ML20125D336

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Insp Rept 50-458/92-32 on 920927-1107.Violations Noted. Major Areas Inspected:Operational Safety Verification, Maint & Surveillance Observations & Review of Complex Surveillance Test
ML20125D336
Person / Time
Site: River Bend Entergy icon.png
Issue date: 12/08/1992
From: Gagliardo J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20125D293 List:
References
50-458-92-32, NUDOCS 9212150106
Download: ML20125D336 (23)


See also: IR 05000458/1992032

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APPENDIX B

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection Report: 50-458/92-32

Operating License: NPF-47

Licensee: Gulf States Utilities

P.O. Box 220

St. Francisville, Louisiana 70775-0220

Facility Name: River Bend Station

Inspection At: St. Francisville, Louisiana

Inspectior. Conducted: . September 27 through November 7, 1992

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Inspectors: W. F. Smith, Senior Resident Inspector

D. P. Loveless, Resident Inspector

R. B, Vickrey, Reactor Inspector, Plant Systems Section,

Division of Reactor Safety

D. L. Kelley, Reactor Inspector, Test Programs Section,

Division of Reactor Safety

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Approved: ) M JL P

. E.'pliardo, Chief, Project Section C . Dalel

Inspection Summar_y

Areas Inspected: Routine, unannounced inspection of onsite response to.

events, operational safety verification, maintenance and surveillance

observations, review of a complex surveillance test,. followup of an unresolved

item, review of motor operated valve- signature testing errors,= onsite review

of a licensee event report, and occupational health and safety inspections.

Results:

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  • Overall, the licensee's response to operational events during the report

period was acceptable (paragraph 2.8).

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  • A noncited violation was identified for failure to make a timely report-

of a plant shutdown initiation required by Technical

Specification 3.0.3. The licensee's actions to identify and correct the

problem were good (paragraph 2.3).

e The licensee's approach and response to increasing drywell pedestal sump

levels were considered appropriate to the circumstances (paragraph 2.4).

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9212150106 921210

PDR ADOCK 05000458

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e The licensee's response to a failed 120 Vac distribution panel was

considered to be good. However, a noncited violation was identified for

failure to follow preventive maintenance procedures prior to the event

(paragraph 2.5).

  • A violation was identified for initiating high volume containment purge

with one train of the standby gas treatment system inoperable

(paragraph 2.7).

  • Overall, the licensee operated the facility in a safe manner during the

report period (paragraph 3.5).

  • A violation was identified for failure to demonstrate the operability of

offsite ac power sources when one diesel generator was inoperable for

greater than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. The Technical Specification action statement was

not entered for this planned equipment outage (paragraph 3.1). A

similar weakness was seen during surveillance testing of the diesel-

driven fire pumps when both pumps were taken out of service and the

condition was not logged (paragraph 5.2).

e While housekeeping improved in some areas of the plant, some areas

required attention (paragraph 3.2).

4 * A noncited violation of security plan implementation procedures was

identified for issuing of a key card to an individual whose training had

expired. The Director of Nuclear Station Security committed to

implementing an active computerized system to correct the root cause of

this problem. This approach was excellent (paragraph 3.3).

e Overall, the maintenance activities observed during this report period

were good (paragraph 4.4).

e The work and controls to repair a containment unit cooler breaker were

considered good. System engineering support and- electrical foreman

oversight for the activity were identified as strengths (paragraph 4.2).

e The workers were knowledgeable of the job requirements and techniques

for repair of the Division I standby diesel generator. The acceptance

criteria were met for the work observed (paragraph 4.3).

e Overall, the licensee's performance of surveillance tests during the

report period was good (paragraph 5.3).

e The licensee's performance of the Division I standby diesel generator.

surveillance on October 13 was excellent, with a possible weakness

indicated in the implementation of the licensee's indepsndent'

verification program (paragraph 5.1).

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e During surveillance testing of diesel fire pumps, an operator ased a

broom handle to verify tank level when the permanent level indicator was

out of service (paragraph 5.2). l

e The completed documentation for surveillance inspections of the

Division I standby diesel generator was good. The specific required

sign offs were completed and the quality control hold points were

observed. The procedure changes were well documented and were properly

reviewed and approved (paragraph 6.1),

e One violation was identified for failure to have adequate procedural

controls covering maintenance activities on the Division I standby

diesel generator (paragraph 7.1). A similar weakness was seen during

Feedwater Pump C maintenance in that work instructions were not ,

sufficiently detailed and workers were not trained for the correct  !

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installation of the pump seal (paragraph.4.1).

e The licensee appropriately evaluated potential motor operated valve  ;

testing errors and was taking satisfactory corrective actions

(paragraph 8.1).

e One noncited violation was identified for failure to comp.ly with

Technical Specification 3.0.4 when the automatic depressurization system  ;

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was inoperable. The operators were alert in recognizing these problems,

and the licensee took prompt corrective action. Operator identification

of the problem was viewed as a strength (paragraph 9.1).

Summary of Inspection Findings:

  • Violation 458/92032-1 was opened (paragraph 2.7).
  • Violation 458/92032-2 was opened (paragraph 3.1).

6 Violation 458/92032-3 was opened (paragraph 7.1).

  • Four noncited violations were identified (paragraphs 2.3, 2.5, 3.3, and

9.1).

e Unresolved Item 458/92026-1 was closed (paragraph 7.1).

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e Licensee Event Report 458/92-018 was closed (paragraph 9.1).

Attachments:

e Attachment 1 - Persons Contacted and Exit Meeting

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DETAILS

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1 PLANT STATUS

At the beginning of this inspection period, the reactor was in Mode 1, at ,

80 percent power.

Power had been reduced to facilitate repairs to Main Feedwater Pump C. On  !

October 7, 1992, power was further reduced by about 1 percent upon initiating R

a plant shutdown as required by Technical Specification 3.0.3, in response to

the inoperability of both trains of control room ventilation. One train was-

promptly restored and the shutdown was terminated. Following the feedwater

pumo repairs, the reactor was returned to 100 percent power on October 9.

