! 0; 3 ;4 i 6 10 i8 i l;5 ! 7 ;7 i i c ; 9: 0;9,77 1 (VEN T Of 5Cnip f EON gi On August 15, 1977, the Main Steam Line 2 Isolation Valve, MS100, closed ,
7 a2 gl due to a control air leak. This placed the station in the Action Stata "';
7 33 .
g j ment of Technical Specification 3.7.1.5. The valve was declared inopera i n3
@] ble and left in the closed position. (NF-33-77-55) }
7 99 EL 1 O
CNE nNL Cr%*coar N T Conr 'aS"'* eow El CI D I ( Ej iV I AI L!Vi Oi ?I Sveh("a" ua7v"3;41""d'a 1q i v.o]
7 89 to in 12 i; 43 44 43 4, CAU5F DESCRIPTION
@[ The instrument air moisture trap bowl had failed at the threads. The ;
i 9 ..
@l89valve closes on a loss of instrument air.
P
]
g k . I 7 6G g s i EIs u % 'o e ' set e s t a t us pe5IENa v osscovt nv ca.se nirvic'e b I IIJ
'b I N '! I DJ ( ,', _]
7 0 7 to iJ 44 41 46 E3 Nt* s = court %s
<*f t t a5E D os at i.t Ast muouN1 or at tevetv LOCAt eeN c' et Lt ast
~3 3 3 l_ ZJ , lij 9 50 l
is NA me l l NA 43 oJ
- t nSoNNEL E XPOSUAt$
Nv** w9 * ' 1 * .C e s.f son
- 3 1010!
7 89 I'l lZ]
ti i2 OF.S5A iJ bJ rin50NNEL INJU8erE5 NUMO C 84 01 sc . s P f 'Of*
$ 1,01 e,
0! 01 ! NA [
1 is ia m oF F 5 tit CONSE 0ttt NCES NA> ^
i LOSS oH Dauact to F ActLily
]
otsc.i. tion
- @
r a evetZ l NA w
I fueLICITY i
@le, NA -
m l
apostioNat s aCf ons 8 i NA l
> e .
tb j 4
r ee n NAug Jacque Lingenfelter/ Stan 3atch (4197 259-5000, Ext. 251 PHONC 4
DVR #105-1 8001270M3
l J
. TOLEDO EDISCN COMPANY C/ DAVIS-3 ESSE UNIT ONE NUCLEAR POWER STATION SUPPLEMENTAL INFORMATION FOR LER NP-33-77-55 DATE OF EVENT: August 15, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Main Steam Isolation Valve MS100 failing closed due to control air leak.
Conditions Prior to Occurrence: The plant was in Mode 3, with Power (MWT) = 0 and Load (MWE) = 0.
Description of Occurrence: At 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> on August 15, 1977, Main Steam Line 2 Isolation Valve MS100 closed due to a control air leak. This placed the station in the Action Statement of Technical Specification 3.7.1.5 which requires both Main Steam Isolation Valves to be operable in Mode 3, Hot Standby.
Main Steam Isolation valve MS100 was declared inoperable and left in the closed position. Station Instrument and Control personnel were notified of the failure.
(~')
Desiunation of Apoarent Cause of Occurrence: The investigation by Instrument and Control personnel found that the valve operator instrument air coisture trap had f ailed it the plastic bowl threads. This component failure caused a loss of instru-ment air to the valve-which closes (fails safe) without air pressure acting on the operator.
Analysis of Occurrence: The purpose of the Main Steam Isolation Valves is to iso-late the affected steam generator in the event of a main steam line break down-stream of the isolation valve. Since the main steam isolation valve failed closed and remained closed, no threat to the health ande. safety of the public or to station personnel occurred.
Corrective Action: Maintenance Work Order 77-1695 wa_s writ, ten to investigate the main steam isolation valve closure and repair as needed. It was decided the moisture traps were not needed and should be removed on both main steam isolation e.. es.
This work was completed on August 17, 1977. Facility Change Request 77-231 was initiated for written approval of the moisture trap.
G
'/- Failure Data: No previous similar events have occurred.
1 -
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