ML20217B312

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Safety Insps 50-324/91-01 & 50-325/91-01 on 910101-31. Violation Noted.Major Areas Inspected:Maint & Surveillance Observation,Operational Safety Verification,Onsite Review Committee & Response to Events
ML20217B312
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 02/11/1991
From: Christensen H, Prevatte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20217B269 List:
References
50-324-91-01, 50-324-91-1, 50-325-91-01, 50-325-91-1, NUDOCS 9103120056
Download: ML20217B312 (21)


See also: IR 05000324/1991001

Text

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s Pto UNITED STATES

g ug'o, NUCLEAR REGULATORY COMMISSION

.I' ~* REGION H

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101 MARIETT A STREET.N.W.

ATLANT A, GEORGI A 30323

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Report No. 50-325/91-01 and 50-324/91-01

Licensee: Carolina Power and Light Company

P. O. Box 1551

Raleigh, NC 27602

Docket Nos. 50-325 and 50-324 License No. DPR-71 and DPR-62

Facility Name: Brunswick 1 and 2

Inspection Conducted: January 1 - 31, 1991

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Lead Inspector:

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L. Prevatte

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' Cate' Signed

Other Inspectors: W. Levis

D. J. Nelson

R. E. Carroll

Approved By:  % 2/// [7/

'H. Christensen, Section Chief Date Signed

Reactor Projects Branrh 1

Division of Reactor Projects

SUMMARY

Scope:

This routine safety inspection by the resident inspector involved the areas of

maintenance observation, surveillance observation, operational safety

verification, onsite review committee, onsite followup of events, onsite

response to events, in-office report review, action on previous inspection

findings, and meetings with local officials.

Results:

In the areas inspected, one apparent violation was identified for the failure

to follow procedures while calibrating a process computer point on the feedwater

control system. This resulted in work being accomplished with the unit at

100 percent power that should have been scheduled and accomrlished with the

unit in cold shutdown. This resulted in a plant trip a..a emergency core

cooling system accuation. This event demonstrated continuing weaknesses in the

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9103120056 910212

PDR ADOCK 0D000324

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licensee's work control process. This _ event is similar to Violation

324/90-29-01 and 325,324/90-29-05, paragraph 4.a. In addition, a non-cited

violation -in the area of cold weather preparation was also identified,

paragraph 4.b.

A fuel bundle was dropped 127 inches while reloading the core. The licensee's

root cause investigation of this event was timely and effective, paragraph 7,

Unit 2 was operated at essentially 100 percent power until the Reactor trip on

Janua ry 25, 1991. After completion of the required restart items, the unit was

restarted on canuary 30, 1991. Unit I continued in a refueling outage. Core

reload was completed and the unit-is presently in the process of restoring

equipment to an operational status and preparing for the ILRT.

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REPORT DETAILS

'1. Persons Contacted

Licensee Employees

  • K. Altman, Manager - Regulatory Compliance

F. Blackmon, Manager - Radwaste/ Fire Protection

  • S. Callis, On-Site Licensing Engineer

T.,Cantebury, Manager - Unit 1. Mechanical Maintenance

  • G. Cheatham, Manager - Environmental & Radiation Control

R. Creech, Manager - Unit 2 I&C Maintenance

  • M. Foss, Supervisor, Regulatory Compliance
  • J. Harness, General Manager - Brunswick Steam Electric Plant

W. Hatcher, Supervisor - Security

  • R. Helme, Manager - Technical Support

J. Holder, Manager - Outage Management & Modifications (0M&M)

M. Jones, Acting Manager - Project Assessment

R. Kitchen, Manager - Unit 2 Mechanical Maintenance

B. Leonard, Manager - Training

J. Leviner,. Manager - Engineering Projects

  • J. Moyer, Technical Assistant to Plant General Manager
  • R. Oates, On-Site Licensing Engineer

B. Poteat, Administrative Assistant to Plant General Manager

R. Poulk, Manager - License Training

  • C, Robertson, Shift Manager

J. Simon, Manager - Operations Unit 1

W. Simpson, Manager - Site Planning and Control

S. Smith, Manager - Unit 1 I&C Maintenance

  • J.-Spencer, General Plant Manager - BSEP (Effective February 1, 1991)
  • R. Starkey, Vice President - Brunswick Nuclear Project

R. Tart, Manager - Operations Unit 2

J. Titrington, Manager - Operations Staff

  • R. Warden, Manager - Maintenance

- K. Williamson, Manager - Nuclear Engineering Department (Onsite)

B. Wilson, Manager - Nuclear Systems Engineering

Other licensee employees contacted included construction craftsmen,

engineers, technicians, operators, office personnel, and security force

members.

  • Attended the exit interview

H. Christensen, Section Chief Division of Reactor Projects, was on site

January 14, 15 and 16, 1991, to tour the plant, meet with the resident

inspectors and plant management.

Acronyms and initialisms used in the report are listed in the last

paragraph.

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2. Maintenance Observation (62703)_

The inspectors observed maintenance activities, interviewed personnel, and

reviewed records to verify that work was conducted in accordance with

approved procedures, Technical Specifications, end applicable industry

codes and standards. The inspectors also verified that: redundant

components were operable; administrative controls were followed; tagouts

were adequate; personnel were qualified; correct replacement parts were

used; radiological controls were proper; fire protection was adequate;

quality control hold points were adequate and observed; adequate

post-maintenance testing was performed; and independent verification

requirements were implemented. The inspectors independently verified that

selected equipment was properly returned to service.

Outstanding work requests were reviewed to ensure that the licensee gave

_ priority to safety-related maintenance.

