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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20211B1671999-07-13013 July 1999 Special Rept on 990614 Re Test of Scram Set Point of Two of Five Low Primary Coolant Flow Safety Sys Channels.Caused by Trip Set Points Being Too Close to TS Limits.Compliance Procedure 23 Will Be Revised ML20236Y5941998-08-0606 August 1998 Special Rept:On 980706,operator Noted That One Sample Listed as Inches Long on Loading Sheet,Only 2 Inches Long.Errors Constitute Observed Inadequacy in Implementation of Administrative & Procedural Control.Procedures Revised ML20236S1711998-07-15015 July 1998 Ro:On 980615,large & Rapid down-shift on Three Different Meter Indications from One Ni Drawer Was Discovered.Caused by Failed Preamplifier in Wide Range Amplifier Subject Ni Drawer.Replaced Cabling,Detector & Preamplifier ML20198K9441998-01-0808 January 1998 Special Rept:On 971209,reactor Shutdown by High Power Scram Initiated by Wide Range Monitor of Nuclear Instrument Sys. Caused by Unanticipated Positive Reactivity Insertion. Reflector Sample Opened & Inspected ML20197D2751997-12-15015 December 1997 Ro:On 971026 & 1106,slight Elevation of Fission Products Were Detected in Primary Coolant Water Analyses.Caused by Slight Fabrication Flaw in Element MO-460.Surveillance of Bwx Technologies Fabrication Techniques Will Be Increased ML20196G8891997-07-15015 July 1997 Special Rept:On 970616,scram Setpoint for Low Flow Scram for Heat Exchanger 503A Leg Was 25 Gpm Below TS Limit.Caused by Drifting of Setpoint of Vutronik Monitor Switch DPS-928A. Adjusted Trip Setting & Retested Trip Setting ML20116E2621996-07-30030 July 1996 Ro:On 960701,emergency Generator Shutdown on High Coolant Temp.Caused by Sheared Water Pump Shaft.Replaced Defective Pump ML20100J3991996-02-22022 February 1996 Ro:On 960123,reactor Was Shut Down by Manual Scram When Console Operator Determined That Regulating Blade Was Inoperable.Caused by Seized Bearing on Gearbox Input Shaft. Bearing Replaced ML20097J4391996-01-26026 January 1996 Special Rept:On 951227,reactor Shutdown Occurred Due to Reactor in Operation W/Regulating Blade in Degraded Condition.Replaced Dowel Pin ML20082P4491995-04-19019 April 1995 Special Rept:On 950320,reactor Startup Occurred W/Source Range Monitor in Degraded Condition.Shutdown Taken by Console Operator ML20073K3221994-09-30030 September 1994 Special Rept:On 940902,reactor Scram Occurred Due to Failure of Inner Airlock Door Drive Sys.Airlock Door Drive Sys Repaired ML20069E0241994-05-25025 May 1994 Special Rept:On 940426,shift Supervisor Noted Decreasing Power Trend on Wide Range Monitor Chart.Problem Quickly Identified to Be One Loose & One Missing Set Screw in Motor to Gearbox Coupling.Missing Set Replaced W/New One ML20058M7421993-09-27027 September 1993 Ro:On 930907,determined That Scram Setpoint for Low Flow Scram for HX 503B Leg Below LSSS of 1625 Gpm Required by TS 2.2.Caused by Defective Alarm Trip Unit.Defective Alarm Trip Unit Replaced W/Spare Unit ML20056D8771993-08-12012 August 1993 Ro:On 930712-26,reactor Operated W/Operability of Automatically Closing Reactor Containment Isolation Door in Degraded Condition.Caused by Actuating Cam Maladjusted.Cam Readjusted & Tightened ML20125B6951992-12-0202 December 1992 Ro:On 921104,channel 4,5 or 6 95% Downscale Annunicator Received,Annunicator Locked in & Then Cleared Several Times. Caused by Setscrew,That Engages Motor Shaft to Gear Box, Coming Loose.Motor Shaft Modified to Add Flat Surface ML20099A7051992-07-20020 July 1992 Special Rept:From 920622-23,reactor Operated W/Unreliable Radiation Monitoring of Exhaust Stack Effluent.Caused by Pieces of Sheet Metal,Used as Bending Vanes,Breaking Loose & Disconnecting from Sampling Line.Probe Reconnected ML20099B6231992-07-20020 July 1992 Special Rept:On 920623,discovered Lower than Normal Chart Recorder Indication on Stack Radiation Monitor Gas Channel. Caused by Pieces of Sheet Metal Impacting Kinetic Probe. Tygon Tubing Connection Replaced W/Solid Tubing ML20086N1101991-12-10010 December 1991 Special Rept:On 911111,differential Pressure Indications Showed That One of Two Primary