ML20206M798

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Insp Rept 50-312/86-41 on 861201-870212.Unresolved & Open Items Identified.Major Areas Inspected:Activities Supporting Restart & Ensuring Safe Operation of Plant After Restart, Including Stated Phases of Sys Review & Test Program
ML20206M798
Person / Time
Site: Rancho Seco
Issue date: 04/07/1987
From: Callan L, Dyer J, Howell A, Isom J, Martin T, Pierson R, Sharkey J, James Smith, Danielle Sullivan
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
To:
Shared Package
ML20206M774 List:
References
50-312-86-41, IEB-79-27, IEB-80-04, IEB-80-4, IEB-85-003, IEB-85-3, NUDOCS 8704200196
Download: ML20206M798 (65)


See also: IR 05000312/1986041

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OFFICE OF INSPECTION AND ENFORCEMENT

DIVISION OF INSPECTION PROGRAMS

Report No.: 50-312/86-41

Licensee: Sacramerito Municipal Utility District

P. O. Box 15830

Sacramento, California 95812

Ducket No.: 50-312

Facility Name: Rancho Seco

Inspection Conducted: December 1, 1986 - February 12, 1987

Inspectors: blY

  • J. E. Dybr, Inspection Specialist, IE

4bf67

Jate

Team Leader

TDXl &

T.~0. M in, Inspec ~ ore Specialist, IE

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Date

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"A. T. fjdwelT, Inspection Specialist, IE Date

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' *J' A. Isp, Inspection Specialist,

-

IE

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Date

0 2+' b!! Yl4lB7

R. C. Fier n, I spection Specialist, IE Date

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A N. Eharkey, IMpection Specialist, IE

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bD. Str ' tli, spection Specialist, IE

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'Date

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  • D. J. Spilivan, Jr., Ins ~pt c'thon Specialist, IE

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[fo te' i

Accompanying Personnel: *L. Miller, RV; *W. Ang, RV; *A. Johnson, RV;

  • B. Faulkenberry, RV; *S. Miner, NRR; *G. Overbeck,

WESTEC; *G. Morris, WESTEC; *D. Prevatte, WESTEC;

  • P. flilliken, WESTEC; *E. Dunlap, WESTEC; *S. Kobylarz,

WESTEC; *R. Pettis, IE; *T. Lee, NRR.

Approved-by: V7 2

  • L. J. Call { Chief, Performance Appraisal Section IE IDote
  • Attended Exit Meeting on February 12, 1987.

8704200196 870410

PDR ADOCK 05000312

O PDR

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Scope:

A special, announced inspection was performed of the activities and programs

established by the licensee to support plant restart and to ensure the safe

operation of the plant after restart. The problem identification and resoletion

phases of the Systems Review and Test Program were reviewed for eight selected

systems.

Results:

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Seventeen unresolved items and 27 open items were identified in this report

and will be followed up by the NRC.

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. TABLE OF CONTENTS

Augmented Systems Review and Test Program Inspection

at Rancho Seco

(Inspection 50-312/86-41)

Page

1.0 INSPECTION 0BJECTIVES.............................................. 1-1

2.0 SUMMARY OF SIGNIFICANT FINDINGS ................................... 2-1

3.0 DETAILED INSPECTION FINDINGS ...................................... 3-1 r

3.1 System Review and Test Program ............................... 3-1

3.2 Selected Review of System Design Features .................... 3-10

3.3 Engineering Programs ......................................... 3-15

3.4 Surveillance and Inservice Testing ........................... 3-21

3.5 Operations and Training ...................................... 3-26

3.6 Maintenance .................................................. 3-30

3.7 Quality Programs ............................................. 3-33

3.8 Restart Organization and Management .......................... 3-36

4.0 UNRESOLVED ITEMS .................................................. 4-1

5.0 MANAGEMENT EXIT MEETING ........................................... 5-1

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1. INSPECTION OBJECTIVES

The objectives of the Augmented Systems Review and Test Program team inspection

at Rancho Seco Nuclear Generating Station were to (1) assess the adequacy of

the licensee's activities in support of plant restart and (2) evaluate the

effectiveness of the licensee's established programs for ensuring safety during

plant operations after restart.

To accomplish the first objective, the team reviewed the Rancho Seco Systems

Review and Test Program (SRTP) which was developed to upgrade 32 important

plant systems by identifying problems, correcting the identified deficiencies

and testing the systems to verify proper operation. The team reviewed the

problem identification and resolution phases of the SRTP as documented in

revision 1 of the selected system status reports, but the testing program

could not be reviewed as it was not adequately developed at the time of this

inspection. The following 8 systems were selected from the 32 SRTP systems

for detailed review by the inspection team:

(1) Auxiliary Feedwater

(2) Main Feedwater

(3) Instrument Air

(4) Emergency Feedwater Initiation and Control (EFIC)

(5) 4160 Volt AC

(6) 480 Volt AC

(7) 120 Volt AC

(8) 125 Volt DC

To accomplish the second objective, the team reviewed the programs as implemented

for the eight selected systems for the following functional areas:

(1) Systems Design Change Control

(2) Maintenance

(3) Operations and Training

(4) Surveillance and Inservice Testing

(5) Quality Assurance

(6) Engineering Programs

(7) Restart Management

The specific findings in each area are presented as observations that the

inspectors believe to be of sufficient importance to be considered in a

subsequent evaluation of the licensee's performance. Some observations may

be potential enforcement findings. These observations, referred to as

unresolved items, will be followed up in future NRC inspections.

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2. SUMMARY OF SIGNIFICANT FINDINGS

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, The more significant findings pertaining to the adequacy of the System Review

and Test Program (SRTP) and the effectiveness of programs to ensure continued

safe operations after restart are summarized below. Although some strengths

were identified in each of the areas inspected, the following sumary focuses

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on the significant weaknesses identified during the inspection. Section 3

provides detailed findings, both strengths and weaknesses, in each of the areas

inspected. The ' observation numbers in brackets after the individual summary

items are provided for reference to the corresponding discussion in Section 3.

I 2.1 System Review and Test Program Concerns

, 2.1.1 Although the SRTP problem identification process appeared generally

effective, the inspection team identified instances where the licensee's

investigation into the identified problems lacked sufficient engineering
and operational depth. The following are examples of technical concerns

with the AFW system identified by the team that had remained undetected through

the licensee's problem review process.

1 (1) Past testing of the AFW pumps has not demonstrated them to be capable of

providing the flow required by Technical Specifications. [3.4.2(1)]

(2) The condensate storage tank (CST) pressure relief valves appeared to have

been set above the design pressure of the tank and were not receiving the

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required inservice testing and the CST vacuum breakers appeared to be

incorrectly sized. [3.2.1(2)and3.4.2(4)]

(3) The turbine overspeed trip setting for the dual drive AFW pump appeared

to be set above the maximum speed rating for the electric motor connected

to the common shaft. [3.1.1(1)]

(4) The SRTP evaluation of pump damage due to the runout condition experienced

during the December 26, 1985 event did not consider potential pump

degradation. Additionally, the proposed AFW system design for restart,

with the Emergency Feedwater Initiation and Control (EFIC) System

modifications, was still susceptible to pump runout under certain

l situations. At the exit meeting, the licensee committed to install

flow limiting devices in the AFW system to prevent pump runout. [3.1.1(5)]

2.1.2 At the time of the inspection, the SRTP priority system and restart

plan did not identify all problems that were to be corrected before restart.

. The team identified several problems that affected safe plant operation and

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were not currently scheduled for completion before restart. At the exit

meeting, the licensee committed to correct the identified problems affecting

safety and provide the NRC with a list of all problems that would be corrected

before restart. [3.1]

! 2.1.3 Selected System Status Reports (SSRs) did not appear to be properly

1 controlled considering their importance as basis for the NRC development of

the restart Safety Evaluation Report (SER). [3.8.1(3)]

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j 2.2 System Design Change and Engineering Concerns ,

! 2.2.1 The following deficiencies were identified with modifications being

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accomplished during this outage and not reviewed by the SRTP:

(1) After installation of the larger BA and BB batteries, certain circuit

breakers on 125 Vdc buses SOA and SOB will apparently be too small for

interrupting short circuit current. [3.2.2(1)]

(2) Inadequate implen,entation of design requirements resulted in the Interim

Data Acquisition and Display System (IDADS) computer inputs being incorrect

for the 125 Vdc bus failure and the AFW pump runout alarms. [3.2.2(6)]

(3) Modifications to the instrument air system appeared to provide incomplete

analyses for environmental qualification, specify incorrect components to

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accomplish the intended design function, and incorrectly display installation

of components on the fabrication drawings. [3.1.2]

2.2.2 Examples of deficiencies were noted in the design calculations reviewed

j by the team including the use of incorrect methods, assumptions, design inputs

and acceptance criteria. Additionally, in some instances calculations did

not exist to support the design analyses. [3.3.4]

2.2.3

Significant

used for plant deficiencies

operations were

and design noted in the

engineering control [3.3.3

projects. of sy] stem drawings

} 2.3 Programmatic Concerns

2.3.1 The surveillance and inservice testing program was found to have

deficient procedures, improper procedure implementation, and inadequate

evaluation of test results. [3.4]

2.3.2 Deficiencies were identified with the implementation of administrative

procedures for the control of plant systems and equipment status tracking.

[3.5.1]

2.3.3 The Rancho Seco quality assurance (QA) program had previously been

identified as a major problem area. Improvements had been initiated in the

QA program, but the team identified significant deficiencies in this area

because the improvements were not implemented at the time of the inspection.

These improvements were delayed as a result of QA involvement with the SRTP

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process and, consequently, the QA program was not ready to support an operating

plant. [3.7]

2.3.4 Licensee corrective action programs had not been managed effectively

in the past and at the time of this ins)ection adequate management attention was

still not being applied to this area. 3.7.3]

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3. DETAILED INSPECTION FINDINGS

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3.1 System Review and Test Program

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The activities in support of the System Review and Test Program (SRTP) were

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reviewed for each of the eight chosen systems to assess (1) the adequacy of the

activities proposed to resolve. identified problems, (2) the appropriateness of

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the scheduled resolution of identified problems with respect to restart, and

! (3) the thoroughness of system testing recommendations. Identified problems,

proposed resolutions and assigned scheduling priorities were documented in

l systems status reports (SSRs). In general, the SSRs were found to be gooo

assessments of known system weaknessess. Although the team found some apparent

weaknesses, the types of problems identified by the licensee are indicative of

a quality program that has improved the safety at Rancho Seco. The following

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subsections further describe the depth of review provided by the SRTP and

weaknesses observed by the inspection team.

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3.1.1 Auxiliary Feedwater System

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2 The auxiliary feedwater (AFW) system status report identified 55 problems, of

l which 36 required resolution before restart. The team had the following

concerns:

(1) Problem 31 identified that the turbine driven AFW pump P-318 was not

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adequately

Pump P-318tested

is a dual anddrive the turbine (electricoverspeed setpoint

motor / steam may)be

turbine pump incorrect.with both

drivers on the same shaft. The licensee identified that the high overspeed

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setpoint of the turbine may overpressurize the AFW system. The engineering

analyses to resolve this issue were in progress and not reviewed by the

team. Additionally, there were no periodic testing requirements and

previous overspeed tests conducted after maintenance activities did

i not measure system pressure because the turbine was uncoupled from the

, pump shaft during the test The team identified the additional concern

1 that the turbine overspeed setpoint may be too high to protect the electric

! motor on the common shaft. The overspeed trip point for the turbine driver

may be as high as 4650 rpm. The motor was designed to National Electric

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Manufceturers Association (NEMA) MG-1 standards that specify that it be

capable of withstanding overspeeds of 20% over synchronous speeds (NEMA

MG-1, Part 20.44). Synchronous speed is 3600 rpm, yielding a rated

overspeed of 4320 rpm. The team was concerned that a turbine overspeed

, event could damage the motor, potentially rendering the pump inoperable.

l The licensee committed tu confirm with the manufacturer that the motor

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can withstand the turbine overspeed conditions or reduce the turbine

overspeed setpoint.

Problem 31 also discussed testing the turbine to determine the time duration

, required between stopping and restarting the turbine without causing an

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overspeed trip. Stopping the turbine is accomplished by shutting the steam

1 admission valve (FV-30801), which trips a solenoid valve to depressurize

the. governor control oil, thereby shutting the throttle valve. If the

steam admission valve is reopened before the control oil pressure bleeds

down and the throttle valve shuts, the turbine could overspeed and trip.

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The testing recommended in Section 4 of the SSR was to be performed with

the turbine uncoupled and did not require measuring the time required for

control oil to depressurize and shut the throttle valve. Consequently,

it did not appear that the issues concerning motor overspeed, system

overpressurization, or minimum required shutdown time before restarting

the turbine would be answered by the proposed tests. The resolution of

issues concerning the AFW pump turbine overspeed trip setpoint and testing

will remain'open pending followup by the NRC (50-312/86-41-01).

(2) Problems 27 and 48 identified that emergency operating and casualty

procedures should be revised to stop the AFW pump if flow could not be

controlleo by other means. The team was concerned that the proposed

procedure revisions outlined in the SSR documents did not include a caution

that restarting the turbine too soon after stopping it may cause a turbine

overspeed trip. The licensee stated that they intended to include the

caution in the revised emergency operating and casualty procedures after

obtaining test information to resolve problem 31. This item will be

followed up by the NRC headquarters or Region V offices as part of item

50-312/86-41-01 concerning AFW turbine overspeed testing.

(3) Problem 54 stated that the AFW flow rate to a once-through steam generator

(OTSG) may exceed the maximum allowable flow of 1800 gpm. This was a limit

imposed by Babcock and Wilcox (B&W) to prevent tube damage or failure of

steam generator tubes due to flow induced vibration. This problem was not

- scheduled for resolution before restart, even though a B&W analysis

identified that a flow of 2130 gpm to an OTSG at 600 psig was possible.

The team's review of the B&W analysis indicated that it may not be

sufficiently conservative considering the Ranch Seco specific design and

other scenarios could produce higher flows even with the new emergency

feedwater initiation and control (EFIC) system. The EFIC system at Rancho

Seco is similar to the EFIC system installed at Crystal River which controls

AFW flow based on OTSG level and not flow rate. An event recently occurred

at Crystal River Unit 3, where flow to a single OTSG exceeded 1800 gpm.

The team was concerned that a similar event could occur at Rancho Seco.

During the exit meeting on February 12, 1987, the licensee comitted to

perform analyses that are expected to allow reduction in the required AFW

flow such that flow limiting devices can be installed. This item will

remain open pending hRC followup inspection.(50-312/86-41-02).

(4) Problem 3 indicated that the existing flow instrumentation on the full-flow

test line did not provide accurate measurement because downstream piping

was subjected to main condenser vacuum. This problem was not scheduled

for resolution before restart. Because reliance could not be placed on

the full-flow test line flow indication, the licensee opted instead to

measure condensate storage tank level change with time to perform AFW pump

performance testing. For reasons stated in Section 3.4.2(1) of this report,

this alternate method could conceal that the AFW pumps may not be providing

the flow required by Technical Specifications. During the exit meeting

on February 12, 1987, the licensee committed to installing appropriate

modifications prior to restart to improve the accuracy of the full-flow

test line indication such that AFW pump flow can be measured directly.

This item will remain open pending followup by the NRC (50-312/86-41-03).

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- (5) Problem 43 was concerned with potential . damage to the AFW pumps due to

i runout that occurred during the plant transient on December 26, 1985.

The resolution statement indicated.that the pump vendor would be contacted

to provide a determination of whether any degradation occurred to the

internals of the AFW pumps during the 17 minutes the pumps operated in a

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runout condition. However, the licensee informed the team that instead

of contacting the venoor, they planned to resolve this problem based on

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a study performed in February 1984 in response to IE Bulletin 80-04,

" Mein Steam Line Break with Continuous Feedwater Addition," which indicated

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that the pumps could survive beyond 30 minutes operating at maximum pump

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runout flow conditions. This study did not address the extent of damage

or long term pump degradation that could occur when operating at pump

runout conditions. During the inspection, the licensee committed to

resolve this issue with the pump vendor. Additionally, the team was

concerned that pump runout could still occur with the AFW system design

i proposed for plant restart. As discussed in Section 3.1.1(3) of this report, i

l the licensee committed to perform analyses that are expected to allow

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reduction of the required minimum AFW flow such that flow-limiting devices

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Can be installed. The determination of the effects of having operated an

AFW pump at runout will remain open pending NRC followup of the licensee's

i corrective actions (50-312/86-41-04).

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l (6) Problem 55 indicated that AFW pump performance calculations were required

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to establish the minimum required AFW pump head to provide 760 gpm to

1 a steam generator at 1050 psig pressure. Calculation Z-FWS-M2081, "AFW

System Minimum Head Requirements," Rev. O, dated January 12, 1987, was

performed to resolve this problem statement. It concluded that the minimum

. required head as measured at the pump discharge was 1087.3 psig with a net

flow to the steam generator of 760 gpm. The calculation further stated

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that if the condensate storage tank is at a level greater than the minimum

Technical Specification limit corresponding to 250,000 gallons the required

head should be decreased by a pressure representing this difference in

level. However, this conclusion was incorrect because the required head

, should instead be increased by this amount. This error could have caused

i a non-conservative error of as much as 17 psig in the acceptance criteria

l for the performance testing. Additionally, the calculation contained an

j incorrect conversion factor to convert from psi to feet of water. In

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attempting to change the conversion factor for water at 70*F to water at

J 90*F, an incorrect relationship was used causing the weight densities to

i be reversed. This error resulted in a 6.6 psig error in the non-conser-

vative direction. Instead of requiring that the pump develop 1093.9 psig,

j the calculation only requires 1087.3 psig. The licensee acknowledged these

l errors during the inspection and agreed to correct the calculation. This

! item will remain open pending NRC followup inspection to confirm that the

errors have been corrected and that appropriate acceptance criteria are

reflected in surveillance testing procedures for the AFW pumps ,

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(50-312/86-41-05).

