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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program IR 05000346/19980211999-08-0606 August 1999 Refers to NRC Insp Rept 50-346/98-21 Conducted on 980901- 990513 & Forwards Nov.Two Violations Identified Involving Failure to Maintain Design of Valve & Inadequate C/A for Degraded Condition Cited in Encl NOV 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy 1999-09-09
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program PY-CEI-NRR-2438, Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & Pnpp Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls 05000346/LER-1998-001, Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached1999-09-0909 September 1999 Forwards Rev 1 for LER 1998-001,which Updates Corrective Actions & Revises Completion Date Re Implementation of Changes to Plant Emergency Operating Procedure.List of Commitments Attached ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps 05000346/LER-1998-009, Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl1999-08-0606 August 1999 Forwards LER 98-009-01,IAW 10CFR50.73(a)(2)(ii)(B). Commitments Made by Util Are Encl ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete 05000346/LER-1998-012, Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached1999-07-0707 July 1999 Forwards LER 98-012-01,which Is Being Submitted to Provide Addl Info Re 981018 Occurrence.Commitment List Attached ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20196A6601999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E9561999-05-28028 May 1999 Forwards Update to NRC AL 98-03,re Estimated Info for Licensing Activities Through Sept 30,2000 ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 ML20207E7801999-05-21021 May 1999 Forwards Application for Amend to License NPF-3,allowing Use of Expanded Spent Fuel Storage Capacity.Proprietary & non- Proprietary Version of Rev 2 to HI-981933 Re Cask Pit Rack Installation Project,Encl.Proprietary Info Withheld ML20206N0231999-05-0606 May 1999 Forwards License Renewal Applications for Davis-Besse Nuclear Power Station,Unit 1 for ML Klein,Cn Steenbergen & CS Strumsky.Without Encls ML20206D2421999-04-28028 April 1999 Forwards Combined Annual Radiological Environ Operating Rept & Radiological Effluent Release Rept for 1998. Rev 11, Change 1 to ODCM & 1998 Radiological Environ Monitoring Program Sample Analysis Results Also Encl PY-CEI-NRR-2382, Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl1999-04-21021 April 1999 Forwards 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for FY98 Also Encl ML20206B8831999-04-17017 April 1999 Forwards 1634 Repts Re Results of Monitoring Provided to Individuals at Davis-Besse Nuclear Power Station During 1998,per 10CFR20.2206.Without Repts ML20205K5641999-04-0707 April 1999 Forwards Response to NRC 980415 RAI Re GL 96-06, Assurance of Equipment Operability & Ci During Design-Basis Accident Conditions. Rept FAI/98-126, Waterhammer Phenomena in Containment Air Cooler Swss, Encl ML20205K3871999-04-0707 April 1999 Forwards Copy of Application of Ceic,Oec,Ppc & Teco to FERC, Proposing to Transfer Jurisdictional Transmission Facilities of Firstenergy Operating Companies to American Transmission Sys,Inc.With One Oversize Drawing ML20205J1171999-03-29029 March 1999 Forwards Rev 1 to BAW-2325, Response to RAI Re RPV Integrity, Per GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity. Rev Includes Corrected Values in Calculations PY-CEI-NRR-2377, Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1)1999-03-29029 March 1999 Submits Decommissioning Repts for Bvps,Units 1 & 2,Davis- Besse Nuclear Power Station,Unit 1 & Perry Nuclear Power Plant,Unit 1,per 10CFR50.75(f)(1) ML20205F5961999-03-27027 March 1999 Forwards Comments on Preliminary Accident Sequence Percursor (ASP) Analysis of 980624 Operational Event at Dbnps,Unit 1, as Transmitted by NRC Ltr ML20205D4791999-03-26026 March 1999 Forwards Rept Submitting Results of SG Tube ISI Conducted in Apr 1998.Rept Includes Description of Number & Extent of Tubes Inspected,Location & Percent wall-thickness Penetration for Each Indication of Imperfection ML20205L2031999-03-26026 March 1999 Submits Correction to Dose History of Tj Chambers.Dose Records During 1980-1997 Were Incorrectly Recorded Using Wrong Social Security Number.Nrc Form 5 Not Encl ML20205C7371999-03-25025 March 1999 Certifies That Dbnps,Unit 1,plant-referenced Simulator Continues to Meet Requirements of 10CFR55.45(b) for Simulator Facility