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On October 18, the licensee again entered the shutdown action statement for

Technical Specification 3.0.3 because both trains of control room-ventilation

were inoperable. Power had been decreased to approximately 75 percent power,

until one train was returned to an operable status. Reactor power was then

restored to 100 percent.

At the end of this inspection period, reactor power was at 100 percent.

2 ONSITE RESPONSE TO EVENTS (93702)

2.1 Highl_y Radioactive Waste Labeled Low Level Waste

On October 1, 1992, the inspectors were informed by the licensee's acting

radiological controls director that two bags of solid radioactive waste were

found in a low activity box, each containing highly radioactive material. One

bag was reading 14,000 millirem per hour on contact bi was labeled less than

2 millirem per hour, and the other was reading 800 miliirem per hour and was

not labeled at all. These issues were addressed in NRC Inspection

Report 50-458/92-33, dated November _ 10, 1992.

2.2 118 Megawatt Electrical Grid Transient

At 9:46 a.m., on October 6, 1992, the facility experienced a 118 megawatt-

electrical _ grid trancient. This was apparently caused by faulty switching at

the Waterloo Substation. As a result of this transient, multiple

uninterruptible power supply inverter and digital radiation monitoring system

alarms were received, which was expected.

In addition to the expected alarms, the containment annulus pressure control

system was lost, resulting in the initiation of Division I and II containment

annulus mixing and standby gas treatment to control annulus pressure. Also,

the Division I control building air handling unit and the supporting chiller

trinped off (Division II was already out of service).

The standby gas treatment system, an engineered safety feature (ESF), started

on the above non-ESF signal. The Shift Supervisor did not make a 4-hour

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report pursuant to 10 CFR 50.72(b)(2)(ii) until 3:17. p.m., when directed to do

so by his management, on the basis that reportability was in doubt. River

Bend Nuclear Procedure RBNP-030, Revision 1, Change Notice 3, " Initiation and

Processing of Condition Reports," specifically listed the initiation of-

standby gas treatment on annulus pressure control system low flow as a non c.SF

control function and, therefore, was not reportable. The licensee concluded

that ESF component actuations, such as this event, which are caused by non-ESF-

control functions were not reportable. The inspector reviewed the licensee's

final reportability determination, and had no other questions on

reportability.

2.3 Inoperability of Both Control Building Filter Trains

At 2:21 p.m., on October 7, 1992, the licensee was notified by an independent

laboratory that the charcoal sample taken from control room ventilation filter

Train A had failed the methyl iodide penetration test. After every 720 hours0.00833 days <br />0.2 hours <br />0.00119 weeks <br />2.7396e-4 months <br />

of operation the charcoal adsorbers must be sampled-and analyzed for 'a methyl

iodide penetration of less than 0.175 percent, as required by Tachi.ical

Specification 4.7.2.d.

At 2:53 p.m., after validating the report, the licensee's radiological

protection representative notified the control room. At the time, Filter

Train B had been out of service for preventive maintenance. Consequently, the -

Shift Supervisor declared the plant in Technical Specification 3.0.3, which

required initiation of a plant shutdown within I hour. The entry time was

logged in as of 2:21 p.m. With the preventive maintenance work completed on

Train B, and only closure paperwork remaining, the shift. supervisor expedited

completion of the paperwork. At 3:07 p.m., the shutdown was initiated by

reducing reactor power from 79 percent to approximately 78 percent, power was

then held at 78 percent to allow time for the paperwork to clear on Train B to

minimize the down power transient. At 3:48 p.m., the paperwork on Train B was

cleared and the unit operationally tested. Technical Specification 3.0.3 was

exited and, by 4:30 p.m., power was restored to 79 percent.

The licensee reported the shutdown initiation required by Technical

Specifications at 5:41 p.m., but 10 CFR 50.72 requires a report to be made

within I hour of the initiation of such a plant shutdown; therefore, the

report was about 1 1/2 hours late. This was a violation of NRC regulations.

When the inspector questioned the delay, the licensee explained that the Shift

Supervisor was in doubt as to the reportability of this event because he felt

the shutdown would not be completed. Licensee management- had already

recognized and identified the violation and promptly counselled the shift'

supervisors involved in reporting the event, and the event described in

paragraph 2.2 above. These untimely reports were incorporated into operating

experience reviews so that all control room operators would understand the

licensee's policy to report on time when in doubt. In view of the minor

safety significance of this issue and the prompt corrective action taken, this

violation will not b6 subject to enforcement action because the licensee's-

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efforts in correcting the violation meet the criteria specified in Section VII

of the NRC's Enforcement Policy.

2.4 Overflow of the Reactor Drywell Pedestal Drain Sump

Between September 29 and October 2, 1992, the operators made several

unsuccessful attempts to pump down the drywell pedestal sump to maintain sump

water level within the detectable range of the sump level instruments. When

either pump was energized, the sump level did not . decrease, and the pump motor

current was equivalent to a nonloaded value. The pumps, located-in the-

drywell, were not accessible during power operation. The licensee's review

concluded, based on drywell temperatures, radiation monitor readings, and a

steady leak rate of about 0.02 gallons per minute (gpm), that the leak did not

appear to be reactor coolant. Condition Report 92-0823 documented the problem

and indicated that the unidentified leakage determination required by

Technical Specification 3.4.3.1 could not be performed if pedestal sump level

should rise above the level indicator range.

On October 6, while performing an operability evaluation, the licensee's

engineers discovered that the sump was already filled to overflowing and that

water level indications were changing at 185.4 gallons per inch of level, in

lieu of 9.9 gallons per inch, which was true when the level was in the sump.

