LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORVML18016A344 |
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Site: |
Harris |
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Issue date: |
03/12/1998 |
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From: |
Verrilli M CAROLINA POWER & LIGHT CO. |
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To: |
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Shared Package |
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ML18016A343 |
List: |
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References |
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LER-97-021, LER-97-21, NUDOCS 9803180350 |
Download: ML18016A344 (5) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:RO)
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18022B0551998-05-20020 May 1998 LER 98-005-00:on 980420,TS Verbatim non-compliance Was Determined.Caused by Misinterpretation of TS Requirements. Issued Memo to Reemphasize Need to Comply W/Literal Meaning of TS Requirements in Verbatim manner.W/980520 Ltr ML18016A4061998-04-30030 April 1998 LER 98-002-01:on 980121,determined Ssps (P-11 Permissive) Testing Deficiency.Caused by Inadequate Review of Initial Ts.Will Revise & Perform Surveillance Test Procedures to Verify Operability of P-11 Permissive ML18016A3841998-04-13013 April 1998 LER 98-004-00:on 980313,design Deficiency Related to Indequate Runout Protection for Turbine Driven AFW Pump Was Identified.Caused by Inadequate Original AFW Sys Design. Evaluation (ESR 98-00100) Will Be completed.W/980409 Ltr ML18016A3441998-03-12012 March 1998 LER 97-021-02:on 980210,identified Failure to Properly Test non-safety Related Pressurizer Porv.Caused by Inadequate Surveillance Test Procedures.Revised Operations Surveillance Test OST-1117 to Include Testing of Subject PORV ML18016A3291998-02-27027 February 1998 LER 98-003-00:on 980129,failure to Perform Shutdown Margin Calculation Required by TS Surveillance Requirements Occurred.Caused by Ambiguity in TS 3.1.3.1.c.Procedures revised.W/980227 Ltr ML18016A3211998-02-20020 February 1998 LER 98-002-00:on 980121,solid State Protection Sys Testing Deficiency Occurred.Caused by Inadequate Review of Initial Tech Specs.Ts Testing Frequency for P-11 Permissive Revised. W/980217 Ltr ML18016A3131998-02-0909 February 1998 LER 98-001-00:on 980109,potential Condition Outside Design Basis Related to Instrument Air Sys Leak Causing SG pre- Heater Bypass Isolation Valves to Be Inoperable Was Noted. Caused by Inadequate Design Control.Generated Jco 98-01 ML18016A2641997-12-18018 December 1997 LER 97-024-00:on 971118,SSPS Testing Deficiency Was Noted. Caused by Inadequate Testing Scheme Provided by Ssps Vendor. Revised procedure.W/971218 Ltr ML18016A2501997-11-24024 November 1997 LER 97-023-00:on 920721,RCS PIV Testing Deficiency Was Noted.Caused by Failure to Consider All Testing Variables During Initial Sp Development.Surveillance Tp OST-1506 Was Revised to Incorporate Correction factor.W/971124 Ltr ML18016A2201997-10-22022 October 1997 LER 97-021-01:on 970922,discovered That Spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements.Revised Daily Surveillance Procedures ML18016A2081997-10-14014 October 1997 LER 97-016-01:on 970608,reactor Trip Occurred,Due to Personnel Error While Attempting to Adjust Power Range Nuclear Instrumentation Channel Following Performance of Calorimetric.Procedures revised.W/971014 Ltr ML18016A2111997-10-14014 October 1997 LER 96-008-02:on 960425,turbine Trip/Reactor Trip Occurred. Caused by High Resistance Connection Resulting from a Phase Switch Jaw & Blade Contacts.Failed a Phase Disconnect Switch on Breaker 52-7 Replaced ML18016A1931997-09-29029 September 1997 LER 97-022-00:on 970829,TS Required Shutdown Due to Expiration of AFW Lco.Caused by Personnel Error.Completed Repairs TDAFW Pump & Returned Plant to Svc on 970831. W/970926 Ltr ML18016A1891997-09-12012 September 1997 LER 97-020-00:on 970814,inadequate Fire Protection Provided for safety-related EDG Fuel Oil Transfer Pump Cables Resulted in Operation Outside Design Basis.Caused by Engineering Oversight.Established Fire watches.W/970912 Ltr ML18016A1881997-09-12012 September 1997 LER 97-021-00:on 970814,spent Fuel Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Misinterpretation of Ts.Directions Provided to Operations.W/970912 Ltr ML18012A8641997-08-18018 August 1997 