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 Issue dateTitleTopic
ML20042F35430 April 1990Special Rept Re Failure to Prevent Performance Degradation of Reactor Bldg Cooling Units.Caused by Mgt Deficiency & Inadequate Program.Cooling Unit Declared Inoperable & Removed from Svc for Cleaning & Placed Back in OperationTemporary Modification
Operability Determination
ML20024E6604 August 1983RO 83-18:on 830804,during Maint Insps on Hydraulic Snubbers, Two Small Bore Snubbers Identified as Being Installed on RCS Hot Leg Vent Piping Downstream of Valves RC-V15A & B.Caused by Personnel Error
ML20024C1271 July 1983Ro:On 830623,visual Insp Revealed Three Broken Holddown Springs.Investigation Incomplete.Ro 269/83-13 Will Be Submitted by 830721
ML20024C4181 July 1983Ro:On 830525,fire Barrier Penetrations Found Nonfunctional. Caused by Design Deficiency.Fire Watch Posted,Penetrations Repaired & Procedures RevisedFire Barrier
Fire Watch
Hourly Fire Watch
ML20024C41429 June 1983Ro:On 830509 & 12,fire Barrier Smoke Exhaust Penetrations 3-K-5-2,3-C-5-3 & 4 Found W/O Seal & 3-C-5-3 Did Not Have Fusible Damper,Respectively.Caused by Inadequate Info & Insufficient Guidance Provided by Design EngineeringFire Barrier
Fire Watch
Hourly Fire Watch
ML20023B65129 April 1983ROs 269/83-10 & 287/83-04 Re 821212 & 830303 Loss of Containment Integrity.Mgt Audit in Progress.Summary List of Completed & Remaining Activities,W/Projected Completion Dates,Encl
ML20027B85821 September 1982Ro:Advising That 820820 Occurrence Involving Loss of Electric Power to Valve CCW-8 Determined Not Reportable. Operability of Valve Demonstrated.No Further Action Required
ML20027B76916 September 1982RO 269/82-14:investigation Re Reactor Bldg Penetrations That May Not Have Been Leak Rate Tested Incomplete.Rept to Be Submitted by 820930
ML20052A3299 April 1982Informs That Review Per RO-269/82-07 Has Determined That Plant Design & Const Predate Std Re Westinghouse SAI-1 Type Relays Not Meeting Full Surge Requirements
ML20052A4262 April 1982RO 269/82-06:on 820306,steam Generator 1B Indicated Tube Leak of 0.08 Gpm.Incident Under Investigation.Next Rept Expected by 820416
ML20050A54318 March 1982Ro:On 820318,water W/Ph of 3.5 Was Discharged from Secondary Waste Water Neutralizing Tank WT-T-1 Into Plant Discharge Effluent Stream.Caused by Accidental Overflow of Approx 2,500 Gallons of Water from Neutralizing Tank
ML20050A97512 March 1982RO 287/82-04:on 820226,3A2 HPI Normal Makeup Nozzle Found to Have Broken Thermal Sleeve Tack Welds.Investigation Revealed Cracks in Safe End & Upstream Piping.Next Rept Expected by 820409
ML20049J55425 February 1982Ro:Advising of Delay Until 820311 to Provide Complete Rept of RO-281/82-03 Re Steam Generator Tube Leak
ML20040F7615 February 1982Ro:On 820122,during Visual Insp of Core Barrel Assembly, Thermal Shield & Shock Pad Bolts Found Broken & Shock Pad Was Skewed.Thermal Shock Bolts to Be Replaced.Loosened Shock Pad Evaluation Underway
ML20040E68728 January 1982RO 269/81-50:on 811229,reactor Bldg Cooling Unit C Declared Inoperable Due to Inability to Open Discharge Valve 1LPSW-24.Investigation & Rept Expected to Be Completed by 820211
ML20040C8428 January 1982Suppl 3 to RO 269/81-11:re Broken Lower Thermal Shield Bolts.Caused by Intergranular Stress Corrosion Cracking in Region of Pronounced Microstructure Transition at head-to-shank Fillet.Bolts Replaced.Drawings EnclStress corrosion cracking
ML20039C63323 December 1981RO 81-14:nine Pipe Support & Structural Interfacing Areas Identified Requiring Further Evaluation & Potential Corrective Action.Failure of Pipe Supports Could Damage safety-related Components.Followup Rept Expected in 14 Days