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3.1.2 Instrument Air System

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. The instrument air system status report identified 31 problems, of which 12

l were to be corrected prior to restart. Six of these related to providing

i reliable backup air for various valve control functions for the main feedwater

i (MFW) and AFW system EFIC modifications. The team considered the prioritization

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f given these problems to be acceptable, but had technical concerns in the .

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i following five areas associated with the addition of backup air supplies:

l (1) The overpressure protection for the main and startup feedwater control

i valve actuators appeared inadequate. Pressure in the supply air bottles

i could be as high as 2400 psig, while the valve actuators were rated for

j 150 psig maximum air pressure. A pressure control valve maintained the

i pressure at the valve actuator at less than 150 psig. Pressure relief,

in the event of pressure control valve failure, was achieved by a relief

! valve built into the pressure control valve and a rupture disk in the air

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line to the actuator. .However, the relief valve was set for 200 psig

4 dnd the rupture disk Was designed to relieve at 225 psig. Application of

' air pressures as high as 200 psig to these actuators could cause failure

i of the actuators or failure of the valves themselves. This could cause

loss of the isolation function required in these MFW lines to mitigate

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steam generator overfill. The licensee committed to reducing the setpoint

i of the overpressure protection devices to 150 psig.

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(2) The safety-related pressure control valves, excess flow valves, and

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adjustable check valves for the backup air supplies for the EFIC modifica-

tions were not seismically qualified. At the conclusion of the inspection,

analyses were in progress by the licensee to qualify this equipment.

(3) The check valve design chosen for the backup air system appeared to be-

the incorrect design. The EFIC backup air modifications contained excess

i flow valves that were intended to act as check valves to isolate the

i backup air supply frop the normal air supply. However, as originally

specified, these valves could pass up to 5 standard cubic feet per minute

(SCFM) in the reverse direction without the valve closing. Such a condition

could occur if the pressure control valves for the backup air bottles did

not provide tight shutoff under normal conditions or if a low level pressure ,

cecay situation existed in the normal instrument air supply. In wither

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case the backup air bottles could be bled down unnecessarily, potentially

j compromising the availability of this supply. The backup air system was

i designed to provide at least a 2-hour supply of air. Calculations performed

i to determine the bottle pressures corresponding to the 2-hour and 3-hour

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alarm points considered normal' air usages and some unknown leakages, but

failed to consider the potential backflow through the excess flow v61ves,

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Consequently, leakage through these check valves could~ prevent the backup

dir supplies from fulfilling their design function.

The inspection team's position was that check valves allowing no backflow

! would be the appropriate choice in this application. The licensee main-

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tained that the system could be made to work as is, and the following

!, commitments were made to resolve the team's concerns:

j (a) The actuation setpoint for the excess flow valves will be reduced

i from 5 SCFM to the minimum practicable setpoint which will still

allow sufficient flow in the normal direction from either the

l normal air or backup air system to actuate the valves being

J supplied at their required speeds. This will be determined by

preoperational testing.

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(b) The final setpoint flows will be factored back into new 2-hour and

3-hour required supply pressure calculations.

(c) Operating procedures will be established to monitor backup bottle

pressure on a daily basis and to take remedial action if excessive

leakage is indicated.

(d) Periodic testing procedures will be established to determine if

excess flow valves are within the limits established by (a) and (b)

above.

The team determined that the licensee's commitments described above could

provide the necessary assurance of the reliability of the backup air system.

(4) The pressure control valves for the EFIC backup air system appeared to be

an inappropriate design for their specified application. Pressure control

valves were installed to regulate backup air to the valve actuators if the

nonnal air supply pressure dropped below 90 psig. Above this pressure the

valves should provide tight shutoff to prevent loss of air from the bottles.

The currently specified pressure control valves were not designed for tight

shutoff under zero demand conditions. Should these valves leak through,

either the excess flow valves addressed in Section 3.1.2(3) above will not

actuate, in which cose the air will flow into the normal air system, or the

leakage will be sufficient to close the excess flow valve and the pressure

to the volve actuators will build to the point that the relief valve or

rupture disk will actuate, dumping the backup air to atmosphere. It was

the team's position that the specified pressure control valves were

inappropriate for this application because they unnecessarily diminish

system reliability. The licensee maintained that these valves were

appropriate and the system reliability would be acceptable. Additionally,

the licensee maintained thet commitments documented in Section 3.1.2.(3)

would compensate for these valves.

(5) The fabrication drawings for the EFIC backup air supply for the pressure

control valves and the excess flow valves were found to show the velves

installed with an improper orientation. However, the in/out ports for

the excess flow valves were properly labeled despite the volve outline

being shown backwards. In the case of the excess flow valves, the drawing

orientation error had been discovered during fdbrication and the valve

was installed correctly. However, the fabrication organization had not

provided feedback to the design organization of the error and the drawings

had not been changed. This could cause problems later in plant life should

the pressure control valves be replaced using the same fabrication drawings.

These drawings were being corrected at the conclusion of the inspection.

The apparent failure by the licensee to ensure that safety-related components

of the instrument

associated drawings airwere

system weremaintained

properly seismically (qualified and to ensure thatas discussed in

3.1.2(5), respectively) will remain unresolved pending followup by the NRC

(50-312/86-41-06).

3.1.3 Main Feedwater System

The main feedwater (MFW) system status report review was limited to examination

of the system problems with emphasis on safety-related espects of the system.

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Unlike the AFW and instrument air systems, a detailed examination by the

inspection team of engineering activity to resolve system problems or modifi-

cations was not performed. Of the 55 problems identified in the SSR, 10 were

scheduled to be completed before restart. Although the problem description

and the testing recommendations were not very detailed, the team, in general,

found them to be adequate. However, the following list of MFW problems were

not scheduled for resolution prior to restart, but were considered by the

inspection team to significantly affect plant reliability and should be

resolved before restart:

No. Problem Statement

6 Faulty MFP Lovejoy Control Response

9 MFW Startup Flow Control Valves Stick Closed

Occasionally and Have Slow Response to OTSG

Level Change

12 NFW Flow Control Valve Positioning During Transients

18 Correct Casualty Procedure C.26 For MFP Operation

With Low Condenser Vocuum

19 Correct Casualty Procedure C.10 For Action On Loss

Of One MFP

22 Update P&ID M-580, Sheet 1

31 MFP Control From Lovejoy to Bailey H/A Station Is

Not Performing As Designed

45 MFP Governor Is Slow To Respond

The licensee had made a similar determination prior to the start of this

inspection and a Restart Manager Memorandum dated February 3,1987 authorized

release of resources to resolve these problems. These problems and their

resolution will be reviewed by the NRC (50-312/86-41-07).

3.1.4 Emergency Feeowater Initiation and Control (EFIC) System

The inspection team's review of the EFIC System SSR focused on the technicel

adequacy of engineering change notice (ECN) - 5415 to install this new system

and the various sub-ECNs. Reviews were conducted of the following sub-ECNs of

ECN-5415:

Sub ECN Description

A Installation of OTSG Level Taps

B Installation of OTSG Level Transmitters

C Installation of new Main Steam Line Pressure

Transmitters / Deletion of Pressure Switches

Q Signal Conversion Cabinet Indication Loop Modifications

AC Installation of MOVs on two ADV Isolation Valves

AH Installation of HISS Console Extension

3-6

_ . ,-. - - _ _ - - . _ _

- - - - -- --. --

_ _ ___ - . . _ _ _

l

. .

The following concerns were identified during the review:

(1) The excess flow check valves located in the steam generator low level

sensing line to separate the EFIC system from Integrated Control System

.

(ICS) were not environmentally qualified. These valves contain age-

'

sensitive material (Viton 0-rings) and will be located in a harsh

temperature and radiation environment. During the inspection, the

i

'

licensee initiated actions to qualify these valves. This item will be

followed up in a future NRC inspection (50-312/86-41-08).

!

l (2) The EFIC system design appeared susceptible to inadvertent initiation

i upcn a single failure of an OTSG level sensing line. This appears to

deviate from the Rancho Seco Updated Safety Analysis Report (USAR) Section
7.1.1.1, " Single Failure," which stipulates that no single failure will

initiate unnecessary protective system action except when satisfying

, this criteria could prevent protective action with a single failure. Both

l the OTSG 1evel and pressure instrumentation appear susceptible to initation

i on a single failure of a sensing line. The OTSG level instrumentation has

two low level and two high level taps, each of which provides inputs to

l two channels of the EFIC initation logic. Similarly, the steam pressure ,

instrumentation has one tap in each steam line which supplies two channels

! of the initiation logic. A single failure in the commori sensing line at

'

any of the level or pressure taps will satisfy the two out of four initation

logic for the EFIC system and start the AFW system. -

I The team acknowledges that the probability of a failure of the common

sensing lines for the OTSG high level tap or steam pressure taps is small,

but the probability of spurious initiation due to the failure of an OTSG

low level common sensing line may be enhanced by other design features.

! First, excess flow valves are installed in the common instrument lines at

! each of the taps. They were originally not environmentally qualified and

l are intended to close upon failure of downstream piping to minimize the

! effects of a potential break. However, they will actuate closed at a flow

i rate well below that of a line break. Second, there were mechanical

) fittings downstream of the excess flow check valves which are subject to

i leakage. If leakage through any of these joints or at any of the

i instruments themselves reached the setpoint of the excess flow valve, it

j will actuate closed, isolating the lower legs of the level instruments

associated with that level top and producing the same spurious initiation

'

<

, effects as a failed correon sensing line.

l The team was concerned that EFIC system sensing instrumentation was

currently designed such that certain failures will initiate unnecessary

1 protection system action and potentially cause transients. Additionally,

j it appeared that the deviation from Section 7.1.1.1 of the USAR was not

identified in the 10 CFR 50.59 evaluation for the EFIC system modification.

These concerns will remair. unresolved pending followup by the NRC

(50-312/86-41-09).

) (3) The licensee's planned test program as outlined in the EFIC System SSR did

not' verify that whenever any channel was placed in the maintenance bypass

i position, the remaining channels would not be inhibited or degraded. The

i team considered that such testing would be appropriate to demonstrate that

I the channels which provide signals for the same protective function, be

j independent and physically separated such that the likelihood of interactions

i

3-7

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_ - _ - - - _ _ _ _ _ _ - _ _ _ - _ _ _ _ _ - _ _ _

i

1

. O

between channels during maintenance is reduced as required by Institute of

Electrical and Electronic Engineering (IEEE) Standard 279-1971, " Criteria

for Protection Systems for Nuclear Power Generating Stations." During the

inspection, the licensee indicated that post-modification testing would

incorporate appropriate provisions to fully test the maintenance bypass

feature. This item will remain open pending followup by the NRC

(50-312/86-41-10).

3.1.5 125 Vdc System

Battery replacement, new diesel generators, and changes to the 120 Vac vital

bus system loads for the EFIC system modifications were all identified in the

system status report as the major changes that affected the 125 Vdc system.

Additionally, 22 valid problems were identified by the licensee, and the team

agreed with the actions and scheduling of resolution for all but four of these

problems. The following problems were discussed with the licensee who agreed

that they should be completed before restart:

(1) Problem 6 identified several deficiencies with operating procedure A.61,

"125 Volt DC System", which affect safe plant operation.

(2) Problem 9 identified instances where battery room temperatures exceeded

l design temperatures in the summer months, but did not identify that

l battery temperature could go below minimum design temperatures in the

winter months. The team noted that battery temperatures in batteries BC2

and BA2 were several degrees below the minimum temperatures used in design

calculations [see Section 3.4.4(1)]. The proper control of battery

temperature can impact the various design analyses of the 125 Vdc

system as identified in Section 3.2.2(1) of this report.

(3) Problem 20 identified that the power filter capacitors had reached the

end of their useful life for only one of six Class 1E battery chargers

in the auxiliary building. However, problem 20 did not identify that the

other five chargers also required capacitor replacement. New capacitors

had been ordered for all six battery chargers to replace the existing

components, but the SSR only identified charger H4BB as requiring capacitor

replacement and this was scheduled for resolution after restart. The

licensee stated that the problem statement and resolution of the SSR would

be expanded to include the refurbishment of all six aging Class 1 battery

chargers before restart.

(4) Problem 22 identified open nonconformance reports (NCRs) that were not

scheduled to be resolveo prior to restart. Two of the NCRs (S-5504 and

S-5548) concerned deformed vital battery terminal posts. The team

determined that these two NCRs affected the operation of the safety related

battery.

The implementation of the corrective actiuns discussed above for the 125 Vdc

system will remain open pending review by the NRC (50-312/86-41-11).

3.1.6 120 Vac Vital Power System

The vital 120 Vac power system was being modified during this outage to

transfer new loads to the buses located in the Nuclear Services Electrical

Building (NSEB). The team reviewed the 15 problems in the SSR identified by

the licensee and agreed with all but the following items:

3-8

. _ _ _ _ _ . - _ _ _ .- ._. _ __ _ _.

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. .

2

(1) Problem 7 identified that the licensee's response to IE Bulletin 79-27,

i " Loss of Non-Class-1E Instrumentation and Control Power System Bus During

4 Operation," needed updating. The licensee's proposed resolution was to

l analyze the existing electrical systems and determine actions to be taken -

after restart. The team was concerned that the 120 Vac systems modifica-

!

tions installed after issuance of IE Bulletin 79-27 did not comply with

the requirements for indication in the control room and that current

i casualty procedures did not provide the diagnostic problem solving '

corrective actions required by this bulletin. .At the exit meeting, the

licensee agreed to implement the recommendations of their study of IE

t Bulletin 79-27 prior to restart. This commitment appears to upgrade the

j following problems to be accomplished before restart:

Problem 2 - No control room indication on opening of vital 120 Vac breakers.

!

}

Problem 5 - Casualty procedures do not exist for loss of 120 Vac vital

j buses. .

.

(2) Problem 6 identified that operating procedure A.62, "120 VAC Vital System " '

did not list a load schedule and was not scheduled for completion prior

to restart. The team considered the load schedule important for reliable

.j plant operations.

! (3) Problem 12 identified that there was no positive local indication of

individual circuit breaker position on the 120 Vac panels. The tripped -

'l and shut positions of the breakers were too close to distinguish by

relying solely on the visual indication of the breaker switches. The

i

team considered positive indication of individual 120 Vac circuit breakers

j to be important for safe plant operations.

I

At the exit meeting the licensee committed to resolve the issues identified

above with the 120 Vac vital system before restart. .This issue will remain

i open pending followup inspection by the NRC (50-312/86-41-12).

I

! 3.1.7 480 Vac System

}

There were no major modifications identified for this system. Of the 43

problems in the SSR identified by the licensee, the team agreed with the

priority and resolution of all but the items listed below:

l (1) Problem 10 identified that no 480 Vac loads were alarmed for loss of

power. The licensee planned to perfom a study after restart to determine

which loads should be alarmed. There was no schedule for completing

the alarm installation for those loads identified by'the study. The team

determined that the study and required alarm installation should be ,

accomplished before restart.

j (2) Problem 11 identified deficiencies with various casualty procedures for the

t 460 Vac system that should be corrected before restart. l

(3) Problem 16 identified poor local indication for some 480 Yac system ,

3

< circuit breakers caused by defective springs which should be replaced l

'

before restart. l

l

'

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. d

(4) Problems 25, 33 and 34 identified deficiencies with Procedure A.59, "480 Vac

System Operating Procedure," which should be corrected before restart.

(5) Problem 46 identified a discrepancy with drawing E-108, Sheet 30, that

was used for plant operations and should be corrected before restart.

(6) Problem 26 identified that there was no indication for loss of 480 Vac

circuit brehker control power and should be corrected prior to restart.

'

This item will be resolved as part of the actions required by IE Bulletin

.

79-27 discussed in Section 3.1.6(1) of this report.

.

(7) Problem 19 identified inconsistencies with the alarms for losses of the

i various 480 Vac system load centers and motor control centers (MCCs) which

may confuse the operators. This item should be resolved prior restart.

.

l The resolution of the items identified above pertaining to the 480 Vac system

will remain open pending followup by the NRC (50-312/86-41-13).
3.1.8 4160 Vac System

The installation of safety-related diesel generators GEA2 and GEB2 and the

,

tie-in to the 4160 Volt busses were identified as the major modifications for

i this system. Of the 42 valid problems identified in the SSR, the team agreed

l. with the priority and resolutions of all but the four listed below:

I (1) Problem 8 identified instances where protective relays in the switchgear

' had been modified by slotting a hole on the magnet base to help with

calibration of the relay. The licensee did not know how this would affect

i the seismic and environmental qu611fication of the switchgear. This

problem should be resolved before restart.

!

! (2) Problem 25 identified that there was no indication for loss of de control

i power to the 4160 Vac switchgear. This issue should be resolved prior

to restart as part of the implementation of IE Bulletin 79-27 respunse

,

items oiscussed in Section 3.1.6(1) of this report.

> (3) Problem 32 identified that there was no procedure for operation of the

i startup transformers. Specifically, there was no formal procedure

I identifying the required system checks for the transformers that should

} be performed before they are placed in service. This procedure should

i be develuped and issued before restart.

l (4) Problem 33 identified deficiencies with the casualty procedures for the

electrical transformer cooling system which should be corrected before

j

restart.

The resolution of identified problems with the 4160 Vac system before restart

i will remain open pending followup by the NRC (50-312/86-41414).

'

3.2 Selected Review of System Design Features '

i To assess the completeness of the licensee's identification of system problems,

l safety-related design features were reviewed by the inspection team on a sampling

! basis. The design features selected for review were not the subject of a

!

3-10

- . - _ - - - -,.- . - -_- .. -- . _ - _ - - . - - - - -

. .

l

problem identified in system status reports. The findings and observations

resulting from these reviews are discussed below, categorized by engineering

discipline.