The inspectors observed / reviewed portions of the following maintenance

activities:

90-AQPT1 Overhaul of 1A Service Water Screen Wash Pump

91-AACX1 Refuel Bridge

91-AAZS2 Post Packing Adjustment Motor Current Checks for HPCI Valve

2-E41-F003

91-ABTT1 Unit 2 Recirculation Pump Discharge Valve B32-F031B Stem

Repair

Violations and deviations were not identified.

3. SurveillanceObservation(61726)

The inspectors observed surveillance testing required by Technical

Specifications. Through observation, interviews, and record review, the

1.nspectors verified that: tests conformed to Technical Specification

requirements; administrative controls were followed; personnel were

qualified; instrumentation was calibrated; and data was accurate and

complete. The inspectors independently verified selected test results and -

proper return to service of equipment.

The inspectors witnessed / reviewed portions of the following ' test

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activities:

l 2MST-AM127M Suppression Pool Temperature Monitor Functional Test.

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2MST-APRM22Q APRM B and LPRM Group B Channel Calibration Functional Test

PT-02.6.6 Primary Containment Airlock Interlock Operability Check

PT-80.1 Reactor Hydrostatic Test

Violations and deviations were not identified.

4. Operational Safety Verification (71707)

The inspectors verified that Unit 1 and Unit 2 were operated in compliance

with Technical Specifications and other regulatory requirements by direct

observations of' activities, facility tours, discussions with personnel,

reviewing of records and-independent verification of safety system status.

- The= inspectors verified that control room manning requirements of 10 CFR

50.54 and the technical specifications were met. Control operator, shif t

supervisor, clearance, STA, daily and standing instructions, and

-jumper / bypass logs were reviewed to obtain information concerning

operating trends and out of service safety systems to ensure that there

. were no conflicts with Technical Specifications Limiting Conditions for

Operations. Direct observations of control room panels and instrumenta-

tion and recorder traces important to safety were conducted to verify

operability and that operating parameters were within Technical Specifica-

tion ' limits. The inspectors observed shift turnovers to verify that

system status continuity was maintained. The inspectors verified the

status of selected control room annunciators.

Operability of a selected Engineered Safety Feature division was verified

weekly by insuring that: each accessible valve in the flow path was in

its correct position; each power supply and breaker was closed for

j components that must activate upon initiation signal; the RHR subsystem

cross-tie valve for each unit was closed with the power removed from the

L valve operator; there was no leakage of major components; there was proper

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lubrication and cooling water available; and conditions did not exist

, which could- prevent fulfillment of the system's functional requirements.

l Instrumentation essential to system actuation or performance was verified

operable by observing on-scale indication and proper instrument valve

lineup, if accessible.

The inspectors verified that the licensee's health physics

policies / procedures were followed. This included observation of HP

practices and a review of area surveys, radiation work permits, postings,

and instrument calibration.

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The inspectors verified by general observations -that: the security

. organization was properly manned and security personnel were capable of

l performing their assigned functions; persons and packages were checked

prior to entry into the protected area; vehicles were properly authorized,

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-searched and escorted within the PA; persons within the PA displayed photo

identification badges; personnel in vital areas were author ned; effective

1 compensatory measures were employed when required; and security's response

to threats or alarms was adequate.

The inspectors also observed plant housekeeping controls, verified

position of certain containment isolation valves, checked clearances, and

verified the operability of onsite and offsite emergency power sources,

a. Unit 2 Scram

Unit 2 scrammed from 100 percent power on January 25, 1991. The

scram was due to a turbine trip which resulted from high reactor

water level ~. Water level had increased due to the FWLCS responding

to a loss of feedwater flow signal due to maintenance in progress.

With the FWLCS in three element control, tne loss of a feed flow

input was seen as a loss of a feed flow resulting in an increased

demand signal from the FWLCS to the feedwater pumps. The increased

feedwater flow caused reactor water level to increase to the high

level -setpoint for the turbine trip. This high icvel condition also

trips the feedwater pump turbines.

Subsequent to the trip, RCIC auto initiated and injected to restore

water level. HPCI auto initiated but did not inject due to the short

duration of 'the low level condition. The HPCI injection valve was

manually opened by the C0 to aid in restoring level. All safety

systems operated correctly during the trip. Initially, some

questions existed concerning the failure of SBGT to auto start.and

the ' Secondary Containment Isolation Dampers and RWCU to isolate.

Licensee review of calibration records for the trip-devices for these

components and ERFIS data showed that sufficient trip devices did not

, actuate to cause these occurrences. These instruments were set to

actuate between 117.6 inches and 117.8 inches. The lowest level

recorded on any channel was 116.6 inches. The technical

specification value is greater than or equal to 112 inches.

The-inspector was present in the control room throughout the event

and noted that operator performance following the trip was proper and

in accordance with procedures. Although the time duration of event

initiation to reactor scram was short, approximately 17 seconds, the

inspector noted that the operators did not recognize the cause of the

feedwater transient and took no actions to mitigate it. Similar

conditions were also noted in unit trips on August 16, 1990 and

October 12, 1990, which were caused by FWLCS malfunctions.

The feedwater transient was caused by the lifting of lead C32-A-18 in

panel H12-P612 which removed one feedwater flow input to the FWLCS.