LER 97-019-00:on 970720,turbine Trip/Reactor Trip Occurred. Caused by Three Phase Fault That Collapsed Excitation Field in Main Generator,Resulting in Generator Lockout.Exciter Rotor Assembly Was replaced.W/970818 Ltr ML18012A8581997-08-0808 August 1997 LER 96-018-01:on 960903,manual Reactor Trip Occurred Due to Loss of Normal Sw.Caused by Mechanical Failure of B Water Pump & a Normal SW to Remain Running Once Manually Started.Restored a Normal SW Pump to Svc ML18012A8551997-08-0808 August 1997 LER 96-013-02:on 961028,condition Outside of Design Basis Where RWST Had Been Aligned w/non-seismically Qualified Sys Was Identified.Caused by Failure to Reconcile Operating Procedure Lineups.Established Administrative Controls ML18012A8471997-07-31031 July 1997 LER 97-018-00:on 970701,determined That Plant Procedures Had Not Received Proper Reviews & Approvals.Caused by Failure to Comply W/Plant Administrative Procedure AP-006.Counseled Involved individuals.W/970731 Ltr ML18012A8371997-07-24024 July 1997 LER 97-S01-00:on 970405,unescorted Access Inappropriately Granted to Contract Outage Workers Was Determined.Caused by Personnel Error.Access Files for Individuals Inappropriately Granted Unescorted Access Were Placed on Access Hold ML18012A8291997-07-11011 July 1997 LER 97-017-00:on 970612,failed to Recognize Inoperable Reactor Afd Monitor.Caused by Personnel Error.Operators Involved in Event Will Be Counseled Prior to Assuming Shift duties.W/970711 Ltr ML18012A8301997-07-0808 July 1997 LER 97-016-00:on 970608,reactor Trip Occurred Due to Personnel Error in Adjusting Power Range (Pr) Nuclear Instrumentation (Ni).Issued Night Order Prohibiting Pr Ni Adjustment When Redundant Channel inoperable.W/970708 Ltr ML18012A8241997-07-0202 July 1997 LER 97-015-00:on 970602,inadequate Auxiliary Feedwater Sys Flow Control Valve Surveillance Testing Deficiency Was Identified.Caused by Failure to Recognize Impact on TS 4.7.1.2.1.Readjusted AFW FCV Actuator spring.W/970702 Ltr ML18022B0181997-06-13013 June 1997 LER 97-014-00:on 970514,SI Occurred During Ssps Surveillance Testing.Caused by Inattention to Detail During Recent Rev to Surveillance Test Procedure Being Used.Revised Deficient Surveillance procedures.W/970613 Ltr ML18012A8081997-06-0909 June 1997 LER 97-013-00:on 970508,entry Into Mode-6 Without Operable Components,Resulting in TS 3.0.4 Violation Occurred.Caused by Personnel Error.Personnel Involved counseled.W/970609 Ltr ML18012A8021997-06-0606 June 1997 LER 97-023-02:on 961114,design Deficiency Was Identified in Emergency DG Protection Circuitry.Caused by Inadequate Plant Design.Revised Surveillance Test Procedures OST-1013 & OST-1073.W/970606 Ltr ML18012A8011997-06-0404 June 1997 LER 97-012-00:on 970505,determined That Previous Auxiliary Control Panel Had Not Verified Operability of Interposing Relays.Caused by Misinterpretation of Tss.Reviewed Other Remote Shutdown Panel Transfer circuitry.W/970604 Ltr ML18012A7951997-05-29029 May 1997 LER 96-023-01:on 961114,design Deficiency in EDG Protection Circuitry Was Identified.Caused by Inadequate Original Plant Design.Surveillance Test Procedures OST-1013 & OST-1073 revised.W/970529 Ltr ML18012A7891997-05-22022 May 1997 LER 97-011-00:on 970422,inappropriate TS Interpretation Resulted in Violations of ECCS Accumulator TS & Entry Into TS 3.0.3.Caused by Procedural Inadequacy.Tsi 88-001 Cancelled 970508 & Procedures revised.W/970522 Ltr ML18012A7871997-05-19019 May 1997 LER 97-010-00:on 970418,design Deficiency Determined Re Reactor Coolant Pump Motor Oil Collection Sys.Caused by RCP Ocs Design Detail.Rcp Ocs Enclosures for Each of Three Installed RCP Motors Have Been modified.W/970519 Ltr ML18012A7761997-05-0707 May 1997 LER 97-009-00:on 970407,fuse Was Removed from CR Ventilation Isolation Signal Power Supply Circuitry Due to Personnel Error.Individuals Involved Were counseled.W/970507 Ltr ML18012A7751997-05-0505 May 1997 LER 97-008-00:on 970404,safety-related AHU Not Declared Inoperable During Maintenance on Associated Temperature Switches Resulting in Violation of Ts.Caused by Incorrect Interpretation.Operations Night Order issued.W/970505 Ltr ML18012A6291997-04-24024 April 1997 LER 97-007-00:on 970325,inoperable CCW Sys TS 3.0.3 Entry Made.Caused by Combination of Procedural Inadequacies, Improper Use of Procedure Guidance & Poor Communication. Applicable Individuals counseled.W/970423 Ltr ML18022B0151997-04-17017 