1

3.2.1 Mechar.ical Systems l

(1) The following design features were reviewed and appeared to be technically

correct:

(a) Seismic qualification package for AFW system flow control valves

CV 20527 and CV 20528.

(b) AFW pump available net positive suction head.

(c) Desigr analysis that confirmed the adequacy of a missing anchor

bolt observed during a system walkdown.

. (d) Arrangement of the AFW turbine steam supply piping with respect to

the single failure criterion.

(e) Preliminary seismic analysis for qualification of motor operators

for the main steam dump block valves.

(2) Weaknesses were identified in design features associated with the

condensate storage tank (CST) overpressure and vacuum protection schemes.

It appeared that the adequacy of these design features were not verified

when the AFW system was upgraded to safety grade.

(a) Procedure AP.152, "Feedwater and Condensate Systems," Revision 19,

allowed the set pressure of the relief valves for the CST to be set

as high as 2.5 psig. According to the tank supplier's drawings, the

maximum allowable working pressure and the design pressure for the

tank are both 2.0 psig. Because the CST is a closed tank, the pressure

inside the tank increases as water is added. It appeared to the

inspection team that this would routinely cause the pressure in the

CST to increase above the 2.0 psig design value. The CST is the only

safety-related water source for the AFW system, and Technical

Specifications require that a minimum of 250,000 gallons of water be

available in the tank. The team considered the CST relief valve

'

setpoint upper limit of 2.5 psig to threaten the structural integrity

of the tank.

-

(b) The CST vacuum breakers may not provide adequate underpressure pro-

1

tection for the tank. The sizing analysis for these valves was

i

performed in 1975 by the architect / engineer. The design basis event

that this analysis considered was makeup to the hotwell with both

i

vacuum breakers functioning. For this event a negative pressure of

1.3 inches of water on the CST was calculated; however, the tank was

designed for a negative pressure of cnly 1.0 inch of water. The

! excess negative pressure was judged in the analysis to be acceptable

without explanation. Additionally, the analysis for these valves
did not consider a single failure of one of the two valves as required

by 10 CFR 50, Appendix A, Criterion 34 or more limiting events such

as hotwell makeup and AFW pumps running together. If this situation

3-11

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, _ - _ . - _ _ - . - _ _ - _.

. <

were considered, it is likely that the negative pressure could

significantly exceed the tank's rating.

The apparent failure to provide adequate relief valve and vacuum breaker

protection for the CST will remain unresolved pending followup inspection

by the NRC (50-312/86-41-15).

3.2.2 Electrical Power Systems

The ac and de Class IE systems were reviewed. The team concentrated on

verifying the adequacy of the voltage available at Class 1E equipment, the

continuous and short circuit duty of the distribution equipment, and cable

sizing criteria in regard to ampacity and voltage drop. The documents reviewed

to support this evaluation consisted of the one line diagrams for the Class 1E

systems for the 4160 Vac switchgear, the 480 Vac load centers, the 120 Vac

vital instrument power panels, and the 125 Vdc power panels. Estimates were

made by the team that confirmed the conservative steady-state loading of the

Class 1E distribution panels.

At the time of this inspection the onsite Class IE ac system was being modified

by the licensee to improve its capacity and reliability. The team reviewed

the future distribution system as it was intended for restart and considered

the licensee's plans acceptable.

The team reviewed selected calculations evaluating the accuracy of input data,

the appropriateness of input assumptions, and the methodology and mathematics

of the calculation details. The calculations reviewed included the main ac

voltage study and short circuit calculations; the 120 Vac system inverter

l study and short circuit calculations; the 120 Vac system inverter loading

and breaker coordination calculations; the de system short circuit and battery

sizing calculations; and selected cable ampacity and voltage drop calculations.

In general, these calculations were found to be adequate; however, several

deficiencies were found as described below:

(1) At the time of the inspection, the batteries in the auxiliary building were

being replaced with new, larger capacity batteries. The licensee performed

sizing calculations to establish the amount of margin that existed for

future load growth. The licensee also performed a de short circuit

calculation to verify the compatibility of the new batteries with the

existing de panelboards. The team found that the de short circuit

calculation, Z-DCS-E0612, Revision 1, dated January 2, 1987, contained

conflicting references for the short circuit capacity of the new batteries.

The less severe value was used in the calculation, without justification,

yielding a margin of less than 200 amperes below the rating of the de panel-

board. If the other reference data attached to the calculation were used,

a short circuit above the panelboard rating Would have resulted. In

addition, the team found that the calculation failed to recognize that

the manufacturer's short circuit data was presented at a nominal 77'F

rating. Batteries are electrochemical devices and, as such, the short

circuit current capability of a battery is dependent upon temperature.

At the maximum allowable temperature presently permitted for the licensee's

' batteries 110*F, the de panelboards could be subjected to a short circuit

!

at least 10% above rating. Failure of a de circuit breaker to clear such

{

a fault could result in failure of the battery, caused by melting of the

l 3-12

l

1

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a .

l

- lead components within the battery cells. This design deficiency will I

remain unresolved pending followup by the NRC (50-312/86-41-16). l

(2) At the time of this inspection the safety-related batteries in the NSEB

were being loaded to near capacity by transferring loads from the auxiliary

building batteries. To ensure that the NSEB batteries could accept these

additional loads, battery sizing calculation Z-DCS-E0636 Revision 1, dated

January 3,,1987, was prepared. As part of this calculation a new load

profile was developed based on a review of all loads connected to the de

panelboards. The largest loads being odded to the NSEB batteries were the

safety-related inverter loads transferred from the auxiliary building

batteries. Inverters are constant kVA loads and, therefore, draw a larger

current with the decreasing voltage seen during a battery discharge. This

was not addressed in the calculation. Instead of using a voltage typical

of the expected discharge voltage, the calculation assumed a nominal 125

volt input. The correct discharge voltage would have resulted in a load

current drawn by the inverters approximately 10% higher than assumed in

the calculation and would have changed the result of the calculation by

approximately 6%.

This same calculation included correction factors for aging and minimum

design temperature as recommended by IEEE Standard 485, " Recommended

Practice for Sizing Large Lead Storage Batteries for Generating Stations

and Substations." However, the team found that calculation Z-HVS-1940,

Revision 0, dated July 7, 1986, referen:ed as the basis for the minimum

design temperature, did not substantiate the temperature value used in

the battery sizing calculation. This error could contribute an additional

4 to 6% difference in the final result of the calculation. The calculation

had concluded that approximately 10% margin existed for future load growth.

Because of a 25% correction factor included for aging, no immediate problem

existed with the present loads. The team was concerned that the margin

remaining for future loads was substantially less than calculated by the

licensee. The apparent failure to perform an adequate analysis of the

NSEB battery will remain unresolved pending NRC followup inspection

(50-312/86-41-17).

(3) As part of the team's evaluation of the 4160 Vac and 480 Vac systems,

selected input data for the short circuit and voltage regulation studies

were verified. The team found that the voltage regulation calculation

Z-EDS-E0076, Revision 4, dated January 4,1987, was adequate. This

calculation computed the 4 kV and 480 Vac bus voltages for a transmission

voltage range of 244 kV to 214 kV. As a result, the licensee determined

that if the minimum transmission voltage was held at 216 kV, sufficient

margin would be present to ensure that the starting voltage at the motor

terminals would be above the minimum required 75% of motor nameplate

voltage. All major motors in the 4 kV and 480 V systems were considered

and the motors that are most distant electrically, in terms of feeder cable

voltage drop, were the motors selected for the study. The team confirmed

that all buses were loaded to realistic values for this study. A minor

discrepancy was found concerning the voltage transfonnation ratio used in

the calculation for startup transformer number two. The calculation

used a 230 kV to 4.36 kV ratio and the referenced one line diagram

E-101, which indicated a 221 kV to 4.36 kV ratio. The team confirmed

that the calculation correctly used the transformation ratio from the

actual voltage tap selected at the transformer. This item will remain

3-13

-.. . . - - - -. - - . - . -- .- -- - -

!'

. .-

! open pending NRC review of the corrected one line diagram, E-101 ,

(50-312/86-41-18).

1

! (4) The inspection team was unable to verify that the correct startup

! transformer impedances were used in short circuit current calculation

'

Z-EDS-E0120, Revision 2, December 31, 1986, performed by Bechtel using

j the TE 502 "FAULTX" computer program, Rev. O. The licensee acknowledged

i

that an apparent discrepancy of almost 6 percent existed in the noncon-

i

servative direction and drafted a preliminary calculation indicating that

under worst case conditions a margin of about 1 percent between breaker

j rating and the available short circuit current would still exist at the

motor control centers. The apparent failure to use the proper data in

this calculation will remain unresolved pending NRC followup inspection

}

(50-312/86-41-19).

(5) One power cable was found not to be sized in accordance with USAR commit-

ments. USAR Section 8.2.2.11.H.11 stated that power cables are sized for

i. 125% of full load current of the equipment served. In response to inspec-

i tion team concerns about power cable thermal insulation, the licensee

'! developed a preliminary calculation that showed one power cable, between

i battery charger H4BAC and de Bus SOA, was found marginally acceptable

i based upon actual load currents and would not have satisfied the 125%

) USAR criteria. The apparent failure to meet a USAR commitment will

d remain unresolved pending followup by the hRC (50-312/86-41-20).

(6) The team reviewed the electrical schematics supporting the auxiliary

feedwater system modifications installing EFIC. Two examples were found

j of an apparent breakdown in the interface between the designers and the

interim data acquisition and display system (IDADS) computer group.

i

(a) The electrical distribution system in the NSEB was monitored in the

j control room by IDADS. The dc bus voltage was an input to the

computer as a 125 volt analog signal. The IDADS computer group

! incorrectly interpreted this as a bistable input and set the bus

failure alarm at zero volts, eliminating alarms at degraded bus

i voltages. The correct setpoint should have been no lower than 105

j volts.

j (b) The AFW pump runout alarm was developed by a combination of a pump

l low discharge pressure signal and a delayed pump running signal

j from the motor circuit. The purpose of the delay was to provide

-

time for the pump to come up to speed so that an unintended alarm

j

would not be received on startup. Although the logic diagram, 1205, ,

-

Sheet 3. Revision 6, indicatea the required time delay, this feature

I had not been provided in the actual circuit, either by hardware or by

{ computer software.

j These examples of an apparent failure to correctly translate intended

i design features into plant systems will remain unresolved pending followup

} by the NRC (50-312/86-41-21).

,

i (7) Electrical protection provided for equipment in the AFW system was reviewed.

} The team determined that adequate overload protection was provided for the ,

l 1000 horsepower auxiliary feedwater pump motors. However, no thermal

overload protection or overload alarms were provided for the safety-related

{

i

I

'

l 3-14

i

. .

motor operated valves. Although these features are not a regulatory

requirement, having neither of these features is not censistent with

general industry practice. The inspection team was concerned with the

potential for undetected degradation of a valve operator's motor that

would cause the motor to fail when subjected to design basis conditions.

The licensee stated at the exit meeting that this matter would be reviewed

for consideration at Rancho Seco. This item will remain open pending NRC

review of the licensee's resolution (50-312/86-41-22).

3.3 Engineering Programs

During the inspection, the team examined a large cross section of engineering

design and output documents. The documents reviewed by the team are identified

in Appendix B of this report. The review of these documents and technical

discussions with the licensee's engineering staff formed the bases for the

following observations.

3.3.1 Nuclear Engineering Procedures Manual

Rancho Seco implemented a Nuclear Engineering Procedures Manual in 1985 to

provide an integrated system of procedures and references for design and

construction. This manual, although not entirely complete, contained over

500 procedures covering topics such as administration, design control, pro-

curement, design criteria, design guides, specifications, system design bases,

and Construction procedures. At the time of this inspection the system design

basis section was approximately 25% complete; however, overall this comprehen-

sive manual was considered a strength.

In addition to numerous procedures identified in Appendix B of this report, the

following procedures from the Nuclear Engineering Practices Manual that affected

general design process were reviewed:

4101, " Design Process," Revision 0

4106, " Design Calculations," Revision 0

4109, " Configuration Control," Revision 5

4110. "Interdiscipline Document Review," Revision 1

4112, " Drawing Change Notice," Revision 1

With the exception of the deficiencies identified in Section 3.3.3, the licensee's

procedures governing design and modification control activities were considered

odequate.

3.3.2 Safety Evaluations

The licensee's procedures governing the performance of safety evaluations were

reviewed; Quality Control Instruction (QCI) 5. " Safety Review of Proposed

Facility Changes," Revision 2, and QCI 18, " Safety Review of Proposed Procedures

and Procedure Changes," Revision 1. A review of several safety evaluations

indicated that these procedures were being properly implemented. However, these

procedures lacked detailed guidance for determining the existence of an un-

reviewed safety question and lacked requirements governing the qualifications

of personnel making and reviewing 10 CFR 50.59 determinations. These weaknesses

were identified by the licensee and addressed in draft procedure QCI 5 " Safety

l Review of Proposed Changes, Tests and Experiments." This item will remain open

pending NRC review of the implementation of this draft procedure (50-312/86-41-23).

3-15

i

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l

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l

l

3.3.3 Drawing Control Program l

l

The following deficiencies were found in the drawing control program: j

l

(1) No procedure existed to control the distribution of updated drawings. 1

Nuclear Engineering Procedure (NEP) 4109, " Configuration Control," l

Revision 5, had a transmittal form for drawing changes but had no specific I

instructions for its use. At the time of this inspection, the licensee <

'

l had prepared draft procedure AP.85 " Site Control Document," intended to

control the distribution of updated drawings. This draft procedure

addressed issues such as controlled distribution lists, field use of

controlled drawings, stamping conventions, drawing change notice (DCN)

distribution, control room drawing distribution, and handling and distri-

bution of controlled aperture cards.

(2) The controlled drawing files were not being maintained up-to-date. The

licensee used drawings on yellow paper to indicate the construction

completion of modifications made to the plant. One or more yellow drawings

were then incorporated into new revision white drawings. The licensee's

control of these yellow drawings was found to be inadequate. A comparison

Was made of the yellow drawings on file for drawing numbers M-500 to M-599,

which are the system piping and instrument diagrams (P& ids). This

comparison was made between site document control (SDC), the control room,

and the controlled crawing file room in Trailer 0 used by the nuclear

engineeringdepartment(NED). The following deficiencies were found with

these drawing files:

(a) Drawing M-562, "P & I Diagram Waste Gas System," Revision 23, was found

in SDC and the NED. However, a yellow drawing, detailing DCN 37, was

outstanding against drawing M-562, Revision 23. The applicable yellow

sheet necessary to determine the effect of this DCN was not available

at either SDC or the NED. The control room had Revision 24 of drawing

M-562, which had incorporated DCN 37.

(b) Dr6 wing M-532 " Steam Generator System," Sheet 1, Revision 6, had

three applicable yellow drawings for DCNS 19, 20, 41d 26 as indicated

4 by the SDC yellow drawing file. In the NED, the aperture card for

M-532 incorrectly indicated that only DCN 19 was applicable to this

drawing. The yellow drawings for DCNs 20 and 26 were not available

in the NED, nor in the control room for DCN 26.

,

(c) The NED had drawing M-533, "High Pressure Feedwater Heater System,"

Sheet 4, Revision 10, and the control room had Revision 9 of this

same drawing.

(d) Drawing M-541, " Plant Cooling Water System," Sheet 1, Revision 4,

was found in the control room. However, a yellow drawing, detailing

DCN 5, was outstanding against drawing M-541, Revision 4. The

applicable yellow sheet necessary to determine the effect of this

DCN was not available in the control room.

3-16

. -. -. .. - -- -. _ - . . -.

. .

1

(e) Drawing M-543, " Component Cooling Water System," Sheets 1 and 2, 1

P.evision 2, was found in the control room. However, a yellow drawing, '

detailing DCN 5A, was outstanding against drawing M-543, Revision 2.

The applicable yellow sheets necessary to determine the effect of this

DCN were not available in the control room.

l

During this inspection, the licensee management representatives agreed to

perform a complete verification of their drawing files and committed to

conduct a quality assurance (QA) audit of SDC activities. The failure of the

licensee to have a procedure to control drawing distribution and to maintain

current drawing files will remain unresolved pending followup by the NRC

(50-312/86-41-24).

3.3.4 Engineering Calculations

The team was concerned that in many instances the general quality of design

calculations did not meet the requirements of American National Standards

Institute (ANSI) N45.2.11. " Quality Assurance Requirements for the Design of

Nuclear Power Plants," Section 4.2. Of over thirty calculations reviewed,

approximately 80% contained errors or inconsistencies of varying aegrees of

significance. Approximately 7% had errors that, had they gone undetected,

could have had a nonconservative effect on plant design.

(1) The following are examples of calculation deficiencies where incorrect

results were obtained or an incorrect method was used for design

>

calculations:

(a) Calculations to detemine the minimum AFW recirculation flow were

l

performed in 1972, 1974, and twice in 1984, each giving different

results, and each still ir, effect. It appeared that only the 1974

calculation was utilized, yet the other calculations had not been

superseded, and there were no annotations to this effect on any of

the calculations. Furthemore, there was no mechanism for dis-

tinguishing preliminary from final calculations. The recirculation

flow determination was on important input to the determination of

AFW pump operability as discussed in Section 3.4.2(1) of this report.

(b) Calculation Z-FWS-M-2081, Revision 0, dated December 23, 1986, was

performed to determine the acceptance criteria for AFW pump discharge

) pressure routine testing. According to the calculation, the minimum

acceptable discharge pressure was to be adjusted to account for the

level of the condensate storage tank. The arithmetic sign for this

,

adjustmentwasincorrect[Section3.1.1(5)].

(c) Calculations Z-IAS-M2084, M2085 and H2086, Revision 0, dated

December 30, 1986, incorrectly applied the perfect gas law.

