ML20210S265
ML20210S265 | |
Person / Time | |
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Site: | Clinton ![]() |
Issue date: | 02/09/1987 |
From: | Knop R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
To: | |
Shared Package | |
ML20210S188 | List: |
References | |
TASK-2.B.4, TASK-TM 50-461-87-02, 50-461-87-2, NUDOCS 8702170594 | |
Download: ML20210S265 (33) | |
See also: IR 05000461/1987002
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U. S. NUCLEAR REGULATORY COMMISSION
REGION III
Report No. 50-461/87002(DRP)
Docket No. 50-461 License No. NPF-55
Licensee: Illinois Power Company
500 South 27th Street-
Decatur, IL 62525
Facility Name: Clinton Power Station
Inspection At: Clinton Site, Clinton, IL
Inspection Conducted: December 16 through January 26, 1987
Inspectors: T. P. Gwynn
, P. L. Hiland
R. N. Gardner
src %<
R. C. Knop, Chief g g
Approved By:
Projects Section IB Date
Inspection Summary
Inspection on December 16 through January 26, 1987 (Report
No. 50-461/87002(DRP))
Areas Inspected: Routine, unannounced safety inspection by the resident
inspectors and a region-based inspector of licensee action on previous
inspection findings; licensee action on 10 CFR 50.55(e) report; applicant
action on Three Mile Island (TMI) action plan requirements; licensee event
report' review and followup; review of allegations; Region III request;
operational safety verification; engineered safety feature system walkdown;
onsite followup of events at operating reactors; and management meeting.
Results: Of the areas inspected, no violations or deviations were identified
in nine areas. One violation was identified in the area of onsite followup
of events (paragraph 10.b. - failure to follow and/or provide procedures).
While the violation was of minor safety significance, licensed operators
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made a number of errors that could have been prevented had they used adminis-
trative controls available.One unresolved item was identified in the area of
operational safety verification involving degradation of the secondary
containment gas control boundary (paragraph 8).
g21]Q $$$ 1
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DETAILS
1. Personnel Contacted
Illinois Power Company (IP)
- R. Campbell, Manager - QA
- W. Connell, Manager - Nuclear Planning & Support
- G. Edgar, Attorney
- R. Freeman, Assistant Plant Manager, Maintenance
- W. Gerstner, Executive Vice President
- J. Greene, Manager - Nuclear Station Engineering Department (NSED)
- D. Hall, Vice President, Nuclear
- H. Lane, Manager, Scheduling and Outage Management
- J. Miller, Assistant Power Plant Manager, Startup
- J. Perry, Manager - Nuclear Program Coordination
- R.~ Kerestes, Director, NSED Field Engineer
- F. Schwarz, Director, Outage Maintenance Support
- F. Spangenberg, Manager - L&S
- E. Till, Director, Nuclear Training
- J. Wemlinger, Supervisor, Operations Training
- J. Wilson, Manager - CPS
- R.'Wyatt, Director, Nuclear Program Assessment
Soyland/WIPC0
- J. Greenwood, Manager Power Supply
Nuclear Regulatory Commission - Region III
- B. Davis, Deputy Regional Administrator, Region III
- T. Gwynn, Senior Resident Inspector, Clinton
- P. Hiland, Resident Inspector, Clinton
- R. Knop, Chief, Projects Section IB
- R. Warnick, Chief, Projects Branch 1
- Denotes those attending the monthly exit meeting on January 26, 1987.
- Denotes those attending the management meeting on Jarvary 16, 1987.
The inspectors also contacted and interviewed other licensee and
contractor personnel.
2. Licensee Action On Previous Inspection Findings (92701/92702)
a. (Closed) Open Item (461/86028-09): Fire Protection Administrative
Controls. During a previous inspection, the inspector identified
that fire protection administrative controls were not fully
implemented.
During this report period, the licensee stated that their fire
protection program had been fully implemented. In order to verify
implementation, the inspector selected a random sample of five fire
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protection surveillance requirements for review. The inspector's
sample included the following procedures:
CPS No. 9071.01' Diesel Driven Fire Pumps Operability Test
CPS No. 9071.06 Visual Inspection of Spray and Sprinkler System
Piping and Heads
CPS No. 9071.08 Fire Protection C02 System Valve Position Check
CPS No. 9071.19 . Monthly _ Fire Protection Valve Line-Up _
CPS No. 9071.25 Fire Protection C02 Weekly Operability Check '
The inspector reviewed the associated inspection checklists for
the above procedures that had been completed and stored in the
licensee's record storage vault. The review performed was to
ascertain if the administrative controls established were being
implemented. For this review, the inspector verified that required
inspection frequencies (monthly, weekly) were met; that noted.
deficiencies were documented and required maintenance work requests
were initiated; completed inspections were reviewed for acceptable
results; and that when unacceptable results were documented, followup
inspections were performed to verify corrective action taken. For
the sample selected, the inspector _ concluded that the licensee was-
implementing the administrative controls that had been' established.
The inspector reviewed the licensee's action taken in response to
a concern identified by offsite fire department personnel. As
documented in Inspection Report 50-461/86028, offsite fire
department personnel stated that a self contained breathing
apparatus (SCBA)'was found to have an empty cylinder during a
drill. Since the concern expressed was not identified to the
licensee at the time of the drill, the specific SCBA was not
identified. However, the licensee revised its control over SCBAs
intended for use by offsite fire department personnel. Previously,
, offsite fire department personnel . received SCBA equipment from a
licensee storage locker when responding to the Clinton Power
Station. In an " Acquisition Agreement" dated September 30, 1986,
the licensee provided SCBA equipment to three offsite fire
- departments for their general use and in particular for their use
when responding to the Clinton Power Station as a secondary fire
protection service.- The inspector concluded the licensee's actions
adequately addressed the expressed concern.
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The inspector noted that construction activities at Clinton Power
Station have been reduced to a level consistent with the startup
- phase of operation. Housekeeping requirements have been monitored
i - on a continuous basis by the inspector and minor deficiencies
f identified have been promptly corrected by.the licensee. The
inspector observed the performance of routine fire watches and fire
watches stationed in areas where grinding or hot work was being
,. performed. No deficiencies in fire watch performance have been
- identified.
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_ Based onithe inspector's review of administrative records, actions
taken-by the'. licensee regarding concerns with control of SCBA
equipment, and the noted housekeeping and fire watch performance,
the inspector concluded that .the fire protection' program for Clinton
Power Station was being fully implemented. This item is closed,
b. -(Closed)OpenItem(461/86054-05): Deficiencies related to
watertight doors. During a previous . inspection, watertight doors in
the plant were' observed to have numerous minor hardware deficiencies '
indicating inoperable status. Testing and. maintenance programs had ,
not been established for'these doors.
As. documented in Inspection Report 50-461/86060, paragraph 2, this
item remained open pending completion of corrective actions to.
upgrade reliability of the watertight doors-(plant modification
.HC-20).and pending approval of the maintenance procedure for
watertight doors.
The licensee presented this item to the inspector for closure. All
watertight doors in the plant had been modified in accordance with
minor modification HC-20 through supplement 1 and a formal procedure
for maintenance of watertight doors (CPS No. 8250.01) was approved
for use on December 4, 1986. This information provided the basis '
for closure of this item. ,
The inspector-had noted apparent improvement in the reliability
of plant watertight doors through routine tours of the facility.
Discussion with the licensee's licensing staff indicated that
only four_ maintenance work requests (MWRs) had been issued on
-watertight door deficiencies since completion of modification
HC-20 on November 4, 1986. Of those four MWRs, only two involved
inoperability of.the affected door; the other two involved degraded
, performance of the closing mechanism which remained operable. This
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data indicated an improved reliability as compared to previous NRC
, observations.
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! . Finally, the-licensee completed testing of watertight door seals
) in accordance with the manufacturer's specifications. All doors
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had acceptable test results after necessary adjustments by the
maintenance department. This item is closed.
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c. (Closed)OpenItem(461/86074-04): The licensee agreed to review
their maintenance training program to determine if an interim
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program or changes to the existing program were warranted prior
!- to the completion of INP0 accreditation.
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The licensee completed their evaluation of the current maintenance
, training program and presented their results to the resident
inspector for review. Both the IP Maintenance Department and the
i IP Nuclear Training Department participated in the review. Their
( review identified the following:
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'(1) The current INP0 accreditation program will resolve all
training weaknesses observed by the NRC.
(2)l.The current training program is implemented and additional:
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efforts'are being focussed on_ supporting emergent training- ,
requirements that arise from specific problems in the plant.
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Their review concluded that any attempt to develop an interim
training program would take nearly as long as developing and
-implementing the INP0 required program and that development of
an: interim training program would result in costly delays in the
accreditation schedule.