April 1997 LER 97-006-00:on 970318,breach Was Identified in Thermo-Lag Fire Barrier Wall Due to Inadequate Initial Design,Poor Construction Methods & Incomplete as-built Design.Visual Insp of Thermo-Lag Barrier Walls performed.W/970417 Ltr ML18012A6041997-04-0303 April 1997 LER 97-004-00:on 970304,in-plant Spent Fuel Cask Handling Activities Conducted Outside Design Basis.Caused by Lack of Understanding of Requirements.Operations Placed on Hold Pending NRC Review & Approval of procedures.W/970331 Ltr ML18012A6031997-03-31031 March 1997 LER 97-003-00:on 970227,steam Generator Low Level Protection Circuitry Outside Design Basis Occurred.Caused by Inadequate Failure Modes & Effects Analysis Performed as-built Piping Configuration for S/G Level.Review performed.W/970331 Ltr 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18017A9181999-10-0808 October 1999 LER 99-008-00:on 991008,CR Emergency Filtration Sys Tech Specs Occurred.Caused by Site Personnel Failed to Recognize That Blocking Open CR Emergency Filtration Sys.Procedures Revised.With 991008 Ltr ML18017A9151999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Shearon Harris Npp. with 991012 Ltr ML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18017A8671999-09-10010 September 1999 LER 99-007-00:on 990811,determined That Cvis ARMs High Alarm Setpoints Were Not within TS Limit.Caused by Not Having Procedure to Verify If Cvis ARM High Alarm Setpoints Were within TS Requirements.Revised Procedures.With 990910 Ltr ML18017A8621999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Harris Nuclear Plant.With 990908 Ltr ML18016B0481999-08-0404 August 1999 LER 99-006-01:on 981124,noted Failure to Comply with TS 4.0.4 & TS 3/4.6.3, Civs. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Was Revised ML18017A8361999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Shearon Harris Nuclear Power Plant.With 990811 Ltr ML18016B0151999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Shearon Harris Npp. with 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18016A9801999-06-0404 June 1999 LER 99-006-00:on 981124,failed to Comply with TS 4.0.4 & TS 3/4.6.3, Civ. Caused by post-maint Testing That Did Not Adequately Test Control Circuitry & Verify Isolation Time Following Maint.Procedure Will Be Revised.With 990604 Ltr ML18016A9851999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990614 Ltr ML18017A8981999-05-12012 May 1999 Technical Rept Entitled, Harris Nuclear Plant-Bacteria Detection in Water from C&D Spent Fuel Pool Cooling Lines. ML18016A9581999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Shearon Harris Nuclear Plant,Unit 1.With 990513 Ltr ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML18016A9111999-04-12012 April 1999 LER 99-005-00:on 990313,plant Exceeded ESFAS TS 3.3.2,Action 21.Caused by Inadequate Procedure Rev Preparation.Licensee Revised Applicable Maint Surveillance Test Procedure (MST-10072) to Identify TS Required Actions.With 990412 Ltr ML18016A8971999-04-0808 April 1999 LER 99-004-00:on 990312,unit Trip Was Noted.Caused by Degraded Condition of SG Water Level Flow Control Valve. Replaced Positioners on All Three FW Regulating Valves.With 990408 Ltr ML18016A8941999-04-0505 April 1999 Revised Pages 20-25 to App 4A of non-proprietary Version of Rev 3 to HI-971760 ML18016A9101999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Shearon Harris Nuclear Power Plant.With 990413 Ltr ML18016A8661999-03-31031 March 1999 Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept. ML18017A8931999-02-28028 February 1999 Risks & Alternative Options Associated with Spent Fuel Storage at Shearon Harris Nuclear Power Plant. ML18016A8551999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Shearon Harris Npp. with 990312 Ltr ML18016A8261999-02-22022 February 1999 LER 99-003-00:on 990123,noted That Plant Was Outside Design Basis Due to Isolation of Fire Protection Containment Sprinkler Sys.Caused by Human Error.Restored Containment Sprinkler Sys to Operable Status.With 990222 Ltr ML18016A8531999-02-18018 February 1999 Non-proprietary Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFP 'C' & 'D'. ML18016A8111999-02-12012 February 1999 LER 99-002-00:on 990114,RT Due to Not Removing Temporary Device from Relay Following Calibration Was Noted.Caused by Human Error.Counseled Personnel Involved in Event.With 990212 Ltr ML18016A7971999-02-0505 February 1999 LER 