Coolant Isolation Valves Did Not Seat Properly.Caused by Valve Steam Falling Out of Valve Actuator.Actuator Key Replaced & Bottom Slot Recrimped ML20079L7191991-10-29029 October 1991 Ro:On 910930,primary Coolant Isolation Valve V507A Took Longer than Normal to Close & Differential Pressure Indications Indicated Valve Failed to Seat Properly.Caused by Valve Stem Binding.Valve Will Be Replaced ML20246A1031989-06-15015 June 1989 Ro:On 890603,discovered That Drive Chain Had Fallen Off Drive Gear for Regulating Blade Rotary Limit Switch.Reactor Shutdown Initiated.Chain for Rotary Limit Switch Assembly Returned to Drive Gear & Tension Adjusted ML20248G6241989-03-28028 March 1989 Ro:On 890302,reactor Operated for 2 H & 33 Minutes W/ Emergency Generator Local Switch in Stop Position.Caused by Personnel Error.Subj Local Switch Placed in Remote Position. Operator Involved Counseled.Checksheet Revised ML20206B9931988-10-31031 October 1988 Revised 881019 Special Rept on 880921 Event Re Reactor Operation W/Regulating Blade Being Inoperable.Second Sentence in Ltr Corrected ML20195D4911988-10-28028 October 1988 Ro:On 880929,difference of 10 F Between Temp Indications for Primary Loop a & Loop B Observed.Caused by Small Amounts of Resistance Introduced Into Compensation Loop Leads. Connection for Compensation Loop Will Be Double Checked ML20205N8811988-10-28028 October 1988 Ro:On 880929,Tech Spec Deviation Occurred Due to Intermediate Range Monitor Channel 3 Indicating Downscale & Associated Short Period Rod run-in & Scram Trip Inoperable. Caused by Breakdown of Cable Insulation.Cabling Replaced ML20205H8961988-10-19019 October 1988 Ro:On 880921,Channel 4 High Power Rod run-in Occurred & Regulating Blade Would Not Respond in Either Automatic or Manual Mode.Caused by Gear Box Assembly W/Internal Drive Gear Ridden Up Shaft Due to Loose Set Screw.Drive Repaired ML20154L3981988-09-15015 September 1988 Ro:On 880818,emergency Generator Cranking Limit Indication Found Tripped & Plant Failed to Start Lamp Energized. Caused by Linkage Lubrication Problem.Preventive Maint (PM) Procedure Added to PM Schedule ML20235G4991987-09-24024 September 1987 Ro:On 870825,closed Indicating Light for Automatically Closing Reactor Containment Isolation Door Did Not Turn On. Caused by Addl Drag Reducing Coast Distance of Door.Motor Drive Stop Microswitch Readjusted ML20206D0031987-03-31031 March 1987 Ro:On 870305,test Signal Simulating High Temp Fed to 980A Meter Relay Trip Unit,But Meter Relay Contacts Failed to Open.Caused by Decreased Capacitance Value in Meter Relay Control Circuit.Meter Relay Trip Unit Replaced ML20214N8381986-11-24024 November 1986 Ro:On 861030-31,reactor Operated W/Seal for Inner Airlock Door Deflated Due to Bleed Valve in Abnormal Position.Caused by Personnel Error.Procedures Will Be Revised & Addl Pressure Gauge Will Be Added to Air Supply Sys ML20214P2841986-09-10010 September 1986 Ro:On 860815,emergency Pool Fill Sys Discovered in Abnormal Lineup Due to Valve PIV-1 Being Closed.Caused by Improper Clearing of Red Tag Indicating Valve Opened on 860501. Reactor Startup Checksheet Revised to Ensure Valve Opened ML20211K3891986-08-20020 August 1986 Ro:On 860729,dosimeter Vendor,Rs Landauer & Co,Reported That TLD Finger Dosimeter Recorded 23,560 Mrem for June 1986.On 860609,employee Packed Tm-170 Wafers for Shipment.Committee to Investigate Exposure Activated ML20134E2881985-08-13013 August 1985 Ro:On 850718,during Front Panel Checks Prior to Reactor Startup,Rod run-in Trip Function for Power Range Monitor 5 Found Inoperable.Possibly Caused by Loose Pin Connection. Trip Unit Module Replaced & Operability Checked Weekly ML20126J4661985-05-31031 May 1985 Ro:On 850519,chain Link on Drive Chain for Regulating Blade Position Indicator Failed.Caused by Broken Drive Chain Link. Drive Chain Link Repaired & Regulating Blade Driven Full in for Position Indication Reset ML20112E1321985-03-18018 March 1985 Ro:On 850220,nuclear Instrumentation Channel 6 Power Range Monitor Indication Dropped from Indicated Power of 104% to 92%.Cause Not Determined.Down Scale Alarm of 75% Will Be Changed to 95% ML20112F0111985-01-11011 