In view of. Policy Statement on Training and-Qualification of Nuclear
Power Plant Personnel (50 FR 11147 dated March 20,1985),the
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licensee's schedule for achieving INP0 accreditation of their
maintenance training program, and the lack of any substantive
evidence that maintenance personnel are not adequately trained. -
this item is closed.
- d. (0 pen) Open Item-(461/85005-32): Verify that procedures to ensure
independent verification of system lineups are complete before fuel
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loading (TMI Item II.K.1.10).
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This item was previously reviewed as documented in Inspection Report
-50-461/86064, paragraph 2.a. Since that inspecticn, the licensee
revised procedure CPS No. 1401.01, Conduct of Operations, to include
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clarified criteria for independent verification of system lineups
and to include a listing of plant systems that required independent
verification. In addition, the licensee reviewed operating. "
procedures containing valve and/or electrical lineups to determine
if the clarified criteria were met and initiated action to make
necessary revisions.
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The inspector reviewed the actions taken by the licensee and
verified that necessary reviews and revisions were either completed
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or scheduled to be completed in a meaningful time frame. In
!- particular, the licensee had reviewed all system operating
! procedures for systems to be declared operable to support the
initial criticality milestone and had scheduled reviews / revisions
for other operating procedures to be completed prior to required
milestones. (Some exceptions were taken to this general statement
where the licensee had a high. level of confidence in the currently
h approved. procedure being conservative). The inspector verified that
L the following procedures had been revised to include independent
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verification of important valve and electrical lineup:
E CPS No. 3315.01, Containment Monitoring (CM)
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CPS No. 3101.01, Main Steam (MS, IS, & ADS)
I CPS No. 3310.01, Reactor Core Isolation Cooling (RI)
l CPS No. 3302.01, Reactor Recirculation (RR)
CPS No. 3402.01, Control Room HVAC (VC) ;
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CPS No. 3306.01, Source / Intermediate Range Monitors (SRM/IRM)
CPS No. 3308.01, Local / Average Power Range Monitors-(L/APRMS)
The licensee intends to complete review and revision of all
operating procedures requiring independent verification by June 30,
1987. That will include review and revision of some procedures
that currently (conservatively) require independent verification of
- omponents that exceed the criteria established in CPS No. 1401.01.
The inspector identified some minor discrepancies in CPS No. 1401.01,
Appendix C (for example, the reactor recirculation [RR] system was
not listed but did require and was provided with independent
verification) which were pending correction by the licensee.
e. (0 pen) Open Item (461/85015-07): " Confirm necessary revisions to
EPGs made, E0Ps upgraded, and operators trained before fuel load
(SSER4-13.6.3.1)." Paragraph 13.6.3.1 of Supplement 4 to the SER
required verification that revisions were made to the CPS emergency
procedure guidelines (EPGs), that emergency off-normal procedures
(E0Ps) were upgraded, and that the operators were trained prior to
fuel load. In Inspection Report 50-461/86059, the inspector
determined that the requirements were fulfilled with the exception
of the combustible gas control EPG and E0P which was scheduled for
completion after fuel load.
The inspector reviewed the status of this item with the licensee
and with the NRC Licensing Project Manager (LPM). The licensee
indicated that a generic combustible gas control EPG had been
developed by the Hydrogen Control Owners Group (HC0G) and submitted
, to the NRC Office of Nuclear Reactor Regulation (NRR) for review on
l December 1, 1986. The licensee plans to endorse the HC0G submittal
once NRC review has been completed. The licensee estimated that
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six months would be required to complete the NRC review and that
additional time would be required to complete plant specific work
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necessary to achieve an E0P for use at CPS.
Discussion with the LPM indicated that the licensee's schedule for
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this item was consistent with the rest of the industry and that
operation above 5% of full power using interim combustible gas
control procedures was acceptable. The inspector will review this
, matter further when the licensee has prepared the applicable E0P.
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f. (0 pen) Open Item (461/86011-01): The licensee committed to having
seven radiation chemistry technicians (RCTs) complete all (36)
qualification cards by 5% power.
! The licensee provided information to the inspector for closure of
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this item. That information indicated that nine RCTs had completed
all qualification requirements necessary to act as the on-shift
(ANSI /ANS 3.1 qualified) RCT. Only five of those RCTs were
l qualified to operate the Post Accident Sampling System Panel (PASS),
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A. sixth qualified PASS operator assigned to the Nuclear Training
Department as an instructor was available to respond to emergencies.
The licensee stated that another individual in the Chemistry
Department was being trained to operate PASS.
The Supervisor-Chemistry had a high level of confidence in the
ability of the chemistry group to augment the normal shift
complement with PASS qualified personnel to respond to any emergency
in the required time. The inspector noted that three of the six
qualified individuals (a team leader, a PASS operator, and a third
individual preparing the chemistry laboratory for PASS analysis)
were needed to perform post-accident sampling; that the licensee
had not specifically demonstrated the ability to augment the normal
shift to meet PASS requirements; and that the ability to augment the
shift with a sufficient number of qualified personnel was related
to the number of qualified personnel available. The inspector, in
consultation with Region III management, agreed that the. licensee
had met their commitment concerning the number of qualified
personnel necessary to man the shift and thus their commitment to
5% power was met. This item will remain open pending review and
verification of RCT qualification records by a Region III based
specialist inspector.
The quidelines of CPS No. 1890.30, Post Accident Sampling Program,
indicated that a minimum of six PASS qualified individuals was
desired to ensure the availability of qualified personnel. The
licensee stated that a plan was being formulated to enhance the
PASS program to provide three staff professional (technical)
individuals to act as PASS team leaders. When implemented, that
plan will provide additional PASS qualified individuals to respond
to emergencies, increase the depth of the organization (i.e., more
than the minimum number of qualified personnel available), and
improve leadership provided for PASS teams. The licensee stated
that this plan will be finalized and the appropriate individuals
qualified by April 1, 1987. This is.an open item pending NRC
review of the licensee's actions (461/87002-01).
g. (0 pen) Open Item (461/86054-14): Deferred Testing Activities.
The Clinton Power Station Operating License paragraph 2.D.
granted a number of schedular exemptions to the performance of
test activities. These exemptions deferred testing to a specific
milestone. The status of these deferred test activities was
reviewed by the inspector during this report period and is
tabulated below:
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Deferred Tests Deferred Tests
System Milestone Completed Remaining
Turbine Electrohydraulic Reactor Heatup ATP-EH-01 NONE
Control (EH)
Traversin Incore 5% Power PTP-TP-01
Probe (TP
Off Gas (0G) Reactor Heatup PTP-00-01 NONE
PTP-0G-02
PTP-V0-01
XTP-00-12
Containment Initial PTP-CM-01 NONE
Monitoring (CM) Criticality
Leakage Initial PTP-LD-01 NONE
Detection (LD) Criticality
Fuel Pool Cooling 5% Power * PTP-FC/SM-01
and Cleanup (FC)
Fuel Handling (FH) 5% Power * PTP-FH-01
In-place. Filter on Initial XTP-00-12(VC) NONE
Control Room HVAC (VC) Criticality
HVAC Testing For: Reactor Heatup* PTP-VA-01 NONE
PTP-VQ-01
Aux. Building (VA) PTP-00-01(VA)
Dry Well Purge (VQ) PTP-00-01(VQ)
Dry Well Cooling (VP) PTP-00-01(VP)
Containment XTP-00-12(VQ)
Building (VR) PTP-00-01(VR)
Turbine Building (VT) PTP-00-02(VW)
Radwaste Building (VW) PTP-00-01(VT)
Fuel Building (VF) PTP-00-02(VT)
PTP-00-01(VW)
PTP-00-02(VF)
PTP-00-02(VR)
XTP-00-12(VW)
PTP-00-02(VA)
- This milestone or before removal of the reactor pressure vessel
head after initial criticality.
During this report period, the inspector verified the licensee
had evaluated the results of the above completed deferred test
activities. The inspector reviewed each of the above completed
test summaries and verified the test results were reviewed and
approved in accordance with the licensee's program.
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-This item will remain open pending the completion'of the remaining
deferred tests.
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h. (0 pen) Open Item (461/86074-02): _ Procedure comment control forms
(CCFS) were being used to-identify suggested procedure improvements.
This.use was not controlled by plant administrative procedures.
The NRC. inspector.was-concerned that these CCFS had not been .,
. reviewed to determine their technical . impact and the need for an '
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immediate-procedure revision.