(2) The following are examples of calculation deficiencies where assumptions

were either incomplete, incorrect, nonconservative, unjustified or not

properly documented:

(a) Calculations Z-IAS-M2084, M2085, and H2086, all Revision 0, dated )

December 30, 1986, concerning backup air bottle sizing, did not '

3-17

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_ - - . - - _ .__ __ ___

. 4

i

assume leakage back through excess flow valves as described in Section .

3.1.2(3) of this report.

(b) Calculation Z-FWS-M1742, Revision 0, dated Se ember 26, 1985,

concerning motor-operated valve stem nut acce ability, assumed

uniform thread loading. This is not considered a valid assumption

in general industry practice.

(c) Calculation Z-FWS-M0254, Revision 0, dated February 9,1984,

concerning AFW system pressure drop, inappropriately assumed friction

factors for clean pipe and assumed no pressure drop for AFW ring

headers.

(d) Calculation 2-FWS-K1798, Revision 0, dated January 13, 1986, concerning

steam trap loads, assumed an ambient temperature of 75 F which is not

conservative because the piping is located outdoors.

(e) Calculation Z-IAS-0123, Revision 0, dated November 17, 1986, concerning

AFW flow orifice differential pressure, used a fluid temperature of

68'F. Calculation Z-FWS-I-0091, Revision 0, dated March 7, 1985,

concerning the same subject, used a fluid temperature of 115'F.

.

(f) Calculation Z-IAS-M2085, Revision 0, dated December 30, 1986,

concerning backup air bottle sizing gave no basis for 5 cycles of

valve operation in 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

(g) In calculation Z-FWS-M2045, Revision 0, dated October 25, 1986,

concerning AFW system resistance, the flowpath chosen as " worst

Cdse" Was not justified.

(h) In calculation Z-FWS-M1798, Revision 0, dated January 13, 1986,

concerning load on steam traps, 900 psig was assumed to be a

conservative pressure with no explanation.

(i) In calculation Z-FWS-1742, Revision 0, dated September 26, 1985,

concerning worn valve stem nut acceptability, the assumption that

the nut had a single lead thread contradicted data item 1 that stated

that the thread is a double lead.

(j) Calculation Z-FWS-M2081, Revision 0, dated January 12, 1987, con-

cerning minimum AFW pump head requirements, assumed AFW pump

recirculation flow of 60 gpm at rated flow conditions with no source

of this data identified.

(k) Calculation Z-FWS-M2081, Revision 0, dated January 12, 1987, con- I

cerning minimum AFW pump head requirements, implicitly assumed that

the condensate storage tank is at atmospheric pressure when the tank

is actually closed and can be under vacuum or pressure conditions.

(1)' Calculation 2-DCS-E0636, Revision 1, dated January 3,1987, concerning

NSEB battery sizing, assumed a battery minimum temperature based on the

referenced HVAC calculation (Z-HVS-M1940, Revision 0, dated July 23, l

1986) which did not justify the temperature assumed.

l

l

3-18

. .

(3) The following are examples of calculation deficiencies where design inputs

were incorrect or not identified: ,

(a) Calculation Z-DCS-E0612, Revision 1, dated January 2,1987, concerning

de short circuit margin, contained conflicting references for the  :

'

short circuit capacity of the new batteries [Section 3.2.2(1)(a)].

(b) Calculation M19.29, Revision 0, dated March 5, 1985, concerned AFW

system flows. An orfice was not identified or described, the source

of the system resistance curve was not identified, and the formula

source was not identified.

(c) Calculation Z-FWS-M2081, Revision 0, dated January 12, 1987, con-

cerning minimum AFW pump head requirements, identified the wrong

calculation as the basis for using zero pressure drop through the

AFW ring headers.

(d) Calculation Z-FWS-M1742, Revision 0, dated September 26, 1985, con-

cerning worn valve stem nut acceptability, gave no reference for the

stem nut data on page 6 of the calculation.

(e) Calculation Z-FWS-I-0123, Revision 0, dated November, 17, 1986,

concerning AFW flow orifice differential pressure, used an incorrect

internal pipe diameter of 6.065 inches instead of 5.761 inches.

(f) Calculation Z-DCS-E0612, Revision 1, dated January 2,1987, concerning

dc system short circuit, did not correct the input for maximum

battery temperature [Section 3.2.2(1)].

(g) Calculation Z-DCS-E0636, Revision 1, dated January 3,1987, concerning

NSEB battery sizing, did not correct the input for inverter load for

lower voltages experienced during battery discharge [see Section

3.2.2(2)].

(4) The following are examples of calculation deficiencies where acceptance

criteria were not identified or were incorrect:

(a) Calculation Z-ZZZ-IO132, Revision 0, dated January 1, 1987, concerning

qualification of excess flow valves, had no stated acceptance criteria.

(b) Calculation Z-FWS-M1742, Revision 0, dated September 28, 1985, con-

cerning valve stem nut acceptability, did not identify increased

friction effects or increased bearing stresses at thread faces as

acceptance criteria considerations. It also used incorrect criteria

for determining shear stress acceptability.

(5) The following are examples where the purposes of calculations were not

clearly stated or were in conflict with the actual usage of results:

(a) Calculation Z~ZZZ-10132, Revision 0, dated January 1, 1967, concerning

qualification of excess flow valves, was documented as having been

performed for the purpose of environmental qualification. This

calculation did not address environmental qualification.

l

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l . ;

(b) The stated objective in calculation Z-FWS-I-0091, Revision 0, dated

March 7, 1985, concerning AFW flow orifice bore sizing, was to

!

calculate the beta ratio and bcre diameter of orifice plates.

However, this calculation appeared to be an independent check of

a vendor's calculation to confirm orifice differential pressure.

(6) Some calculations could not be understood without recourse to the originator

Ncause of a lack of explanation of logic, non-use of dimensional units,

and references used that were not cited. Examples were calculations

Z-IAS-M2084, M2085, and M2086, Revision 0, dated December 30, 1986,

concerning backup air bottle sizing; calculation Z-FWS-M1798, Revision 0,

dated January 13, 1986, concerning steam trap loading; and calculation

Z-FWS-M1742, Revision 0, dated September 28, 1985, concerning valve stem

nut acceptability.

(7) The following are examples where calculations were either not available or l

not performed: '

(a) Seismic analysis for condensate storage tank and appurtenances.

(b) Seismic and environmental qualification of excess-flow check valves

and seismic qualification of backup air pressure control vahes and

adjustable check valves [see Sections 3.1.2(2) and 3.1.4(1)].

(c) Establishing the basis for the 0 to 1300 gpm flow range for AFW flow

instrument to meet a Regulatory Guide 1.97 commitment.

(d) Determining the setpoint corresponding to the condensate storage tank

level alarm when only 40 minutes of water remains in the tank.

During the inspection, in response to the team's concerns, the licensee initiated

a program to increase the level of confidence in calculations not reviewed by

the team to ensure that calculations are of appropriate quality. The signifi -

cant points of the program are (1) complete review of all calculations by

system design engineers to ioentify obsolete calculations and incorrect

references, (2) have a calculation review tearn independently review a broader

selection of calculations associated with restart for technical adequacy, and

(3) develop good practice guidelines for preparing calculations, including

techncial and documentation concerns. The failure to perform adequate calcula-

tions will remain unresolved pending NRC followup inspection (50-312/86-41-25).

3.3.5 Design Output Document Control

The licensee's control over design output documents that make up design change

4

packages was considered weak. Numerous completed design change packages were

reviewed, and none of these contained a listing or inventory of the design

output documents that the completed design change package was supposed to contain.

Under these circumstances, a person doing the closeout checking or subsequent

review of design changes could not be certain that the completed package

contained all the necessary documents or that all the requireo considerations

had been addressed in the change.

3-20

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i .

3.4 Surveillance and Inservice Testing

The team conducted a technical review of the surveillance and inservice test

(IST) programs as implemented on the AFW,125 Vdc and 4160 Vac systems. The

test procedures for the other five selected systems were being revised and were

not available for review during the inspection. This review included an

evaluation of the technical adequacy of the testing procedures and test results ,

'

to verify system components functioned as required by Technical Specifications.

The scheduling of testing to meet the periodic requirements of ASME Section XI

dnd Technical Specifications were not reviewed. The specific observations made

by the inspection team are discussed below.

3.4.1 Prograntnatic Testing Concerns

The team identified the following conceras about the licensee's test program

that pertain to all the reviewed systems:

(1) The licensee was operating without an approved Inservice Testing (IST)

program. The current IST program apparently expired on April 17, 1986

and the licensee could not pruvide a documentation that an extension

beyond this date had been approved. A new submittal was in the preliminary

stages of development and was not available for the team to review. The

apparent failure to have an approved IST program will remain unresolved

pending followup by an NRC inspection (50-312/86-41-26).

(2) The licensee's trending program for pump and valve test data appeared

inadequate. For an example, the Inservice Inspection Data Log used for

the AFW pumps' history file had no entries for 1985 and 1986 despite

surveillances performed during this period. The team was concerned that

failure to trend test data precluded using this information to detect

pump degradation. The apparent failure to trend pump and valve test data

will remain unresolved pending followup by the NRC (50-312/86-41-27).

3.4.2 Auxiliary Feedwater System Testing

The test data and technical adequacy of the following AFW system test procedures

were reviewed during the inspection:

  • SP 210.01A, " Monthly Turbine / Motor Driven Auxiliary Feed Pump P-318

Surveillance and Inservice Test," Revision 23

SP 210.01B, " Monthly Motor Driven Auxiliary Feed Pump P-319 Surveillance

and Inservice Test," Revision 23

SP 210.010. "Quorterly Steam and Auxiliary Feed System Velve Inspection

and Surveillance," Revision 09

SP 210.01F, " Cold Shutdown Auxiliary Feedwater Pump Flow Test and Check

Valve Full Stroke Test," Revision 08

Test for Loss of Four Reactor Coolant Pumps and SFAS Actuation,"

Revision 02

SP 210.011, " Auxiliary Feedwater Check Velve Integrity Test," Revision 01

3-21

. 4

  • SP 210.01J, " Refueling Outage Main Steam to Auxiliary Feed Pump Turbine

Check Valve Integrity Test," Original

  • SP 213.01, " Inservice Test and Inspection of Pumps," Revision 12
  • SP 214.01, " Inservice Testing and Inspection of Valves," Revision 06
  • SP 214.02, " Inservice Testing of Relief / Safety Valves " Revision 02

SP 214.03, " Locked Valve List," Revision 33

A.51, " Auxiliary Feedwater System," Revision 31

l Supply," Draft

The following concerns were identified as a result of this review:

(1) AFW pump flow had not been determined accurately or acceptably during

surveillance testing. Technical Specification 4.8.1 requires that the

AFW pumps be capable of delivering 780 gpm to a steam generator at 1050

psig and that this be verified on a monthly basis. Surveillance Procedures

SP 210.01A and SP 210.01B established acceptance criteria for the AFW pump

flow rates at 840 gpm to account for 60 gpm recirculation flow diverted to

the main condenser. The AFW pump capacity was determined by measuring the

change in CST level over a period of time when the CST was isolated from

everything except the AFW pump being tested. The surveillance procedures

allowed the use of either the installed level instrument (LI 35803) or a

temporary clastic tubing sightglass connected along the side of the CST.

Using these testing methods, the measured capacities for the punips have

been as low as 847 gpm indicating marginal AFW pump performance. The team

had the following concerns about the licensee's past determinations of

pump capacity using this method:

(a) There did not appear to be an adequate basis for the recirculation

value of 60 gpm. Testing performed in 1974 indicated that recir-

culation flow could be in the range of 37.0 gpm to 70.5 gpm.

Additionally, calculations dated November 6,1972, (unnumbered) and

February 9,1984 (Z-FWS-M0254) indicated that minimum recirculation

flow rates could be 86 gpm and 89 gom, respectively. The team was

concerned that actual recirculation flows greater than 60 gpm would

be non-conservative ano could affect the determination of pump

operability.

(b) The accuracy of the installed CST level instrument, LI 35803, had not

been validated using a two-point calibration check since its replace-

ment on August 4, 1984. Consequently, the licensee had not verified

that the level instrument wobid respond properly over the test range.

Single point validations performed with the plastic tubing revealed

that often there was a wide discrepancy between the two readings. On

these occasions LI 35803 was aligned to agree with the plastic tube

level. These differences could have been due to the level instrument

tape slipping its track during a level change in the tank.

l

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4

.

1

(c) The plastic tubing sightglass may have been vented to atmosphere during

testing while the CST was pressurizeo by nitrogen to approximately

'

2 psig. Testing under this condition would generate a non-conserva-

tive error in the pump capacity test when the level in the CST tank

was lowered. The inspection team's concern that, in fact, the

plastic tubing sightglass was vented during testing is based upon

,

the following evidence: (1) interviews with operations personnel

, and instrument and controls (I&C) technicians revealed that in several

,

cases the sightglass was vented during normal plant operations,

(2) there was no procedural guidance or requirement for connectin ,

the plastic tubing sightglass to the CST during testing; and (3) g

data recorded for the level instrument validations indicated levels

! as high as 47 feet when the tank overflow line was at 43 feet 9 '

inches, suggesting that the tank was pressurized and the sightglass

vented when the data was recorded (the licensee stated that this

could also result from a difference in the zero reference for the two

measurementmethods). The surveillance records reviewed by the team

were ambiguous regarding the status of the sightglass or even if

the sightglass was used instead of LI 35803 as the measurement device

for the AFW flow tests.

The inspection team identified the potential calibration problems with

, LI 35803 to the licensee on January 13, 1987. Subsequently, the licensee

issued Licensee Event Report (LER) 87-05 to confirm the team's concern and.

further identified problems with correcting the CST level change for

miscellaneous flows during testing. The issues concerning the plastic

tubing sightglass and the validity of the 60 gpm recirculation flow were

identified to the licensee after issuance of LER 87-05. This item will

remain unresolved pending followup by the NRC (50-312/86-41-28).

(2) The acceptance criteria for the stroke times of identical air operated AFW

flow control valves, FV-20527 and FV-20528, were different. The licensee

was unable to justify this difference. The team was concerned that this

difference may represent a maintenance problem or an undocumented design

modification. This will be carried as an open item pending clarification

by the licensee (50-312/86-41-29).

.

'

(3) The following deficiencies were identified with the AFW surveillance

I

procedures:

'T

(a) Procedure SP 210.01A failed to check the backseat of AFW pump discharge

check valve FWS-048. The procedure incorrectly specified that the

, cross connect valve, HV-31827, be shut during the test lineup. With

this valve shut the downstream side of the check valve was isolated

from its pressure source, AFW pump P-318. This condition has existed

since September 22, 1985, when SP 210.01A, Revision 21, was approved.

In addition, licensee reviews of revisions 22 and 23 had not detected

this error.

(b)- SP 210.01A, Revision 23 and SP 210.01B, Revision 23 did not specify

i

fixed locations for bearing temperature measurements of the AFW pumps.

l This was contrary to the provisions of American Society of Mechanical

Engineer (ASME)Section XI, Article IWP-4310 and the NRC Safety

Evaluation Report (SER) of September 25, 1984, which granted relief

from certain IST requirements for pumps and valves specified by ASME

3-23

_ _ _ . _ _ _ _ _ _ . . _ _ . . _ __. - . -

  • 6

Section XI. Further, the failure to ensure fixed locations for these

temperature measurements invalidated the data with respect to its

value for providing trending information.

(c) SP 213.01, Revision 12, did not specify ALERT or ACTION RANGES for

pump differential pressure or pump flow for AFW pumps P-318 and P-319.

This did not meet the requirements of ASME Section X1, Article

IWP-3000. Additionally, failure to provide alert or action ranges

for suction pressure for pumps P-261, P272, P-291, P-318, P-319,

P-472 and P-482 was previously identified in NRC inspection report

50-312/85-23.

(4) Testing of the CST pressure relief valve, PSV-35804A, had apparently

exceeded the periodicity specified by SP 214.02. According to licensee

records, PSV-35804A was last tested on August 20, 1977, although SP 214.02

specified a required testing periodicity not to exceed five years.

The apparent failure by the licensee to develop and implement adequate procedures

for testing of the AFW system will remain unresolved pending followup by the NRC

(50-312/86-41-30).

3.4.3 4160 Vac System Testing

The following procedures, comprising the 4160 Vac system surveillance program,

were reviewed for technical adequacy:

  • SP 206.02A, " Refueling Interval Diesel Generator "A" SFAS Start Test,"

Revision 04

  • SP 206.028, " Refueling Interval Diesel Generator "B" SFAS Start Test,"

Revision 04

  • SP 206.07A, " Nuclear Services Buses 4A and 4A2 Monthly Voltage Protection

Surveillance," Revision 02

SP 206.07B, " Nuclear Services Buses 4B and 4B2 Monthly Voltage Protection

Surveillance," Revision 02

  • SP 206.08A, " Nuclear Services Bus 4A Voltage Protection Calibration  ;

Surveillance," Revision 01

  • SP 206.08B, " Nuclear Services Bus 4B Voltage Protection Calibration

Surveillance," Revision 01

EM.126A, " Refueling Testing and Maintenance of Diesel Generator "A","

Original

  • EM. 126B, " Refueling Testing and Maintenance of Diesel Generator "B","

Original

EM. 144, " Testing of Protective and Control Relays," Revision 09

  • EM. 177A, " Function Test of Nuclear Services Bus "A" and "A2" Unloading

Scheme," Revision 08

3-24

, .

' EM.1778, " Function Test of Nuclear Services Bus "B" and "B2" Unloading ;

. Scheme," Revision 09  ;

1

EM.196A, " Monthly Test of Nuclear Services Buses 4A and 4A2 Voltage l

Protection," Revision 04 i

EM.196B, " Monthly Test of Nuclear Services Buses 4B and 482 Voltage

Protection," Revision 03

EM. 198A, " Calibration and Testing of Nuclear Services Buses A and A2

Unloading and Voltage Protection," Revision 01

  • EM.198B, " Calibration and Testing of Nuclear Services Buses B and B2

Unloading and Voltage Protection," Revision 01

These procedures were determined to be adequate for demonstrating system func-

tionality and operability.