January 1985 Ro:On 841213,emergency Generator Stalled 45 After Assuming Emergency Electrical Loads During Emergency Generator Load Test CP-17.Cause Not Found.Stalling Did Not Recur During Subsequent Tests.Mods Will Reduce Starting Load ML20091Q9251984-06-0808 June 1984 Ro:On 840511,personnel Airlock Doors Operated Out of Sequence,Allowing Both Inner & Outer Doors to Open at Same Time.Caused by Outer Airlock Door Gasket Pulled Partly from Seat.Gasket Replaced ML20079K7491984-01-13013 January 1984 Ro:On 831215,emergency Generator Gasoline Engine Electrical Interlock Protective Circuit Tripped.Caused by Bent & Nearly Grounded Electrical Connecting Wire Spade Lug.Trip Sensor Leads Placed to Prevent Grounding ML20081J0821983-11-0101 November 1983 Ro:On 831003,during Full Power,Site Electrical Power Lost & Emergency Generator Operated in Degraded State.Cause Probably Due to Addition of STP Gas Treatment on 830923. Gas Pumped from Generator Tank.Sys Refilled ML20066H9661982-11-17017 November 1982 Ro:During 821021 Shutdown to Change Flux Trap Samples,Flux Trap Sample Hold Down Device Determined Improperly Installed During 821018 Shutdown.Caused by Hold Down Rod Assembly Pinned High.Device Properly Repinned ML20054F6981982-05-25025 May 1982 Ro:Advises of Mod to Corrective Action Noted in Informing NRC of Valve Left Open in Line That Penetrates Containment Wall.Red Danger Tags on Valves Outside Containment Removed,As Pipe Cap Insures Flow Path Isolated ML20062C0151978-10-31031 October 1978 Ro:On 781022,control Blade B Unexpectedly Dropped from Drive Magnet & Hung Up Approx 7 Inches Above Full Insertion. Probably Caused by Broken Outer Race of One of Eight Vertical Guide Bearings 1999-07-13
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20212D4471999-09-20020 September 1999 Safety Evaluation Supporting Amend 31 to License R-103 ML20211B1671999-07-13013 July 1999 Special Rept on 990614 Re Test of Scram Set Point of Two of Five Low Primary Coolant Flow Safety Sys Channels.Caused by Trip Set Points Being Too Close to TS Limits.Compliance Procedure 23 Will Be Revised ML20206A9681999-04-21021 April 1999 Revised Page 4 to MURR QA Plan ML20202G9051998-12-31031 December 1998 Operations Monthly Summary for Univ of Mo Research Reactor for Dec 1998 ML20207A6981998-12-31031 December 1998 Reactor Operations Annual Rept for 980101-1231, for Univ of Missouri Research Reactor Facility.With ML20202G9171998-11-30030 November 1998 Operations Monthly Summary for Univ of Mo Research Reactor for Nov 1998 ML20202G9271998-10-31031 October 1998 Operations Monthly Summary for Univ of Mo Research Reactor for Oct 1998 ML20154M3301998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Univ of Missouri Research Reactor ML20154M3401998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Univ of Missouri Research Reactor ML20236Y5941998-08-0606 August 1998 Special Rept:On 980706,operator Noted That One Sample Listed as Inches Long on Loading Sheet,Only 2 Inches Long.Errors Constitute Observed Inadequacy in Implementation of Administrative & Procedural Control.Procedures Revised ML20154M3431998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Univ of Missouri Research Reactor ML20236S1711998-07-15015 July 1998 Ro:On 980615,large & Rapid down-shift on Three Different Meter Indications from One Ni Drawer Was Discovered.Caused by Failed Preamplifier in Wide Range Amplifier Subject Ni Drawer.Replaced Cabling,Detector & Preamplifier ML20154M3651998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Univ of Missouri Research Reactor ML20154M3731998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Univ of Missouri Research Reactor ML20154M3841998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Univ of Missouri Research Reactor ML20246P9931998-03-31031 March 1998 Monthly Operating Rept Summary for Mar 1998 for Univ of Missouri Research Reactor ML20246Q0231998-02-28028 February 1998 Monthly Operating Rept Summary for Feb 1998 for Univ of Missouri Research Reactor ML20203H4271998-02-26026 February 1998 Safety Evaluation Supporting Amend 30 to License R-103 ML20246Q0201998-01-31031 January 1998 Monthly Operating Rept Summary for Jan 