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The licensee revised CPS ~No. 1005.01, " Preparation, Review,
i- Approval,.and Implementation of and Adherence To Station Procedures
and Documents" on January 8, 1987, to include requirements concerning
control of CCFS initiated against issued station procedures. The
procedure changes were responsive to the.NRC concern. In addition,
all CPS departments reviewed outstanding CCFS to determine if any
'were of sufficient significance to warrant revision of the affected-
procedure prior to the normal biennial review. A small number of
CCFS were identified which resulted in the initiation of procedure
revisions. Those revisions were scheduled for completion by
! required. plant milestones.
The licensee's QA organization performed a surveillance'of the
Operations Department procedure files (Surveillance Q-09456 dated
December 15-16,1986) to determine how CCFS generated against
issued procedures were handled. Their surveillance verified the
information discussed.above and also determined.that the procedure ,
- files were not up to date (i.e., the files contained CCFS which had
already been resolved, contained CCFS against procedures that had
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been cancelled,.etc). The licensee's QA department scheduled an
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additional surveillance to verify action taken to correct the 1
identified concern. '
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This item will remain open pending completion of tne' licensee's
actions and verification that the plant staff is adhering to CPS
{ No. 1005.01 for control of CCFS.
- 1. (Closed) Unresolved Item (461/86059-01): The basis for closure .
r of CR 1-86-07-009 concerning performance of safety related work
without approved procedures required additional justification.
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The licensee presented this item to the inspector for closure.
CR 1-86-07-009 was revised to provide assurance that work performed
, prior to issuance of approved work procedures for core drilling and
concrete expansion anchor installation was adequately controlled,
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, documented, and inspected. No violations were identified. Work
p control procedures were approved, as follows:
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CPS No. 8901.16, Core Drilling, revision 0 dated September 13,
1986.
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CPS No. 8199.01, Concrete Expansion Anchor Work, revision 0
dated August 25, 1986.
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In addition, the licensee scheduled training for maintenance
supervisors and planners to assure that all cognizant personnel
understood the need to have approved procedures to control safety
related work. That training was scheduled for completion on
February 2,1987. Completion was being tracked by centralized
consnitment tracking item (CCT) No. 044013. This item is closed.
j. (Closed) Violation (461/86037-02): Procedure CPS No. 9052.02,
Low Pressure Core Spray Valve Operability Checks, did not provide
sufficient detailed instructions and/or appropriate acceptance
criteria for determining that important activities had been
satisfactorily performed.
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This item was previously reviewed, as documented in Inspection
Report 50-461/86060. At that time, this item remained open pending
completion of revisions to certain surveillance test procedures
identified in attachment B of the licensee's letter U-600689.
Those revisions were required to be completed prior to initial
reactor criticality. In addition, CPS No. 1011.05, CPS Surveillance
Procedure Guidelines, was scheduled for revision by October 20,
1986, to address the reporting of all failures to meet surveillance
test acceptance criteria to the shift supervisor. The licensee had
provided interim guidance to all plant personnel in plant manager's
standing order (PMS0) No. 30 regarding the reporting of test
failures.
The inspector verified that the licensee had completed revision
to surveillance test procedures required to be completed prior to
initial criticality. Several minor editorial /non-technical
discrepancies identified during this inspection were corrected by
the licensee.
The inspector noted that CPS No. 1011.05 had not been revised as
scheduled by the licensee. Discussion with cognizant licensee
personnel indicated that PMS0 No. 30 remained in effect and that the
revision was scheduled and expected to be completed by January 30,
- 1987. This information provided a sufficient basis for closure of
i this violation.
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k. (0 pen) Violation (461/86060-02): Corrective actions in response to
IPQA Audit Q38-86-10 and IPQA Surveillance Finding M-86-005 were
not effective to prevent recurrence. The licensee had identified
l deficiencies in the processing of Maintenance Work Requests (MWRs)
l for evaluation of post maintenance testing. The corrective action
l performed was not effective as evidenced by additional deficiencies
l identified by an NRC inspection conducted subsequent to the
licensee's corrective action.
During this report period, the licensee formally responded to the
subject violation. The licensee was unable to respond to the
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violation in the thirty days required by the Notice of Violation
! dated October 17, 1987. The licensee verbally communicated to NRC
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Region III their inability to meet the thirty day requirement and
the written response dated December 19, 1986, was considered
acceptable.
The inspector selected a sample of 47 MWRs that had been closed
between August and December 1986, to verify the specific corrective
action taken by the licensee.
The review performed was to ascertain if the closed MWRs were
being evaluated for post maintenance testing (PMT) requirements
in accordance with the licensee's controlling procedure CPS No.
1401.01, " Conduct of Operation", revision 11, dated December 31,
1986. For each of the MWRs selected, the associated PMT evaluation
was performed in accordance with CPS No. 1401.01. The inspector
was able to locate each PMT evaluation form in the licensee's record
storage vault; in the system status files maintained in the main
control room; or in the Plant Staff Technical Department. The
inspector concluded through this review that the licensee's specific
corrective action was adequate.
The corrective action taken to prevent further violation included
revising the implementation procedure to require a copy of the
completed MWR be received by the PMT evaluator prior to closing out
the MWR in the computer file. In addition, the PMT evaluators had
been relocated with maintenance planners. The inspector verified
the above actions were in place; however, the formalized change to
the MWR Preparation and Routing Procedure, CPS No. 1029.01 was not
completed at the end of.this inspection period. The licensee stated
that the revised procedure would be issued January 30, 1987. This
item will remain open pending the issuance and the inspectors review
of this revised procedure.
1. (0 pen) Violation (461/86065-03): Procedure CPS No. 1016.01, CPS
Condition Reports, was not followed in that corrective action plans
were not approved prior to implementation; block 2 of the condition
report form was not always filled out; and reviews of condition
reports (CRs) by various departments did not identify and correct
the violations that existed.
The licensee responded to this violation in letter U-600806 dated
January 6, 1987. This letter was late in meeting the 30 day
response requested by the notice of violation. The licensee's
response to the violation appeared adequate to address the substance
of the violations.
The inspector reviewed CPS No. 1016.01, revision 15 dated
November 24, 1986 and verified that the changes reflected in the
licensee's letter, Attachment A, paragraph I.a., had been
incorporated. The inspector also reviewed several recent CRs and
verified that they had been processed in accordance with the revised
administrative controls.
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The-inspector reviewed records'of training provided to personnel
responsible for the review of condition reports and verified that
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the cognizant records coordinator had been included in the required
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training.
Discussion with plant staff personnel indicated that the additional
procedure revision was scheduled to be completed on March 31, 1987,
and that the revision was expected to be completed on schedule.
Thisl violation will remain open pending completion of the actions
discussed in Attachment A, paragraph II.a.
m. (0 pen) Violation (461/86065-04): Three examples of inadequate
surveillance procedures.
The licensee responded to this violation in letter U-600806 dated
January 6, 1987. Review of the licensee's response indicated that
the response adequately addressed two of the three examples in the
NOV (examples B & C). However, that response limited the scope of
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the licensee's corrective actions to first time performance mode 1,
2, & 3 surveillance procedures. The inspector noted that the first
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example of the violation involving the Standby Liquid Control Pump
Operability Test procedure was not a first time performance
3 surveillance procedure-and that the problem encountered did not
involve installation of jumpers or lifting of leads. The licensee
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agreed to review this matter further to determine if additional
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corrective' action was needed and to provide a supplementary response
L to this NOV.
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The inspector reviewed PMS0-30, revision 3 and verified its
implementation. The PMS0 provided the controls identified in
the licensee's response and appeared to have been effective in
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reducing the number of events resulting from first time performance
- of surveillance procedures.
This violation will be reviewed further after receipt of the
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licensee's supplemental response.
n. (0 pen) Violation (461/86065-05): Eight examples of failure to
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follow procedures during the conduct of initial fuel load
operations.
The licensee initially responded to this violation in letter
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- U-600806 dated January 6,1987. At the request of Region III,
the licensee provided additional information concerning the
corrective actions taken for each of the eight examples cited
in letter U-600823 dated January 21, 1987. The license's
supplemented response to the violation appeared adequate to
address the substance of the violations.
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The inspector reviewed the specific corrective actions taken by the
licensee in response to each violation cited and verified, based on
a sample ~ of the actions taken, that their corrective actions had
been implemented as stated.
Concerning the generic corrective actions addressed in letter
U-600806, Attachment B, the inspector verified a sample of_ the
corrective actions taken by direct observation of the corrective
actions in progress and through interviews of various plant and
plant management personnel. The actions taken by the licensee
appear to have been effective in reducing the nuinber of personnel
errors and the frequency of reportable events. Additional NRC
concerns regarding the conduct of plant operations were identified,
as documented in paragraph 10.b. of this report. The licensee's
additional corrective actions will be reviewed with their response
to that violation.