99-001-00:on 990106,SF Pool Water Level Was Not Maintained Greater than 23 Feet Above Stored BWR Fuel Assemblies.Caused by Fasteners Bending Under Specific Circumstances.Increased Water Level.With 990205 Ltr ML18022B0631999-02-0404 February 1999 Rev 0 to Nuclear NDE Manual. with 28 Oversize Uncodable Drawings of Alternative Plan Scope & 4 Oversize Codable Drawings ML20202J1161999-02-0101 February 1999 SER Accepting Relief Requests Associated with Second 10-year Interval Inservice Testing Program ML18016A8041999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Shearon Harris Nuclear Power Plant.With 990211 Ltr ML18016A7941999-01-29029 January 1999 LER 98-004-01:on 980313,identified Design Deficiency Re Potential Runout of Tdafwp.Caused by Inadequate Original AFW Sys Design.Operability Evaluation Was Completed on 980313 & Addl Engineering Analysis Was Performed by Vendor ML18016A7801998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Shearon Harris Npp. with 990113 Ltr ML18016A7671998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Shnpp,Unit 1.With 981215 Ltr ML18016A9731998-11-28028 November 1998 Changes,Tests & Experiments, for Harris Nuclear Plant.Rept Provides Brief Description of Changes to Facility & Summary & of SE for Each Item That Was Implemented Under 10CFR50.59 Between 970608-981128.With 990527 Ltr ML18016A8351998-11-28028 November 1998 ISI Summary 8th Refueling Outage for Shearon Harris Power Plant,Unit 1. ML18016A7411998-11-25025 November 1998 Rev 1 to Shnpp Cycle 9 Colr. ML18016A7211998-11-17017 November 1998 LER 98-007-00:on 981023,turbine Control Anomaly Caused Manual Rt.Caused by Failure to Incorporate Verbal Vendor Guidance in Operating Procedures.Addl Vendor Guidance Will Be Verified & Added to Procedures.With 981117 Ltr ML18016A7071998-11-0303 November 1998 Rev 0 to Harris Unit 1 Cycle 9 Colr. ML18016A7201998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Shearon Harris Nuclear Power Plant.With 981113 Ltr ML20154F8701998-10-0606 October 1998 Safety Evaluation Authorizing Proposed Alternative to Requirements of OMa-1988,Part 10,Section 4.2.2.3 for 21 Category a Reactor Coolant Sys Pressure Isolation Valves ML18016A6201998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Harris Nuclear Power Plant.With 981012 Ltr ML18016A5971998-09-21021 September 1998 Rev 1 to Harris Unit 1 Cycle 8 Colr. ML18016A5881998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Shnpp,Unit 1.With 980914 Ltr ML18016A5071998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Shearon Harris Nuclear Plant.W/980811 Ltr ML18016A9431998-07-0707 July 1998 Rev 1 to QAP Manual. ML18016A4841998-07-0707 July 1998 LER 97-002-01:on 970207,determined That Cold Weather Conditions Resulted in Mfiv Being Potentially Inoperable During Period 970117-20.Caused by Inadequate Design of HVAC Sys.Implemented Mods to Steam Tunnel HVAC Sys ML18016A9371998-06-30030 June 1998 Technical Rept on Matl Identification of Spent Fuel Piping Welds at Hnp. ML18016A4861998-06-30030 June 1998 Monthly Operating Rept for June 1998 for SHNPP.W/980715 Ltr ML18016A4701998-06-30030 June 1998 LER 97-021-03:on 980210,discovered That SFP Water Level Had Not Been Verified Greater than 23 Feet Above BWR Fuel Assemblies.Caused by Misinterpretation of TS Requirements. Will Submit TS Change Request to Revise TS 3.9.1.11 ML18016A4491998-06-0808 June 1998 LER 98-006-00:on 980508,failure to Perform Insp & Preventive Maint on MCCB as Required by TS Was Noted.Caused by Inadequate Sps.Tested 9 Pressurizer Heater Bank Breakers by Cycling each.W/980608 Ltr ML18016A4521998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Shearon Harris Nuclear Power Plant.W/980612 Ltr ML18016A7711998-05-26026 May 1998 Non-proprietary Rev 2 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris Spent Fuel Pools 'C' & 'D'. 1999-09-30
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NRC FORM 366 ILB5)U.S.NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)(See reverse for required number of digitslcharacters for each block)APPROVED BY OMB NO.3150 0104 EXPIRES 04I30/96 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANOATORT WfORMATION CO(LECTIN REDDEST: 506 HRS.REPORTED (ESSONS lEARHEO ARE INCORPORATED WTO THE UCENSING PROCESS AND FEO BACK TO INDUSTRY.fORWARD COMMEHTS REGAROWG BURDEN ESTIMATE TO THE WfORMATNN AHO RECORDS MANAGEMENT BRANCH IT 6 f33L US NUClEAR REGUlATORY COMMISSION, WASHWGTON.