At 6 p.m., the operators entered Technical Specification Action 3.4.3.1.b,

which allowed operation to continue for only 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; then, if the leakage

detection system was not restored, required the plant to be shut down within

the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. By October 7, engineering provided a detailed operability

evaluation and method to determine unidentified leakage using a manual

calculation that accounted for the 185.4 gallon per inch level changes. The

operators exited the action statement on October 7, after receiving the

operability evaluation and making a change to the procedure used to determine-

leakage. The evaluation was reviewed by the inspector with assistance from

the Region IV Division of Reactor Safety and the NRC Office of Nuclear Reactor

Regulation. No unacceptable conditions were identified.

Throughout the period from identification of the sump pump failures on

October 2 until the end of this inspection period, unidentified reactor

coolant leakage remained steady at a rate of approximately 0.02 gpm. On

October 15, the licensee implemented a prompt modification request to shift

the indicating range of the pedestal sump level indicator from 0 to 36 inches,

to 30 to 66 inches to allow for optimum outage planning for the sump pump

repairs and leak investigation.

The inspector reviewed the modification documentation and noted that it was

complete and in compliance with 10 CFR 50.59. There was sufficient margin

(about 5 feet)' before the water could touch the cables extending downward from

the withdrawn source range and intermediate range nuclear instruments. The

slow and steady rise of the water on the pedestal area floor indicated that

the leak was not deteriorating. The licensee planned to reduce power on

November 17 to inspect the drywell pedestal area, to assess the leakage

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source, and to repair the-pedestal sump pumps. The inspector concluded that

the licensee's corrective actions were appropriate. .

2.5 Loss of Neutral from 120 Vac Power Supply

On October 16, while troubleshooting equipment problems, electrical

technicians determined that the neutral wire from the feeder transformer to

Division I 120 Vac Distribution Panel ISCV*PNL8Al had failed open. This

placed the two bus bars in the panel electrically in series. The licensee-

measured phase-to-ground potentials of approximately 260 volts on one phase

and 0 volts on the other phase of the panel. Subsequently, the licensee de-

energized Panel ISCV*PNL8Al and declared it inoperable. De-energizing this

panel affected the following Division I equipment:

e Control Room Chillers lA and 1C

e Control Room Local Intake Radiation Monitor RMS*RE13A

e Fuel Building Filtration Train Fan 3A

e Main Steam Leakage Control System

o Penetration Valve Leakage Control System

o Remote Shutdown Panel

Technical Specification 3.8.3.1 requires that the Division I ac power

distribution system be energized with the reactor-at power. Therefore, with

Panel-ISCV*PNL8Al deenergized, the action statement requires the licensee to

reenergize the panel within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or be in at least hot shutdown within the

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next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. The licensee repaired the neutral cable and verified that the

voltages were acceptable. The operators declared the power distribution

system operable. However, because the loads on the panel may have been

subjected to overvoltage conditions, the licensee declared each of the loads

from Panel lSCV*PNL8Al inoperable until appropriate testing and inspection

could be performed to evaluate the circuits.

The operability evaluations included inspection, replacement of parts,

continuity checks, and engineering evaluations of equipment voltage ratings

for each load. Subsequent actions included energized voltage checks and

conducting applicable functional checks or surveillance tests, as appropriate.

The inspectors reviewed the licensee's operability evaluations and determined

that the licensee appeared to have taken appropriate measures to declare each

load operable.

As of the end of this inspection period the iicensee had not determined the

root cause.of the failed neutral connection in Panel ISCV*PNL8A1. As part of

the overall corrective action, the licensee performed visual inspections of

other distribution panels and found no similar problems. However, several old

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construction and startup tags were identified that had not been removed.

Also, some panels were found to contain an excessive amount of dirt and

debris. The licensee documented these findings for future corrective action.

The inspectors reviewed the licensee's maintenance history for 120 Vac

distribution panels. The licensee had completed preventive maintenance on six

of the 21 safety-related 120 Vac distribution panels associated with

Divisions I and II. The inspectors reviewed the six completed work packages.

For Panel ISCV*PNL2G1, the inspectors noted that the recorded neutral bus-to-

station ground resistance value was "Im+," which could be interpreted to mean

greater than 1 megohm. That was well above the acceptance criteria limit of

less than 1 ohm specified in Preventive Maintenance Procedure PHP-1015

" Preventive Maintenance of 125, 120/208V Distribution Cabinets (AC&DC)." The

licensee promptly checked that panel, and other panels inspected and tested by

the same individual, and found the resistances to be satisfactory.

The licensee concluded that this was a documentation error and that the safety

significance was minimal. In view of the licensee's prompt action to

reconcile the data and the absence of safety significance, a violation will

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not be cited, because the licensee's efforts met the criteria specified in

Section VII of the NRC's enforcement policy.

2.6 Main Circulation System Hypochlorite Tank Leak

On October 20, 1992, while filling, the licensee discovered a leak on the

10,000 gallon hypochlorite receiving tank. The leak rate was acout 0.2 gpm.

The fill was terminated, and the licensee installed a temporary patch. The

tank was surrounded by a berm, so no leakage was released to the adjacent

ground. No chlorine fumes were sensed in the plant vital and protected area.

The licensee's environmental personnel were notified, and the 'appropt late

authorities were notified. The Senior Resident Inspector was also informed.

The event was reported to NRC pursuant to 10 CFR 50.72(b)(2)(vi). The

inspector reviewed the licensee's corrective actions and concluded that the

licensee's approach appeared appropriate.

2.7 Containment Purae with Standby Gas Treatment Inoperable

On September 24,1992, at 12:05 a.m., control room operators initiated a

containment purge through the standby gas treatment system Filter Train A. At

the time, Filter Train B was re mved from service for maintenance. Technical

Specification 3.6.1.9 requires thet the primary containment purge 36-inch

supply and exhaust isolation valves be closed, except if the standby gas

treatment system is in the purge flow path and both trains of the standby gas

treatment system are operable.

Upon reviewing the control room logs the next day, the shift supervisor

realized that the Technical Specification did not allow this operation.