This violation remains open pending licensee verification that
all corrective measures indicated in the response to the notice
of violation, attachment B, have been completed.
o. (0 pen) Violation (461/86065-06): Two examples of performance of
plant operations without approved procedures.
'
The licensee responded to this violation in letter U-600806 dated
January 6, 1987. That letter was late in meeting the 30 day
response requested by the Notice of Violation. Review of the
licensee's response indicated that the response did not address the 4
apparent violation of CPS No. 1011.01, Test Programs and Control.
The licensee stated that CPS No. 1011.01 would be revised to provide
controls over the type of activity described in the Notice of
Violation. The licensee is planning to revise their response to
this Notice of Violation to reflect the corrective actions to be
.
taken. This violation will be reviewed further after receipt of
l the licensee's revised response.
t
p. (0 pen) Violation (461/86065-07): Four examples of failure to meet
plant technical specifications.
The licensee responded to this violation in letter U-600806 dated
January 6, 1987. The inspector performed a preliminary review of
the response to this violation during this report period. In
conjunction with the response provided, the inspector performed
a detailed review of Licensee Event Report (LER) 86-009-01
associated with this violation. Results of the inspector's review
l of LER 86-009-01 are contained in paragraph 5.a. below. At the
, conclusion of this report period, the inspector's review of the
!
licensee's response to this violation was still in progress. The
results of this review will be reported in a future inspection
report. This item remains open pending completion of that review.
!
l
l
13
l
-- . .- .
- .
-
.
p
,
an <c""
. <. .
~.
q -(0 pen) Violation (461/86074-05): Failure't'o follow approved
procedures for control of Temporary Modifications. .This violaf. ion
.
identified a number of deficiencies in the 1Nplementadon of
administrative controls for temporary modifications.
The licensee responded to this violation in letter U-600819 dated
January 20, 1987, in a timely manner. The inspector noted that
,
the licensee expected to be in full compliance on January 31, 1987.
This item will remain open, pending the inspector's review of
corrective actions taken by the licensee.
No violations or deviations were identified. +.,
y .
y.
,
3. Licensee Action on 10 CFR 50.SS(e) Report (92700)
a. (Closed) 10 CFR 50.55(e) Item (461/86006-EE): Watertight Seals s
and Openings in Vital Area Boundaries.
This item was previously inspected as documented in Inspection
Report 50-461/86060.
During this inspection, the inspector reviewed the licensee's final
report submitted by letter U-600765 dated November 24, 1986; a '
supplemental final report submitted by letter U-600825 dated
January 26, 1986; and portions of additional quality records
related_to corrective actions taken by the licensee. Those
documents included the following:
CPS No. 1029.01, Maintenance Work Requests, revision 10 and 14
CR 1-86-11-171
CR 1-86-08-020
CR 1-86-12-014
CR 1-86-12-029
' Plant Modification Packages A-67, A-71, and A-73
Plant Modification Package A-47 (10 CFR 2.790 information)
Chairman's Final Report on 55-86-06, letter Y-82470 dated
October 31, 1986.
!
Review of the above documents indicated that the licensee's
, corrective actions had been completed; that additional findings
concerning the floodproofing of the CPS Screenhouse had been
'
i submitted to the NRC in a supplemental report; and that the
I
licensee's corrective actions had addressed both the specific
- and generic implications of the identified deficiency.
The inspector noted that a violation related to this matter
(461/86048-03) was pending enforcement action by the NRC.
Additional reviews related to this matter will be tracked by
the violation. This item is closed.
b. (0 pen) 10 CFR 50.55(e) Report (461/86007-EE): Broken Tack Welds
on Anchor Darling Globe Valves.
14
_ , . _ . _ - . _ _ . . _. _ - . _ - . _.
y } '
~ =L+s:
yQ v -
Q -*
[?
, .
5f This matter was previously reviewed as documented in Inspection
rM _
'
Report 50-461/86072. That report determined that the licensee's
m planned corrective actions were deferred to the first refueling
outage but the licensee had not provided sufficient justification
'
~for operation of 32 potentially affected valves during the first
-
,
operating cycle.
C The licensee provided letter Y-83108 dated January 13, 1987 to
supplement the final report on this deficiency. That letter
-
provided the engineering justification for operation of the affected
valves through the first operating cycle. However, the licensee's
review did not account for system operation to provide long term
decay heat removal after a postulateo accident involving damage to
the plant. Although the likelihood of such an accident is small,
the plant systems are designed to operate under those conditions
. and should not be adversely affected by this identified deficiency.
'
' The3fcensee conducted additional reviews and determined that two
of the affected valves (1E12-F003A/B) may be operated in a throttled
mode during long term decay heat removal after a postulated accident.
The licensee's engineering justification provided a sufficient
i basis to justify removal of administrative controls from all valves
except the two valves documented above. The licensee stated that
administrative controls would remain in place for those two
potentially affected valves pending completion of additional
. engineering reviews.
This matter will be reviewed further during a subsequent inspection.
No violations or deviations were identified.
4. - Applicant Action on Three Mile Island (TMI) Action Plan Requirements
(25401)
The NRC Office of Inspection and Enforcement issued Temporary Instruction
(TI) 2514/01, Revision 2, dated December 15, 1980, to supplement the
Inspection and Enforcement Manual. The TI provides TMI-related
inspection requirements for operating license applicants during the phase
between pre-licensing and licensing for full power operation. It is
divided into two parts. Part I lists requirements that were closed prior
to fuel load. Part 2 lists requirements that must be closed prior to
full power operation. Part 2 of the TI was used as the basis for
inspection of the following TMI item found in NUREG-0737, " Clarification
of TMI Action Plan Requirements".
(0 pen) Item II.B.4.2: Training for Mitigating Core Damage. The licensee
was to complete training prior to full power operation.
During a previous inspection (50-461/86023), part 1 (II.B.4.1) of this
TMI action item was closed based on the licensee's established Mitigating
Reactor Core Damage (MRCD) training program. During this report period,
the inspector verified through review of training records that the Power
Plant Manager had successfully completed the MRCD training. In addition,
15
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the inspector verified that nonlicensed technicians had been provided
training in accordance with the licensee's commitment contained in
section 13.2 of their Final Safety Analysis Report (FSAR). However, the
inspector noted that several technicians had not received the required
training and the licensee was unable to provide the inspector evidence
that those technicians would be trained as committed in the FSAR. This
item remains open pending the inspectors review of actions taken by the
' licensee to complete the training of nonlicensed technicians.
No violations or deviations were identified.
5. Licensee Event Report'(LER) Review and Followup (90712 & 92700)
a. In-Office Review Of Written Reports Of Nonroutine Events At Power
Reactor Facilities (90712)
For the LERs listed below, the inspector performed an in-office
review of each LER to determine that reporting requirements had
been met; that the corrective action discussed appeared appropriate;
that the information provided satisfied the applicable reporting i=
requirements; to determine if appropriate actions had been taken on L_
ay generic issues present; and to determine if any additional NRC
inspection,' notification, or other response was appropriate. Where =
determined appropriate, the LER was scheduled for onsite followup
inspection or other necessary action by cognizant NRC personnel.
(1) (Closed)LERNo. 86-006-00 (461/86006-LL) [ ENS No. 06499 and
06569]: Automatic Initiation Of Essential Service Water Due
To Transient Pressure Drop In Nonessential Service Water.
(2) (Closed)LERNo. 86-008-00 and 86-008-01 (461/86008-LL) [ ENS
No. 06552]: Containment Isolation Of The Instrument Air System
Due To Procedural Inadequacy.
LER 86-008-01 indicated that LER 86-008-00 had been superseded
in its entirety by LER 86-009-01. As discussed in (3) below,
the information previously contained in LER 86-008-00 was
included in LER 86-009-01. This LER is closed.
(3) (Closed) LER No. 86-009-00 and 86-009-01 (461/86009-LL) [ ENS
No. 06568]: Automatic Actuation Of An Engineered Safety
, Feature Due To Procedural Inadequacy and Technical
Specification Violation Due To Operator Error.
As documented in Inspection Reports 50-451/86072 (paragraph
6.b.) and 50-461/86073 (paragraph 3.b.), LER 86-009-00 did
not accurately describe all the facts surrounding the subject
event. The inspectors onsite followup of this event was
documented in Inspection Report 50-461/86065 which resulted
in the issuance of several violations (461/86065-04C, 06B,
07A,B,C). Follcwup of the licensee's corrective actions
will be tracked by the open violations.
16
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.
..
During this report period, the licensee issued LER 86-009-01.