DC 20555000l, AHO TO THE PAPERWORK REDUCTION PROJECT (3150.OI04L Off)CE'F MANAGEMENT ANO BUDGET, WASHINGTON.
OC 20503.FACIUTY NAME ll)Harris Nuclear Plant Unit-1 DOCKET NUMBER (2)50-400 PAGE (3)1 OF 5 TITLE (4)Technical Specification Surveillance Procedure Review Project Identified Deficiencies.
EVENT DATE{5)MONTH OAY YEAR LER NUMBER (6)YEAR SEOUENTIAL NUMBER REVISION NUMBER REPORT DATE{7)MOIITH OAY YEAR FACIUTY NAME OTHER FACILITIES INVOLVED (6)DOCKET NVMBER 2 10 98 97-021-02 3 12 98 FACILITY NAME DOCKET NUMBER 05000 OPERATING MODE (9)POWER LEVEL{10)100%THIS REPORT IS SUBMITTED PUR 20.2201(b) 20.2203(B)(1) 20.2203(B)(2)(i) 20.2203(B)(2)(ii)SUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one o 50.73(B)(2)(i) 20.2203(B)(2)(v) 50.73(B)(2)(ii) 50.73(B)(2)(iii) 50.73(B)(2)
Uv)20.2203(a)(3)(il 20.2203(B)
(3)(iil 20.2203(B)(4) r more)(11)50.73(a)(2)(viii)50.73(B)(2)(x) 73.71 OTHER 20.2203(B)(2)(iii)20.2203(B)
(2)(iv)50.36(c)(1) 50.36(c)(2)LICENSEE CONTACT FOR THIS LER (12)50.73(B)(2)
{v)50.73(a)(2)(vii)
Specify in Abstract below or in NRC Form 366A NAME TELEPHONE NUMBER (Inetude Area Code)Michael Verrilli Sr.Analyst-Licensing (919)362-2303 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT{13)CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS SUPPLEMENTAL REPORT EXPECTED (14)YES{If yes, complete EXPECTED SUBMISSION DATE).X NO EXPECTED SUBMISSION DATE (15)MONTH DAY YEAR ABSTRACT (Limit lo 1400 spaces, i.e., BpproximBtoly 15 single.spaced typowri((en lines)(16)On August 14, 1997, with the plant at approximately 100%polver in mode I, a condition was identiTied during the on-going Technical Specification (TS)Surveillance Procedure Review Project related to inadequate maintenance of Spent Fuel Pool water level.Specifically, Technical Specification (TS)3/4.9.11 requires that"at least 23 feet of water shall be maintained over the top of irradiated fuel assemblies seated in the storage racks." This depth of water will provide sufficient"scrubbing" to remove 99Fo of the assumed 10%iodine gap activity released from the rupture of an irradiated fuel assembly.Contrary to this requirement, water level has not been verified greater than 23 feet above the boiling water reactor (BWR)fuel assemblies received from CP&L's Brunswick Plant, which are currently stored in the Harris Plant fuel pools.These BWR assemblies have a bail handle that extends approximately 6 inches above the top nozzle base plate.When the BWR storage racks were installed in 1991, the 23 foot water level reference mark was established from the top nozzle base plate of the BWR fuel seated in the storage racks, not from the top of the bail handles.This approach was determined at the time to be conservative since the base plate elevation exceeds that of the fuel rods which would be the source of any released fission gasses.However, verbatim compliance with the TS requirements would require 23 feet of water over the BWR fuel assembly structure, including the top bail handle.This condition was caused by a misinterpretation of TS requirements and design mputs during the establishment of the 23 foot water level reference mark and the subsequent setup of water level indicators, when the BWR fuel storage racks were initially installed at the Harris Plant.Corrective actions included directions to Operations to maintain and monitor fuel pool level at or above 23 feet 7 inches to ensure required water level over the BWR bail handles.This was completed by issuing an Operations ni)Eight order and revising the daily surveillance procedures.