Consisting Solely of plant-referenced Simulator.Acceptance Test Program & Test Schedule,Encl ML20205E3551999-03-19019 March 1999 Requests That Proposed Changes to TS 6.8.4.d.2 & TS 6.8.4.d.7 Be Withdrawn from LAR Previously Submitted to NRC ML20204J6361999-03-17017 March 1999 Forwards Firstenergy Corp Annual Rept for 1998 & 1999 Internal Cash Flow Projection as Evidence of Util Guarantee of Retrospective Premiums Which May Be Served Against Facilities PY-CEI-NRR-2375, Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage1999-03-15015 March 1999 Forwards List That Details Util Insurers,Policy Numbers & Coverage Limits for Two Power Plants,Per Requirements of 10CFR50.54(w)(3) Re Reporting of Property Insurance Coverage ML20204E6821999-03-12012 March 1999 Requests That Listed Changes Be Made to NRC Document Svc List for Davis-Besse Nuclear Power Station,Unit 1 1999-09-09
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.lohn K. Wood 419-249-2300 Vice President - Nuclear far 419-321-8337 Docket Number 50-346 License Number NPF-3 Serial Number 1-1153 April 9, 1998 United States Nuclear Regulatory Commission Document Control Desk Washington, D. C. 20555-0001
Subject:
Response to Inspection Report Number 50-346/98002 (DRP)
Ladies and Gentlemen:
{
Toledo Edison (TE) has received Inspection Repon Number 50-346/98002 (TE Log Number 1-3948) and the two enclosed Notices of Viohtion (NOV) which require a response.
The responses to the violations contained in IR98002 are provided in Attachment I to this letter .
The first NOV of the Inspection Report deals with failure to properly implement procedures at l the Davis-Besse Nuclear Power Station (DBNPS). The management of the DBNPS recognizes l the importance of the two occurrences associated with this violation and their potential impact on '
l plant safety and reliebility. As a result, the Potential Condition Adverse To Quality Reforts for l these oct ,rrences have been categorized within the corrective action process to receive increased
! management review and over-site, l
The management of the DBNPS continues to emphasize self-checking and verbal communications in the course of daily operations in an effort to prevent errors founded in human performance deficiencies. Emphasis on these strategies has been effective in reducing errors of the type identified in the violation examples. Although the first violation is based in part on deficient procedural implementation, the deviations resulted from non-intentional human errors.
Differentiation of human performance issues from a resultant procedural violation is necessary to i achieve continued improvement in the operation of the DBNPS.
)
For the purposes of clarification relative to the first violation, the Inspection Report body j contained references to the inadvertent isolation of Reactor Coolant Pump seal injection. The !
event cited involved inadvertent isolation of seal return. g
- d \
9804160086 980409 PDR ADOCK 05000346 0 PDR
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Docket Number 50-346 License Number NPF-3 Serial Number 1-1153 Page 2 Should you have any questiccs or require additional information, please contact Mr. James L.
Freels, Manager - Regulatory Affairs, at (419) 321-8466. i l
Very truly yours, D L /laj enclosure cc: A. B. Beach, Regional Administrator, NRC Region III S. J. Campbell, DB-1 NRC Senior Resident Inspector A. G. Hansen, DB-1 NRC/NRR Project Manager Utility Radiological Safety Board 1
l 1
I
't
$' l d
,, Docket Number 50-346
, License Number NPF-3 Serial Number 1-1142 At,tachment i Page1 i
Reolv to a Notice of Violation (50-346/98002-01IDRP1) l Alleged Violation i I. Technical Specification 6.8.1 states, in pa:r, that written procedures be established, I implemented and maintained covering surveillance and test activities of safety-related equipment and that written procedures be established, implemented and maintained covering the applicable procedures recommended in Appendix A of Regulatory Guide (RG) 1.33, November,1972.
A. Technical Specification Surveillance Requirement 4.4.6.2.1.d states, in part, that a I reactor coolant system water inventory balance be performed at least once per 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> during steady state operation.
Procedure DB-SP-03357, Revision 01,"RCS Water Inventory Balance," implements Technical Specification Surveillance Requirement 4.4.6.2.1.d. Step 4.1.10 of Procedure DB-SP-03357 requires that Demineralized Water Isolation Valve l DW-6831B be opened.