This LER incorporated all the information that had been
contained in LER-008-00 as noted in (2) above. The inspectors
review of LER 86-009-01 indicated that the licensee had
provided a complete description of the subject event. The
inspector confirmed by review of training records and licensee
correspondence that corrective action stated in LER 86-009-01
had been or was being implemented. Since several of the
corrective actions identified in this LER are also applicable
to the violations issued in Inspection Report 50-461/86065,
completion of all corrective actions will be reviewed and
documented during the inspector's followup to those violations.
This LER is closed.
(4) (Closed) LER No. 86-020-00 (461/86020-LL) [ ENS No. 06857]:
Tripping of Level Transmitter Results in Automatic Switching
of High Pressure Core Spray Pump Suction Valve Alignment.
The inspector noted that a similar event occurred on January 7,
1987, (see paragraph 10.b.(3) of this inspection report) which
indicated that the root cause of this event may not have been
accurately identified. Further review will be performed when
the licensee completes.their investigation of that event. This
LER is closed.
(5) (0 pen) LER No. 86-019-00 (461/86019-LL) [ ENS No. 06856 and
07000]: Engineered Safety Feature Actuation Due To A Spurious
High Output Alarm on the Main Control Room Air Intake Process
Radiation Monitor.
This matter will be reviewed further on rect et of the
licensee's supplemental report, scheduled u. January 30,
2
1987.
(6) (0 pen) LER No.'86-017-00, 86-017-01, and 86-017-02
(461/86017-LL) [ ENS No. 06670]: Engineered Safety Feature
Actuation Due To Spiking On Intermediate Range Monitor A.
'
This LER remains open pending receipt and review of the
licensee's supplemental report. The licensee's supplemental
report was scheduled for submittal on January 31, 1987.
(7) (Closed) LER No. 86-023-00 (461/86023-LL) [ ENS No. 07123]:
Automatic Actuation of the Reactor Protection System (RPS)
Due To Utility Personnel Error.
No violations or deviations were identified.
b. Onsite Followup Of Written Reports Of Nonroutine Events At Power
Reactor Facilities (92700)
For the LERs listed below, the inspector performed an onsite
followup inspection of each LER to determine whether responses to
17
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.
the events were adequate and met regulatory requirements, license
conditions, and commitments and to determine whether the licensee
had taken corrective actions as stated in the LER.
'
(1) (0 pen)LERNo. 86-004-00(461/86004-LL)[ENSNo.06413]:
Unplanned Automatic Initiation Of Standby Gas Treatment System
Due To Inadequate Procedures.
This LER was previously reviewed as documented in Inspection
Report 50-461/86072. At the conclusion of that inspection,
there was an open question concerning this LER.
The licensee stated that their engineering review of trip logic
seal-in circuitry indicated that there were no additional uses
of logic similar to that which caused this event. For that
reason, no additional corrective action was required and a
supplement to the LER was not necessary. After receipt of this
information, another event occurred (see paragraph 10.b.(9) of.
this report; ENS No. 07565) which may involve similar logic
functions. The licensee's review of that event was considering
the potential similarity in trip logic but was not complete at
the conclusion of this inspection. This LER remains open
pending review of the licensee's results and verification that
the use of trip seal-in logic which caused this event was
isolated to the five radiation monitors discussed in the LER.
(2) (0 pen)LERNo. 86-021-00 (461/86021-LL) [ ENS No.06913]:
Reactor Water Cleanup Pump Room High Temperature Trip Due To
Personnel Error.
This event was previously reviewed as documented in Inspection
Report 50-461/86073, paragraph 3.e.
During this inspection, the inspector reviewed the LER and
verified implementation of selected corrective actions being
taken by the licensee. No significant discrepancies were
identified but actions were not complete. In particular,
LER 86-020-00 corrective actions 7, 8, and 9 were not complete
at the time of this inspection. One minor item concerning
inclusion of specific information in the LER related to a
personnel error was discussed with the IP licensing department.
The inspector interviewed the Manager - Nuclear Station
Engineering Department concerning corrective actions regarding
lifted leads and jumpers. The recommendations of the
licensee's jumpers and lifted leads task force had been
forwarded to NSED for evaluation. The licensee was scheduled
to have a general plan for addressing jumpers and lifted
leads (in terms of the CPS design and the need to interrupt
electrical continuity for maintenance or surveillance work)
by the middle of February 1987. The licensee was planning to
complete the identification and scoping of necessary plant
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modifications by mid-1987 with the modification themselves to
be completed based on an individual schedule.
This LER remains open pending completion of the licensee's
corrective actions and review of the licensee's plan for
addressing the Lifted Leads Task Force recommendations.
No violations or deviations were identified.
6. Review of Allegations (99014)
a. (Closed) Allegation (RIII-86-A-0161): On October 27,.1986,
Region III submitted the following concerns to IP for their review
and followup. On December 11, 1986, IP notified Region III by
letter U-600779 that their review and followup was completed. The
inspector reviewed IP's response to the concerns as documented
below.
Concern No. 1
Transco did not have the insulation top to place over valves, so
they continued to work without the valve tops. As a result, dirt
from the insulation process was trapped between the pipes and the
insulation. The individual thought the feedwater piping was the
system involved.
Review
The inspector reviewed the licensee's letter; reviewed the Transco
stainless steel cleanin
surveillance (CQ-01693)g of procedure SC-0394;
stainless steel piping reviewed
washdown an IPQA
techniques; and performed an inspection of a portion of the
insulated carbon steel feedwater piping. The inspector determined
the following:
(1) The allegation was assumed to be substantiated due to the ,
! lack of documentation which clearly reflected the date of
installation of the insulation tops for feedwater valves.
(2) The feedwater piping was carbon steel covered with a fairly
tight fitting insulation. Carbon steel would not be adversely
i
affected by dirt.
. (3) Due to the tight fit of the insulation surrounding the
l feedwater piping, only a limited amount of dirt and debris
.
could have been accessible to that piping. Any such foreign
niatter trapped between the piping and the insulation would
have negligible affect on heat transfer across the insulation.
.
l
(4) A specific Transco stainless steel cleaning procedure was used
at Clinton. Furthermore, the IPQA surveillance (CQ-01693)
conducted in November 1985 concluded that stainless steel
i
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cleaning operations were being performed in accordance with the
Transco procedure. Thus, it appears that sufficient controls
existed to prevent foreign matter from being trapped between
stainless steel piping and its insulation.
Conclusion
The allegation was assumed to be substantiated based on the lack
of documentation which identifies the date of installation of the
feedwater valve insulation tops. However, there is no safety
concern associated with this matter. This allegation is closed.
Concern No. 2
The individual heard that several voids existed in the concrete wall
between the Diesel Generator and Fuel Building. The individual
thought that the approximate locations of the voids were between
Column Lines AD and AC on either the 762' or 770' elevations. The
individual also heard that the voids were probably repaired.
Review
The inspector reviewed the licensee's letter; reviewed the concrete
pour traveler for the concrete wall immediately above the area
identified in the concern; and performed a visual inspection of the
subject wall.
The inspector identified the following:
(1) As documented in concrete pour traveler F-W-8-4, voids were
previously identified in the concrete wall in the general area
identified in the concern. The voids were subsequently
repaired by the licensee as documented on Quality Control
Inspection Reports C-83-879 and C-83-1350 and Nonconformance
Report (NCR) 3451.
l (2) A visual inspection of the subject concrete wall did not reveal
l the existence of additional voids.
Conclusion
t
l This allegation was substantiated in that voids had been identified
'
by the licensee in the general area of concern. However, the
j licensee had properly identified and documented these voids and .had
completed action to repair these voids. The actions were determined
to have been effective based on a satisfactory visual inspection of
the subject concrete wall by the inspector. This allegation is
closed.
I
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20
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Concern No. 3
The inner bioshield wall was covered with "20 gauge reflective
insulation" and the insulation was improperly installed. Gaps and
dents existed in the insulation and dirt was trapped behind the
insulation. Also, sheet metal screws were missing and holes existed
in the insulation.
Review
The inspector reviewed the licensee's letter; reviewed the April 4,
1986, Bioshield Insulation Completion / Acceptance punchlist; and
performed a visual inspection of the inner bioshield wall
insulation.
The inspector determined the following:
(1) On April 4, 1986, a walkdown of the inner bioshield wall
insulation by Illinois Power (IP) identified approximately 33
items requiring rework. A number of these items were similar
to the types of concerns identified in the allegation. The '
insulation was subsequently rejected by IP on May 5,1986. On
July 3, 1986, the insulation was accepted based on the rework
of the 33 items and a subsequent satisfactory walkdown by IP.
(2) The visual inspection of the inner bioshield wall conducted by
the inspector on January 23, 1987, identified no deficiencies
in the installed insulation.