Additional actions will include reviewing this event with appropriate Engmeering personnel to emphasize the importance of verbatim TS compliance and an evaluation of the fuel pool level alarm setpoints.
This revision is submined to report an additional condition identified during the on-going Technical Specification Surveillance Procedure Review Project.This condition involved the failure to properly test the non-safety related Pressurizer Power Operated Relief Valve (1RC-116), which resulted in a violation of TS surveillance requirements.
9803180350 9803i2 PDR ADQCK 05000400, S PDR KRC FORM 366A I4.99I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION US.NUCLEAR RECULATORT COMMISSION FACIIITT NAME In Shearon Harris Nuclear Plant-Unit//1 OOCRET 50400 lER NUMBER IBI SEOUENTIAL RDtISION NUMBER NUMBER 97-021-02 PACE 13I 2 OF 5 TEN'r pr moro spooo N rorfrri od.oso oddn ooof oopris of HRC form ZEQI (I 7)EVENT DESCRIPTION:
On August 14, 1997, with the plant at approximately 100%power in mode 1, a condition was identified during the on-going Technical Specification (TS)Surveillance Procedure Review Project related to inadequate maintenance of Spent Fuel Pool water level.Specifically, Technical Specification (TS)3/4.9.11 requires that"at least 23 feet of water shall be maintained over the top of irradiated fuel assemblies seated in the storage racks." As described in the TS Bases section for this TS, this depth of water will provide sufficient"scrubbing" to remove 99%of the assumed 10%iodine gap activity released from the rupture of an irradiated fuel assembly.Contrary to this, water level has not been verified greater than 23 feet above the boiling water reactor (BWR)fuel assemblies received from CP&L's Brunswick Plant, which are currently stored in the Harris Plant (HNP)fuel pools.These BWR assemblies have a bail handle that extends approximately 6 inches above the top nozzle base plate.When the BWR storage racks were installed in 1988, the 23 foot water level reference mark was established from the top nozzle base plate of the BWR fuel seated in the storage racks, not from the top of the bail handles.This approach was determined at the time to be conservative since the top nozzle base plate elevation exceeds that of the fuel rods which would be the source of any released fission gasses.However, verbatim compliance with the TS requirements would require 23 feet of water over the BWR fuel assembly structure, including the top bail handle.The method of verifying adequate water level in the Spent Fuel Pools at HNP involved confirming that the low-level alarm was not present.The low level alarm setpoint was established at 23 feet 2.5 inches and was consistent with the 23 foot reference mark from the top nozzle base plate.Therefore water levels could have dropped below 23 feet above the top of the BWR assembly bail handles and not result in a low level alarm.The following additional Technical Specification Surveillance related deficiencies have been identified by the on-going comprehensive TS Surveillance Procedure Review Project.The TS Surveillance Procedure Review Project was originally committed to in LER 95-07 dated September 28, 1995.On September 22, 1997, a design deficiency in the Fuel Handling Building Emergency Exhaust System (FHBEES)was determined to be reportable.
Specifically, the FHBEES contains two units (E-12&E-13)which each consist of a fan, charcoal adsorber beds and HEPA filters.To prevent degradation of the charcoal bed removal efficiency, the units contain heaters to control the humidity of the air passing through the charcoal.To prevent potential auto-ignition of the charcoal in the idle unit due to heat from the decay of radionuclides captured by the charcoal, the system is designed to provide cooling flow or"bleed flow" (approximately 5%of total flow)through the idle unit.NRC Reg.Guide 1.52 and the HNP Final Safety Analysis Report (FSAR)section 6.5.1 indicate that the bleed flow passes from the discharge of the idle unit to the suction of the on-line unit.Any releases would thus be filtered through a charcoal filter with the appropriate design efficiency.
Contrary to this, the bleed flow on the FHBEES units passes from the discharge of the idle unit to the discharge of the on-line unit.Since the heaters that control relative humidity do not run when the unit is not in service, the humidity in the idle unit is not controlled.
Therefore, efficiency of the charcoal in the idle unit could potentially be degraded and air flowing through this idle unit c'ould be filtered with an efficiency lower than the assumed 95%contained in the FSAR chapter 15 fuel handling accident analysis.This would have resulted in higher calculated off-site doses had fuel movement occurred as assumed in the FSAR analysis and allowed by plant procedures.
Therefore, this condition is being voluntarily reported as a condition that could have resulted in operation outside the design basis of the plant per 10CFR50.73.a.2.
ii.Also on September 22, 1997, a condition involving inadequate surveillance testing of the FHB and RAB Emergency Exhaust system charcoal adsorber beds was determinied to be reportable.