This was dor.e in accordance with Step 7.1 of OPIC-CPU 001, Calibration

of an Analog Process Computer Point, Revision 12, which had been

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approved by the Unit 2 SCO a few minutes earlier. The SCO gave

permission and signed the WR/J0' to authorize the performance of the

calibration of the computer point based primarily on the Calibration

Summary Sheet, Attachment 13A of the procedure, which stated NONE

under the Required Plant Conditions Section. The NOTE which is

included at the top of the sumary sheet, states that the " Summary

Sheet is provided as an aid to the shift foreman and shall not be

substituted for the existing prerequisi'.as and precautions stated in

the procedure." Step 3.3.1 of the prerequisites of the procedure

stated that the unit be in cold shutdown or refuel to perform the

test.

The licensee's maintenance procedures require that the maintenance

foreman review work packages generated by the maintenance planners

and have the work scheduled through SWFCG if he determines that the

work can be. performed with assigned manpower and existing plant

conditions. SWFCG reviews the submission of these requests, resolves

conflicts between the different work groups and establishes the

schedule for the performance of maintenance activities. During the

review for the work planned for the week of January 20, the involved

maintenance foreman submitted 5 preventive maintenance routes to

SWFCG to be performed. SWFCG specifically questioned the feasibility

of performing 3 of the tests with the unit at power. Upon review by

the foreman, he concluded that two of the tests could not be

performed but that the third, performance of OPIC-CPU 001, could be

accomplished with the unit running. He based his conclusion on

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reviewing the procedure's summary sheets. SWFCG did not review the

work package themselves nor cause an ACR to be generated when they

determined that 2 of the tests could not be performed at power.

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Two I&C technicians performed procedure OPIC-CPU 001. Neither noted

the -prerequisite specifying the required plant shutdown -conditions

even though one technician signed the step immediately preceding the

step which indicated that they had permission to begin the

calibration. In-fact, the prerequisite which stated the required

plant conditions was the only prerequisite in the procedure.

l The inspector reviewed the WR/JO which indicated this work needed to

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be performed. A due date of December 24, 1990 is shown with an

overdue date of May 5,1991. The frequency is stated as every 18

months. Plant operating mode was lef t blank. 0MMM-004, Preventive

Maintenance, Revision 3, Section 5.3, states that, when a preventive

maintenance route is initiated and a frequency of 18 months is

assigned, the route should be reviewed to determine if it is

refueling outage related. If so, a frequency of "R0" should be

assigned. In addition, Section 5.3.4.2.1 states that the planner may

enter the plant operation mode (1-5) or leave the field blank. Mode 5

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should be used for PM routes with -a "R0" or other outage related

frequency. The Unit I rcute, which performs this same procedure,

specifies "R0" for required frequency. These routes were developed

prior- to the implementation of OMMM-004. Subsequent to its

implementation in July,1988, only the Unit I route was updated to

reflect the latest requirements.

Two SR0s, the Unit 2 SCO and SF, also signed the WR/JO which finally

allowed this work to begin. They did not review the prerequisites of

the test but relied upon the summary sheet and the fact that the work

was scheduled by SWFCG.

There were many potential barriers which should have prevented this

event. Although the glaring weaknesses involve the 1&C technicians

and their foreman, other work groups demonstrated deficiencies. The

maintenance planning organization, maintenance procedure writers,

SWFCG, and finally the licensed operators on shif t all had the

opportunity to recognize the error in performing this calibration at

power.

As.a result of the Unit 2 scram on August 19, 1990 and the trip of an

RPS bus on Unit 1 on August 22, 1990, the licensee instituted several

measures to correct work control weaknesse>. These measures, which

were discussed in response to violations dated October 17, 1990 and

December 28, 1990, included the stoppage of work, institution of pre

and post-job briefings, training of appropriate personnel, discussing

these events and performing " Reducing Human Error Training." In the

case of the event on January 25, 1991, a pre-job briefing was held

with the foreman and 2 technicians. This brief did not review the

prerequisites of the procedure. In addition, the two technicians and

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the foreman had received " Reducing Human Error" training. Two

i individuals, including the foreman, received this training on

December 3,1990. The other technician received the training on

November 15, 1990.

The failure to follow procedure 0PIC-CPU 001 with respect to not

' satisfying the prerequisites of the procedure is a Violation

l Failure to Meet Procedure Prerequisites, (324/90-01-01). The

i inspector recognizes that the willfulness and falsification issues

L which surfaced in the August 19, 1990 trip are not present in this

l case. However, the same issue, that is, the f ailure to adequately

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control maintenance work in the plant existed in the August 19, 1990

and August 22, 1990 events and occurred again on January 25, 19s1.

Since the corrective actions which were in place for the previous

violations could have reasonably been expected to prevent the

occurrence of this violation, the violation is characterized as a

similar violation.

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b. On Jannry 23, 1991, when the outside temperature reached a low of 22

degrees F, the inspector noted that protective measures to shelter

and supply of supplementary heating were not provided for the diesel

fire pump fuel tank. Section 5.0, Note 15 of 01-43, Freeze

Protection and Cold Weather Bill, Revision 6, states that the fire

pump fuel oil tank requires sheltering and supplementary heating at

25 degrees F to maintain operability. Item 9 of Attachment 2 of this

procedure requires the outside auxiliary operator contact maintenance

who will provide portable heating and windbreaks for the diesel fire

pump tank. In addition, the outside A0 is to ensure that the

temperature of the tank area remains greater than 23 degrees F.

On this particular occasion, the outside auxiliary operator notified

maintenance to take the appropriate actions at 25 degrees F.

However, maintenance was not equipped to respond quickly and did not

understand the urgency of these measures. Consequently, these

measures were not in place several hours later when the inspector

toured the area. Subsequently, the licensee has staged windbreaks

and provided heating for the area.