Technical Specification 3.6.1.9, Action Statement b, states that, without both

trains of the standby gas treatment system operable, discontinue 36-inch purge

system operation and close the open 36-inch valves or otherwise isolate the

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penetration within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> or be in at least hot shutdown within the next

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

According to the logs, the control room operators secured the purge and

isolated the system at 4:05 a.m. The licensee complied with the Technical

Specification action statement time frama.

Control room operators started the containment purge to support the backwesh

of a reactor water cleanup system demineralizer. The task was being performed

in accordance with System Operating Procedure (S0P)-0090, " Reactor Water

Cleanup System." S0P-0090 directed the operator to Section 5.4 of SOP-0059,

" Containment HVAC System."

The inspector reviewed Section 5.4, SOP-0059, and noted that a caution

statement read, "Only one Standby Gas Treatment train shall be operating in

the Containment Purge mode and both trains of Standby Gas Treatment must be

operable to use Standby Gas Treatment in the Containment Purge mode (Tech Spec 3.6.1.9.b.)." The operators failed to heed this statement in performing the

containment purge.

The inspector concluded that the operators' failure to follow S0P-0059 is in

violation of the licensee's Technical Specifications (Violation 458/92032-1).

Condition Report 92-0806 was initiated on September 24, 1992; however, as of

the end of this inspection period, the licensee had not implemented

appropriate corrective action. On November 6, the licensee discussed plans to

revise S0P-0059 to add a procedural step in lieu of the caution discussed

above, to incorporate the event into departmental training, to add a similar

caution to S0P-0090, and to add a related question to the operator

qualification test data bank.

2.8 Conclusions

e Overall, the licensee's response to operational events during the report

period was acceptable.

  • The plant responded as designed to the large,118 megawatt electrical

grid transient. The licensee's reportability determination of the event

was appropriate.

e A noncited violation was identified for failure to make a timely report

of a plant shutdown initiation required by Technical Specifications.

The licensee's actions to identify and correct the problem were good.

e The licensee's approach and response to increasing drywell pedestal sump

levels were considered to be adequate to ensure safety.

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e The licensee's response to a failed 120 Vac distribution panel was

considered to be good. However, a noncited violation was identified for

failure to follow preventive maintenance procedures prior to the event.

  • The licensee's approach to control a leak in the hypochlorite receiving

tank was considered adequate,

e A violation was identified for initiating high volume containment purge

with one train of the standby gas treatment system inoperable.

3 OPERATIONAL SAFETY VERIFICATION (71707)

The objectives of this inspection were to ensure that this facility was being

operated safely and in conformance with regulatory requirements, and that the

licensee's management control system was effectively discharging its

responsibilities for continued safe operation.

3.1 Control Room Observations

On October 10, 1992, the inspector noted a control room log entry at 1:43

p.m., where the Division I standby diesel generator was inoperable in the

maintenance mode to allow pre-start checks. At 3:01 p.m., a log entry was

made returning the diesel generator to an operational status. Techr,ical

Specification 3.8.1.1, Action b, required, with one diesel generator

inoperable, the demonstration of the operability of certain offsite AC sources

within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. The operators indicated that the checks were not performed.

The operators stated that, even though placing a diesel generator in

maintenance mode rendered it inoperable, the Technical Specification action

statement was not normally entered since it has taken less than 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to do

the prestart checks.

Condition Report 92-0833 was written to enter the problem into the licensee's

corrective action program. The inspector concluded that the practice of'not

entering the Technical Specification action statements for planned, short-

equipment outages was poor. The inspector discussed the issue with the

licensee. The licensee issued a night order requiring the operators to enter

into the control room log any short duration equipment inoperability as a

"short term limiting condition for operations." Failure to comply with

Technical Specification 3.8.1.1 is a violation of NRC regulations

(Violation 458/92032-2).

3.2 Plant Tours

During this inspection period, the inspectors conducted numerous inspection

tours of the plant. While some improvement was seen in housekeeping, some

areas of the plant required attention. In particular, at elevation 95 feet of

the turbine building near the south door, anticontamination clothing, trash,

pieces of material, and maslin cloths were scattered. This area had been set

up for release of nonradioactive material. This reflected a poor attitude on

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the part of the licensee's staff to ensure the careful and orderly release of

material. The inspectors discussed the issue with the licensee and corrective

actions were taken.

3.3 Security Coservations

Throughout the inspection period, the inspectors verified that persons within

the protected area properly displayed their key cards. Vital area portals -

were verified locked and alarmed based on passing through the portals ar.1 upon

visiting the central and secondary alarm stations.

On October 15, 1992, a visiting NRC inspector was issued his protected arer

badge and key card and entered the protected area. Several hours later a

dosimetry clerk identified that the inspector's general employee training had

expired several months earlier. The inspector exited the area and his key _

card access was deleted from_the system.

The licensee determined that the trainiag department had failtd to notify the

security department that the inspector's training had expired. The training

departuent prepared a list of those individuals no longer qualified once each

month. This list was used by security to remove the individuals' key cards

from active status. The visiting inspector's name was inadvertently

overlooked during this process.

The licensee's investigation identified three problem areas:

e The computer printouts were not user-friendly and required a manual

search to prepare the list each month.

e There was no verification process. One clerk prepared and issued the

monthly list independently.

e The list was hastily prepared on the last day of each month, resulting

in a high potential for error.

Training department personnel revised Training Program Procedure TPP-7-018,

" General Employee Training," under Interim Procedure Change IPC-7-018-5-3, to

define how this list of unqualified individuals will be prepared. This

revision included time frames designed to eliminate haste, independent

verification of the list prior to issuance, and use of a better-quality

compc'ar printout, more suited to developing this list. In' addition, the

licensee performed an audit to determine that key cards were only issued to ,

trained, qualified individuals. No additional discrepancies were identified.

Additionally, the licensee has committed to change the data in the access

computer program to make it an active system. Under this system, individual

key cards would carry an expiration date based on the training expiration

date. -Therefore, if a personnel error allows an expired badge to be issued,

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the computer would not allow the individual access to the protected area. The

licensee established a schedule date of December 1,1992, for implementation.