Specifically, HNP NR M A l4 I NRC FORM 366A I495I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUClEAR REGULATORY COMMISSION FACILITY NAME ui Shearon Harris Nuclear Plant~Unit Nl BUCKET 50400 lER NUMBER IBI YEAR SEOUENTML REYISION NUMBER NUMBER 97-021-02 PAGE I3I 3 OF 5 TEXT pr coro oproo N rorpriod.ooo orrdrreoor oopeo ot rdRC Fore 36atl (IT)EVENT DESCRIPTION: (continued)
Technical Specifications require that a laboratory analysis be performed on the charcoal"after every 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> of charcoal adsorber operation".
The hours of operation have only been accumulated based on the time period that the on-line unit was in service.The accumulation should also have included the time that bleed flow was passing through the idle unit.This condition was considered to be a violation of TS surveillance requirements 4.7.6.c and 4.9.12.c.On February 10, 1998, an additional TS testing deficiency was identified during the on-going TS Surveillance Procedure Review Project.This deficiency involved past testing of the non-safety related Pressurizer Power Operated Relief Valve (PORV, 1RC-116, EIIS Code:AB-RV), which was not performed at the correct plant conditions per the requirements of TS surveillance requirement 4.4.4.1.Specifically, TS 4.4.4.l.b states that"each PORV shall be demonstrated OPERABLE at least once per 18 months by: (b)Operating the valve through one complete cycle of full travel during MODES 3 or 4, prior to going below 325 degrees F".Testing to satisfy this surveillance requirement has been performed by the"Pressurizer Safety Grade PORV Operability
-Quarterly Test" Operations Surveillance Test procedure (OST-1117).
Past performance of this test was credited for satisfying the entire TS surveillance requirement.
However, testing of 1RC-116, the non-safety related PORV, was not included in OST-1117.1RC-116 has been tested by the"Pressurizer PORV-Quarterly Operability Test" (OST-1503) to satisfy In-service Inspection requirements.
However, OST-1503 is performed in MODE 5 with Reactor Coolant System temperature less than 200 degrees F.Therefore, 1RC-116 has not been tested in the mode and plant conditions specified by TS 4.4.4.1.b.
The failure to include 1RC-116 in the scope of test procedure OST-1117, occurred during implementation of amendment 27 to the Harris Plant Operating License (TS)in September 1991.This amendment was generated to address the concerns stated in NRC Generic Letter 90-06"Power Operated Relief Valves and Block Valves in PWR Plants".CAUSE: The original condition was caused by a misinterpretation of TS requirements and design inputs during the establishment of the 23 foot water level reference mark (above the BWR top nozzle base plate)and the subsequent setup of water level indicators, when the BWR fuel storage racks were initially installed at the Harris Plant.Cause for Additional Items Identified:
Item 1: The cause of the FHBEES design deficiency was engineering oversight during initial plant design and construction.
Item 2: The cause of the TS surveillance violation related to charcoal testing after 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> of operation was incorrect interpretation of TS testing requirements.
Surveillance test procedures were initially set up to satisfy the 720 hour0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br /> requirement based on accumulation of hours for the in-service unit only.Item 3: The cause of the pressurizer PORV (1RC-116)testing deficiency was inadequate surveillance test procedures.
The changes made to TS 4.4.4.1 in amendment 27 were not understood by the plant staff and the associated development of OST-1117 did not ensure proper testing of 1RC-116.SAFETY SIGNIFICANCE:
There were no actual safety consequences associated with this event.Adequate water depth (23 feet)has been maintained above the active fuel rods, which would be the source of any released fission gasses.This ensures the iodine removal capability required by TS in the event of a ruptured irradiated fuel assembly.This condition is being reported per 10CFR50.73.a.2.i as a condition prohibited by Technical Specifications.