During this time period, the motor driven fire pump was operable.

Therefore, the safety significance of this event is minor. However,

it displays several weaknesses. Temperatures had been predicted to

be . in the low 20's that evening, yet prior planning had not been

accomplished to ensure that the diesel fire pump fuel oil tank would

be protected. Instead, the licensee's staff waited until the

established temperature to take action and then found out that they

could not respond quickly. Operations did not followup and

maintenance did not inform operations that these actions would not be

completed expeditiously. The failure to inmplement their freeze

protection procedures is a Violation: Failure to Implement Freeze

Protection Procedures, (325,324/91-01-02). However, this NRC

identified violation is not being cited because criteria specified in

Section V.A. of the NRC Enforcement Policy were satisfied.

Two violations and no deviations were identified.

5, Onsite. Review Committee (40700)

The inspectors attended selected Plant Nuclear Safety Committee meetings

conducted during the period. The inspectors verified that the meetings

were conducted in accordance with Technical Specification requirements

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regarding quorum membership, review process, frequency and personnel

qualifications. Meeting minutes were reviewed to confirm that

decisions / recommendations were reflected in the minutes and followup of

corrective actions was completed.

. Violations and deviations were not identified.

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6. Onsite Followup of Events (92700)

The below listed events were reviewed to verify that the information

provided met NRC reporting requirements. The verification included

adequacy of event description and corrective action taken or planned,

existence of potential generic problems and the relative safety

significance of the event. Onsite inspections were performed and

concluded that necessary corrective actions have been taken in accordance

with existing requirements, license conditions and commitments, unless

otherwise stated.

a. (CLOSED) . LER 1-89-04, Unplanned Auto Isolation of Reactor Water

Cleanup System Inlet Outboard Isolation Valve G31-F004 Due to

Spurious Actuation of Steam Leak Detection Instrumentation. This

unexpected partial Group 3 PCIS isolation was due to inadequate

clearance research. The steam leak detection temperature modules are

known to be susceptible to spurious trips upon being energized. The

distribution panel that supplies the affected temperature module was

being re-energized at the time of the actuation. The Group 3

isolation was not expected because operators did not thoroughly

research the system drawings to determine all isolations that could

occur. A HPCI isolation signal was expected but HPCI was already

isolated. Therefore, no actuations were anticipated. The Group 3

isolation would not have been prevented - only anticipated - had

thorough research been conducted. Since this event and numerous

other clearance problems, the licensee has improved the clearance

process such that events of this type have been minimized.

b. (CLOSED) LER 1-89-19, Failure of the Service Water System to Meet

Design Requirement. This report documented the failure of the

service water system to meet the requirements for system hydraulic

capability, cross-tie leakage and the motor reliability. This item

was discussed in the NRC Diagnostic Team inspection conducted in

April and May 1989, and was the subject of an enforcement conference

held in the Region II office. A Notice of Violation 89-34-47 was

issued as a result of the above action. This violation and the

licensee's actions taken to resolve this issue were disnussed in

l detail and the violation was closed in Report No. 325,324/90-52.

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Based on the information contained in that report, this item is also

closed.

c. (CLOSED) LER 1-89-21, Inadvertent Divisi7n 1 LOCA Initiation During

Test Perfo.mance as a Result of Miscommunication and Failure to

Verify Voltage. This event occurred during the performance of an MST

when .an I&C technician placed test lead on an incorrect terminal to

take a resistance measurement without verifying the absence of

vol tage. This resulted in the initiation of an inadvertent LOCA

initiation signal. All systems performed as designed. After

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verification that an event did not exist, the signal was reset. The

licensee has determined the root cause of this event and has provided

counselling and training to the involved technicians. This subject

was also discussed with the remaining technicians during scheduled

maintenance real time training. The applicable test procedures were

. revised to delete the resistance measurement that was being taken

when the event occurred since an evaluation has determined that it is

not a required step.

d. (CLOSED) LER 1-89-24, Failure to Test Seventeen Primary Containment

Isolatior. Valves Per Technical Specification 4.6.1.1.a, Due to Failure

to Recognize Testing Applicability. The root cause of this event was

a weakness in the design basis documentation that did not identify

all of the design criteria, Technical Specifications and affected

procedures for the above valves. A Regulatory Compliance TS

Interpretation 85-01 was issued in 1985 that identified PCIS valves

as those valves that require LLRT and-did not include valves that

fall under other criteria. The design engineer who iscued these

modifications to be installed on the above valves placed blame on the

interpretation and not adequately researching these components to

verify whether or not testing was a requirement. The licensee has

updated the PT for valve testing to include the missing valves. A

Design Deficiency Report (DDR) was initiated and routed' to all NED

personnel to insure that they understand this issue and to prevent

recurrence. The DDR has been entered into the design feedback

system. One of the valves was deleted from the list when it was

removed as a temporary repair and was not placed back on the list

when the valve was replaced under the direct replacement program. It

, appears that, on this event, operations . failed to review this DR

package and revise the necessary documentation. Operations had been

provided training on this event and applicable procedure changes have

been initiated to improve and strengthen the direct replacement

program,- These changes appear to be adequate to resolve this item

and prevent repetition.