Issuance of a key card to an individual who was not properly trained is a

violation of security plan implementation procedures. However, the licensee-

identified violation is not being cited because the criteria specified in

Section VII of the NRC's Enforcement Policy were satisfied.

3.4 Radiation Protection Activities

On October 28, while inspecting the " hot" (radiologically controlled) machine

shop area, the inspectors observed radwaste workers sorting out numerous

yellow poly bags containing potentially radioactive trash, tools, and

material. The workers were in street clothes and were wearing cotton glove

liners, apparently to protect their hands from possible contamination. Some

of the bags were torn due to sharp edges on the material inside. While no

clothing or skin contaminations occurred, the inspectors questioned the

practice of handling these bags without protective clothing such as rubber

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gloves. The licensee upgraded the protective clothing requirements for this

work.

3.5 Conclusions

  • Overall, the licensee operated the paint in a safe manner.

e A violation was identified for failure to determine within I hour the

operability of offsite ac power sources when one diesel generator was

declared inoperable. A poor operating practice in entering Technical

Specification action statements was revealed by this issue.

  • While housekeeping improved in some areas of the plant, some a eas

required attention,

o A noncited violation of security plan implementation procedures was

identified for issuing of a key card to an individual whose training had

expired. The Director of Nuclear Station Security committed to

implement an active computerized system to correct the root cause of

this problem. This planned approach was excellent.

4 MONTHLY MAINTENANCE OBSERVATIONS (62703)

The station maintenance activities addressed.below were observed and

documentation reviewed to ascertain that the activities were conducted in

accordance with the licensee's approved maintenance programs, the Technical

Specifications, and NRC Regulations.

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4.1 Repair of Reactor Feed Pump

On October 2,1992, the inspector observed portion; of the replacement of the

rotating assembly f?r Reactor feed Pump C. The work was authorized under

Maintenance Work Order (MW0) R158697. The pump had been vibrating excessively

and, thus, it became necessary to reduce plant power to about 80 percent and

secure the pump for repairs. The inspector reviewed the work package and

found that it did not contain a high level of detail. The inspector noted

from the documentation that the repairmen doing the work were trained and

qualified to do the job. They performed the work in a profess: inal manner and

exhibited good radiological and housekeeping practices. The radiological

protection measures appeared appropriate to prevent the spread of

contamination and minimize exposures. Woro steps were appropriately

documented.

On October 6, after the pump was reassembled, the operators attempted to fill

the pump by opening the suction valve, but the inboard mechanical shaft seal

leaked and water began to flash to steam. The operator then isolated the

pump. -The inspector discussed the possible causes for the failure of the seal

with maintenance supervisory and management personnel and found that an 0-ring

gasket had moved out of position during assembly of the seal. Special clips

to hold the seal together during the assembly and alignment process were not

used and, as a' result, the seal did not function as designed. The inspector

noted that the repair procedure, Corrective Maintenance Procedure CMP 9019,

Revision 6B, " Reactor Feed Pump Disassembly, Inspection, Rework, and

Reassembly," did not address the clips, and the training and briefings given

to the repairmen did not assure correct assembly of the seal. Maintenance

personnel explained to the inspector that there once was a detailed procedure

in place that addressed the seals, but they could not find it. Failure to

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have an adequate procedure and/or adequate training of the repairmen

demonstrated a weakness in the licensee's maintenance program which resulted

in over 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> delay in getting the pump back in service and also caused

unnecessary additional work in a radiologically contaminated area. The seal

was successfully reworked and the pump returned to service.

4.2 Repair of Containment Unit Cooler IB Breaker

On October 30, 1992, the inspector observed maintenance activities associated

with Breaker IEFS*ACB076 for Containment Unit Cooler 18. The work was

authorized under MWO R158388 and was initiated to correct deficiencies

identified during preventive maintenance activities. The inspector noted

that, while there was no clearance established for this work, there were

sufficient electrical interlocks to permit a safe breaker rack-out. The

operaM rs properly authorized the work. The inspector also noted that the

appropriate shutdown Technical Specification action statement had been

entered. The job was witnessed by a quality control representative, who

verified the correct replacement parts and ensured that the shelf life of

consumables had not expired. The inspector verified that the electricians

were trained and qualified to perform the work.

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The electricians noted excessive wear on the freme where the holding pawl

shaft was attached and the system engineer decided to replace the breaker with

a spare currently installed in another panel. The HWO was properly revised

within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, and the system engineer assisted in verifying the spare as

being the proper breaker. The spare breaker was installed and retested in

acco,' dance with the MWO, and the faulty breaker was retained for inspection

and evaluation by the vendor. The inspector verified that the operators had

conducted an operational test of the unit cooler uefore exiting the Technical

Specification action statement, in view of the short outage time (72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />)

allowed by the Technical Specifications, the electrical maintenance foreman

provided full time supervision and support of the electricians. The system

enoineer and foreman involvements were strengths.

4.3 Leak in Diesel Generator Cylinder Head

On October 16, 1992, the %spector observed maintenance on Division I standby

diesel generator. The wu t was being performed under MW0 R059324. This work

order was written to trouoleshoot lubricating oil flow to the turbocharger.

During the maintenance, the licensee identified a small amount of water in the

oil and concluded that the leak was caused by a defect in a subcover hold down

bolt socket in cylinder Head No. 4. The licensee planned to issue a special

report on the causes and corrective actions for this failure.

The inspector observed the maintenance repairmen replace the cylinder head.

The proper clearances were in place, and the repairmen were following the job

plan. Adminittrative signoffs and approvals were in place. Cleanliness

controls were in effect and the repairmen were policing fellow workers on

materials controls. The repairmen appeared knowledgeable of the job

requirements and techniques.