3.4.4 125 Vdc System Testing

A review of the 125 Vdc system surveillance program was performed. The

following concerns and comments were noted during the review:

(1) The team was concerned that the proposed surveillance procedures failed

to ensure that hattery cell temperature was above the minimum design

temperature specified in the battery sizing calculations. On January 13,

1907, the team observed battery room and cell temperatures below their

minimum design values for the NSEB batteries. The licensee was in the

process of upgrading their battery maintenance and surveillance procedures

to be in line with the industry recommendations contained in IEEE Standard

450, "Recoranended Practice for Maintenance Testing and Replacement of

Large Lead Acid Storage Batteries." This effort should correct the

concern identified above.

(2) The inspection team observed th61 the electrolyte level for most of the

cells of the BA battery in the auxiliary building were outside the specified

acceptance range. This is significant because the battery manufacturer

specified the battery cell capacity assuming the electrolyte level to be

at the full mark. The licensee's procedures required the electrolyte level

to be maintained within 1/8 inch of the full mark, but on January 13, 1987,

the team found numercus electrolyte levels that were 3/4 to 1 inch below

the full mark. A review of weekly battery surveillance records indicated

that this battery was consistently noted as having low electrolyte levels

since it was installed in July 1986. No nonconformance reports for this

condition had been issued prior to this inspection and no corrective

action was evident. In reponse to the team's concern, Occurrence

Description Report 87-93, was issued on January 23, 1987.

(3) The team reviewed annual maintenance reports for the auxiliary building

batteries as required by Maintenance Procedure EM.161, " Station Battery

Charger Routine." The teum found numerous incorrect entries in both the

required and actual values on the data sheets. These entries involved

current limits, over voltage relay setpoints, equalizer voltages, and

float voltage settings. Additionally, the applicable load design data

sheet (Drawing E1011, Sheet 93) referred to in the procedure did not

3-25

,

i

contain all the required values. The licensee had recently undertaken

a training program to ensure complete and accurate maintenance records.

Further, recently 1mplemented Procedure MAP 002, " Control of Maintenance

Activities," dated February 4,1987, requires a review of all completed

work packages by a maintenance engineer.

The inadequacies identified above regarding battery surveillance and testing

will remain unresolved pending followup by the NRC (50-312/86-41-31).

3.5 Operations and Training

In the area of operations, the inspection team evaluated the adequacy of

operator shift manning and experience; control of ongoing activities; normal,

casualty, and emergency operating procedures; and licensed operator training.

This evaluation focused on how each of these elements interfaced with the

operation of the eight selected systems reviewed during this inspection.

Additionally, the team assessed the adequacy of operations department activities

required to support plant restart. The team was unable to determine the

adequacy of the majority of the nonnal and casualty procedures because the

procedure revision effort was incomplete. Similarly, the team could not

assess restart simulator training effectiveness because the training had not

been performed, nor was the team able to walk through the selected systems to

assess operator knowledge because of the extensive modification activity in

progress.

3.5.1 Control Room Operations

The inspection team observed various aspects of control room operations. The

following observations were made during the course of the inspection:

(1) The inspection team observed two control room shift turnovers (January 7

and 9,1987) and considered them thorough and effective. Ongoing discussions

with control room operators throughout the period of the inspection revealed

that their overall level of knowledge and professionalism appeared adequate.

Access to the control room was effectively controlled.

(2) The team reviewed 10 MFW and AFW system safe clearance tag control sheets.

Safe clearances were administratively controlled by Procedure AP.4A, " Safe

Cleerance Procedure Danger Tags," Revision 5. Several deficiencies were

noted where the administrative requirements of Procedure AP.4A were not

properly implemented:

(a) The applicable piping and instrumentation diagram (P&ID) used to

establish the clearance boundary was not noted for clearance No.

31519.

(b) The date and time the tags were attached were not referenced for

clearance No. 31777.

(c) Partial clearance of tags was noted for clearance Nos. 31808 and 31889,

but the reasons for tag clearance were not listed in the " REMARKS"

section for the two clearances.

3-26

!

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, .

(c) Two different job supervisors for the clearances listed in (c) did

not sign the "RE-ISSUED T0" block after the clearances had been

re-issued following a partial clearance.  :

!

(e) Missing initials and component positions for both the " ATTACHED" and l

" REMOVED" sections of the Clearatice Request / Authorization Fonn were l

noted for Nos. 31465, 31808, and 31889.

Although the specific safe clearalice administrative deficiencies noted

above did not pose a threat to plant safety, the team was concerned that

the lack of attention to detail manifested by these deficiencies could

lead to situations where plant operators and supervisory personnel are

provided ambiguous or incorrect safety system status. In such situations,

,

operators may not respond appropriately during normal or off-normal

evolutions, thereby resulting in conditions that could be adverse to safe

plant operations.

(3) A review of the Abnormal Tag System maintained in the control room was

conducted by the team. These tags were issued and maintained in accordance

with Procedure AP.26, " Abnormal Tag Procedure," Revision 12. Several

weaknesses were observed with the implementation of this procedure:

(a) Approximately 60 abnormal tags were greater than one year old at the

time of the inspection and required a nonconformance report (NCR)

to be issued against them. Of these 60 tags, approximately one-third

did not have an NCR written against them. AP.26 required writing a

NCR to provide an administrative method for the plant nuclear engineering

department to determine if the temporary plant modification should be

made permanent. The inspection team was concerned that the failure

to issue the required NCRs reflected not only a lack of procedure

compliance but also a potential for allowing minor plant modifications

to occur without plant engineering involvement.

(b) Contrary to the provision of AP.26 which prohibit using abnormal

tags to implement setpoint changes, two cases were noted where

abnormal tags were used to change M0V torque switch settings. This

was an additional example of an insufficient level of plant

engineering involvement in determining the adequacy of a change to

plant systems or system equipment components.

(c) Several instances were observed in which monthly reviews required by

AP.26 had not been documented or performed, particularly by mechanical

maintenance and the operations department.

(d) System quality assurance (QA) class was not designated for several

tags as required by AP.26. This is significant because all QA Class

1 system abnonnal tags require the approval ci~ the Plant Review

Committee (PRC) within one working day after the tag is issued.

(4) The. Information Sticker Log, administered by Special Order 86-35, was

instituted as part of the corrective action following an incident in

November 1986 where a bank of pressurizer heaters were burned up because

operators relied on instruments that were out of service. The purpose

of this log was to establish controls for hanging information stickers

-

3-27

. i

dnd tracking the status of system instrumentation and components. The

team found three weaknesses related to this process.

(a) Two stickers were still hanging even though they had been cleared

from the log several weeks before.

(b) Four stickers did not have the associated work request number listed

in the' log.

(c) No monthly audit, as required by the governing procedure (Speciel

Order 86-35), had been conducted since the log's inception in

November 1986.

Based on the examples discussed above regarding administrative deficiencies

in the safe clearance tag system, the abnormal tag system, and the information

sticker log, the team concluded that the Rancho Seco operations personnel did

not always exhibit the requisite attention to detail that would ensure adequate

control of plant and system status. The resolution of these administrative

weaknesses will remain unresolved pending followup by the NRC (50-312/86-41-32).

3.5.2 Operating Procedures

The Operations Department had a major program in progress to upgrade the

operating, casualty, annuncidtor, and emergency operating procedures (EOPs).

A full-time procedure writing staff of approximately 10 licensed operators

had been supporting this effort. The team could not assess the overall adequacy

of the upgraded procedures because many selected procedures had yet to be

rewritten or were in draft form at the time of the inspection. Delays in

procedure revisions were attributable primarily to incomplete modification

work. However, the inspection team reviewed in detail Operating Procedure

A.51, "Auxilidry Feedwater System," Revision 31 and draft Revision 32, and

noted the following weaknesses:

(1) The AFW pump P-318 turbine overspeed alarm on the Interim Data Acquisition

Display System (IDADS) in the control room was not listed in either the

current or draft procedure A.51 as an indication of turbine overspeed.

(2) The AFW System Status Report (SSR), Revision 1, identified AFW pump motor

stort time limitation inconsistencies among A.51, Surveillance Procedure

SP 210.01, and the vendor technical manual. The team also found the AFW

system training manual guidance to be inconsistent. Discussions with

licensee personnel revealed that the licensee had contacted the vendor,

but could not resolve the issue because of a lack of sufficient information

from the vendor.

The adequacy of revised plant operating procedu m s, as well as the specific

Wedknesses noted above for A.51, will remain open pending followup by the NRC

(50-312/86-41-33). .

3.5.3 AFW Pump Runou*

The alarm indication used for a runoet condition of the AFW pumps provided

ambiguous information. Runout is a high flow, low pressure condition that

can lead to ext.essive vibration and pump degradation. The runout alarm, as

installed, will actuate on low discharge pressure only. During pump startup

3-28

.

- _

-

, .

when pressure is low, the alarm was intended to be bypassed with a time delay

until the pump reaches rated speed [Section 3.2.2(6)]. The annunciator

response procedure for the runout alarm instructed the operator to throttle

back on AFW flow on receiving this alarm without checking other indicaticns.

The inspection team was concerned that a condition could exist that the runout

alarm could be received if the AFW pumps failed to come up to rated speed

thereby indicating low discharge pressure but not pump runout. In this case,

the operator may take inappropriate corrective action by throttling back AFW

flow. The lack'of precise inoication of pump runout without having compensatory

procedural guidance and training will remain open pending followup by the NRC

(50-312/86-41-34).

3.5.4 Licensed Operator Training

The review of the licensee's restart licensed operator training program

focused primarily on training for the systems being modified; training on

priority-one operating, casualty, and emergency operating procedures (EOPs);

simulator training; and other training commitments identified in the Rancho

Seco Action Plan for Performance Improvement. In general, the team found that

there were sufficient training mechanisms in place to support the operations

department preparation for startup. The team was unable to evaluate the

implementation effectiveness of this training program, because: training on

revised AFW operating procedures and E0Ps had not been accomplished; no

simulator training had been performed; and not all of the modifications

training had been completed. During the inspection, the team developed two

Concerns.

(1) System training manuals have been in distribution throughout the plant-for

past several years. These manuals were not controlled, nor were they

maintained current by the training department. As a result, these manuals

did not, in many cases, reflect the as-built condition of the plant. Since

initial distribution, significant modifications to plant systems have

altered system configuration and operating parameters in many instances,

as evidenced by the recent modifications to the AFW and instrument air

systems. Even though much information in these manuals is no longer

dccurate, the inspection team noted that licensed operators, plant

engineers, and other site personnel routinely refer to them. The team

Wds Concerned that incorrect information obtained from these manuals

may guide plant personnel to erroneous conclusions or actions. At the

exit meeting the licensee indicated that the policy regarding the use of

these training manuals would be reviewed and appropriate action taken.

(2) The training department has established a program to ensure that operations

personnel receive the appropriate level of training on the large number of

operations department procedures that are being written or revised. In l

general, procedures that are undergoing minor revisions will be placed

into the Operator Reading Assignment Program, and new procedures or

procedures undergoing major revisions will either be placed into the

classroom training cycle or be " walked through" in the plant or at the

simulator. After reviewing the licensee's tentative list of procedures

j that require classroom training, the team noted that the following procedures

were undergoing major revisions but were not intended to be included in

the classroom training cycle:

3-29

<

_ _ . _ . _ , . _ . . -

. - . - -

' .  ;

,

.

A.58 "4.16 KV Electrical System," Revision 9

' A.59 "480 V Electrical System," Revision 22

A.61 "125 Volt DC System," Revision 8

A.62 "120 Volt AC System," Revision 9

4 A.73 " Reactor Non-Nuclear Instrument System," Revision 9

B.4 " Plant Shutdown and Cooldown," Revision 41

C.110 " Loss of 480 V Bus 3A1," Revision 2

C.112 " Loss of 480 V Bus 382," Revision 2

C.143 " Loss of 480V MCC S2El," Revision 6

The team was concerned that these procedure revisions may be too complex

to be adequately addressed by the Operator Reading Assignment Program.

The resolution of the training concerns discussed above will remain open pending

followup by the NRC (50-312/86-41-35).

,

3.6 Maintenance

.

l The inspection team reviewed the revised maintenance procedures and related

documentation for both preventive and corrective maintenance for the eight

! selected systems. The licensee's efforts for enhancing the reliability of

safety-related equipment for the selected systems were also reviewed, with

3

particular emphasis on the motor operated valve (MOV) refurbishment program.

4

3.6.1 Motor Operated Valve Overhaul and Refurbishment Program

i

The licensee has identified significant design and maintenance problems during

MOV refurbishment and testing. The team focused on the results to date on the

MOVs that are subject to the requirements of IE Bulletin 85-03, " Motor Operated

Valve Common Mode Failures During Plant Transients Due to Improper Switch

, Settings." The team considered the licensee's effort in this area to be note-

worthy. The scope of the original program has been expanded well beyond the

bulletin requirements to encompass all plant MOVs, a total of 173 valves.

However, the team was concerned with the nature of the licensee's M0V overhaul

dnd refurbj5hment fincings.

(1) As of January 13, 1987, 15 out of 20 valves subject to IE Bulletin 85-03

had faileo testing because of under/overthrusting conditions. An over-

thrust condition was defined as exceeding the allowable limits for the

valve or operator in either the open or closed direction. Within the valve

operator, individual limits could also be exceeded for the motor or spring

pack. Overall, 38 out of 69 MOVs tested failed to meet the design thrust

values. The licensee considered any MOV assembly that exceeded the valve

or operator limits to be inoperable as outlined in Sacramento Municipal

Utility District (SMUD) letter JEW 86-667 issued in October 1986. Final

resolution of the MOV thrusting issue may require MOV spring pack replace-

ment, different operator gearing, complete MOV assembly replacement, or

, valve replacement. Each failed MOV must be handled on a case-by-case basis

i because of the unique variables in its plant application. In the interim,

l M0V. assemblies that have been categorized as underthrusting have had the

torque switch set at the highest possible setting, pending final resolution.

Conversely, MOV assemblies classified as overthrusting have had the torque

switch set at the lowest value.

1

1

3-30

f

- - - , , , - -r- - , . - , -m. -,,- ~ , - - - - - - - - - -, ..m. -~w - --w-- , - - - , - - - - ,

- .- -- . - -- -_ - - - .

!

.

l b

(2) During testing the licensee identified four DC powered MOVs, including

FV-30801 (steam admission valve to P-318), with undersized electrical

cabling. These MOVs had been converted from ac power to de power during

this outage by ECN A 5415U. However, because of apparent inadequate-design

review, the electrical cabling from the motor control center to the MOV

.

l'

motor was not evaluated for postulated accident conditions at minimum

available voltage.

>

Following the conclusion of the onsite inspection, the licensee documented the i

MOV operability problems that have resulted from the expanded MOV refurbishment

and overhaul program in Licensee Event Report (LER)87-006, dated February 17,

1987.

3.6.2 Maintenance Procedures

The inspection team reviewed the following technical procedures for repair of

plant equipment:

i

l

EM.117, "Limitorque Maintenance," Revision 8

EM.117A, " Testing of Limitorque Motor Operated Valves Using M0 VATS "

,

Revision 1

- M.103, " Valve Inspection and Maintenance," Revision 1

4 M.22, " Auxiliary Feed Pumps and Turbine," Revision 4

M.114 " Maintenance Cleanliness Control," Revision 6

' M.115, "Limitorque Valve Actuator SMB00, and SMB000 Corrective

Maintenance Procedure," Original and Revision 1

,

M.116, "Limitorque Valve Actuator SMB-0, SMB-1, 2, 3, 4 Corrective

Maintenance Procedure," Original

] " Control of Mechanical Measuring Devices," Revision 2

! MT.013,

In general, the procedures appeared to be technically adequate. However, the

'

following two weaknesses were noted:

(1) MOVs with a relatively fast stroke time use a motor brake to overcome

stem inertid after the valve has been stroked, thus preventing the valve

disc from becoming wedged in the main seat or on the back seat. However,

no preventive maintenance procedures or requirements had been established

to periodically inspect the brake rotating friction disc for excessive

wear. The brake vendor, Dings Company, specified a rotating friction

,

disc thickness of 0.180 to 0.190 inch. During the inspection, the licensee

'

revised their M0V corrective maintenance procedures to include preventive

maintenance activities for the brakes. However, Procedure M.115

"Limitorque Valve Actuator SMB 00, and SMB 000 Refurbishment and Corrective

'

Maintenance Procedures," Revision 1, stated that the rotating friction

disc should be replaced if the disc was not 0.080 to 0.190 inch thick.

Additionally, M.115 did not include or reference Vendor Instruction

Bulletin Number 4603 that specified rotating friction disk replacement

criteria of one-sixteenth inch total wear. Failure of the motor brake

i could result in jamming the valve disc in its seat, thus preventing further

i valve manipulation.

1 (2) Specific maintenance procedures applicable to safety-related air-operated

t

valves (e.g., FV-20527, FV-20528, FV-20575, and FV-20576) had not been

ceveloped. The adequacy of air-operated valve maintenance procedures was

of particular interest to the inspection team in light of the December 26,

3-31

.

=g-y. e-w- mi -ww<=.----- --r----x- - , - . - -=--rt-" -w "MP-*B'"+" 4 - + " - ' " *

. ;

1985 overcooling event. During that event, the manual operator for the

A AFW (ICS) air-operated flow control valve (FV-20527) failed, in part,

because the hanawheel was improperly mounted.

The weaknesses noted with corrective maintenance procedure M.115 and the lock

of maintenance proceaures for air-operated valves will remain an unresolved

item pending followup by the NRC (50-312/86-41-36).