1998 for Univ of Missouri Research Reactor ML20198K9441998-01-0808 January 1998 Special Rept:On 971209,reactor Shutdown by High Power Scram Initiated by Wide Range Monitor of Nuclear Instrument Sys. Caused by Unanticipated Positive Reactivity Insertion. Reflector Sample Opened & Inspected ML20203L0531997-12-31031 December 1997 Reactor Operations Annual Rept,970101-1231, for Univ of Missouri Research Reactor Facility ML20202H4091997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Univ of Mo Research Reactor ML20197D2751997-12-15015 December 1997 Ro:On 971026 & 1106,slight Elevation of Fission Products Were Detected in Primary Coolant Water Analyses.Caused by Slight Fabrication Flaw in Element MO-460.Surveillance of Bwx Technologies Fabrication Techniques Will Be Increased ML20202H3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Univ of Mo Research Reactor ML20202J1151997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Univ of Missouri Research Reactor ML20202J1201997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Univ of Missouri Research Reactor ML20211B2871997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Univ of Missouri Research Reactor ML20210R2701997-07-31031 July 1997 Univ of Missouri Research Reactor Operations Monthly Summary,July 1997 ML20196G8891997-07-15015 July 1997 Special Rept:On 970616,scram Setpoint for Low Flow Scram for Heat Exchanger 503A Leg Was 25 Gpm Below TS Limit.Caused by Drifting of Setpoint of Vutronik Monitor Switch DPS-928A. Adjusted Trip Setting & Retested Trip Setting ML20149L3761997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Univ of Mo Research Reactor ML20141H6451997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Univ of Mo Research Reactor ML20141H6581997-04-30030 April 1997 Monthly Operating Rept for April 1997 for Univ of Missouri ML20141H6691997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Univ of Missouri ML20136D7211997-03-0606 March 1997 Safety Evaluation Supporting Amend 29 to License R-103 ML20141H7421997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for University of Missouri Research Reactor ML20141H6421997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Univ of Mo Research Reactor ML20141H7001996-12-31031 December 1996 Monthly Operating Rept for Univ of Missouri Research Reactor for Dec 1996 ML20138Q6601996-12-31031 December 1996 Reactor Operations Annual Rept for 1996 ML20141H7221996-10-31031 October 1996 Monthly Operating Rept for Univ of Missouri Research Reactor for Oct 1996 ML20116E2621996-07-30030 July 1996 Ro:On 960701,emergency Generator Shutdown on High Coolant Temp.Caused by Sheared Water Pump Shaft.Replaced Defective Pump ML20141H6781996-06-30030 June 1996 Monthly Operating Rept for Univ of Missouri Research Reactor for June 1996 ML20149L3721996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Univ of Mo Research Reactor ML20117L1091996-05-13013 May 1996 Univ of Missouri Research Reactor Operations Monthly Summary for Apr 1996 ML20117L1001996-03-31031 March 1996 Univ of Missouri Research Reactor Operations Monthly Summary for Mar 1996 ML20117L0951996-03-13013 March 1996 Univ of Missouri Research Reactor Operations Monthly Summary for Feb 1996 ML20117L0841996-03-0606 March 1996 Univ of Missouri Research Reactor Operations Monthly Summary for Jan 1996 ML20100J3991996-02-22022 February 1996 Ro:On 960123,reactor Was Shut Down by Manual Scram When Console Operator Determined That Regulating Blade Was Inoperable.Caused by Seized Bearing on Gearbox Input Shaft. Bearing Replaced ML20097J4391996-01-26026 January 1996 Special Rept:On 951227,reactor Shutdown Occurred Due to Reactor in Operation W/Regulating Blade in Degraded Condition.Replaced Dowel Pin ML20101F5381995-12-31031 December 1995 Revised Pages III-1 & VII-1 to 1995 Operations Annual Rept ML20100M7821995-12-31031 December 1995 Univ of Mo Research Reactor Reactor Operations Annual Rept Jan-Dec 1995 1999-09-20
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l
[ .. Rssearch Reactor Center -
Research Park Columbia. Missouri 65211 II ,
Telephone (573) 882-4211 FAXi573]882=3443
- UNIVERSITY O# MISSOURl-COLUMBIA -
December 15,1997.