The int $ector evaluated the results of the rocker arm test as descrs ed in

Step 10 in Revision 4 of the job plan The repairmen blue checked in valves

and checked the rockers in ace.ance with the vendor manual recommendations.

The clearances were checked against the acceptance criteria and found to be

satisfactory.

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4.4 Conclusions

  • Overall, maintenance activities observed during this report period were -

good.

e During Feedwater Pump C maintenance, the licensee exhibited a weakness

in getting sufficient detail into the procedure and/or providing

sufficient training or briefing of the repairmen. As a result,

potentially contaminated feedwater sprayed out of the inboard seal,

causing delays and otherwise avoidable rework in a contaminated zone.

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e The work and controls to repair a containment unit cooler breaker were

considered good. System engineering support and electrical foreman

oversight for the activity were identified as strengths,

e The workers were knowledgeable of the job requirements and techniques t

for repair of the Division I standby diesel generator. The acceptance

criteria were met for the work observed.

5 BIMONTHLY SURVEILLANCE OBSERVATIONS (61726)

The inspectors observed the surveillance testing of safety-related systems and

components to verify that u.e activities were being perfo.med in accordance

with the licensee's approved programs and the Technical Specifications.

5.1 Division 1 Diesel Generator Operability Test

On October 13, 1992, the inspector observed the performance of an oserability

tv:t of the D' sion I standby diesel generator, as required by Tec1nical

Specification 4.8.1.1.2.a using Surveillance Test Procedure STP-309-021,

Revision 9A, " Diesel Generator Division 1 Operability Test." The test was

performed by a reactor operator trainee under the direct supervision of a

licensed reactor operator. The control operating foreman provided additional

oversight. The operator followed the applicable procedure in a step-by-step

manner, and self-checking was evident. The inspector watched as the control

room operator verified prerequisites completed and then performed a manual

start of the diesel generator. The timing test was satisfactorily completed

using a calibrated stopwatch.

The inspector went to the diesel generator room after the machine achieved

rated load. The diesel was functioning well with no fuel oil or lubricating

oil leaks of any consequence. Upon reviewing the official, signed off copy of

the above referenced procedure, the inspector noted that the independent

verification signature blank was not signed off at Step 7.5.1 This step

closed the turbocharger prelube valve after starting the diesel to prevent the

electric lubricating oil circulating pump from tripping during diesel

shutdown, thus starving hot bearing surfaces from needed lubricating oil.

Upon questioning the equipment operator, he stated that the verification was

done, and then another operator, who stated he did the verification, promptly

signed the verification signature blank. This demonstrated a possible

weakness in the licensee's independent verification program. This was

discussed between the inspector and the Assistant Plant Manager-0perations,

Radwaste and Chemistry, who agreed to review the procedure for possible

revision 'to clearly indicate what must be independently verified and when.

The rem 4inder of the diesel generator surveillance test was condur :nd in an

excellent manner. All acceptance criteria were met.

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5.2 Diesel-Driven Fire Pump Operability Test

On October 26, 1992, the inspector observed the performance of Surveillance

Test Prccedure STP-251-3205, " Diesel Fire Pump Operational Test," and STP-251-

3101, " Fire Protection Water System Minimum Water Volume Check." The portions

observed included the operability test of Diesel Fire Pump 1A as required by

Technical Specification 4.7.6.1.2.a.1 and 4.7.6.1.2.a.2.

The inspector observed preparations for these tests and determined that the

prerequisites were met. The inspector noted that the operator used a broom

handie as a dip stick to determine the level in Fuel Oil Tank 1F0F-TKlA

because the permanent level indicator was out of service. Technical

Specification 4.7.6.1.2.a.1 required the licensee to verify that the fuel day

tank contained at least 300 gallons of fuel. Additionally, Surveillance Test

Procedure STP-25 -3205 required that the operator verify that there was

sufficient fuel to operate the engine without going below 300 gallons.

The operations supervisor careed that using a broom handle as a substitute dip

stick was not the appropritte way to perform this procedure. Initially, the

licensee measured the broom handle and determined that the mark was 1 inch

above the level that is equivaient to 300 gallons. Therefore, the licensee

concluded that the Technical Specification requirements had been met.

Previously, the licensee had reviewed the maintenance history on the process

level indicator for the tank. The indicator had failed a number of times.

Therefore, the licensee had placed a hold on the repair of the indicator for

engineering to evaluate the use of a better design. This review had been

delayed for some time. By the end of the inspection period, the licensee had

repaired the process level indicator for fuel Oil Tank 1F0F-TKlA.

The inspector reviewed the records for nuclear equipment operators and

determined that the operator was qualified to perform these tests.

The inspector reviewed both procedures and determined that they met the

Technical Specification surveillance requirements. The tests were

appropriately released for performance and were included in the surveillance

test progress 109 The inspector noted that Surveillance Test

Procedure STP-251-3205 removed both Fire Pumps A and B from service. However,

the c' 3 trol room log did not document entry into the action statement. The

licensee indicated that the practice had been to not enter action statements

for short-term items. This issue is discussed in paragraph 3.1 of this

report.

The inspector reviewed the calibration records for level Indicator 1FPW-Lil3A

and Flow Indicator IFPW-F1109. Each instrument was within its calibration

cycle. The inspector reviewed the data sheets following the tests ano

determined that all parameters met the Technical Specification acceptance

criteria. Both tests were performed within the time frames required by

Technical Specifications.

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5.3 Conclusions j

e Overall, the licensee's performance of surveillance tests during the  !

report period was good.

e The licensee's performance of the Division I standby diesel generator

surveillance on October 13 was excellent, except for a possible weakness

indicated in the implementation of the licensee's independent

verification program.

  • Weaknesses were identified during the surveillance of the fire aumps in

that an operator was forced to use a broom handle to verify tan (' level

when the permanent indicator was out of service, and the removal of both

diesel-driven pumps from service was not logged to allow tracking of

Technical Specification requirements.