3.6.3 Mainte. nance Program Administration

The team reviewed the licensee's program for administrative control of

preventive and corrective maintenance. This review included maintenance

schedules, documentation of work accomplished, equipment history, and trending

of equipment maintenance. The following procedures were reviewed:

AP.3, " Work Requests," Revision 35

AP.33, " Calibration and Control of Test Equipment," Revision

AP.42, " Maintenance Information Management System," Revision 5

AP.46, " Nuclear Operations Technical Manual Control Procedure,"

Revision 3

AP.51, " Maintenance Instructions " Original

AP.301, " Maintenance Procedure Description and Format," Revision 3

AP.650, " Preventive Maintenance Program," Revision 5

AP 700, " Nuclear Operations Training Program," Revision 4

These procedures were found to be generally adequate and were considered to

provide effective overall administrative controls for plant maintenance. The

team reviewed the implementation of these procedures on approximately 90 work

requests and identifieo the following concerns:

(1) Trending analysis, as described in paragraph 5.7.2 of AP.650, had not

been implemt.nted. AP.650 required that trend analysis generally consist

of a graphic display of parameter (s) plotted versus time to provide a

visual image of any rapid change or a slow gradual trend that may occur.

The licensee's current program for trending Preventive Maintenance Program

data information consisted only of a record of maintenonce measurement

data in columnar format. The licensee stated that implementation of the

trend analysis program, as defined by AP.650, had been postponed until

new computer software was obtained. At the time of this inspection, no

firm commitment date for software acquisition had been established.

Implementation of the trend analysis program will remain an open item

pending followup inspection (50-312/86-41-37).

(2) Equipment history, as described in paragraph 5.7.1 of AP.650 and AP.42,

" Maintenance Information Management System (MIMS)," was divided between

two separate files; preventive maintenance (PM) records and corrective

maintenonce records. Completed PM work requests were entered in MIMS and

functioned as part of the equipment history file. Selected information

from completed corrective maintenance work requests was also entered into

MIMS. The team reviewed the equipnent history files for 12 selected

safety-related components and found the information to be minimally

acceptable. For example, FV-30801 (steam admission valve to the

turbine-driven AFW pump P-318) equipment history contained no information

on corrective or preventive maintenance since 1977. The team was concerned

that recurring equipment problems over a period of a few years that would

3-32

_ _ _ - ._ _ _ _ _ _ _ _ _ . _ _ _ . . __.

s ..

be indicative of an undesirable trend or generic component deficiency could

,

go undetected if the equipment history files were incomplete.

AP.650, paragraph 5.3.2, described the criteria for PM selection and

, frequency, including equipment. history reviews. During the inspection

period, the licensee was in the process of revalidating the basis for

preventive maintenance, particularly vendor recommendations. For example,

the mechanical maintenance department was reviewing all controlled vendor

mdnuals and equipment histories to ensure that the scope of the PM program

was adequate. The team felt that this was a comprehensive and sound

! approach for validating the PM basis; however, a review of existing

equipment history records would provide only limited information

concerning recurring equipment failures. Because the equipment history

a records did not reflect the full spectrum of maintenance activities cver

the life of the plant, the benefits of a comprehensive records review

in revalidating preventive maintenance requirements were diminished.

Interviews with licensee management revealed that they were aware of the

problem and had initiated maintenance technician lectures on the importance

of equipment history and information required for work requests.

(3) The responsibility for determining adequate post maintenance testing was

not clearly established by AP.650 for PM work requests. Revision 35 to

AP.3, " Work Requests," assigned the responsibility for determining adequate

i post maintenance testing to the planning department for corrective

maintenance work requests. Prior to this procedure revision, responsi-

] bility for post maintenance testing rested principally with the maintenance

,

foreman. During the inspection peroid the licensee was developing a

detailed procedure for use by planning department retest engineers for

ensuring adequate post maintenance testing for all maintenance activities. -

3.7 Quality Programs

The inspection of quality programs included a review of quality assurance (QA)

audits, QA surveillances, and corrective action programs. The following Quality

Control Instructions (QCI), Administrative Procedures (AP) and Quality Assurance

Implementing Procedures (QAIP) were reviewed during this inspection:

'

QCI No. 1, " Processing of Nonconforming Reports - NCR," Revision 5

l QCI No. 2, "SMUD Nuclear Operations Quality Assurance Audit Program,"

Revision 2

QCI No. 5. " Safety Review of Proposed Facility Changes," Revision 2

QCI No. 16, " Trend Analysis Program," Draft

AP 22, " Occurrence Description Reports (0DRs) Reporting and Resolution,"

Revision 12 ,

,

QAIP No.1, " Quality Assurance Audit Procedure," Revision 6

QAIP No. 2, " Quality Assurance Surveillance Procedure," Revision 6

i QAIP No. 6 " Surveillance Oriented QA Surveillance Program (500AP),"

Revision 3

'

3-33

l

1

- -. . _ - - - . _

-.- _ . - .

.,- . - _ . - . -- . _

- - - .._

. <

The licensee was making significant improvements in the various quality programs,

including major revisions to QA procedures, staff restructuring, and an increase

in QA staff size. However, significant deficiencies were identified with the

Operations QA Program because the planning improvements were not implemented ,

at the time of the inspection. These improvements were delayed as a result of )

QA involvement with the SRTP process and, consequently, the program at the time '

of the inspection was not ready to support an operating plant.

3.7.1 QA Audit Program

An independent audit of the QA program, performed in November 1986 by a

contractor to the licensee, identified significant problems regarding missed

audits, insufficient auditor training, inadequate corrective actions, and

inconsistent application of the audit process within the SMUD organization.

Corrective actions were in progress for these audit findings and were scheduled

to be implemented prior to restart. The team had the following additional

observations about the audit program-

(1) The licensee's QA audit tracking program provided the status of all

required audits and identified that several audits had exceeded their

periodicities as identified in procedure QCI-2 and that some audit reports

were not issued until four months after audit completion. Interviews

with audit personnel revealed that these delays were due to the large

SRTP effort and the changing audit report formats being implemented at

the time of the inspection.

(2) The licensee was developing a more technical approach toward auditing.

These audits were termed " vertical audits" and were intended to be

performed by a team that would review all the applicable QA programmatic

aspects associated with a safety system. Four of these " vertical audits"

were scheduled to be conducted prior to startup to provide additional

assurance that plant safety systems were ready to support operation. The

licensee provided the NRC inspection team a draft outline of the audit

scope and objectives. On the basis of the outline, the team determined

that the audit method appeared to be innovative and capable of having a

positive effect on safety.

(3) In some cases, corrective actions associated with past audits appeared to

be ineffective. Audit findings were considered closed when an adequate

response was received that represented a commitment by the audited

organization to correct the problem. The audited organization was not

held accountable for implementing the action. Further, these responses

were often late and did not provide a schedule for implementing the

corrective actions. The commitments were tracked as open items and

received QA followup but no action was taken to ensure that the audited

organization was correcting identified problems. At the time of the

inspection, the QA followup list ,1dentified valid audit findings from

1982 that had not been corrected.

(4) The Management Safety Review Comittee reviewed the audit reports when

published and the audit report cover page after audit findings were closed

by QA. This cover page referenced the correspondence that documented

finding closure but did not summarize what was done to correct the finding.

Audit findings of ten were not closed for several months and, without

further information or supporting documentation for reference, this method

3-34

4

-- - - ,-

- ._ - - - -

b .

of closecut review seemed superficial. At the time of the inspection, the

licensee was in the process of revising their reporting format, tracking

mechanism, and closecut requirements for audit findings, which may improve

this process.

The deficiencies in the QA audit program will remain open pending followup

by the NRC (50-312/86-41-38).

3.7.2 QA Sur'veillance Program

The QA surveillence program was intended to complement the QA audit program

by providing a review of on-going plant activities. However, the team

identified the following deficiencies with the QA surveillance program

procedures and implementation which appeared to detract from this purpose:

(1) Procedure QAIP No. 6 did not require or suggest the use of a checklist

to perform QA surveillance activities. Consequently there was no

inaication that a checklist was used for any of the approximately 30

surveillance reports reviewed during this inspection.

(2) The corrective action mechanism normally used to resolve QA surveillance

findings was considered weak. A review of approximately 30 QA surveillance

.

reports revealed that most of the deficiencies identified were classified

only for QA follow-up activities. As a result, the responsible plant

'

organization was not held accountable and the action taken to correct

the deficiency end to prevent recurrence was not documented. As an

example, QA Surveillance Report 491, conducted in October 1985, identified

several errors on a piping & instrument diagram (P&ID) M-580, " Main Lube

011." This drawing showed components that did not exist in the system

and other components actually installed in the system were not shown.

A note on this surveillance report indicated that QA wculd followup on

these ceficiencies. At the time of this inspection, these deficiencies

were not corrected even though this P&ID was revised in October 1986

and surveillance report 491 was signed off as closed. This issue was still

being carried in the MFW SSR as Problem 22.

(3) ho evidence was found of trending the issues generated from these

surveillonces. Interviews with QA management personnel revealed that

there was no working file of completed surveillance reports available l

in the QA offices, thus making it difficult for licensee managenent to i

review previous reports. l

The licensee statea that the QA surveillance program was being revised to

incorporate these issues. This item will be held open pending followup by

the NRC (50-312/86-41-39).

3.7.3 Corrective Action Program

In addition to the corrective action deficiencies regarding QA audits and

surveillances previously discussed in Sections 3.7.1 and 3.7.2, the following

additional weaknesses were noted in the licensee's corrective action program:

(1) The licensee did not appear to have a mechanism to uniformly ensure that

significant conditions adverse to quality would be reported to the appro-

priate level of management. This oppears to be contrary to 10 CFR 50,

3-35

_ . - . _ .

.. ___

- - - - - - -. - - _.

. 4

Appendix B, Criterion XVI. In some cases, such as reportable events, the

Occurrence Description Report process would escalate management attention

to meet reportability requirements. However, there did not appear to be

any systematic method to identify from all sources problems that could be

considered significant conditions adverse to quality. At the time of the

inspection, the licensee had issued a draft procedure for review which

dddresSed this problem.

(2) The licensee's trending program did not attempt to relate deficiencies to

The QA Department issued a monthly "NUMARC Trend Report,"

'

a coninon cause.

which looked at performance indicators, but did not analyze for the root

causes underlying the observed deficiencies or identify similar findings 1

from different sources. An example of this lack of trending and inadequate

corrective actions was that, since 1984, two QA Audit Reports (0-733 and

0-812), four QA Surveillance Reports (163,165,163A and 491), and the

LRS management report of November 1984 have identified problems with the

control of drawings at the station. However, the inspection team still

found significant problems with the drawing control program during this

inspection (see Section 3.3.3).

(3) The teani was concerned about the licensee's re' ponse s to NRC inspection

report findings. At the time of the inspection there were nearly 300

<

open or unresolved items that were in the process of being closed out by

i the licensee, some of which were over 2 years old. Additionally, NRC I

inspection report 50-312/85-23 identified significant problems with the

in-service test program at Rancho Seco in May 1985. The inspection team

identified similar problems with different systems during this inspection

(see Section 3.4).

, The inspection team concluded that the corrective action programs at Rancho

i Secu had not been managed effectively in the past and that adequate management

j attention was still not being applied to this area at the time of the inspection.

! The lock of effectiveness of the licensee's corrective action program will

remain open pending followup by the NRC (50-312/86-41-40).

4

3.8 Restart Organization and Management

The inspection team evaluated the licensee's existing restart implementation

orgariization and the planning and progress toward achieving the nuclear

organization which will exist at restart. The focus of the inspection was on

the followup of previously identified management problems, the planning and

mdnagensent processes initiated to accomplish required actions related to

restart, and management programs designed to change previous practices at

Rancho Seco.

.

!

3.8.1 Plant Performance and Management Improvement Program

'

'

The inspection team evaluated the Plant Performance and Management Improvement

Program (PP&MIP) to determine its overall integrity, completeness of input, and

consistency of operation. The PP&MIP was implemented by means of Rancho Seco-

Quality Control Instruction 12 (QCI-12) which set forth a phased approach

to performance improvement and restart of the Rancho Seco plant and controlled

,

the major steps in the process: investigation, validation, approval, implemen-

l tation, and closure. The investigation phase provided for a variety of inputs

into the QCI-12 process, inclucing NUREG-1195, " Loss of Integrated Control

i

t

j 3-36

,

e,- nnn--,--- - - - - w e,- c--. .- , ,-, ,~,----n-w- -- --~a n, e , -- . - - ~ --n w--- -+e----, - -~ ,

_ .. __ _- . _ . ___ _ __ . _ _ .- __ __ _

, .

System Power and Overcooling Transient at Rancho Seco on December 26, 1985,"

- the B&W Owners Group Safety and Performance Improvement Program (SPIP), staff

'

interviews, and systems engineer recommendations and other relevant sources.

During the validation phase, each valid restart item was assigned a priority and

was included in an appropriate System Status Report (SSR). In the approval phase,

i

a management-level board, the Performance Analysis Group, reviewed each item

i in each SSR and assigned action to ensure implementation, testing and closure.

i The end product of the QCI-12 process is the restart System Review and Test

Program (SRTP) which is intended to verify, with emphasis on system test, that-

the actions taken will be sufficient for the Rancho Seco plant to return to

i safe operation.

'

As a result of this review, the team identified three areas of concern regarding

the PP&MIP:

(1) Existing open items from the LRS Management Appraisal Report were not

included in the PP&MIP and the 001-12 process. This report, issued in

!

November 1984, represents a comprehensive management appraisal of SMUD

! and the nucleer organization at Rancho Seco by LRS Consultants, a

i licensee contractor. The LRS Report was specifically identified as

d required input to the PP&MIP on Page 1-8 of the " Rancho Seco Action

Plan for Performance Improvement," Amendment II. This item was discussed

l

with licensee management who agreed to review the open recommendations

! in the LRS Report for possible inclusion into the PP&MIP. This will

remain an open item pending followup by the NRC (50-312/86-41-41).

I

I (2) Although the problem identification phase of the QCI-12 process seemed

j to be generally adequate and apparently functioned with integrity, i

weaknesses were uncovered in the validation and approval phases. As

j discussed in Sections 3.1, 3.2, and 3.3 of this report, the team

identified several examples of a lack of engineering and operating detail ,

! and depth in the QCI-12 review of selected safety systems. At the exit t

j meeting on February 12, 1987, the licensee was informed that, as a result

'

of the apparent weaknesses relating to operating and engineering depth and

l

oetail, additional measures to revalidate the adequacy of those reviews i

l would be appropriate. The licensee shared the same concern and agreed to '

i assess the need for further action. This item will remain open pending

i followup by the NRC (50-312/86-41-42). ,

I

l (3) The SSRs did not appear to be properly controlled considering their use

j as a basis for the NRC Safety Evaluation Report (SER) for restart

i authorization. At the beginning of the inspection, the licensee's '

practices allowed changes to the SSRs after their review by the NRC

without notifying the NRC. The team considered the SSRs to be commitments

j to the NRC for problem resolution and testing once they were reviewed,

4

and, therefore, any subsequent changes to the SSRs should be controlled.

d

During the inspection, the licensee developed a process for controlling I

! the SSRs and keeping the NRC informed of all changes. This item will

l

remain open pending NRC review of the final procedures implementing the

SSR_ control process (50-312/86-41-43).

1

1

3.8.2 Restart Priority Review Team

The efforts of the QCI-12 Priority Review Team (PRT) were reviewed as part of

the assessment of the integrity of the QCI-12 process. The PRT wcs chartered

i 3-37

i

>

--

. ;

by the Restart Implementation Manager (RIM) to review the engineering-related

Priority 1 items. The PRT was composed of operators who considered each item

in the strict context of the QCI-12 priority criteria. They reviewed 205

Priority 1 items; of these, 92 were found to meet the criteria for Priority 1,

44 for Priority 2, and 35 for Priority 3. Additionally, 34 items were

determined not to meet the criteria for Priority 1, 2, or 3. These findings

were forwarded to the Performance Analysis Group (PAG) with a recommendation

to effect the priority changes. Of the Priority 1 items recommended for

downgrading, the PAG accepted the recommendation of the PRT in 61 cases, but

retained the original priority in 47 cases. The PRT effort represented an

attempt to reduce the number of engineering changes and modifications required

for restart from an operations point of view. The team considered that the

hesitancy of the PAG to concur in all cases was an indication of the integrity

of the QCI-12 process.

3.8.3 "Make It Happen" Program

The team evaluated the "Make It Happen" Program by means of interviews and

document review to determine program content and planning status as it related

to the restart effort. This program was attempting to effect a shift in Rancho

Seco " culture" from one of non-commitment and failure toward one of success and

commitment to a safe and successful startup. The program was intended to

contribute to higher productivity, quality, niorale, and safety by means of

employee and management training, individual coaching, and employee involvement.

Team interviews and document review revealed the following:

1

(1) The program was based upon similar successful attempts to change culture

and behavior in other organizations.

(2) The individuals responsible for the program at the working level had the

appropriate background, training, and experience.

(3) The program had the backing and involvement of plant management up to the

highest level, including the Deputy General Manager.

The team considered that the concept and planning for the "Make It Happen"

Progrcm were satisfactory but that it was too early to judge its progress or

its effectiveness.

3.8.4 Restart Organization and Transition Planning

The team evaluated the existing restart implementation organization and the

progress and planning toward putting a final SMUD nuclear organization in

place. The team was not confident that the planning and progress of the

transition supported the scheduled restart date. The goal was to have this

final organization approved, in place, and manned by May 1987. This goal

appeared unrealistic to the team for the following reasons:

l

'

(1) The existing restart implementation organization contained significant

vacancies. Of seven key management positions, two (Quality Assurance and

Licensing) were not filled by SMUD employees as the principal or deputy.

This seemed to undermine the concept that SMUD managers would understudy

l

l 3-38

l

. _

._

. - - -- -_.

i .

experienced contractor personnel as the principal or deputy during restart

implementation. The licensee expected that these positions would be filled

l by April 1, 1987.

(2) Implementation of the final nuclear organization has been delayed. The

transition schedule indicated that this organization would be in place by

February 1,1987. The licensee anticipated that it would be in effect on

April 1,1987.