e. (CLOSED) LER 1-89-25, Failure to Fulfill Surveillance Requirements

of Technical Specification 4.11.2.1. This event involved the loss of-

ability to sample the stack radiation release due to a frozen sample

line during extreme cold weather conditions. This had resulted from

a lack of insulation on a three foot section of line where they exist

in the stack. An investigation determined that this condition had

existed since initial installation. Drawings indicate that this line

should have been heat traced but was not. The licensee took

compensatory measures during this event to monitor all input into the

stack. This and other routine monitoring would have identified

unacceptable releases at that time. The uninsulated sample line has

been repaired and an E&RC evaluation determined that no 10 CFR 20 or

10 CFR 50 limits were exceeded during this event.

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f. (CLOSED) LER 1-89-26, Loss of E3 Bus While Deenergizing Bus 2D for

Scheduled Maintenance. Due to past difficulties in performing this

evolution, operations and the system engineer had developed

handwritten instructions on how to perform this task. These written

instructions were not explicitly followed since the SR0 performing

the evolution disagreed with the instructions. During the event, the

DC logic did not perform as designed. An investigation determined

that the Engine Room Manual Control Relay B (EMCR-B) had its normal

contact arrangement reversed (normally open vice closed). This

contact is located in the " Loss of Emergency Bus Diesel Start Relay"

circuit of the ECCS logic. In conjunction with the Control Room

Manual Control Relay (CMCR), EMCR-B serves to block a DG auto start

when the master / slave breakers are opened and the DG is operating in

the Control Room Manual or Engine Room Manual Mode. The reversed

contact in the DC logic did not play an active role in the event.

The deviation from the normal sequence was that the auto start

circuit for DG 3 was initiated by opening the master / slave breaker

instead of an undervoltage or Bus E3, The remaining logic performed

as designed. An investigation into the reversed cartridge was not

able tc reveal when this occurred. A review of the 3 remaining DGs

did not reveal a similar problem. The EMCR-B relay was corrected

under WR/JO 89-BBHEl. The primary cause of this event was not having

an adequately approved procedure for this task. The existing

procedure did not -address running loads and the handwritten

instructions confused the SRO. In addition, the reversed cartridge

allowed a different signal to be inputed to the DC logic than was

normally expected. Specific procedural guidance for removing

rotating -loads from an E bus prior to opening the master / slave

breakers when switching power from the normal- feed to the DG have

been developed and implemented. The inspector reviewed the plant

electrical system Operating Procedure OP-50, Revision 28 for Unit 2

and Revision 15 for Unit 1, to ensure that this action had been

completed,

g. (CLOSED) LER l-90-09, Required Surveillance Not Performed on Unit I

and.2 E11-F013A and E11-F0138 PCIS V?lves. During the performance of

PT-2.2.4a, Primary Containment Integrity Verification, Containment

External, it was determined that the requirements of TS 4.6.1.la were

not being met for the above valves. These valves do not get an

automatic isolation signal and were not being verified closed every

31 days as required by TS. This was not being done since the valves

were not listed in the above PT. The safety significance of this

event was minimal since the location of these valves is normally

below the water level in the suppression pool which would provide a

water seal. The procedure has been modified to list the above

valves. The inspector reviewed the. revised procedure and the

licensee's other corrective actions taken as a result of the above

event and determined that they appear adequate to prevent repetition.

This item is therefore closed.

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h. (CLOSED) LER 2-89-03, RWCU Group Ill isolation During Performance of

HPCI MST. The inadvertent RWCU isolation was caused by a technician

lifting the wrong lead from a scan module located in panel H12-614.

The mistake was attributed to the congestion of the wiring in the

back of the cabinet and the fact that the modules are not labelled in

the back of the panel . The licensee has developed and installed a

map on the back of the cabinet to assist the technician in locating

the correct module. The -inspector has observed, through direct

observation,.that the maps are installed for both units and have been

useful to the technicians when they perform surveillance tests in

these panels.

i. (CLOSED) LER 2-89-05, HPCI Declared Inoperable Due to a Limitorque

Corporation Software Error. A software error with the Motor Actuator

Characterizer (MAC) diagnostic equipment supplied by Limitorque

resulted in closing torque switch settings for the SMB-3 actuator to

be approximately 800 foot-pounds higher than actual. This

discrepancy was found by the licensee in concert with limitorque

while troubleshooting one of the licensee's SMB-3 actuators at

Limitorque's test facility. At the time of discovery, Unit I was in

a refueling outage and Unit 2 was operating.

The licensae's evaluation determined that this condition rendered the

Unit 2 HPCI injection valve inoperable since the MAC equipment had

previously been used to set the torque switch for this actuator.

Other SMB-3 actuators had either not had their torque switches set

usinc +he MAC equipment or the licensee put in place appropriate

compenstory measures to ensure that the valves could perform their

function. The Unit 2 HPCI injection valve torque switch setting was

adjusted to the correct value during a power reduction several days

later. Subsequent to this event, the licensee has received new

software from Limitorque correcting the discrepancy. The problem was

determined to be unique to the SMB-3. Affected valves have been

properly adjusted using this new software,

j. (CLGitb) 1.ER 2-89-13, . Failure of the HPCI Auxiliary Oil Pump Seal .

The inspectors reviewed the licensee's material- evaluation of the

failed seal. Examination showed that the adhesive joining the

elastomer and the metal had f ailed. Chemical analysis further

revealed that the failed adhesive was chemically different from the

good adhesive. This difference could be attributed to the seal being

constructed with an off specification adhesive or degradation from

service due to high temperatures or incompatibility with the pump

media. The licensee found no evidence that high temperatures

occurred during the operation of the system. Adhesive material was

also demonstrated to be compatible with the pump media. The root

cause of this failure was, therefore, not established. General

l

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12

Electric recommended retaining the same seal material as it has been

used successfully at many other facitities. If additional failures

occur, further actions will be considered.

k. (CLOSED) LER 2-89-14, Failure of the Drywell to Drywell Head Flange

Outer Seal During Local Leak Rate Testing. The licensee performed a

material analysis of the failed gasket at their Harris E&E Center.