6 REVIEW OF A COMPLEX SURVEILLANCE TEST (61701)

This portion of the inspection consisted of the review of the documentation

for the surveillance activities associated with vivision I Standby Diesel

Generator LEGS *EGIA performed during Refueling Outage 4. This review was

started with inspectins and observations of the work as documented in NRC

Inspection Report 50-0 1/92-24.

6.1 Discussion

The inspector reviewed four of the completed diesel generator vendor

procedures implemented by STP-309-7614, " Diesel Generator Inspection -

Division I and Division II." The procedures were performed on the Division I

diesel generator. The four vendor procedures reviewed were:

  • RF0-430, " Inspect gear train for Worn, Broken, Chipped or Otherw ae

Impaired Gear Teeth"

e RFO-412, " Fuel Injection Equipment Examination and Maintenance"

  • RFO-448, " Cylinder Head Removal and Reinsta11ation"

e RF0-459, " Cylinder Block Top Deck inspection by Visible Dye Penetration

Method"

The inspector reviewed the above completed procedures to verify that they were

the correct revision, changes were properly annotated in the procedure and had

been approved, quality control hold points were identified, and acceptance

criteria (documented where required) and step sign-of fs had been completed.

The inspector noteo that the procedures were vendor qeneric procedures and

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were updated prior to use,

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6.2 Conclusions  !

e The completed documentation for surveillance inspections of the

Division I standby diesel generator was good. The specific. required

sign offs were completed and the quality control hold points were

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observed. The procedure changes were well documented and properly

reviewed and approved.

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7 FOLLOWUP OF AN UNRESOLVED ITEM (92701)

7.1 (Closed) Unresolved Ittm 458/9226-01: Appropriateness of Procedural

Controls for the Inspection and Reassembly of the Division i Standby -

Diesel Generator

On' July 8, 1992, while licensee personnel were adjusting the valve settings on ,

the Division I standby diesel. generator, the~ engine failed to turn past top

dead-center on Cylinder 5 using the barring device. This event was reviewed

and documented in NRC-Inspection Report 50-458/92-26.

The ins)ector further reviewed the actions taken by the mechanics in

reassem)1ing the engine. Specifically, the licensee-stated that, when

installing the valve rocker arm, a good routine practice was to back out the

adjusting screw first. Had this step been performed, the engine would not

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have been damaged.

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Procedural controls are required by Technical Specification 6.8.1 for

maintenance .affecting safety-related equipment. The 3rocedures and job plans ,

for the work performed failed to require that the mec1anics properly set the

adjusting screw prior to reassembly. This is a violation

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(Violation 458/92032-3).

This violation was, considered for enforcement discretion; however, the~

licensee did not take adequate corrective action following.the discovery of

the' problems with Cylinder 5. -The licensee did.not perform Inspections which

would have identified the additional three bent push rods, prior to running -

the diesel generator, which had the potential for further damaging the safety-

related engine. Although the bent rods were found during a scheduled ,

inspection, it= is unclear that the_ bent push rods would have been readily

identified by inspecting personnel. Additionally,'the licensee has had ..

several recent events involving inadequate procedures and the acceptance of

the: inadequacies by plant maintenance personnel. Important maintenance steps

have been= missed because of the licensee's reliance on the skill-of-the-craft

when specific procedural steps would have been more appropriate.

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7.2 Conclusions 1

A violation was identified for failure to have adequate procedural controls

covering the maintenance activities on the Division I standby diesel

generator.

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8 REVIEW OF MOTOR OPERATED VALVE SIGNATURE TESTING ERRORS (92701)

8.1 10 CFR Part 21 Notification from liberty Technologies

On October 2,1992, the licensee received a 10 CFR Part 21 notification from

Liberty Technologies that discussed errors in the software supplied with the  ;

vendor's valve operation and test evaluation system (VOTES). The notification

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discussed two defects. First, the values for Young's Hodulus and Poisson's

Ratio used in the software was not precise enough to provide the +/- 3.5

percent accuracy assumed in the V0TES error analysis. The second problem

involved calibration errors of the strain gauge when the calibrator was placed

on the threaded portion of the stem PS'"a the antirotation device on small

diameter high-lead stems. This erec was +"A wr the fact that smaller stems

tended to twist, which caused a thin twg et diau cr that offset the

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thickening caused by the thrust of ti.. hatcr.

The effect was that the actual torque of tue valve motor was as much as

7 percent higher than previously calculated ;or valve stems made of 410-SS

material. This is the most commonly used ma'erial for valve stems ai River

Bend Station. However, the concern affected all valves already tested.

The licensee identified 34 valves in which the calibrator could have been

attached to the threaded portion of the stem above the antirotation device.-

for the stem geometries at River Bend Station, the licensee determined that

the predominant torque correction factor was less than 8 percent. However,

the licensee indicated that for a few valves it may be somewhat higher.

Both of these issues caused the indicated thrust to be less than the true

thrust. Therefore, the licensee determined that the thrust margins were not

in question. The concern was in exceeding the maximum allowable thrust

limits. The vendor performed weak link calculations for the licensee in the

past that showed considerable margins. Additionally, these margins were based

on continuous duty ratings. Therefore, based on a limited number of cycles

the margins would be even larger.

Based on this preliminary review, the licensea had provided an interim

operability call for all motor-operated valves previously tested with the

VOTES. Valve specific reviews were underway, and the licensee had obtained

new software which would make corrections to the recorded test data. The

licensee stated they would evaluate the specific valve operability if any of

the corrected values exceeded the allowable limits.

On October 28, the inspectors observed testing of the V0TES system on a

licensee mock-up. The technicians involved were knowledgeable of the system

and the restrictions. The problems identified in the 10 CFR Part 21

notification were well understood, and the impact was being evaluated. The

NRC is still reviewing the implementation of Generic Letter 89-10 on motor-

operated valve testing at River Bend Station.

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8.2 Conclusions

The technicians involved were knowledgeable of the VOTES system and the

restrictions. The problems identified in the 10 CFR Part 21 notification were

well understood, the impact was being evaluated, and the licensee was taking

appropriate corrective actions.