ML20011A72321 October 1981Ro:On 811019,four Liquid Waste Releases Were Made W/O Adequate Sampling.Caused by Failure to Make Change to Sample Point.Procedure Revised to Specify Correct Sampling Point for Sys Configuration
ML20010F6794 September 1981RO 270/81-14:on 810821,2A1 Reactor Coolant Pump Electrical Penetration Was Discovered Depressurized & Could Not Be Repressurized w/SF6 Gas.Cause Not Stated.Investigation & Complete Rept Will Be Sent by 810918
ML20038C81725 August 1981Ro:On 810814,tritium Concentrations in Downstream Water Samples Exceeded Tech Spec Control Level for Second Quarter of 1981.Analysis of Max Dose Estimates Concluded That Concentrations Will Not Adversely Affect Public Health
ML20010A8725 August 1981RO 269/81-11,Suppl 1:on 810715,core Barrel Assembly Thermal Shield Bolts Found Broken.Cause Not Stated.Search for Loose Parts Turned Up All Missing Thermal Shield Parts Except for One Thermal Shield Bolt Head.Investigation Continuing
ML20009E73528 July 1981Ro:On 810717,fire Suppression Water Sys Found Inoperable. Caused by Open Main Control Source Breakers.Breakers Closed & Sys Successfully Tested
ML20038C8036 July 1981Ro:On 810210,radioactivity Levels of Aquatic Vegetation Samples Exceeded Control Level by Greater than 50 Times.Info Supersedes 810225 Submittal
ML20009F4311 July 1981Ro:On 810630,during Performance of Normal Power Procedure, Backup Function of Units Isolating & Transfer Diodes on 125 Volt Dc Instrumentation & Control Sys Was Observed. Proposed Tech Spec Change Will Be Submitted
ML20009H2701 April 1981RO:810319 Determination Declaring Portions of Low Power Injection Sys Seismically Inoperable Was Premature.Hanger Noncomformance Repaired within 48-h Per IE Bulletin 79-14. Item Not Reportable Per Tech Spec 6.6.2.1a(9)
ML20005A87725 February 1981Ro:On 810219 Analytical Results of Aquatic Vegetation Samples Collected on 810210 Indicated That Radioactivity Levels Exceeded Tech Specs.Cause Not Stated
ML19345A97417 November 1980RO 80-013/03L-0 Committed to Forwarding Final Valve Testing Evaluation by 801101.Investigation Requires More Time than Anticipated.Requests Extension Until 801219
ML19337A86323 September 1980RO 80-17:determined Insufficient Documentation to Demonstrate That Brakes on Motor Operators for Purge Valves AH-V1B & AH-V1C Environmentally Qualified.Redundant Valves Fully Qualified
ML19338F54623 September 1980RO 80-17:on 800923,determined That There Is Insufficient Documentation to Demonstrate Environ Qualification of Brakes on Motor Operators for Purge Valves AH-V1B & AH-V1C. Cause Not Stated.Corrective Action Will Be Submitted
ML19330C3044 August 1980Ro:On 800716,during Radiation Emergency Exercise,Use of Emergency Notification Sys Phone Line Became Uncertain, Making Accurate Info Transfers Questionable.Recommends That Microphone Headset Be Made Available to Allow Mobility
ML19326E20622 July 1980RO 80-15/4P:confirming 800722 Telcon,On 800721,river Water Discharge Temp Was More than 3 F Below Inlet River Water Temp for Approx 6-h.Incident Will Be Reviewed to Determine Corrective Action.Review to Be Included in Followup Rept
ML19326E08427 June 1980RO 80-12/IP:during Review of Equipment Required by IE Bulletin 79-01B,found That post-accident Pressure & Temp Would Be Higher than Postulated in NSC 730705 Rept.Short & long-term Action to Be Discussed in Followup Rept
ML19323H3426 June 1980RO-80-10/1P:on 800603,B&W Ltr Informed Util of Potential Reportability of Steam Generator Tube Rupture Safety Analysis.Caused by Nonconservative Error in Fsar.Corrective Action Will Be Addressed in Followup Rept
ML19323D51523 April 1980RO 80-07/TP:on 800423 Results of Radiographic Exams of Piping Welds Associated W/Reactor Bldg Penetrations 415-16 for Leak Rate Test Sys Showed Several Welds Not within Tech Specs.Unit Is Shut Down
