Section 6.0 of Development of RCS Pts...& Recommended Surveillance Withdrawal Schedule for Waterford Unit 3ML20062M144 |
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Waterford |
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Issue date: |
12/29/1993 |
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From: |
ASEA BROWN BOVERI, INC. |
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To: |
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Shared Package |
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ML20062M119 |
List: |
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References |
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C-MECH-ER-021-0, C-MECH-ER-021-R00, C-MECH-ER-21, C-MECH-ER-21-R, NUDOCS 9401060218 |
Download: ML20062M144 (9) |
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Category:GENERAL EXTERNAL TECHNICAL REPORTS
MONTHYEARML20195C3041999-05-28028 May 1999 Annual Rept on ABB CE ECCS Performance Evaluation Models ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20198H3911998-07-14014 July 1998 Non-proprietary Rev 5 to HI-961586, Thermal-Hydraulic Analysis of Waterford-3 Spent Fuel Pool ML20248E7781998-06-0101 June 1998 Annual Rept on ABB CE ECCS Performance Evaluation Models ML20198H4681998-05-20020 May 1998 Non-proprietary Rev 1 to HI-981942, Independent Review of Waterford Unit 3 Spent Fuel Pool Cfd Model ML20247A3891998-05-0101 May 1998 SG Eddy Current Examination (8th Refueling Outage) ML20199F5831998-01-29029 January 1998 Errata Change Pages for Rept HI-971628,for Section 8.6.1.2 & Table 8.1.Change Pages Submitted to Assure Consistency Between LAR & Calculations Performed for SFP Structural Analysis ML20198H4641998-01-28028 January 1998 Non-proprietary Rev 1 to HI-91700, Dynarack Validation Manual ML20141G7081997-07-0505 July 1997 To Rept on Vortexing in Condensate Storage Pool ML20140F1491997-04-16016 April 1997 Rev 3 to 10CFR50.59 Safety Evaluation ML20137G2141997-03-27027 March 1997 Non-proprietary Version of Licensing Rept for Reracking of Waterford 3 Sfps ML20094H4141995-11-0303 November 1995 Thermo-Lag Installed to Tested Fire Barrier Evaluation (GL 86-10 Evaluation) ML20086T3561995-07-31031 July 1995 Individual Plant Exam for External Events ML20094H4001995-05-30030 May 1995 Pyrolysis Gas Chromatography Analysis of 3 Thermo-Lag Fire Barrier Samples ML20078F1001995-01-31031 January 1995 Summary of Waterford 3 Criticality Safety Analysis for Fuel Enrichments Above 4.1 W/O U-235 Taking Credit for Fixed Burnable Poisons ML20078Q2951994-11-0909 November 1994 3 Ses Tsc/Osc Tabletop 4,941109 ML20078Q3111994-11-0707 November 1994 3 Ses EOF Tabletop 4,941107 ML20078Q2851994-10-12012 October 1994 3 Ses Tsc/Osc Tabletop 3,941012 ML20078Q3051994-10-10010 October 1994 3 Ses EOF Tabletop 3,941010 ML20078Q2741994-09-20020 September 1994 3 Ses Tsc/Osc Tabletop 2,940920 ML20078Q3021994-08-15015 August 1994 3 Ses EOF Tabletop 2,940815 ML20078Q2731994-05-25025 May 1994 3 Ses Tsc/Osc Tabletop 1,940525 ML20078Q3001994-05-23023 May 1994 3 Ses EOF Tabletop 1,940523 ML20062M1441993-12-29029 December 1993 Section 6.0 of Development of RCS Pts...& Recommended Surveillance Withdrawal Schedule for Waterford Unit 3 ML20059D3971993-10-31031 October 1993 Rev 0 to Development of RCS Pressure Temp Limits for 20 EFPYs (Fluence = 2.29 X 10(19) n/cm(2)) & Recommended Surveillance Withdrawal Schedule for Waterford Unit 3, Final Rept ML20198H3711991-11-12012 November 1991 Non-proprietary HI-91700, Dynarack Validation Manual ML20086C4241991-09-0505 September 1991 Design Engineering Program Assessment Executive Summary ML20073K8451991-03-31031 March 1991 Entergy Nuclear Performance Rept,Mar 1991 ML20199F5531991-03-31031 March 1991 Chin Shan Analyses Show Advantages of Whole Pool Multi-Rack Approach, from Nuclear Engineering International,Mar 1991 ML20072R2261991-03-20020 March 1991 3 Plant Ref Simulator Certification Package ML20056A7301990-06-30030 June 1990 Basemat Monitoring Program Special Rept 3 ML20246P2561989-07-31031 July 1989 Compliance W/10CFR50.62 Reduction of Risk from ATWS Events ML20245J5071989-07-31031 July 1989 Unit 3 Control Element Assembly