9 ONSITE REVIEW 0F A LICENSEE EVENT REPORT (92700)

9.1 (Closed) Licensee Event Report 458/92-018: Trip System for the "A"

Automatic Depressurization System Inoperable due to Hispositioned Root

Valve

This licensee event report involved a failure to comply with Technical

Specification 3.0.4, which prohibits entry into an operational condition when

the condition required for the Limiting Conditions for Operation are not met.

On September 6, 1992, reactor steam dome pressure was raised to about 100 psig

with the Train A automatic depressurization trip system inoperable, due to an

improperly positioned instrument root valve. The instrument and trip. system

monitored the discharge pressure of Residual Heat Removal System Pump A to

provide a permissive to the Train A automatic depressurization trip system.

The cause was failure to follow administrative requirements to properly change

a surveillance test procedure on August 22, when it became necessary to

connect a test gauge to a different point, thereby requiring the root valve to

be closed for installation and removal of the gauge. The procedure did r.ot

provide for this and, as a consequence, the restoration of this particular

valve was not covered.

While taking logs, the reactor operator noted that the trip units monitoring

the Pump A discharge pressure was reading about 65 psig higher then those

monitoring Pump B. Subsequent investigation revealed that the root valve was

inappropriately shut. Due to the reactor operator's promptness in identifying

the discrepancy, the safety significance of this event was minimal. Train A

automatic depressurization was inoperable for about 1 1/2 hours while it.was

required by Technical Specification 3.3.3 to be operable. The action

statement allowed Train A to be inoperable for up to 7 days before the plant

must be shut down and depressurized to below 100 psig. In addition, reactor

pressure did not exceed the operating range of Pump A, thus the pump could

have injected if called upon. The reactor operator's' actions were considered

to be a strength.

The licensee promptly initiated verification of accessible emergency core

cooling system valves. No additional discrepancies were identified, based on

the inspector's review of the documented valve lineup checksheets. The

licensee also counseled the personnel involved and issued a night order to

inform operations personnel on the lessons learned from this event.

Failure to comply with Technical Specification 3.0.4 was a violation of NRC

regulations; however, this licensee-identified violation is not being cited

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because the criteria specified in Section VII of the NRC's Enforcement Policy

were met.

9.1 Conclusions

A noncited violation was identified for failure to comply with Technical

Specification 3.0.4 when one automatic depressurization system trip system was

inoperable upon changing plant modes. The operators were alert in recognizing

these problems, and the licensee took prompt corrective action. Operator

identification of the problem was viewed as a strength.

10 OCCUPATIONAL HEALTH AND SAFETY INSPECTIONS (93001)

10.1 Corrective Actions to an Industrial Accident

On June 18, 1992, an individual working inside the drywell was injured by a

falling hoist, when the trolley carriage failed. This event was documented in

NRC Inspection Report 50-458/92-24.

NRC Inspection Report 50-458/92-24 concluded that the trolley was installed '

outside of the manufacturer's recommendations, that side lifts were being

performed against the manufacture's recommendations, that frequent inspections

of specific lifting equipment had not been performed, and that inspections of

lifting equipment were poorly documented and the inspection criteria was

vague.

TL inspector reviewed the licensee's corrective action for this event. The

licensee determined that one of the root causes for inadequate inspections was

inadequete training for tool room facility employees. Previously these

personnel had been expected to inspect trollies without appropriate training

or inspection criteria. The licensee had provided training for all tool room

employees on the proper configuration and inspection criteria for beam

trollies, to ensure that all parts were included and in good condition at the

time of issue. The licensee was in the process of developing a more specific

inspection document which will be included in General Maintenance

Procedure (GMP) 0014, " Control of Load Lifting Equipment."

The inspector reviewed a revision to GMP-0017, " General Rigging Practice."

This revision, in Change Notice 92-1264, held the individual in charge of the

lift responsible for ensuring that the trolley had been properly inspected and

identified per the requirements of GMP-0014. The licensee provided a Training

Material Discrepancy Report M-92-018 to incorporate this event into the

training program for rigging practices. The licensee stated that this will

ensure that qualified rigging personnel are trained on the proper

configuration and instal _lation practices associated with trolley use and

,

installation. The inspector reviewed this training material discrepancy

report and verified that it covered the appropriate material.

The inspector noted that the current procedure revisions do not allow the use

of generic beam trollies for applications which require specific trolley

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hoists. In addition, the licensee had painted "NOT FOR USE IN ORYWELL" on all

Harrington type trollies to prevent inadvertent misapplication on the drywell

monorail system.

This occupational health and safety administration item is closed.

10.2 Conclusions

The licensee's corrective actions for the June 18, 1992, event were considered

adequate and should preclude similar events.

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ATTACHMENT 1

1 PERSONS CONTACTED

1.1 Licensee Personnel

D. L. Andrews, Director, Quality Assurance

J. W. Cook, Senior Technical Specialist

T. C. Crouse, Manager, Administration

W. L. Curran, Cajun Site Representative

K. D. Garner, Licensing Engineer

P. D. Graham, Plant Manager

D. N. Lorfing, Supervisor, Nuclear Licensing

S. R. Radebaugh, Assistant Plant Manager, Maintenance

J. E. Spivey, Senior Quality Assurance Engineer

M. A. Stein, Supervisor, Balance of Plant Design Engineering

K. E. Suhrke, General Manager, Engineering and Administration

R. J. Vachon, Senior Compliance Analyst

J. E. Venable, Operations Supervisor

1.2 Other Personnel Contacted

The personnel listed above attended the exit meeting. In addition to the

above personnel, the inspectors contacted other personnel during this

inspection period.

2 EXIT MEETING

An exit meeting was conducted on November 6, 1992. During this m eting, the

inspectors reviewed the scope and findings of the report. The licensee did

not identify as proprietary, any information provided to, or reviewed by the

inspectors.

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