B. Appendix A of RG 1.33, November,1972, Section A.4, requires administrative i procedures for procedure adherence. Procedure NG-DB-00225," Procedure Use and I Adherence," implements RG 1.33, to establish and implement procedures covering adherence.
Step 6.8.1 of Procedure NG-DB-00225 requires, in part, that procedures be performed as numerically sequenced in the body of the procedure.
l Contrary to the above- l A. On January 6,1998, during performance of Procedure DB-SP-03357, Revision 01, i "RCS Water Inventory Balance," Step 4.1.10, a reactor operator erroneously closed Reactor Coolant Pump Seal Return Valve MU-38 instead of opening Demineralized Water Isolation Valve DW-6831B.
B. On February 11,1998, the licensee did not properly perform the sequence of steps in 1 Procedure DB-OP-06001, " Boron Concentration Control," in that a reactor operator failed to complete Step 3.5.18 to open Booster System Bypass Valve WC-3526 while performing Procedure Steps 3.5.17 through 3.5.19.
This is a Severity Level IV viola
I l D*o cket Number 50-346 l
l , License Number NPF-3 l
i Serial Number 1-1142 1 Attachment i Page 2 '
Reason for the Violation A. The valve MU 38 is the containment isolation valve for the Reactor Coolant Pump (RCP) seal return flow path. This violation involved the inadvertent isolation of the RCP seal return flow path. The reason for the wrong valve (MU38) being cycled during the performance of DB-SP-03357 was less than adequate work practices. The causal factor for this occurrence was that self-checking was not applied to ensure the correct component was being cycled. After reading the procedure, the Reactor Operator proceeded to the back Control Room panel with the intent of re-positioning l DW6831B. The switch for MU 38 is directly below the switch for DW 6831B on the back panel. Prior to performing the valve operation, the operator did not apply appropriate seif-checking techniques to verify performance of the correct procedural action.
During the course ofinvestigation of this occurrence, additional conditions were identified and are being addressed in the Davis-Besse Nuclear Power Station (DBNPS) I corrective action program. When the Reactor Operator realized that the wrong valve (MU 38) had been repositioned, he immediately re-opened the valve. The action to 1 re-open MU 38 was the correct operator action in DB-OP-02515, " Reactor Coolant l Pump and Motor Abnormal Procedure." However, this immediate action was inconsistent with management's expectations. Operational expectations in this case would be to identify the incorrect action, notify the Control Room Senior Reactor Operator, refer to the appropriate controlling procedure and take action as directed by the Control Room Senior Reactor Operator.
B. While placing Deborating Demin #2 in service to reduce Reactor Coolant System Boron Concentration, WC 3526, Booster System Bypass Valve was inadvertently left ;
closed. This interrupted the flowpath from the Reactor Coolant System, resulting in !
the lifting of Relief Valve MU 1890 and allowing approximately 30 gallons of Reactor
. Coolant System water to f'ow to the Reactor Coolant System Drain Tank. The reasons for this occurrence involve deficiencies in procedural guidance and inappropriate work ;
practices. '
l There were two causal factors with regard to inappropriate work practices. The procedure DB-OP-06001 was not followed correctly. The licensed Reactor Operator failed to open WC 3526, Booster System Bypass Valve as required by procedure DB-OP-06001. The procedure being used by the operator had been previously used to perform a deboration, which is repeatedly performed over a period of approximately one month near the end of an operating cycle. Since the procedure copy had been previously used and signed off to perform a deboratiu, during a previous deboration, the step for opening WC 3526 had been signed off. The Reactor Operator had not added additional sign off lines or other place keeping measures to the procedure, and was not inidaling each step as he performed the step. The Control Room Senior Reactor Operator was unaware that a procedure was being re-used for that evolution.
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- ~ D'ocket Number 50-346 License Number NPF-3 Serial Number 1-1142 Attachment 1 Page 3 Re-use of the procedure eliminated the place keeping aid (step initials) that serves as a barrier for missing a step during performance.