Conclusion
The allegation was partially substantiated in that a number of the
identified concerns were confirmed to have existed in May 1986.
However, the licensee had properly identified and documented these
concerns and had taken action to resolve these concerns. These
actions were determined to have been effective based on a
satisfactory visual inspection conducted by the inspector. This
allegation is closed.
! No violations or deviations were identified.
L 7. Region III Request (92701)
l
During this inspection period, the licensee performed a review of their
'
l computerized maintenance work request (MWR) milestone listing. The
'
purpose of this review was to identify, from the list of MWRs associated
l with the initial criticality milestone, those MWRs which more correctly
[ were required for either plant heatup or 5% power. As a result of their
j review, 74 MWRs had their associated milestone revised from initial
- criticality to heatup, 5% power, or were given a "can be worked anytime"
l status.
l-
l
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21
e
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.,-
The' inspector selected 13 MWRs from the 74 to determine if their removal
from the initial criticality milestone was compatible with established.
requirements. A subsequent review included a review of associated
technical specifications (TS) and a discussion of each MWR with plant
. personnel.
During the review, the inspector determined that three of the MWRs had
recently been closed. This was indicative of the licensee's stated
objective of completing all MWRs in an expeditious manner. The review'of~
all. but three of the remaining MWRs resulted in no identified concerns.
The-inspector did. identify initial concerns with MWRs C29044, B34737 and
C15708. Each of these MWRs had their. associated milestone changed from'
initial criticality to a "can be worked anytime" status. MWR C29044
pertained to the installation of the Reactor Core Isolation Cooling
(RCIC) headspray line to the reactor pressure vessel. A review of the
Clinton TS for.the RCIC system identified specific operability
. requirements for RCIC depending on vessel head status and plant pressure.
Therefore, the inspector was concerned with the removal of this MWR from ,
. the initial criticality milestone. MWR B34737, which pertained to-
electrical . cables for RCIC, was the subject of similar concern. Finally,
MWR C15708 dealt with an investigation of Intermediate Range Monitor
(IRM) spiking. The concern with this MWR pertained to the fact that the
, subject IRM continues to evidence spiking characteristics while being
- classified as operable and shorting links removed. Continued operation
,
in this manner would increase the probability of future reactor trips.
During discussions with the licensee, the-inspector determined that MWRs
.
.C29044.and B34737 were identified on the IP Open Vessel. Testing Schedule
-as items required for completion prior to initial criticality. In
>
addition, IRM Special Test CPS No. 2830.11, which addresses the IRM
'
spiking problem identified in MWR C15708, was similarly identified on
the Testing Schedule. The inspector reviewed the Testing Schedule and
,
concluded that the work activities associated with MWRs C29044, B343737
and C15708 were adequately identified and controlled.
4
I
Based on the review of the 13 selected MWRs and the discussions with the
licensee, it appears that the milestone revisions for the 74 MWRs were
acceptable.
f No violations or deviations were identified.
.
8. Operational Safety Verification (71707)
The inspectors observed control room shift turnovers and operations,
- attended selected pre-shift briefings, reviewed applicable logs, and
conducted discussions with control room operators during the inspection
period. The inspectors verified the operability of selected emergency
4
systems and verified tracking of LCOs. Routine tours of the auxiliary,
3'
fuel, containment, control, diesel generator, and turbine buildings and
the screenhouse were conducted to observe plant equipment conditions
including potential for fire hazards, fluid leaks, and operating
conditions (i.e., vibration, process parameters, operating temperatures,
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etc). The inspectors verified that maintenance requests had been
initiated for discrepant conditions observed. The inspectors verified
by direct observation and discussion with plant personnel that security
procedures and radiation protection (RP) controls were being properly
implemented.
During a plant tour on January 7,1987, at about 2:30 p.m., the inspector
noted that sealing material (" Bisco Sealant") had been degraded on a
penetration through the secondary gas control boundary. The subject
penetration was located on the 781' elevation of the Auxiliary building
inside the East airlock. The penetration was used for a non-safety
related 1" conduit passing through the airlock into the annular space
within the secondary gas control boundary. The seal provided was
approximately 10" x 20" and the sealant had been cut into several pieces.
The inspector informed the Shift Supervisor of the condition noted above
and the licensee initiated Condition Reports 1-87-01-033 and 1-87-01-034
to document the deficiency and investigate the cause. At the conclusion
of this report period, the licensee was still performing their
investigation. This item will remain unresolved pending the inspectors
review of the licensee's investigation (461/87002-02).
The following routine surveillances were observed by the inspector during
the report period:
-
CPS No. 9080.01, revision 22 , " Division II Diesel Generator
Operability"
-
CPS No. 9031.12, revision 20, "APRM Channel Functional"
The inspector's observations of the above surveillances were limited
in scope. However, the inspector noted that the surveillances being
perfomed were current revisions; the personnel performing the
surveillances informed the control room operator when required by the
procedure; and the personnel performing the surveillances exhibited a
good working knowledge of the surveillance in response to the inspector's
questions.
The inspectors observed plant housekeeping / cleanliness conditions. No
i discrepancies were noted.
- The above reviews and observations were accomplished to verify that
l facility operations were conducted in conformance with the CPS technical
l specifications and the conditions of the operating license.
One unresolved item was identified.
9. Engineered Safety Feature System Walkdown (71710)
The inspectors performed a complete walkdown of the High Pressure Core
Spray (HPCS) system during the report period to verify the system status.
l
At the time the walkdown was performed, the licensee had declared the
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HPCS system operable and meeting all requirements of the plant's
-Technical Specifications.
For the purpose of this walkdown, the inspector utilized the following
system drawings and the checklists contained in the system operating
procedure:
CPS No.;3309.01V001,= revision 1, HPCS Valve Lineup
CPS No.-3309.01V002, revision 0, HPCS Instrument Valve Lineup
CPS No. 3309.01E001, revision 1, HPCS Electrical Lineup
CPS No. 3309.01E002, revision 0, HPCS 120V AC Electrical Lineup
-P&ID M05-1074. sheet 1, revision Y~
C&ID M10-9074, sheets 1 through 4, revision A q
For the inspection performed, the following attributes were observed:
-
System lineup procedures matched the plant drawings.
-
Valve and electrical switch / breaker positioning agreed with
the lineup checklists.
-
Valves were locked when "equired.
-
Equipment conditions appeared correct with no evidence of
damage. (
-
. Equipment and components were properly identified.
-
Interiors of electrical and instrumentation cabinets'were free
of debris, loose material, uncontrolled jumpers, with no
evidence of rodents.
--
Instrumentation was properly installed and functioning.
-
Lubrication was provided, where observable.
-
Housekeeping was adequate and appropriate levels of cleanliness
were being maintained.
-
Support systems essential to system actuation (Division III
Shutdown Service Water and Division III Emergency Diesel) were
operational.
In conjunction with the above, the inspector reviewed the results of
current surveillances perfo ned on the HPCS system to verify Technical
Specification requirements were met. The following surveillance test
results were reviewed:
Surveillance No. Title Frequency Test Date
CPS No. 9051.01 HPCS System Pump Quarterly 10/29/86
Operability
= CPS No. 9051.02 HPCS Valve Operability Quarterly 11/01/86
Test
CPS No. 9051.03 HPCS System Functional 18 months 08/23/86
Test
CPS No. 9051.04 HPCS Automatic Suction 18 months 07/30/86
-0perability
CPS No. 9051.05 HPCS Discharge Header Monthly 01/06/87
Filled and Flow Path
Verification
24
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.
The inspector concluded that the HPCS system was operable based on direct
field observations of the above lineups and inspection attributes. In
addition, the inspector's review of current surveillance tests for the
HPCS system indicated that the plant's Technical Specifications were
being met.
No violations or deviations were identified.
10. Onsite Followup of Events at Operating Reactors (93702)
a. General
The inspector performed onsite followup activities for events which
occurred during the inspection period. Followup inspection included
one or more of the following: reviews of operating logs;
procedures; condition reports; direct observation of licensee
actions; and interviews of licensee personnel. For each event, the
inspector reviewed one or more of the following: the sequence of
actions; the functioning of safety systems required by plant
conditions; licensee actions to verify consistency with plant
procedures and license conditions; and attempted to verify the
nature of the event. Additionally, in some cases, the inspector
verified that licensee investigation had identified root causes of
equipment malfunctions and/or personnel errors and were taking or
11ad taken appropriate corrective actions. Details of the events and
licensee corrective actions noted during the inspector's followup
are provided in paragraph b. below.
b. Details
(1) Engineered Safety Feature (ESF) Actuation - Partial Division II
(Inboard) Containment Isolation (ENS No. 07312)
On December 26, 1986, at about 1:06 p.m. CST, a partial
actuation of the division II containment isolation logic
occurred during performance of post modification testing by
the licensee's C&I maintenance technicians. The actuation
-
resulted in start of division II standby gas treatment and
shutdown service water systems and closure of several inboard
containment isolation valves. The actual cause of the event
was not known but the licensee suspected an error made by the
maintenance technician. The licensee returned plant equipment
to its normal operational status and notified the NRC
Operations Center of the event via ENS at about 3:55 p.m. CST.