(3) There appeared to be no detailed plan for replacing contractor personnel l

with SMUD employees. The utility made extensive use of contract personnel

in areas critical to restart and the team was concerned that, as the

transition from contractor personnel to utility personnel occurred, system

technical intricacies may be overlooked. Due to the extensive contractor

presence at the site, the average tenure of the systems engineers, design

engineers and QA personnel was comparatively short. This in itself is

not a problem provided turnover of duties is sufficiently detailed and

thorough. The team was particularly concerned that system engineers were

less knowledgeable about their assigned systems than what has been

observed at other utilities. Because these personnel have significant

responsibilities for coordinating the SRTP and modification activities

' for restart, they should be trained and knowledgeable on system design

and testing issues.

(4) The team developed a concern about the current level of at-power operating

experience held by many of the licensed operators. A review of licensed

operator staffing revealed that opproximately 50 percent of the licensed

operators had less than one year of at-power operations experience, and  ;

that the current class of licensed operator trainees has never seen the

plant at power during their training program. The team was concerned that

additional experience may be necessary to staff all of the shifts during

the return tu power and subsequent at-power operations, but could not

assess this at the time of the inspection because much of the restart

training, particularly simulator training, had not been accomplished.

After the exit meeting, the licensee provided the team with information

.

regardi.1g their Operations Advisor Program. This program will provide

experienced contractor personnel, all of whom previously held senior

reactor operator licenses on B&W commercial nuclear power plants, as

on shift advisors. If effectively implemen'.ed, this program would mitig6te

the inspection team's concerns regarding the experience level of licensed

operators.

i In the opinion of the team, the factors above complicate the licensee's efforts

to have a complete and mature management team in place by the scheduled restart

dote. The capability of the SMUD nuclear organization to support the schedule

,

restart date will remain an open item pending followup by the NRC

(50-312/86-41-44).

4

,

4

'

3-39

!

l

. . _ - - - . = - , - - - - . - - . . _ _ - - . _ _ . _ . . . _ _ - - _ __ . - - _ - - _ - - - - . _ _ . - _

- - - - . _ _ . _ _ _ _ ,, N--_m _ ----N-__,____

e

I

t

I

_ _

l

l

\ .

4. UNRESOLVED ITEMS l

'

Unresolved items are matters about which more information is required in order

to ascertain whether they are acceptable items, violations, or deviations.

Unresolved items identified during this inspection are discussed in detail l

in Section 3 and summarized below:

Item No. Subject Section

86-41-06 Instrument Air System Modifications 3.1.2

86-41-09 EFIC System 10 CFR 50.59 Analysis 3.1.4(2)

86-41-15 Condensate Storage Tank Overpressure and 3.2.1(2)

Underpressure Protection

86-41-16 DC Circuit Breaker Sizing Calculation 3.2.2(1)

'

86-41-17 Battery Sizing Calculations 3.2.2(2)

86-41-19 AC Circuit Breaker Sizing Calculation 3.2.2(4)

86-41-20 Underrated DC Cables 3.2.2(5)

86-41-21 IDADS Computer Alarm Modifications 3.2.2(6)

86-41-24 Plant Drawing Contrul 3.3.3

86-41-25 Design Calculations 3.3.4

86-41-26 IST Program Approval 3.4.1(1)

86-41-27 Surveillance and Inservice Test Data Trending 3.4.1(2)

86-41-28 AFW Pump Capacity Tests 3.4.2(1)

86-41-30 AFW Surveillance Test Prucedures 3.4.2(3)

'

86-41-31 DC System Surveillance Testing 3.4.4

,

86-41-32 Administrative Control of Plant Systems 3.5.1

E6-41-30 Corrective Maintenance Procedures 3.6.2

!

'

.

4-1

1

I e

5. MANAGEMENT EXIT MEETING

The inspection team leader and selected inspectors conducted an interim exit

with licensee management on January 15, 1987 to provide a summary of issues

,

identified during the first onsite inspection period. A final exit meeting

was conducted at the conclusion of the onsite inspection on February 12, 1987

at the Rancho Seco Nuclear Generating Station. The licensee's representatives

at this final exit meeting are identified in Appendix A. Mr. B. Faulkenberry,

Deputy Regional Administrator, Region V, represented NRC management at this

meeting. The scope of the inspection was discusseo and the licensee was

informed that the inspection would continue with further in-office data review

and analysis by team members. The licensee was informed that some of the

'

.

observations could become potential enforcenent findings. The observations

were presented for each area inspected, and team members responded to questions

from the licensee's representatives.

5-1

J

-

e _ __ _

\ '

.

'

APPENDIX A

.

PERSONS CONTACTED

The following is a list of persons contacted during this inspection. There

were other technical and administrative personnel who also were contacted.

All personnel listed are SMUD employees.

P. Anderson - Electrical Maintenance Engineer

+D. Army -

Manager, Maintenance

G. Aron - Systems Engineer, Auxiliary Systems

+*R. Ashley - Manager, Licensing

S. Bagga - I&C Engineer

M. Basu - Electrical Group Leader

+S. Batch - Testing Coordinator

B. Beebe - NSS Principal I&C Engineer

T. Beeves - I&C Engineer

l. J. Briskin -

Staff Assistant

A. Brown - Superintendent, I&C Maintenance .

  • J. Bufis - Assistant Director, Systems Review and Test Program

R. Columbo - Operations Supervisor

D. Compton - Licensing Engineer

  • B. Conklin - Lead Engineer, Steam Plant Systems Review and Test Program

+*G. Cranston - Manager, Nuclear Engineering

  • B. Croley - Plant Manager (incoming)

R. Crosby - Management Specialist

R. Daniels - Supervisor, Electrical Engineering

+*J. Field - Director, Systems Review and Test Program

L. Fossum -

Deputy Manager, Implementation

+F. Gowers - Deputy Manager, Training

'

J. Hayes - Electrical Engineer

M. Heronimous - Operations Shift Supervisor

J. Irwin -

I&C Maintenance

S. Jacobs - Electrical Engineer

  • J. Janus - Staff Assistant

P. Johnson - Plant Utilities Principal I&C Engineer

T. Khan - Supervisor, Mechanical Systems i

+F. Kellie - Superintendent, Radiological Protection

  • J. King - Systems Engineer, Steam Plant

+S. Knight - Manager, Quality Assurance

+J. Lingenfelte- - Assistant Director, Systems Review and Test Program

C. Linkhart - Superintendent, Electrical Maintenance

C. Linquist - I&C Maintenance Supervisor

+J. McColligan - Inspection Coordinator

D. McGrath - Mechanical Maintenance

D. Micherone - Electrical Engineer

S. Miller - Deputy Supervising Electrical Engineer

R. Nakao - Licensing Engineer

R. Pate - I&C Engineer

+*K. Perkins - Restart Implementation Manager

  • D. Poole - Nuclear Plant Manager (outgoing)

<

M. Price - Superintendent, Mechanical Maintenance

A-1

4

, - . n -- . . , - _ _ . -

c ,_ , .-.-,y_., ,._, r -- . , - , ., .

  • l
  • J. Rockley - Assistant Test Director, Systems Review and Test Program

S. Redeker - Manager, Operations Department .

T. Robertson - Plant Modifications Manager

G. Roy - Staff Assistant

F. Sheehan - Electrical Group Leader

+J. Shetler - Manager, Implementation

+S. Siebenaler - Systems Engineer, Steam Plant

T. Singh - Electrical Group Leader

  • E. Stockman - Systems Engineer, 4160 Vac

N. Thibodaux - Surveillance Specialist

F. Thompson - Supervisor, Technical Training

D. Tipton - Superintendent, Project / Procedure Operations

A. Tuduty - Management Specialist

P. Turner - Manager, Training

+J. Vinquist - Executive Assistant

+*J. Ward - Deputy General Manager, Nuclear

R. Weber - Management Assistant

J. Wheeler - Senior Electrical Maintenance Engineer

  • L. Wittrup - Systems Engineer, EFIC

J. Zott - Fire Protection Principal Engineer

.

\

  • Personnel attending January 15, 1987 exit meeting.

+ Personnel attending February 12, 1987 exit meeting.

A-2

l

l

. _ - - . _ _ . - . . . , - . ., - -- , - , . - . . - - . .

t ' .

APPENDIX B

.

SYSTEMS DESIGN DOCUMENTS REVIEWED

GENERAL ARRANGEMENT DRAWINGS

DRAWING NO. TITLE REVISION

E6.02.1A-41 P.C.B. Internals 0

E7.01-9-51 Plan Arrangement 480V Bus Duct --

ONE LINE DIAGRAMS

DRAWING NO. TITLE REVISION

SK-E132-2 125 VDC and 120 VAC Distribution System N/A

E-108, 120 VAC System Panels 7

Sheet 12

E-107, 125V DC System Panels 4

Sheet 2

E-105, One Line Diagram

Sheet 1 480 Volt System 7

" " "

"

2 7

" 5

36 480 L.C. SWGR S3A2

"

14 460 Volt System 21

"

37 480 L.C. SKGR S3 B2 3

"

8 480 Volt System 26

" " " "

10

8A

" " " "

2

25

" " " "

27 5

" " "

"

31 0

" " "

"

9 24

" " " "

9

9A

" " " "

26 3

" " " " 3

28

" " " "

0

32

E-104, One Line Diagram

Sheet 4 4160 Volt System 6 i

'

" " " "

10

. 1

" " " "

2 9

Sheet 6 4160 Volt Switchgear 54A2 2

Sheet 3 4160 Volt System 11

Sheet 7 4160 Volt Switchgear S4B2 3

B-1

-- ... , . . . -

l

i

1

. -

i

l

l

P&I DIAGRAM

REVISION  !

DRAWING NO. TITLE

M-552 Htg., Vent., & Air Condition Systems 19

M-532 Steam Generator Svstem 23

M-532 Steam Generator System 6

Sheet 1

M-533 High Pressure Feedwater 8

Sheet 3 System

M-536 Condenser System 24

M-590 Plant Air System 34

Sheet 1

M-590 Plant Air System 2

Sheet 2

M-530 HP& Auxiliary Turbines 0

Sheet 2

M-530 HP& Auxiliary Turbines 1

Sheet 2A

M-532 Steam Generator System 3

Sheet 2

M-532 Steam Generator System 4

Sheet 3

, PIPING, HANGER & ASSEMBLY, AND LINE DIAGRAMS

DRAWING NO. TITLE REVISION

20609-1"-DB Reactor Building-Steam Generator 0

E-205A 6" Level Sensing Nozzle

M-331 Feedwater Line 8

M-334 Feedwater Pipe Support Attachments 4

M-486 Rigid Hanger Assemblies 0

Sheet 5-21

M-486 Under Support Assemblies 3

Sheet 6-3

M-487 Under Support Assemblies 1

Sheet 9-136

M-872 Valve Designation List --

Sheet 1

32133-20"DB Piping Isometric & Supports for 19

632133-30"-DB Valves Plus-500 & Plus 501

32134-20"-DB Piping Isometric 11

Sheet 1

M19.09.5-1 BYT-F Installation Dimensions --

M19.09.6-1 Flow Straightener --

M22.02-8-SI 1/4" to 2" Bolted Bonnet --

'

Sheet 1 Globe Valve Forged

B-2

. _____

.t + .

20610-1"DB Reactor Building Steam Gen. 0

-

E-205A 6" Level Sensing Nozzle

20611-1"-DB GEN. E-205B 0

20612-1"-DB GEN. E-205B 0

20601-1 3/4"-CA GEN. E-205A 0

Sheets 1,2

and 3

20601-1 1/4"-DB. GEN. E-205A 0

20602-3/4-CA GEN. E-205A 0

Sheets 1,2,

and 3

20602-1 1/4"-DB GEN. E-205A 0

20603- 3/4"-CA GEN. E-205A 0

Sheets 1,2

and 3

20603-1 1/4"-DB GEN. E-205A 0

20604- 3/4"-CA GEN. E-205A 0

Sheets 1,2

and 3

20604-1 1/4"-DB GEN. E-205A 0

20605-3/4"-CA GEN. E-205B 0

Sheets 1.E

and 3

20605-1 1/4"-DB GEN. E-205B 0

20606-3/4"-CA GEN. E-2058 0

Sheets 1,2

and 3

'

20606-1 1/4"-DB GEN. E-205B 0

20607-3/4"-CA GEN. E-205B 0

Sheets 1,2

and 3

20608-3/4"-CA GEN. E-205B 0

Sheets 1,2

and 3

20607-1 1/4"-DB GEN. E-2058 0

206C8-1 1/4"-DB GEN. E-205B 0

l

STRUCTURAL STEEL, SUPPORTS AND REINFORCED CONCRETE PLAN DRAWINGS

DRAWING NO. TITLE REVISION

0-275 Reactor Bldg. Area 1 West Partial 8

EL (-) 24'-0"

C-351 Steam Generator Lateral Supports 9

B-3

. - - - -- -

.-

- . . - -

, - i

EQUIPMENT OUTLINE & DETAIL DIAGRAMS

.

DRAWING NO. TITLE REVISION

. N6.03-2 Steam Generator Outline 3

N6.03-3 Longitudinal Section Thru Steam 2

Generator

N6.03.-40 List of Material Steam Generator 2

N6.03-70 . List of Drawings 2

E26.03-10-51

LOAD DESIGN DATA SHEET REVISION

E-1011, Sheet 93 7

VENDOR DRAWINGS

DRAWING N0. TITLE REVISION

5392, Sheet 1 ConSeco DWG Condensate Storage Tank H

PRESSURE INSTRUMENT DATA

SHEET REVISION i

I-1454, Sheet 1 0

I-1454, Sheet 2 0

1-1416, Sheet 1 thru 4 0

PIPING DESIGN SPECIFICATION

M-870, Sheets CA-1, CA-2, DB-1

VALVE ASSEMBLY, OUTLINE DRAWINGS & DETAILS

DRAWING N0. VALVE TAG N0. REVISION

M22.43-1, Sheet 1, HV-20517 & 20518 0

M22.43-2, Sheet 1 HV-20517 & 20518 0

M22.43-3, Sheet 1 HV-20517 & 20518 0

M22.18.1-18 14-11N1 (6") 0

M22.35.2-1 HV-20581 0

HV20582

,

h22.38-6, Sheet 1 FV-20531 0

'

FV-20532

M22.44A-1, Sheet 2 HV-20521 0

HV-20522

N21.01.95 PV-20561 2

PV-20562 A,B,C

PV-20563 -

PV-20564

PV-20566

PV20571A,B C i

1

B-4

i

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- -- .- -

.-. . . , . , - , - - --

-s v .

INSTRUMENT INSTALLATION AND ASSEMBLY DETAILS

.

DRAWING NO. TITLE REVISION

I-1192, Instrument Tubing 0

Sheets 1,2 Tray Installation for

and 3 EFIC & ICC Tubing Runs

I-1193, Main Steam

Sheet 1 Pressure Transmitters 0

OTSG & 'A' & 'B'

PT-20545 B&D and

PT-20546 B&D

Sheet 2 OTSG 'B' 0

PT-20545A, PT-20545C

Sheet 3 OTSG 'B'

PT-20546A, PT-20546C

M19.115B-1 Rosemount Model 1153 6 0

Sheets 1,2, Pressure Transmitters

and 3

M19.115A-12 Pressure Transmitters 0

Isolated Gauge & Diff.

Pres. Switches PG3200

M19.115B-2, Model 353C Conduit Seal 0

Sheet 1

'

I1194, Sheet 3 Safety Cat. Inst. Air Sys. O

I/P Mounting Detail

I-1196 Safety Cat. Inst. Air Sys.

Sheet 4 OTSG 'A' ADVs 0

Sheet 5 OTSG 'B' ADVs 0

Sheet 6 OTSG A&B Reactor Yard Area 0

I-1415,

Sheet 1 "B" Main FW Line 32134-20" 0

" "

2 "A" " " 32133-20" 0

1-1157, Check Valve EFV-250 STSES 0

Sheet 6A

I-1157 Thermal Instrument Enclosure 0

Sheet 7

and 9

'

I-1191, EFIC OTSG E-205A Level 0

Sheet 1 Transmitters 0

M19.115A-7 Press Transmitter 0 1

PD3200, PDH3200 l

B-5

l

__ __-

-. . - - _ _ _ _ _ _ _ _ _ _ _ _ _

. .

i

'

M19.115A-11 Diff. Press. Transmitter 0

PD3200, PDH3200

ANALYSES AND MISCELLANE0US DOCUMENTS

ECCS Analyses .