ML19309A78326 March 1980RO 80-06/1P:on 800325,during Refueling Frequency Reactor Bldg Local Leak Rate Test of Valve RB-V7,updated Total Leakage Exceeded Tech Specs.Testing Is Continuing W/Approx 1/4 of Test Program Complete
ML19322B5088 November 1979RO 79-17/1P:on 791108 Support Boltings for Rigid Anchor DHH-127A Found to Be Inadequate in Design & Installation. Details & Corrective Action Will Be Addressed in Followup Rept
ML19282D02915 January 1979RO 269/7827 on 781214:on 781213,reactor Coolant Temp Became Erratic.Feedwater Problem Resulted from Operation of One or More Feedwater Valves.Power Cords Have Been Fitted
ML19263C98430 November 1978RO 270/78-12 on 781105:stop Check Valve from 2AHPI Pump to 2A12C Pump Closed During Flow Test.Valve Was Opened & Check Valve Functional Test Completed
ML19316A3705 June 1978RO 269/78-13:on 780427,primary-to-secondary Leak in 1B Steam Generator Occurred.Caused by Tube Leaks.Tube 69-1 Had Weld Crack.Tube 74-2 Had Circumferential Crack.Cracked & Suspect Tubes explosive-plugged.Investigation ContinuingHydrostatic
ML19312C23621 April 1978RO-269/78-07 & 09:on 780314 & 22,field Flashing Breaker Found Inoperable.Cause for Repeated Inoperability Has Not Been Determined.Faulty Relays Replaced Before 780322 Failure.Recorder Will Be Installed to Monitor Trip Circuits
ML19316A38111 April 1978RO 269/78-08:on 780315,valve FDW-108 Failed to Close.Failure Has Occurred Previously.Caused by Apparent Unsuitability of Valves for long-term Operation in Sys Environ.Valve Stem Lubricated.Valves Will Be Replaced
ML19316A4047 April 1978RO 269/78-06:on 780310,field Flashing Breaker Failed to Close During Startup of Keowee Hydro Unit 2.Breakers & Associated Relays Checked.Circuits Checked.Cause of Breaker Malfunction Unknown.Search for Possible Causes Continues
ML19316A3897 April 1978RO 269/78-10:on 780323,Unit 2 Not Verified Operable within Time Limit.Caused by Personnel Error.Station Procedure, Removal & Restoration of Equipment, Not Properly Used. Personnel Instructed by Operating Engineer
ML19308A75323 March 1978RO 269/78-03:on 780222,Unit 2 Field Flashing Breaker Failed to Close.Cause of Breaker Malfunction Not Determined.Relays in Breaker Control Circuit Were Replaced.Investigation to Control Breaker Sys Faults Continues
ML19316A46415 March 1978RO 269/78-04:on 780301,two Reactor Bldg Cooling Units Found Inoperable Simultaneously.Caused by Insufficient Installation Procedures Allowing Trip Point to Be Set Too Low.Breaker Reset & Trip Setpoint Increased
ML19316A4173 February 1978RO 269/78-01:on 780203,field Flashing Breaker Failed to Close.Controls Checked & Found in Proper Condition.Breaker Checked & Cleaned.Cause of Failure Not Determined
ML19317F3462 February 1978RO 270/78-04:on 780202,nuclear Instruments Found Out of Calibr in Less Conservative Direction & Could Have Prevented Fulfillment of Functional Requirements of Reactor Protective Sys.Cause Not Stated.Administrative Measures Taken
ML19308A5242 February 1978RO 78-08/1P:on 780202,util Informed by NSSS of Deviation Discovered Between FSAR Steam Line Break Analysis & Actual Operating Parameters.Procedure Mod Will Limit Secondary Site Water Volume
ML19308A79731 January 1978RO 269/78-02:on 780105,Keowee Hydro Unit 1 Not Verified Operable within 1-h of Taking Keowee Unit 2 Out of Svc. Caused by Failure to Follow Established Procedures by Personnel.Operators Instructed in Tech Specs
ML19317E04526 January 1978RO 269/77-31:on 771229,leakage of Less than 1 Gallon Per Minute Noted.Caused by Failure of Switch 1PS-364 Diaphragm. Switch 1PS-364 to Be Replaced During Future outage.1PT-21P Switch Recalibr & Returned to Svc