The procedure DB OP-06001 was deficient in the formatting of a procedure step and the omission of relevant information from a caution statement. Direction for this evolution is contained in DB-OP-06001, Subsection 3.5, Deboration Using Deborating Demineralizers. The last step in this Subsection includes a step "WHEN processing is complete, TIJFE restore the Clean Radwaste System Lineups." Since additional processing using the Deborating Demineralizer was expected, this step was not performed and the procedure remained open. The Operators continued to re-use this procedure copy. This provided the conditions for the place keeping device (step initials) to not be available for the Reactor Operator in this event. The step directing opening WC 3526 had already been signed off during a previous performance. A caution statement was provided for step 3.5.17 and stated, "MU 40 shall be open prior to positioning MU 11 to the CLN WST position." This caution is intended to prevent lifting MU 1890, since MU 40 is in the Letdown Flowpath. This exact same condition is also applicable to WC 3526 as well. The caution does not provide information related to the required position for WC 3526. The Reactor Operator specifically remembered rechecking the position of MU 40 prior to placing MU 11 in the CLN l WST position based on this caution, but did not check the position of WC 3526.
1 Corrective Stens that have been Taken and Results Achieved A. After MU 38 was re-opened, DB-OP-06005, " Reactor Coolant Pump Operating Procedure" and DB-OP-02515, " Reactor Coolant Pump and Motor Abnormal Operating Procedure," were referred to and verified, by the operators, that the proper actions were taken. The RCP operating parameters were reviewed including temperature, seal retum flow, and seal cavity pressures. DB-OP-00000, " Conduct Of Operations," Attachment 7, for a component found out of its desired position was l completed. '
The individuals involved in the occurrence were counseled for the areas in which they demonstrated weaknesses. This counseling emphasized management expectations for procedure use practices.
B. The operator involved in this occurrence has been counseled by Operation's management regarding the expectations for procedure use and adherence. This counseling included performance of procedures in the proper step sequence.
The format deficiency within DB-OP-06001, step 3.5.25 was corrected by procedure alteration TA98-0418. Step 3.5.25 now r,ays,"IE no further Deborating Demineralizer processing is planned, THEN restxe Clean Radwaste System Lineups." This change allows the procedure subsection to be closed, while recognizing that further use of the deborating demineralizers has been planned. The Clean Radwaste System lineup can
I Docket Number 50-346
, License Number NPF-3 Serial Number 1-1142 Attachment I l Page 4 1 be left in the proper alignment for demineralizer use and will allow the procedure subsection to be closed.
The omission of relevant procedure information was also corrected by TA 98-0418.
l The caution for step 3.5.17 stated,"MU 40 shall be open prior to positioning MU 11 to l the CLN WST position." The caution has been altered and placed at step 3.5.20 by TA 98-0418. The new caution states "MU 40 and WC 3526 shall be open prior to I positioning MU 11 to the CLN WST position." The altered caution provides l information related to the required position for WC 3526 as well as MU 40.
! Corrective Steos that will be Taken to Avoid Further Violations )
l l A. Procedure implementation mistakes resulting from inadequate human performance have been dealt with both on an individual basis, with the Plant Operations shifts during shift turn-over and in Operator Requalification Training. Individual counseling has been completed for this occurrence. The weaknesses identified in the specific
! actions related to this occurrence will be discussed in Operator Requalification I
! Training and will be completed by Atgust 31,1998.
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( B. The procedure copy of DB-OP-06001 that was being used by the Reactor Operator had been previously used to perform a deboration. During a prior performance, the step for opening WC 3526 had been signed off. The re-use of this procedure l l eliminated the place keeping aid that serves as a barrier for skipping a step during performance. DB-OP-06001, Boron Concentration Control contains lines to be initialed by the operator as each step is performed. The procedures and policies l currently in place at the DBNPS do not provide guidance on the acceptability of re-
! using procedures for multiple performances of the same evolution. NG-DB-00225, Procedure Use and Adherence will be altered to provide direction for this situation.
This action will be completed by . August 31,1998.
Events involving operation of a wrong component have been infrequent at the DBNPS, l based on Plant Operations Section Performance Indicators. A review of Plant Operations Section Performance Indicators for 1996,1997 and 1998 o date was conducted for procedural use errors. The quarterly goals for each quarter of 1996, 1997 and the first quarter of 1998 have been met. Although procedure use events have previously occurred, none of the prior events involved reusing a procedure foi a repetitive evolution. This performance indicator demonstrates recent improvement in this area. In the first two quarters of 1997, six events occurred. In the last two quarters of 1997 and the first quarter of 1998, only two events have occurred, including this one. The current Plant Operations Initiatives for performance improvement are effectively reducing the number of events.