Energy Feedwater System Upgrade

B&W Document Nc! 77-1125999-01

Singer Model 94020 Shand & JURS

Breather Valve Description Product

Data Sheet 94020

Singer Model 92020 Shand & JURS

Automatic Tank Level Gage Product

Data Sheet 92020

SMUD Nuclear Engineering Procedure NEP 4106

Singer Model 31410 Synchro Tr6nsmitter

Product Data Sneet 31410

Singer Model 92302 Shand & JURS

Liquid Level Indicator Product Data Sheet 92302

Shand & JURS Model 93704 Limit Switch

Assembly Instructions93-704

Singer Model 94210 Shand & JURS

Emergency Vent Product Dat6 Sheet 94210

SALP Report No. 50-312/86-29

MAINTENANCE, SURVEILLANCE, OPERATING PROCEDURES & TESTS

PROCEDURE NO. SUBJECT REVISION

A.62 120 Volt AC Vital System S

A.61 125 Volt DC System 7

AP.167 Electrical Equipment 4

A.58 4160 Volt Operating Procedure 9

A.59 480 Volt Operating Procedure 21

EM.104A Weekly Station Class 1 0

Battery Pilot Cell Test

EN.105A Monthly Station Class 1 0

Battery ICV, Specific

Gravity and Ti;mperature Test

EM.106 Station Battery Test 5

Discharger and Equalize Charger

EM.161 Station Battery Charger Routine 1

1.301 Transmitter Calibration Draft

Procedure for EFIC OTSG Level

MT.006 Safety Valve end Relief Valve 2

Setpoint Verification

B-6

'*

$ O

,

SP.210.01A Monthly Turbine / Motor Driven 23

AFP P-318 Surveillance and

Inservice Test

STP.959 Battery BB Performance O

Capacity Test

SP.210.01B Monthly Motor Driven Auxiliary 23

Feed Pump P-319 Surveillance

and Inservice Test

AP.152 Feedwater and Condensate 19

Systems

AP.160 Plant Air System 6

AP.150 Main and Auxiliary Turbine 14

System

AP.151 OTSG Secondary Side 6

A.51 Auxiliary Feedwater System 31

STP.111 Auxiliary Feedwater Header --

Hot Full Flow Test

STP.18 Auxiliary Feedwater System --

Testing

A.51, Sheet 21 Auxiliary Feedwater System Rev. 32

Draft

HZYSB Alarm 9

TEST SPECIFICATION

MODIFICATION NO. ECN NO. REVISION

123 R-0859 0

123 A-5743 0

ELECTRICAL

CALCULATION N0. SUBJECT REVISION DATE

Z-EDS-E0076 Class 1E System Voltage Study 4 1/04/87

Z-EDS-E0111 Derating 250MCM & 350MCM Cable 0 1/30/85

Z-EDS-E0120 Short Circuit Study (AC) 2 12/31/86

Z-VBS-E0523 Load Study for 120V VBS 1 11/05/86

Z-VBS-E0659 Breaker Coordination for VBS 2 1/03/87

Z-DCS-E0544 Voltage Drop in Cables (DCS) 1 12/31/86

Z-DCS-E0600 Battery & Battery Charger Sizing 2 . 1/03/87

Z-DCS-E0612 125 VDC Short Circuit 1 1/02/87

Z-DCS-E0636 Analysis of Existing Batteries 1 1/03/87

Z-DCS-E0678 125 VDC Short Circuit 0 1/04/87

Z-FWS-E0681 M0V Terminal Volts 0 1/04/87

H VAC

CALCULATION NO. SUBJECT REVISION DATE

Z-HVS-M1918 Service Bldg. Battery Cooldown 0 6/16/86

Z-HVS-M1940 NSEB Battery Room Cooldown 0 7/23/86

B-7

. . _. .-. .-

.

o ~ i

MECHANICAL

CALCULATION NO. SUBJECT REVISION DATE

Z-IAS-M2084 ADV Backup Bottled Gas Sizing 0 12/30/86

Z-IAS-M2046 Inst. Air Requirements for 0 10/29/86

ADV's to Cold Shutdown

Z-IAS-M2004 CCW Valves-Backup Air 2 12/30/86

Z-IAS-M2085 T8V'S Backup Bottled Gas 0

Sizing

NA CST Vacuum Breakers Open 1/13/75

and Relief valves

Z-MCM-M1620 Condensate Line Seismic 0 10/15/85

Analysis

Z-FWS-M1742 NOV Stem Nut Thread Strength 0 9/26/85

Z-FWS-M1726 AFW Pump P-318 NPSH 0 8/1/85

Z-FWS-M1798 Condensate Load on Steam 0 1/13/86

Trops

2-FWS-M0253 AFW System Pressure Drop 1 2/1/84

Z-FWS-M0254 AFW System Pressure Drop 0 2/1/84

Z-FWS-M1727 AFW P-318 Impeller Moment 0 8/1/85

Of Inertia Increase

Z-FWS-M0438 High Pressure FW System 2 11/17/86

Z-FWS-M2081 AFW System Min. Head 0 12/23/86

Requirements

Z-FWS-M2045 AFW System Resistance and 0 10/25/86

TDH Requirements

N26.03-5-1 Field Erected Tank Vessel A 3/13/72

Pipe Supports

INSTRUMENTATION & CONTROL

'

CALCULATION NO. SUBJECT REVISION DATE

Z-FWS-10102 Min Flow Required for AFW 1 1/13/87

Z-FWS-10091 Bore Calcs. for AFW Flow 0 3/7/85

Orifice Plates

2-FWS-10123 AFW Flow Orifice DP 0 10/31/86

Z-FWS-10072 AFW Sys. Pressure Drop at 0 10/14/85

Min. Flow

Z-FWS-10052 AFW Flow Element FE-31801 1 9/13/84

M19.09 AFW Flow Element FE-31801 0 9/8/80

7-ZZZ-IO132 Seismic Qual. of Excess 0 1/14/87

Flow Check Valves

Z-PCS-IO111 Computer Input Resistor 0 8/27/86

Sizing

CIVIL

CALCULATION No. SUBJECT REVISION DATE

Z-ZZZ-C0863 Seismic Qual, of Instr. 0 1/14/87

Air Valves

B-8

_

i - .

QUALIFICATION

.

REVIEW RECORD SUBJECT

SQ-001 AFW-CV-FV-20527 & 20528

SYSTEM STATUS REPORT REVISION DATE

Auxiliary Feedwa'ter System 1 11/25/86 l

Emergency Feedwater Initiation and Control System 1 12/5/86 i

Main Feedwater System 1 12/5/86 l

Instrument Air System 1 11/24/86

120 Volt AC Vital Power System 1 12/5/86

125 Volt DC Vital Power System 1 12/5/86

480 Volt AC Distribution 1 12/5/86

4160 Volt AC Distribution 1 12/5/86

SYSTEM DESIGN

BASIS SUBJECT REVISION DATE

5421 Electrical Distribution Open

System (EDS) 480V

5455 Plant Switchgear Open

System (Medium Voltoge)

5482 Vital Bus System (120VAC) Open

5417 Direct Current System (DCS) Open

DESIGN BASIS

REPORT SUBJECT REVISION DATE

ECNA-5415, Rev. 3 Emergency Feedwater 2 11/4/86

Initiation & Control

System (EFIC)

ECNA-3660, Rev. 5 Electrical Distribution 9 12/17/86

System Changes for

NUREG 0737 and NUREG 0696

Requirements

LESIGN GUIDE SyBJECT REVISION DATE

5204.24 Cable Derating Practice Initial 8/7/85

issue

5204.38 Design of DC Power Circuits Initial 8/7/85

issue

5204.40 Application of Battery Initial 8/13/85

Systems in a Nuclear issue

Plant

5204.48 Application of Value Initial 10/15/85

Electric Motor Actuator issue

B-9

- ._ .

. -__

.

, - t

5204.54 Overcurrent Protection Initial 10/15/85 '

Coordination issue

DESIGN CRITERIA SUBJECT REVISION DATE

5104.1 Electrical Systems Design 1 7/24/86

5104.2 Selection and Sizing of 2 11/14/86

'

Power and Control Cables

5104.4 Electrical Motors and Initial 10/15/85

Starters issue

5104.6 Independence of Electric Initial 9/27/85

Systems

ECN # TITLE REVISION

A-5415 Installation of Emergency Feedwater 3

Initiation and Control System

. A-5415A Installation of Steam Generator Level Taps 0

1

A-5415B Installation of Steam Generator Level 2

Instruments

A-5415C Installation of Steam Generator Pressure- 1

Instruments

A-5415D Implementation of FC-3473-03 For NI/RPS

A-5415E Power & Interconnecting Cabling to EFIC 2

and TIE Cabinets

A-5415F Implementation of FC-3478 Rev. 5 for SFAS 1

A-5415J AFW (Upgrade) Valve Modification 2

A-5415K EFIC Internal Modifications 0

'

.

A-5415L Interconnecting Cabling Between EFIC and 0

New Termination Boxes

A-5415M Installation of EFIC Control of AFW P-319 1

and Modification of the Power Supply

For P-319

A-5415N Installation of EFIC Control and Modification 1

of Power Supply of AFW P-318 and Steam

Supply Valve HV-30801

4

ECN # TITLE REVISION

A-5415P Installation of Remote EFIC Control on 0

Shutdown Panel HZSD

A-5415Q Installation of Auxiliary Feedwater Flow 0

and Pumps Discharg Pressure on HISS Panel

A-54155 Installation of Termination Boxes and 0

Interconnecting Cabling Between Termination

BoxesandHISS(E) Console

A-5415T Auxiliary Feedwater Test Valve FV-31855 1

Modification

A-5415V Modification of Power and Control Circuits 1

of AFW Valves SFV-20577 and SFV-20578

A-5415Y Modification of Power and Control Circuits 1

of AFW P-318 and HV-31826 and HV-31827

A-5415W Installation of EFIC ANALOG Control and

Position Indication Loops for AFW FV-20527

and FV-20528

B-10

.-

- - _ - _ - - - . -. - - -

i - o

A-5415X Installation of ANALOG Control and Position 0

. Indication Loops for AFW FV-20531 and FV-20532

A-5415Y EFIC MFW Valve Closure Controls and Change 0

of Block Valve Power Supply

A-5415Z ANALOG Control of ADV From EFIC Cabinets 0

A-5415AA Installation of Power end Controls to AFW 0

HV-20581 and HV-20582

A-5415AB Installation of Motor Operators on Main 0

feedwater Isolation Valves

A-5415AC Installation of Motor Operators on (2) ADV's 0

A-5415AD Installation of Motor Operated Turbine 0

Bypass Isolation Valves

A-5415AE Modification of Main Steam Cross Tie Valve 1

HV-20565 Controls

A-5415AF Adjustable Time Delay of EFIC Initiation 0

A-5415AG Floor Penetration and Support of New HISS 0

Panel for EFIC

A-5157 Auxiliary Feedwater Runout Alarm 0

A-5233 Diesel Driven Air Compressor Installation 1

A-3285 NGS & IAS Cross-Ties 1

A-5743 Instrument Air Back-up for the ADV's 5

R-0859 Instrument Air Back-up for TBV's CCW and 2-

Feedwater System Control Valves

R-0804 N2 & IAS Cross-Ties 0

A-3062 Main Steam to Auxiliary Pump Turbine 0

R-0894 Bushings for Tilt Disc Check Valves 0

R-0040 Upgrade P-318 Impeller 0

FSAR

SECTION SUBJECT

8. Electrical Systems

8.1 Design Bases

8.2 Electrical System Design

8.3 Tests and Inspections

10.2 System Design and Operation

7. Instrumentation and Control

7.1 Protection Systems

7.2.3 Integrated Control System

TECHNICAL SPECIFICATIONS

Surveillance Standards

SECTION SUBJECT

4.6 Emergency Power System Periodic Testing

B-11

- - -_

o ~ r

LIMITING CONDITIONS FOR OPERATION ,

SECTION SUBJECT

3.4 Steam and Power Conversion System

3.7 Auxiliary Electrical Systems

SYSTEM DESCRIPTION

EFIC Auxiliary Feedwater System Description, Revision 1, and Associated

Figures. Auxiliary Feedwater System, B&W Document No. 15-1120580-04

The diagrams listed below may also be affected documents of ECN's previously

listed and therefore will be modified by applicable DCN's.

Schematic, Wiring, Control Logic, Cable Block, Elementary, and Loop Diagrams

DRAWING N0. TITLE REVISION

N28.03-CS, IE-1E Tie Cabinet 0

Sheet 2 ASSY. H4EIB1

E206, Atmospheric Dump Valves

Sheet 164 PV-20571 A,B, and C 0

Sheet 165 PV-20562 A,B, and C 0

1-54, Atmospheric Dump Valves

Sheet 27 PV-20571 A,B, and C 0

Sheet 28 PV-20562 A,B, and C 0

E-382, Wiring Diagram

Sheet 1 EFIC Channel A H4FWA 0

Sheet 2 EFIC Channel B, H4FWB 0

E-342, Wiring Diagram 14

Sheet 7 Miscellaneous Devices

1-205, Control Logic Didgram 6

Sheet 3 P-318 and P-319

E206, EFIC Initial / Test Matrix

Sheet 166 Channel 'A' 0

Shett 167 Channel 'B' 0

E203, Auxiliary Feedwater

Sheet 50C Isol. Valve HV-20577 4

Sheet 50Q Isol. Valve HV-20578 0

E205, Elementary Diagram'

Sheet A Feedwater & Condensate 13

Sheet 1A Test Valve HV-31855 1

Sheet 18C Block Valve HV-20530 0

Sheet 18D Block Valve HV-20529 0

Sheet 20A MOV HV-20560 & HV-20565 0  :

l

Sheet 20C MOV HV-20569 & HV-20596 0

Sheet 20E M0V HV-20597 & HV-20598 1

B-12

i

_ . -

, - _ _ _ _ _ _ _ . , - ~ . - _

i o .

'

Sheet 20H MOV HV-31826 0

Sheet 201 MOV HV-31827 0

Sheet 21 VLV HV-30801 13

Sheet 24 Main Feedwater Control and 13

Start-up Valves

Sheet 27 Spare 4.16 Kv Breakers 4B10 6

Sheet 29 Emer. FW Control Valves 4

FV-20527 and FV-20528

Sheet 29A Emer. FW Control Valves 1 ,

FV-20527 and FV-20528

Sheet 43 AFW Pump P-319 0

Sheet 44 AFW Pump P-318 0  !

Sheet 49 Isolation Valve HV-20581 0 )

Sheet 50 Isolation Valve HV-20582 0 .i

l

Sheet 51 Control Valves FV-20531 & FV-20532 0

Sheet 52 Isolation Yalve HV-20515 0

Sheet 53 Isolation Valve HV-20516 0

Sheet 54 SG EFIC LVL. Control CH 'A' and 0

EFIC Shutdown & Reset CH. 'A' & 'C'

Sheet 55 SG EFIC Level Control CH. 'B' and 0

EFIC Shutdown & Reset CH.' B'& 'D'

Sheet 65 EFIC Initiation Signals to

Tie Cabinets

E-324, Control Console HISS 18

Sheet 1

E-324, Console HISS Plug 0

Sheet 4 Connector Channels A&C

E-342 EFIC System Terminal 0

Sheet 87 Boxes H7J3826 & H7J3827

N28.02-109, Emergency Feedwater 0

Sheets 1&2 Initiation Control System H4FWA

E-382, EFIC Channel A 0

Sheet 1 H4WA

h28.02-91 Emergency Feedwater Initiation 0

Sheet I thru & Control System H4FWA, E-311,

Sheet 5 Control Panel

h25DE Emergency Shutdown Panel

Sheet A

N28.03-16, Power Distribution 0

Sheet 1 (IE- 1E)

N28.03-10, Tie Cabinet Assembly 1

Sheet 1 (IE-1E)

E-382,

Sheet 6 Tie Cabinet A1, H4E1A1 0

Sheet 7 Tie Cabinet B1, H4E181 0

B-13

1

, - - - . - - - - , - - . , . . _ , - - - , - . . . -- -

_- _

a %* J

N28.04-8, Tie Cabinet Assembly 0

Sheet 1 (IE-1E) -

N28.03-15, Power Distribution 0

Sheet 1 (IE-1E)

I-53, AFW Safety Grade Flow 1

Sheet 6 FT- 31802, FT-31803

I-54, EFIC Process Analog 0

Sheets 1 thru 8 Signals, Steam Gen. A&B

Pressure, CH. A,B,C,0

I-53, AFW Safety Grade Flow 0

Sheet 7 FT-31902, FT-31903

153, AFW PMP P-318 SUC.& 0

Sheet 10 Disch, Press. PT-31801,

PT-31803

I-53, AFW PMP P-319 SUC. & 0

Sheet 11 Disch. Press. PT-31901, PT-31903

i

1-1421 EFIC Steam Generator 0

Level Setpoints

i

I-54, EFIC Process Analog 0

i Sheet 9 Signals Steam Generator A Narrow

'

Range level CH. A

l E-205, Main Steam failure Feedwater 3

'

Sheet 24A Valve Isolation 'B'

4

E-342, Misc. Instruments 0

Sheet 82

'

. E-206, ADV Isolation Valve --

'

Sheet 168 HV-20517

& 169 (

E-206, Turbine Bypass 1 solation --  !

Sheet 170 Valve HV-20521 q

6 171

1-54, EFIC Process Analog Isolation --

g

Sheet 9 SG 'A' Narrow Range LYL.CH. A 0  ;

" " " " " " " i

10 B 0

" 11 C 0  ;

" 0 0

-

12

" " " "

"

13

"

'B' A 0 .

" B 0

14

" C 0

15

" 0 0

16

" "

j

"

17

"

'A' WIDE

"

A 0

"

16 B 0

!

B-14

l

1

. . . . - , _ _ _ - - - - ,. , . . - , , - -. . . . - . - , _ - - - . - . . . - - - _ ~ _ . - - . . . , . . , . - - .- ~ - - .

m

I

so o

,

1-54, EFIC Process Analog Isolation

Sheet 19 SG 'A' WIDE Range LYL.CH. C 0

20 D 0

."' 21

"

'B' " " "

"A 0

"

22 B 0

"

23 C 0

"

24 D 0

E-208,

Sheet 13 B Electrical Auxiliaries 3-

" " 13

Sheet 15 " " --

Sheet 68 "

Sheet 8A

" 3

Sheet 20A Nuclear Service Bus Loading 'A' 4

Sheet 20D 4Kv S4A Bus Potential 3

Sheet 50 Electrical Auxiliaries

"

4

" 3

Sheet 56

Sheet 9 Electrical Auxiliaries 16

sheet 20E 4Ky SAB Bus Potential 2

Sheet 57 Electrical Auxiliaries 3

Sheet 57A Nuclear Service Bus Loading 'B2' 0

E-203, Reactor Auxiliaries 10

Sheet 3 Decay Heat Removal Pumps P-261A,8

h23.01-57 S.F.A.A. Digital Subsystem 2

Typical Unit Control

N23.01-26, S.F.A.S. Backlighted 3

Sheet 4 Pushbutton Switches and

Control Switches

E5.02-5-51 HK Stored Energy Breaker 51

E6.02-2 4160 Volt Switchgear 6

l

B-15