This matter will be reviewed further during review of the
licensee's LER.
(2) ECCS Auto Initiation and Injection Into Reactor Vessel (ENS No. 07359)
At about 1:15 p.m. CST on January 2, 1987, division II
Emergency Core Cooling Systems (ECCS) automatically started
25
_ _ _
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.
b
~
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-and injected water into the Reactor Vessel in response.to a
spurious low reactor water level signal. At the time of
occurrence the plant was in mode;5 maintaining reactor water
level at about +170 inches. The division II RHR pumps (B
and C).were secured by plant-operators at a reactor vessel
' level of +200 inches after determination that an actual low
reactor vessel level condition _did not exist. All division
II= equipment responded as-expected and were returned to the
required: standby conditions for mode 5 operation. The
licensee initiated an investigation to determine the cause
of the spurious signal. This matter will'be reviewed further
-during review'of the licensee's LER.
(3) ESF Actuation - Shift of High Pressure Core Spray Suction
~
At about 10:00 a.m. CST on-January 9,1987,' the licensee
-discovered that the High Pressure Core Spray-suction path
had shifted from its preferred source (RCIC storage tank)
to the suppression pool. The licensee's initial investigation
indicated that the realignment occurred the previous day when
a RCIC storage tank level transmitter failed. At the time
of occurrence, the plant was in mode 4 and the High Pressure
Core' Spray system was not an operable ECCS. The licensee is
continuing-to investigate the cause for the RCIC level
transmitter failure. This event was similar to LER
50-461/86020-LL. This matter will. be reviewed further during
-
review of the licensee's LER.
(4) Inadvertent ESF Actuation During Alternate Rod Insertion
Surveillance Test (ENS No. 07468)
At about 8:58 p.m. CST on January 13, 1987, the scram discharge
volume vent and drain valves unexpectedly closed during
performance of surveillance testing on the alternate' rod
insertion system 1 (an ATWS protection feature). Investigation
by the licensee indicated that this ESF' actuation occurred due
to a missing step in the surveillance procedure being used. A
temporary procedure change was initiated and the surveillance
test was subsequently completed without further incident. The
licensee notified the NRC -Emergency Operations Center of this
event at 11:24 p.m. CST via ENS. This matter will be reviewed
further.during review of the licensee's LER.
.
I
(5) Loss of Emergency Response Facility (ENS No. 07472)
On January 14, 1987, at about 9:00 a.m. CST, the licensee
experienced a loss of power to the Emergency Offsite Facility
(EOF). The loss of power occurred when the offsite 138KV
transmission system feeding the EOF had a power failure
apparently due to a tree contacting the transmission lines.
26
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4
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4
The licensee restored power to the 138KV transmission system
and the EOF at about 11:00 a.m. CST. The licensee notified the
NRC. Emergency Operations center of this event at about 10:00
a.m. CST on January 14, 1987. This matter will be reviewed
further during review of the licensee's LER.
(6) Degraded Emergency Response Capability Due to Snow (ENS No. 07520)
-At 11:00 a.m. CST on January-19, 1987, the licensee determined
that their emergency response capability was degraded due to
the degraded condition of area roads that resulted from a
winter snow storm. Approximately 8 inches of snow had fallen
in the preceding 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />;: blowing and drifting snow caused
decreased visibility and made driving in the area hazardous.
The licensee notified the NRC Operations Center of this event
-
at 11:35 a.m. CST. By 1:20 p.m. CST, area road conditions had.
improved to the point that the licensee determined their
emergency response capability was no longer degraded. This
information was comunicated to the NRC Operations Center.
This matter will be reviewed further during review of the
licensee's LER.
(7) Inadvertent Actuation of Division I ECCS Equipment (ENS No. 07545)
>
At about 2:35 p.m. CST on January 21, 1987,. during performance
- - of an operational pressure test of the reactor coolant pressure
boundary, the licensee experienced an inadvertent division I
,
!
ESF actuation. The actuation was caused by a hydraulic
transient in an-instrument sensing line that occurred while
'
an operator was restoring pressure transmitter C34-N005 to
service.
l The hydraulic transient caused a transient reactor vessel water
!
level low - level 2 signal which initiated the Low Pressure
Core. Spray system (LPCS), started the division I emergency
l diesel generator. and shut two containment isolation valves in
l- the instrument air system. The low pressure coolant injection
L mode of the residual heat removal system did not actuate since
r
that system was lined up in the shutdown cooling mode at the
time of the event. In addition, the LPCS did not inject into
the reactor vessel since the reactor vessel pressure was
elevated for the operational pressure test in progress.
i
Upon initiation of the above division I ECCS equipment, the
control room operators verified that an actual low level
condition did not exist in the reactor vessel and restored the
i division I ECCS equipment to the standby mode. The licensee
l
rotified the NRC operations center of this event at 5:10 p.m.
( CST. This matter will be reviewed further during review of the
i
l'
.
27
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_ licensee's,LER; however, as discussed below, the inspector _
performed'a review ~of thelsequence of plant operations that:
- lead-up to thi.s event. 1
-
_
Discussion- >
sThe--inspector interviewed licensed operators on shift at the-
time of this. event to evaluate plant operations that:resulted
in'the need to isolate pressure transmitter C34-N005. :As
- discussed above, the event described was initiated when
-
pressure transmitter C34-N005 was being returned to service.
The inspector's review was primarily limited to interviews of.
-on shift' operators since the sequence of" events documented
below was not documented in the main control room operator's
-log.
-
The licensee was performing an operational pressure test
maintaining'an elevated pressure in.the reactor-vessel via the-
Control Rod Drive system. With the plant in mode.4, Reactor-
Recirculation Pump-A operating in slow speed,.. reactor; vessel-
-and reactor coolant temperature at
_about
pressure at.about
160 degrees 700 psig,t,-the control. room operators were
fahrenhei
requested to-start Reactor-Recirculation Pump-B to allow
continuous recirculation while. testing-the Reactor Recirculation.
-
Pump-A Flow Control Valve. ' Operating the Reactor Recirculation
~
Pump was preventing thermal stratification _in the lower _ portion
-of the-reactor vessel.
Sequence of Events
Sometime before 2:00 p.m., the control room operators attempted
tostartReactorRecirculationPump-B(RRPumpB). After this
first attempt failed, the control room operators noted that?an
annunciator light on control room panel 1H13-P680 (same panel
as the RR pump controls) for "RECIRC PMP B TEMP-INTLK ACTUATED"
was lit..~The applicable annunciator ~ response procedure, CPS
No. 5003.21 identifies the possible cause for this annunciator
as follows:
~
1. Delta-T >50 degrees F between recirgulation loops.
2. Delta T >50 degrees F between vessel dome and either~
recirculation loop.
3. Delta.T >100 degrees F between vessel bottom drain
and vessel dome.
These thermal interlocks prevent undue stress to the reactor
vessel, reactor vessel nozzles, bottom head region, recircula-
i tion pumps, and recirculation nozzels. CPS No. 5003.21 also
provides the operator with actions to take in order to
determine which temperature interlock is causing the alarm.
.
28
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In addition, identification of the interlock relay (K687).and
~
the specific. electrical drawing reference (E02-1RR99, sheet
~10) is provided.
The control room operators then discussed the possible cause
for the annunciated interlock and reviewed control- room-
electrical drawings. The operators decided to place the " Steam
Line Delta T Interlock" bypass switch-located on the Reactor
Recirculation system Low Frequenc
Auxilary Relay Panel (1833-P0018)y Motor Generator
in bypass. This action(LFMG)
was
carried out and a second attempt was made sometime after
2:00 p.m. to start RR Pump B. This second attempt also failed.
The inspector assumed that the annunciated interlock was still
-lit on 1H13-P680 during the second attempt, since the " Steam
Line. Delta T Interlock"~ switch that was placed in bypass
appeared to be the 8 degree F pump cavitation interlock
described in section 5.4.1.3 of-the Final Safety Analysis
Report. 'That bypass switch would have no effect on the
interlock that was preventing the RR pump start.