" Docket Number 50-346
, License Number NPF-3 Serial Number 1-1142 Attachment 1 Page 5 Date When Full Comoliance Will Be Achieved A. Full compliance was achieved on January 6, E ien the valve MU 38 was re-opened to re-establish seal return flow. This action was verified to be correct upon i review of the appropriate procedures.
B. Full compliance was achieved on February 11,1998 when the Reactor Operator re- {
opened the flow path from the Reactor Coolant System to the Makeup Tank which {
allowed relief valve MU 1890 to close.' The relief valve was also confirmed to be l closed per procedural guidance.
Reolv to a Notice of Violation (50-346/98002-03IDRP1) ;
Alleged Violation l
II. 10 CFR 50.72 (b)(1)(ii)(B), "Non-Emergency Events - one hour reports," requires, in part. i that the licensee notify the NRC as soon as practical and in all cases within one hour of the occurrence of a condition that is outside the design basis of the plant.
Contrary to the above, on December 12,1997, the licensee did not notify the NRC within one hour of the discovery that the speed sensing circuitry for EDO #1, equipment required for safe shutdown of the plant dar:ng a postulated fire, was not designed in accordance with
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10 CFR Part 50, Appendix R, design criteria for hot shoit protection. The design deficiency l of the speed sensing circuit is a condition outside the des gn basis of the plant. )
l This is a Severity Level IV violation (Supplement 1).
Reason for the Violation Licensee Event Report (LER)97-015, " Emergency Diesel Generator Tachometer Circuit Outside !
10 CFR 50 Appendix R Design Basis," submitted on January 12,1998, provided an apparent cause for this occurrence. The LER also discussed the delay in immedia'e notification reporting relative to this occurrence being outside the design basis of 10 CFR 50, Appendix R.
When this condition was identified in Potential Condition Adverse To Quality Report 97-1624 on December 12,1997, Technical Specification 3.3.3.5.2 was consulted, which specifies inoperable circuits must be restored to operable status within 30 days, or a Special report must be prepared and submitted. No other actions are required by this Technical Specification. The Shift Supervisor consulted vrith Plant Engineering staff personnel and the Fire Protection Coordinator about how the identified condition affected the Emergency Diesel Generator speed circuit during a hot short scenario. As a result of this discussion, the disconnect switch was considered inoperable and Technical Specification 3.3.3.5.2.b was entered.
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,. Ifocket Number 50-346
,. License Number NPF-3 Serial Number 1-1142 Attachment 1 Page 6 After further review, it was determined on December 18,1997, that the plant was being operated in a condition outside the design basis. It was believed that Technical Specification 3.3.3.5.2 applied to this condition due to the interpretation of the Technical Specification wording about l
control circuitry. Upon further review of this issue and upon review of License Amendment i Request (LAR)92-010 (TE Serial Number 2101, incorporated into the Technical Specifications under Amendment 187), it was realized that the term " control circuitry" only applied to components that would be enabled when a disconnect switch was repositioned to allow local control of associated equipment. Since the EDO 1 tachometer circuit was provided for indication purposes only and performed no control function for the EDG, Technical Specification 3.3.3.5.2 only applied to the ability of the disconnect switch to isolate the control room tachometer.
Corrective Steos that have been Taken and Results Achieved l Upon further evaluation of the condition described in PCAQR 97-1624, it was determined that the design requirements involving a hot short in the EDG 1 tachometer circuit were not being -
satisfied. Potential Condition Advers: to Quality Report 97-1658 was initiated which identified the proper reportability and completed the required one hour notification of the NRC. Corrective actions taken for the EDG tachometer circuit are described in LER 97-015. !
Specific to not notifying the NRC within one hour of discovery in accordance with 10CFR50.72(b)(1)(ii)(B), training was conducted on the interface between the Technical Specifications and situations that represent conditions outside the design basis of the plant. This training was provided to Senior Operating Licensed personnel during Licensed Operator Requalification Training Cycle 98-01 which was completed on February 20,1998.
Corrective Steos that will be Taken to Avoid Further Violations Training will be conducted on the interface between Technical Specifications and situations that represent conditions outside the design basis of the plant for Regulatory Affairs - Compliance Unit personnel that are involved in reportability evaluations. This training will be completed by April 17,1998.
Date When Full Comoliance Will Be Achieved Full compliance was achieved at 1415 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.384075e-4 months <br /> on December 18,1997 when the NRC was notified via the Emergency Notification System of this occurrence in accordance with 10CFR50.72(b)(1)(ii)(B).