The analysis showed that the gasket failed due to a combination of

high drywell temperatures and the use of Nickel Never-Seez as a

gasket lubricant. The licensee implemented ventilation modifications

last refueling outage to reduce drywell temperatures. These

modifications have been effective in lowering drywell temperatures.

'In addition, the licensee has revised their refueling procedures to

use Dow Corning High Vacuum Grease as the lubricant for the drywell

head gasket. The inspector verified, through review of

documentation, that the appropriate procedure changes were made.

1. (CLOSED) LER 2-89-15, PCIS/SDC Suction Valve, 2-E11-F008, Isolated

After Action Taken to Preclude the' Isolation. Corrective action for

this event included individual counseling, procedural enhancements

and training for all operations personnel. The inspector reviewed

the procedure changes and verified they adequately addressed the

identified discrepancies. However, the inspector noted that 4 other

surveillance test procedures, which test similar features and cause

the same isolations, were not updated. Procedure revision requests

had been submitted to update these procedures but no completion date

was provided. The licensee has since stated that these procedures

will be revised prior to their next scheduled use. In addition, an

ACR was generated to address the fact that the licensee considered

their corrective actions for this event complete when, in fact, they

were not.

L m. (CLOSED) LER 2-89-16, Unexpected Isolation of 2-G31-F004 Valve

During SP-89-51 Due to inadequate Clearance Review. This event

occurred during the performance of DG-3 Emergency Bus Energization

! Response Time Test. The procedure called for the removal of the RWCU

l filter demineralizers for service during the test. The shift foreman

L decided not to remove the RWCU system from service because the

l

filters had recently been precoated and the holding pump would lose

i power during the momentary loss of E3 power. This would prevent the

filter resin from being maintained on the septa and require the

filters to be backwashed and precoated. A shift foreman clearance

was used to open the breaker to Division 1 RWCU inboard isolation

vah e 2-G31-F001. However, the operations staff failed to realize

that the non-regenerative heat exchanger outlet temperature high

isolation signal (a non-engineered safety feature -(ESF) isolation

which causes the outboard isolation valve 2-G31-F004 to close), was

also powered from a Division 1 source. Therefore, when power was

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13

lost, the F004 valve closed. This incident was the result of a

failure of operations personnel to adequately review the associated

logic drawings. The inspectors verified that the licensee's

,

corrective actions provided counseling of the personnel involved.

The inspectors also reviewed the attendance records and lesson plan

for the Real Time training provided to operations personnel on the

event.

Violations and deviations were not identified.

7. Prompt Onsite Response to Events - Dropped Fuel Bundle (93702)

On January 2,1991, an irradiated fuel bundle was dropped approximately

ten feet into the Unit 1 core. It was being lowered into its assigned

position in the core matrix at the time ano came to rest in its normal

position. No significant damage was immediately evident and no gas

release was observed. The licensee took proper precautionary actions and

evacuated refueling floor personnel. Reactor coolant and airborne samples

verified no release had occurred.

The licensee initiated a SIIT investigation. The cause of the problem was

determined to be due to a pre-existing fuel handling grapple installation

error that caused the grapple to fail open instead of closed upon loss of

the refuel bridge control power. The grapple consists of two interlocking

"J" hooks that open and close via the action of air operated pistons. A

solenoid valve routes pressurized air to tha pistons to either open or

close the grapple depending on either energizing or de-energizing the

solenoid. . The power for the solenoid is controlled by a simple two

position on/off switch labeled "open" and "close" corresponding to the

grapple position. The solenoid, air supply, and grapple are supposed to

be configured such that the grapple is open when the solenoid is

.

energized. Thus, upon loss of power, the grapple will fail to the safe

closed position. The investigation revealed that the grapple failed open

upon loss of power. This was due to the supply lines between the solenoid

v61ve and the grapple pistons being crossed. Likewise, the control switch

was reversed such that when positioned to "close", the solenoid was

energized instead of de-energized. The result of the two reversals

allowed the grapple to operate normally, i.e., the grapple opened and

closed correctly according to the control switch position, but upon loss

. of power -to the solenoid, the grapple failed open. This problem was

'

masked in the past by the interlocking double "J" design that prevents the

grapple from opening whenever a fuel bundle or other load is .being

suspended.

At the time the fuel bundle was dropped, the following sequence of events

occurred. Af ter initial alignment of the fuel bundle within the core

matrix, the bridge operator increased the lowering speed of the hoist to

maximum. Approximately two feet of the way into the core (corresponding

to the top of the control blade), the bundle encountered some interference

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with surrounding components which momentarily unloaded the grapple and  ;

actuated the hoist's " slack cable" protective feature which caused the

hoist to stop. The delay in stopping the hoist and momentum of the

grapple allowed the interlocking double "J" hook to become disengaged from

the fuel bundle bail. Due to the sudden stop from maximum speed, the

hoist overload protective feature inadvertently acutated causing the

bridge -control power to de-energize. This de-energized the grapple

solenoid and the grapple f ailed open. The bundle handle was now clear of

the grapple._ The interference r2 straining the bundle cleared and the

bundle fell to its final position.

The licensee's investigation revealed the grapple configuration error.