A (4 NRC FORM 366A)I 96)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGUULTORT COMMISSION FACIUTT NAME il)Shearon Harris Nuclear Plant Unit 41 BUCKET 50400 LER NUMBER r6)TEAR StaunnML a~ION NUMBER NUMBER 97-021-02 PAGE O)4 OF 5 TEXT Pr rrrrrrs spsss N r rprdsd.sss sdd)s)psl sopis ol PORC Prrrrrr 36@I (I 1)SAFETY SIGNIFICANCE: (continued)
Safet Conse uences for Additional Items Identified:
Item 1: There were no actual safety consequences associated with this additional item.Had a fuel handling accident occurred in the FHB with the improperly configured bleed flow between the filtration units, the resulting off-site dose rates would not have exceeded the maximum value analyzed in the HNP FSAR and would have remained within 10CFR100 limits.This result is based on the fact that fuel off-load during past HNP refueling outages has never occurred prior to 257 hours0.00297 days <br />0.0714 hours <br />4.249339e-4 weeks <br />9.77885e-5 months <br /> following reactor shutdown, which allowed for substantial iodine decay resulting in a lower fuel handling accident source term than that assumed in the FSAR.It is also based on past charcoal efficiency surveillance testing, which has indicated a worst case value of 98%, which is greater than the 95%assumed efficiency value in the FSAR accident analysis.Administrative controls have also been in place to ensure that filter charcoal is replaced if surveillance testing indicates an efficiertcy less than 99%Therefore, this condition is being voluntarily reported as a condition that could have resulted in operation outside the design basis of the plant per 10CFR50.73.a.2.ii.
Item 2: There were no consequences as a result of the TS surveillance requirement violation based on the charcoal surveillance test results described above.This condition is being reported as a condition prohibited by Technical Specifications per 10CFR50.73.a.2.
i Item 3: There were no safety consequences as a result of the pressurizer PORV (IRC-116)testing deficiency.
Testing has been satisfactorily performed per the requirements of TS 4.4.4.l.b to verify the operability of the two safety related pressurizer PORVs (1RC-114 and 1RC-118).This testing ensures that both safety related PORVs would have been available to operators in the event of a Steam Generator tube rupture accident and for use as low temperature over-pressure protection.
This condition is being reported as a condition prohibited by Technical Specifications per 10CFR50.73.a.2.i.
PREVIOUS SIMILAR EVENTS: There have been no previous events related to inadequate verification of Spent Fuel Pool water level or improperly configured bleed flow between air handling units as a result of design oversight.
HNP submitted LER 96-002 to report numerous deficiencies caused by incorrectly interpreting TS testing requirements during initial surveillance test development.
These were a result of HNP's actions to address NRC Generic Letter 96-01.CORRECTIVE ACTIONS COMPLETED:
1.Directions were provided to Operations to maintain and monitor Spent Fuel Pool water level at or above 23 feet 7 inches to ensure required water level over the BWR bail handles.This was completed by issuing an Operations Night Order on August 14, 1997, revising the Reactor Auxiliary Building Operator Logs on August 25, 1997 and requiring the actual Spent Fuel Pool water level to be entered in the daily surveillance requirement test, rather than the previous practice of confirming the absence of the low level alarm.2.This event was reviewed with appropriate Engineering personnel to emphasize the importance of verbatim TS compliance.
This was completed on October 6, 1997.CORRECTIVE ACTIONS PLANNED: l.A Technical Specification (TS)Change Request will be submitted to the NRC to revise TS 3.9.11 to require that the Spent Fuel Pool water level be maintained at least 23 feet over the top of the irradiated"fuel rods" and not"fuel assemblies".
The Technical Specification Change Request will be submitted prior to June I, 1998.NR M)I I NRC FORM 366A I4 95I LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U5.NUCLEAR REGULATORY COMMISSION FACILITY NAME II)Shearon Harris Nuclear Plant~Unit 41 BUCKET 50400 LER NUMBER IBI YEAR SEOUENTIAL REYISION NUMBER NUMBER 97-021-02 PAGE I3)5 OF 5 TEXT pr moro spooo N nOoi od.ooo odd Iiimo/oooo of h'RC perm 3664I (Ir)Corrective Actions for Additional Items Identified:
Item 1: A Justification for Continued Operation (JCO)was approved and implemented for the FHBEES bleed flow issue on October 10, 1997.A long term resolution for the improperly configured FHBEES bleed flow issue will be provided via Engineering Service Request 97-00737.This will ensure that the systems satisfy the appropriate FSAR and Reg.Guide 1.52 design requirements and will be completed prior to the next fuel off-load.Item 2: As an interim measure, Operations personnel will record run times on both the in-service filtration unit and the idle filtration unit in the FHB and RAB Emergency Exhaust Systems.This was directed by an Operations Night Order on October 15, 1997.Revisions were completed to operations procedures that require recording run times for FHB and RAB Emergency Exhaust System filtration units (OP-170"Fuel Handling Building HVAC" and OP-172"Reactor Auxiliary Building HVAC").These revisions were completed on October 30, 1997.Item 3: Operations Surveillance Test (OST-1117"Pressurizer Safety Grade PORV Operability
-Quarterly Test")will be revised to include testing of 1RC-116 at the appropriate plant conditions.
This will be completed by June 30, 1998.N M AI4 I