Director of Nuclear Reactor Regulation ATTN: Document Control Desk Mail Station F137 US Nuclear Regulator Commission Washington, DC 20555 REFEltENCE: Docket No. 50-186 University of Missouri Research Reactor License R.103
SUBJECT:
Slight elevation of Gssion products detected in primary coolant water analysee
= BTI'HODUCTION The University of Missouri Research Reactor is reporting the detection of a slight elevation of I 131 in the weekly primary coolant analyses required by Technical Speci6 cation 5.2.c
- for the weeks of November 3 und October 20,1997. Typical concentrations of I-131 in the weekly samle analyses are 1.3 r 10 5 to 1.5 x 10 5 pCi/ml. Samples tnken October 26 and November F indicated a concentration of 1-131 of 2.3 x 10 5 pCi/ml. ibis concentration ofI.
- 131 indicates a slight increased level of Ossion products in the primary coolant, but is a factor of 200 less than the Technical SpeciGcation limit for 1-131 of 5 x 10-3 pCi/ml in Technical Speci0 cation 3.9.c. This report is made for informational purposes because the literal interpretation of abnormal occurrenen as denned in Technical Speci6 cation 1.1.d does not specify a threshold for release of Gssion products from a fuel slement even though the concentrations of1131 detected were far below the Technical SpeciGcation Limiting Conditions for Operation.
DESCP.ll' TION Reacto. primary coolant water is sampled and analyzed each week of reactor operation as specided in Technical SpeciGcation 5.2.c. The primary coolant spectroscopy results on the Novtmber 5,1997 sample indicated normal levels ofI-131, but other iodine isotopes were slighsly increased. This analysis coincided with elevated readings on the on-line fission product monitor (PPM) which continuously monitors primary coolant activity. The fission product monitor typically indientes 3000 to 5000 counts / minute. During the week of November 3 the indication increased ta 12,000 to 15,000 counts / minute.
d[,
Additional primary coolant ramples were taken November 6,7 and 8 to monitor 1131 concentrati3n in the primary coolant water to assure we were well below the Technical y
Specification Liniiting Conditions for Operation of 5 x 10 3 pCi/ml (T.S. 3.9.c). The '
'snmple analysis on November 6 indicated an 1131 concentration of 1.6 x 10 5 pCi/ml. g3 Other Gssior -roducts were abo detected in these samples at low levels (i.e., slightly i ater than .ninimum detectable activity).
, , n V 9712290021 971215 PDR ADOCK 05000186'-
ll[lilll!Il111 I!IlIl S pon
i Letter to Dir:etor of Nuclear Itcartor llegulation
- December 15,1997
_ Page 2 Review of previous primary coolant analyses indicated an earlier slight increase in 1131 concentration on October 20,1997. This sample was taken to investigate a slight increase in the fission product monitor indication (about 2000 to 3000 countdminute above normnD.
The results of the 1131 sample on October 20 indicated a concentration of 2.3 x 10 5 pCi/ml, which was considered to be within statistical variation of the en ected concentration because the concentrations were so close to minimum detectable activity.
On November 6, the primary chemist reviewed tha core loadings for the previous three weeks and was able to determine that two fuel elements, MO-458 and MO 460, were common to the cores that ran the weeks of November 3 and October 20,1997, whtn increased b131 concentrations were found. These two elements had accumulated a power history of 126 MWD cach at the end of reactor operation at 0400 on November 10,1997. The Itenctor Manager pinced these elements in the retired category and scheduled them for post irradiation ihspection, Fuel elements MO-458 and MO-400 were stored in pool storage racks a distance apart so that grab samples of pool water couhl be taken ubove them to determine which element was leaking, itesults of the unalyses indicated that MO 460 was the problem element.