The error was easily corrected by interchanging the air hoses and

reversing the open/ closed control switch. The licensee could not

determine when the error occurred and postulated that it has always

existed. The Unit 2 grapple was tested and found to be correct. The

refuel bridge interlocks and hoist are required to be tested by TS 4.9.1.2.a and b and 4.9.6 prior to movement of control rods or fuel

assemblies within the reactor pressure vessel. Toese tests are

implemented by PT-18.1, Refueling Position Interlock Check. The inspector

verified that the PT performs all TS required testing. TS do not require

that the fail-safe feature of the fuel handling grapple be tested.

However, PT-18.1, Section 7.5.9 checks that a test eight does not

disengage when the grapple power is de-energized, but tl2 interlocking "J"

hooks prevent the grapple from opening, thereby, rei fering the test

ineffective for checking the fail closed feature. The licensee determined

that the hoist brake safety features also were 1ot correctly tested by the

PT. The hoist has an electric and mechanical b*ake. The PT tests these

concurrently. Therefore, if one was not functioning, the other would mask

the failure. The licensee revised their procedures and tested the brakes

individually prior to recovery of the dropped bundle. Both performed

-correctly.

The licensee developed Special Procedure SP-91-001, Inspection of Unit 1

Core Cell 10-15 Following Drop of Fuel Bundle LYG612, for inspection of

the affected fuel cell, the dropped bundle, and adjacent areas. Nc

significant damage was detected. The dropped bundle was removed to t1e

spent fuel pool and an appropriate fuel shuffle utilizing a previous

burned bundle as a replacement, was perfomed.

'

Other action was taken to address the control power loss due to

'

inadvertent actuation of the hoist overload protective feature. The

result was that the maximum lowering speed of the hoist has been

temporarily reduced from approximately 20 feet per minute to approximately

14 feet per minute. This has reduced the frequency of inadvertent control

power loss until the actual cause can be determined. The licensee's

investigation has been hampered by poor refueling bridge drawings and

configuration documentation.

l

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L

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15

Further inspection of long term corrective actions will be conducted

pending receipt of the Licensee Event Report.

Violations and deviations were not identified.

.8. In-Office Report Review (90712)

a. (CLOSED) Violation 325,324/89-20-07, Failure to Hold Quarterly

Corporate Nuclear Safety Review Board (CNSRB) Meetings As Specified

in Brunswick Improvement Program (BIP), Item VI-5. As the BIP was

required to be implemented by Confirmatory Order EA-82-106, the

subject violation was cited because the quarterly CNSRB meetings were

discontinued without prior NRC notification / approval. The intended

CNSRB function of- providing independent assessment of potential

safety concerns at CP&L nuclear plants is now captured -by CP&L's

recently implemented Nuclear Assessment Program (Integrated Action

Plan item E5). Based on this and the licensee's November 20, 1989

response, which adequately addressed the failure to maintain in place

regulatory comitments made to the NRC, this item is considered

closed.

9. Action on Previous Inspection Findings (92701) (92702)

a. (CLOSED) Violation 325/89-05-01, Failure to Follow Equipment

Clearance Procedure. This incident involved the failure to establish

adequate clearance for work activities on F010 and F014 valves on the

Standby Liquid Control System. The valves used to isolate this work

did not take into consideration that both the above valves would be

manipulated during the maintenance activity which was permitted by

the established procedure. _The . manipulation of the above valves

resulted in partial draining of the SLC tank. The licensee's

corrective action on the above included establishment of a Clearance

Center staffed by licensed reactor operations personnel and

additional training to operations and maintenance personnel on

procedural revisions made to strengthen the tagging process. The

inspectors reviewed the changes made to the Equipment Clearance

Procedure AI-58-under Revision 29 dated July 7, 1989, and the lesson

plans and attendance sheets for the training conducted for operations

and maintenance personnel on the revised procedure. The Clearance

Center, which was established in 1989, had led to an improvement in

the clearances issued and a marked reduction in clearance errors,

b. -(CLOSED) Violation 325,324/89-20-04, ONS Not independent During Post

Trip Reviews. This violation involved the assignment of an 0NS

member as the team leader of a Site Incident Investigation Team. As

SIIT team leader he was required to sign off on functions that he was

also required by TS 6.2.3.2 to provide independent oversight over.

The licensee corrective action to resolve this item included revision

of Regulatory Compliance Instruction, Site Event Investigation

Process, RCI-06.6, on November 22, 1989, to ensure that ONS are not

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16

assigned any functions on SIITs. A TS interpretation was also issued

to clarify the duties,- responsibility and independence of this

organization. A review of selected Silts since this event indicates

that this problem has been corrected.

c. (CLOSED) Violation 324/89-20-06, Inadenuate G earance, and Violation

3?S/89-44-01, failure to Follow Al-58 for Drawing Research. Both of

the above violations involved a lack of attention to detail in

researching drawings to ensure the adequacy of clearances, in both

the above cases, plant safety equipment was rendered inoperable due

to these errors. The inspector reviewed the licensee's corrective

actions on the above items. These included the establishment of a

task force to study the overall problems associated with clearances

and repetitive errors in this area. The results of this task force's

findings have led to upgrades in Al-58 and the establishment of a

dedicated Clearance Center. This center provides for duplicate and

independent reviews of clearance requests. This center is staffed by

senior licensed operators and has been in operation for approximately

one year. Although some errors have been identified in this new

process, it appears to have led to significant improvement in this

area. Based on the progress to date, these violations are closed.

However, the overall effectiveness of this center and the other

cleararce program improvements will be evaluated further under IAP

item E-2.

Violations and deviations were not identified.