The control room supervisor then reviewed the electrical
drawings again with the assistance of an individual more
intimately familiar with the Reactor Recirculation system
interlocks and determined that the annunciated interlock could
be bypassed by isolating pressure transmitter C34-N005 and
venting the instrument. This pressure transmitter was sensing
the elevated pressure (700#) present in the reactor vessel
due to the ongoing operational pressure test. However, since
reactor coolant temperature was only 160 degrees F, the
relationship for the interlock Saturation Temperature =
Saturation Pressure (Tsat=Psat)[] was Thenot valid.
control '
room supervisor then directed that pressure transmitter
C34-N005 be' isolated and vented. This action was carried out
and the RR Pump B was successfully' started on the third attempt
at 2:30 p.m. The only documentation of the events described
above was'then made in the Control Room Operators log book:
"1430 - Started RR pump B".
Technical Specification Surveillance 4.4.1.4 (applicable in
mode 1, 2, 3.& 4) requires that temperature differentials and
flow rate shall be determined to be within specified limits
within 15 minutes prior-to startup of an idle recirculation
loop. The operating procedure in use, CPS No. 3302.01,
revision 2 " Reactor Recirculation (RR)". required in step
8.2.3.1 that "within 15 minutes prior to starting each Recirc
Pump] verify
flow ... are steps
at the . . . [di/ferential
required temperatures
flow and temperature and and
range loop
log the data in the CR0 [ Control Room Operator] log". As noted ,
above, contrary to the procedural requirements, the operators
attempted to start RR Pump B twice and successfully started the
pump on the third attempt without documenting in the CR0 log
the differential temperatures and loop flow. Subsequent review
29
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.:
.
by the licensee identified 6 of 8 additional RR Pump starts
while in mode 4 where the required CR0 log entries were not
made. The failure to follow approved procedures is a violation
of 10CFR50, Appendix B, Criterion V.(461/87002-03A(DRP)).
The procedure in use, CPS No. 3302.01, " Reactor Recirculation
(RR)", revision 2 dated February 27, 1986, did not address the
plant conditions under which plant operators attempted to start
'RR Pump interlock
an invalid B on January)21,1987 -(i.e.,
. The control room elevated bypassed
supervisor pressure causing
the differential temperature interlock by directing pressure
transmitter C34-N005 be isolated and_ vented. .No attempt was
made by control room operators to revise the procedure or use
other administrative controls immediately available. Those
administrative controls would have provided independent review
of the safety significance and approval of the method used
to bypass this interlock. The failure to provide adequate
instructions in procedure CPS No. 3302.01 or other documented
instructions _is a violation of 10 CFR 50, Appendix B, Criterion
V(461/87002-03B(DRP)).
The inspector noted that the sequence of events described
above may indicate a general unfamiliarity with Technical
Specification requirements. The inspector's basis for.this
observation is the multiple failures to record information
required for RR Pump starts-in mode 1, 2, 3, & 4 coupled with
the short time that the plant has been in mode 4 (about one
month). In addition, the difficulties encountered by the on
shift crew in starting a RR pump under the conditions present
may indicate a weakness in the level of system knowledge by
the operators. These observations were discussed with licensee
management at the conclusion of the report period.
(8) ESF-Actuation of Two Containment Isolation Valves (ENS No. 07564)
At about 7:30 p.m. CST on January 22, 1987, during performance
of a channel functional test (CFT) for reactor water level 1,
the licensee experienced an inadvertent actuation of two
containment isolation valves in the instrument air (IA) system.
. The isolation resulted from the failure of a C&I technician
to properly insulate leads lifted in accordance with the CFT
,
procedure to preclude actuation of the affected containment
isolation valves. The technician had successfully completed 2
of 4 channels to be tested prior to the event by individually
taping back the lifted leads. During performance of the 3rd
channel, the technician taped the lifted leads together thereby
maintaining electrical continuity which resulted in the ESF
j
actuation as reactor vessel water level (simulated for the CFT)
i reached the actuation setpoint. The logic involved is a 1 out
of 4 actuation logic. The licensee restored the IA system to
,
normal and successfully completed the remaining portions of the
j' 30
1
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v.,.,
,.- . , - - .- _ . - - . - . ...-- _
'
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. .,
'
'CFT. 'The licensee notified the NRC Operations Center of this
event at 11:15 p.m. CST:on January 22, 1987. This matter will
be reviewed further during review of the licensee's LER.
(9) ESF Actuation - Closure of Shutdown' Cooling Suction Valve-
-
(ENS No. 07565) ,
,
f
At.about 8:00 p.m. CST on January 22,.1987,-whil'e restoring
from'an operational pressure test of the reactor coolant
- system, the licensee experienced an unexpected closure of the
shutdown cooling inboard suction isolation valve (IE12-F009).
During performance of. the operational' pressure test, valve
1E12-F009lwas open and the valve motor controller was -
deenergized to prevent automatic closure when reactor vessel
pressure was increased. During restoration from the test, the
. procedure in use did not direct the reset of the reactor high
'
pressure seal-in logic (actual reactor vessel pressure was
,
'
below the actuation setpoint at the time of the event). The
plant operators immediately reset the seal-in logic and opened
'
valve 1E12-F009. At the time of occurrence, the plant was in
j . mode 4 and depressurized. The licensee notified the NRC
'
Operations Center of this event at 11:15 p.m. CST on
- . January 22, 1987. This matter will be reviewed further during
j review of the licensee's LER.
v
i One violation was identified.
I 11. Management Meeting (30702)
J
, - On January 16,1987, NRC management met with IP management at the Clinton
'
Power Station Visitor Center to discuss the status of the facility, the
licensee's Monthly Performance Monitoring Management Report and actions
, being taken to enhance the licensee's performance in several areas, and
to discuss the readiness of Clinton Power Station to perform initial
critical reactor operation and to generate electricity. Personnel
- attending the meeting are identified by (#) in paragraph 1. of this ,
! report. "
p
Mr. A. B. Davis, the Deputy Regional Administrator, opened the meeting >
. with a brief discussion of Region III procedures for NT0Ls at the-full
l' power license stage. Mr. Warnick then identified the scope of the
meeting; discussed current Region III areas of concern and an overview
4
of Region III plans for additional inspections at Clinton prior to
making a decision regarding the recommendation for issuance of the full
- power license; and requested that periodic management meetings continue
- monthly for the near future.
.The licensee then provided the status of testing deferred beyond fuel
load; the status of surveillance testing required to be completed to
support plant operation in modes 1 and'2; the status of maintenance and
,
'
modification work required to be completed prior to initial criticality
and subsequent milestones; and the status of deficiency documents
i
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31
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.
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(condition reports, nonconforming material reports, and licensee event
reports) applicable to plant milestones.
The licensee discussed the ::tatus of actions being taken to address
recent NRC concerns related to their maintenance and modification
programs; recent accomplishments and current problem areas. The
licensee stated that management attention was being directed to the
radiation protection (RP) areas to assure the readiness of the RP
program to support critical reactor operation.
The licensee projected completion of all work necessary to achieve
initial reactor criticality shortly after January 25, 1987. The
licensee stated that the Region III Administrator would be contacted
by the IP Vice President - Nuclear prior to his authorizing the plant
operators to make the reactor critical. The licensee further stated
that IP expects to proceed directly in their power ascension program
through test condition 1 at which time they intend to shut down the
reactor for a short, scheduled maintenance outage. The licensee
expected to be ready to need a full power license by the end of February.
NRC (Region III) management acknowledged the licensee's status and plans,
and noted that the Commissioner's agenda currently planned a full power
license briefing for February 24, 1987.
The meeting concluded with a tentative agreement to meet again on
February 13, 1987 at the Clinton site with a similar agenda.
12. Open Items
Open items are matters which have been discussed with the licensee, which
will be reviewed further by the inspector, and which will involve some
action on the part of the NRC or licensee or both. One open item
disclosed during the inspection was discussed in paragraph 2.f.
13. Unresolved Items
Unresolved items are matters about which more information is required in
order to ascertain whether they are acceptable items, violations, or
deviations. One unresolved item disclosed during this inspection was
discussed in paragraph 8.
14. Exit Meetings (30703) '
The inspectors met with licensee representatives (denoted in paragraph 1)
throughout the inspection and at the conclusion of the inspection on
January 26, 1987. The inspectors summarized the scope and findings of
the inspection activities. The licensee acknowledged the inspection
findings. The inspectors highlighted the need for management attention
to internal commitments and the CPS emergency off-normal procedures.
The inspectors also discussed the likely informational content of the
inspection report with regard to documents or processes reviewed by the
32
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! inspectors during the inspection. The licensee did not identify any such
documents / processes as proprietary.
.
The resident inspectors attended exit meetings held between Region III
based inspectors and the licensee as follows:
Inspector (s) Date
.Wohld .1/15/87
Hasse 1/15/87
l Foster- 1/15/87
.
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