Both elements were inspected November 20,1997, by the procedure used for inspection of retired fuel elements. The test includes a visual inspection of the outside surface of plates 1 ,
and 24 and a visual inspection of the fuel plate gaps for any foreign material. The inspection includes a go-no go" test with a gap check tool to ensure no fuel plates have exceeded 10% swelling over their useful life an indicated in the basis far Technicti Specification 3.8.n.
Neither ch, ment indiented abnormalities that could be attributed to reactor operation with !
partial flow blockage of a coolant chminct or excessive swelling of a fuel plate.
ANAINSIS The slightly clevate 11131 cor entre ions in the primary coolant were most likely due to a slight fabrication flav in elemsit MO 460 such as e pit in the cladding in one of the MO-460 fuel plates. Fuel elements typically operate for 150 MWD without any detectabic increase above the normal concentrations of1-131 in the primary. This element had been in the fuel cyclo since May 19pti and previous cores in which it as incorporated indicated no increases in 1 131 until the week of 0ctober 20,1F 37.
The total 1 131 activity in the primary kystem vote ne of 2000 gallons (with a concentration of 2.3 x 10 5 pCi/ml) was approximately 175 pCL This corresponds to 0.5% of the activity allowed in the primary coolaat by the Limiting Conditions for Operation in Technical Specification 3.9.c.
The slight increase in 1 131 ectWity in the primary system was not a threat to the public even if primary water had been taleased. There, in fact, wer, no indicction of elevated airborne 1131 activity during the period of time the reactor ~' operated with slightly elevated 1131 concentrations in the primary water.
For perspective, the peak 1 131 concentration indicated in the primary coolant was only a factor of 2.3 times the 10CPH20, Appendix B, Table 3 limit for release of 1 131 to the sanitary sewer.
Letter to Director of Nuclear Itenctor Readation
+ December 15,1997
- ~ Page3 The reactor operated on two occasions with slightly elevated 1-131 netivity in the primary coolant. Subsequent review of Technient Specifientions revealed that the deGnition of abnormal occurrence related to Ossion product activity in the primary coolant did not have a specific threshold, even though the concentration detected was well bel ow the Limiting Conditions for Operation. The NltC was notified by telephone the week of Novernher 17 of these pecuirences and of our intent to report in written form.
COltHECTIVlWOLLOW.UI' ACTION When the fission product monitor indiented elevated readings, additional spectroscopie analyses were taken to verify that 1131 concentrations were within the limits of Technical Specifiention 3.9.c. The primnry chemist was able to narrow the search for the source of the fission products to two elements by reviewing the elements used in each week's core.
After defueling the suspect elements to pool storage, grab samples above the elements were able to identify MO.460 as the source of the elevated fission product activity. This element and its companion clernent, MO 458, were inspected to verify there were no indientions of fuel plate swelling or foreign material hetween the plates that could account for fission product release. Ornh samples taken above M0 460 after a week out of the core indicated no elevated fission product netivity in the pool water. Lenkage from fuel elements is often undetectable when not in an operating core. Before this element is shipped to DOE na spent fuel, we will carefully monitor the in. cask lench test to ensure it is no longer leaking. We will determine if DOE requires any other special hemdling of this element before it is sent to them as spent fuel.
The fuel vendor, BWX Technologies, Inc. (formerly linhcock & Wilcox), and the program mannger for DOE's university fuel assistance program were notified of this problem. BWX Technologies also provides fuel for the Advanced Test Itenctor (ATID and no other lenkage problems have been experienced at MUllit or ATit with BWX Technologies fabriented fuel.
The program manager for DOE's university fuel procurement indiented they will increase their surveillance of IlWX Technologies' fabrication techniques to ensure high quality fuel to MUltit and ATH.
ENDOHSEMENT:
Sincerely, 1(eviewed and Approved UAkk . w Walt A. Meyer Jr J. Charles McKibben llenctor Manager Associate Director xc: Mr. Alexander Adams Jr, USNHC '
Mr. Tom ilurdick. NHC Itegion ill Dr. Elaine Charlson, Associate Provost, Mt>
Reactor Advisory Committee - fj -
Itenetor Safety Subcommittee ( j jig M ))/ h f(;ri( n/n%7 CHRISTINE M.ERRANTE Notary Public - NMary Seal !
STATE OF MISSOURI Doone County My Commisslan Ex; ires: Al*il 14.19??
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