10. Information Meetings With Local Officials (94600)

The inspectors and the project section chief met with and explained the

'

NRC's' mission and inspection program at the Brunswick Plant to local

officials. Meetings were held with the Mayor of Boiling Spring Lakes on

January 10, the City Managers of Long Beach and Southport and the Acting

Brunswick County Manager and Emergency Management Coordinator on January ,

16 - the Manager of Bald Head Island on January 17, the County Manager and

Director of Emergency Preparedness for New Hanover County and the Manager

of Carolina Beach and the Mayor Pro Tempore of Kure Beach on January 29,

1992. The Mayor for the town of Caswell Beach was contacted but was not

available for a meeting at the present time. The Mayor of Youpon Beach

presently works at the Brunswick Plant and indicated that he was fully

aware of the NRC's mission and role at the Brunswick Plant. The above

towns and two counties comprise all areas within a 10 mile radius of the

plant. The above personnel appeared to be very appreciative of the visits

and were provided with - telephone contact numbers for the resident

inspec tors,-- The Region 11 Section and Branch Chiefs -and the NRC

Headquarters Emergency Response Center.

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17

Local Fublic Docun ent Room

The inspector visited the LPDR for Brunswick which is located at the

University of North Carolina - Wilmington Randall Library. The inspector

found the available documentation to be neatly arranged and properly

categorized according to NRC instructions. Library personnel were

knowledgeable and helpful. The inspector was hble to access recently

issued Brunswick-related documentation from microfiche. All documents

issued since July 1990, are in microfiche form.- The inspector noted that

the files are arranged in broad categories. Within categories,

documentation is filed basco on issuance to the LPDR, not necessarily on

the date of the documentation. This results in the search for a

particular document to be burdensome. For example. the inspector sought a

particular 1989 Resident inspector report by number. This could be

located only-by having the knowledge of the approximate date that it may

_

have been issued in microfiche form. A random search of the microfiche

accession list in the approximate time period was necessary to locate the

appropriate report number. The inspector concluded that the method of

categorizing makes the information virtually unretrievable without some

prior knowledge of the' docummts available, e.g., an individual cannot

easily access all inspection reports for a given year or SALP cycle.

The inspector located a hard copy version of outdated Brunswick custom

Technical Specifications. A search for the curret.t TS was unsuccessful.

A call to the LPDR hotline in Washington rev6aled that no complete

compilation of current TS is maintained, rather, trA4vidual TS amendments

are randomly filed in the broad " licensing" category. The TS in this

form, if the individual amendments could be located, are unusable. The

only compiled document maintained in its current form is the FSAR. The

inspector concluded that, although the pertinent documentation appeared to

be present, the filing system and accessibility is not user friendly and

,

is, therefore, of very limited use to the public.

11. ExitInterview-(30703)

The inspection scope and findings were summarized on Janrny 31, 1991,

with those persons indicated in paragraph 1. The inspect rs described the

areas inspected and discussed in detail the inspection ' fndings listed

below. Dissenting comments were not received f rom 'le licensee.

Proprietary information is not contained in this report,

item Number Description / Reference Paragraph

324/90-01-01 VIOLATION - Failure.to Meet Procedure

Prerequisites, paragraph 4.a.

325,324/90-01-02 NON-CITED V10LATi"1 - Failure to Implement Freeze

Protection Pro :aures, paragraph 4.b.

,

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4

i 12. Acronyms and Initialisms

ACR Adverse Condition Report

AI Administrative Instruction

A0 Auxiliary Operator

APRM Average Power Range Monitor

BSEP Brunswick Steam Electric Plant

CMCR Control Room Manual Control Relay

CNSRB Corporate Nuclear Safety Review Board

CO Control Operator

DC Direct Current ~

DDR Design Deficiency Report

DG Diesel Generator

DR- Direct Replacement

E&E Energy & Environment

ECCS Emergency Core Cooling System

EMCR Engine Room Manual Control Relay .

ERFIS_ Emergency Response Facility Information System

_

ESF Engineered Safety Feature

F Degrees Fahrenheit

FWLCS Feedwater Level Control System

HP- Health Physics

HPCI High Pressure Coolant Injection

IAP Integrated Action Plan

1&C Instrumentation and Control

I E. NRC Office of Inspection and Enforcement

IEEE International Electrical & Electronic Engineers

IFI. Inspector Followup Item ,

IPBS Integrated Planning, Budgeting and Scheduling

LER Licensee Event Report

LLRT Local Leak Rate Test

LOCA Loss.of Coolant Accident

LPDR Local Public Document Room

LPRM Local Power Range Monitor- '

MAC Motor Actuator Characterizer

MST Maintenance Surveillance Test

NED Nuclear Engineering Department

NRC Nuclear Regulatory Commission

01 -Operating Instruction

ONS Onsite Nuclear Safety

0P Operating Procedure

PA Protected Area

PCIS Primary Containment Isolation System

PM Plant Modification

PNSC -Plant Nuclear Safety Committee

PT Periodic Test

QA Quality Assurance

QC. Quality Control

,

(

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RCI Regulatory Compliance Instruction

RCIC Reactor Core isolation Cooling

RHR Residual Heat Removal

R0 Refueling Outage

RPS Reactor Protection System

RWCU Reactor Water Cleanup

SBGT Standby Gas Treatment

SCO- Senior Control Operator

SDC Shut Down Cooling

SF Shift Foreman

SIIT Site Incident Investigation Team

SLC Standby Liquid Control

SP Special Procedure

SRG Senior Reactor Operator

STA Shift Technical Advisor

SWFCG Site Work Force Control Group

TS Technical Specification

URI Unresolved item

WR/JO Work Request / Job Order

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