Drop Time Tech Spec Change Justification ML20155E1311988-10-31031 October 1988 Compliance W/10CFR50.62,Reduction of Risk from ATWS Events ML20207L2881988-09-30030 September 1988 Basemat Monitoring Program,Special Rept 2, from Inception to Aug 1988 ML20155B7181988-09-0909 September 1988 Rev 1 to Louisiana Power & Light Co Response to US-NRC Bulletin 88-005 ML20154D0571988-09-0909 September 1988 Actions Completed by Louisiana Power & Light Co ML20151F1771988-06-30030 June 1988 1987 SALP Progress Rept Updated June 1988 ML20195G8941988-06-20020 June 1988 MSIV Guide Rail Failure Final Rept ML20151B7901988-03-31031 March 1988 1987 SALP Progress Rept W3P87-1746, Emergency Preparedness Exercise1987-10-14014 October 1987 Emergency Preparedness Exercise ML20234C1501987-07-31031 July 1987 Basemat Summary Rept ML20214M5571987-05-27027 May 1987 Draft Waterford 3 Nuclear Plant Island Structure Basemat Summary Rept. W/Two Oversize Figures ML20198H4061987-04-30030 April 1987 Non-proprietary HI-87113, Evaluation of Fluid Flow for In- Phase & Out-of-Phase Rack Motions ML20198H4421987-04-0707 April 1987 Non-proprietary HI-87112, Fluid Flow in Narrow Channels Surrounding Moving Rigid Bodies ML20198H4121987-04-0707 April 1987 Non-proprietary HI-87114, Estimated Effects of Vertical Flow Between Racks & Between Fuel Cell Assemblies ML20198H4371987-01-14014 January 1987 Non-proprietary HI-87102, Study of Non-Linear Coupling Effects ML20215N4601986-10-0101 October 1986 Program to Perform Confirmatory Analyses,Nuclear Plant Island Structure Basemat:Results of Analyses 1999-05-28
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F2891999-10-13013 October 1999 Drill 99-08 Emergency Preparedness Exercise on 991013 05000382/LER-1999-014, :on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B1999-10-12012 October 1999
- on 990910,reactor Shutdown Due to Loss of Controlled bleed-off Flow,Occurred.Caused by Rotating Baffle failure.Two-piece Rotating Baffle of Original Design Was Located & Installed,In Order to Repair RCP 2B
ML20217G7211999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Waterford 3 Ses. with 05000382/LER-1999-013, :on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included1999-09-23023 September 1999
- on 990825,exceeding TS Limits for RCS Cooldown Rate Was Discovered.Caused by Inadequate Content & Inadequate Implementation of TS Requirements.Page 2 of 2 in Attachment 2 of Incoming Submittal Not Included
05000382/LER-1999-012-01, :on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With1999-09-13013 September 1999
- on 990812,potential Operation with Both Control Room Normal Outside Air Intakes Valves Inoperable Occurred.Cause for Event Was Indeterminate.Seat Leakage Requirements Calculated.With
ML20211Q2141999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Waterord 3 Ses.With 05000382/LER-1999-011-01, :on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B1999-08-31031 August 1999
- on 990801,with Plant Operating 100% Power, Lowering RCP Seal Pressures,Along with Dropping Controlled bleed-off (Cbo) & Increasing Cbo Temp Discovered.Caused by fatigue-induced Failure of Rotating Baffle of RCP 2B
05000382/LER-1999-010-01, :on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity1999-08-26026 August 1999
- on 990726,discovered Inadequate Pumping Capacity in Dry Cooling Tower Area.Caused by Inadequate Design Control.Portable Pumps Were Installed in Each Dry Cooling Tower Areas to Ensure Sufficient Pumping Capacity
05000382/LER-1999-009-01, :on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established1999-08-26026 August 1999
- on 990727,discovered App R Noncompliance Condition Involving Inadequate Separation of Safe Shutdown Cables.Caused Design Analysis Deficiency.Compensatory Measures Were Established
ML20210Q6361999-07-31031 July 1999 Corrected Monthly Operating Rept for July 1999 for Waterford 3 ML20210S0581999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Waterford 3.With 05000382/LER-1999-008-01, :on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-021999-07-29029 July 1999
- on 990629,failure to Perform Testing of ESF Filtration Units Per TS Was Noted.Cause for Testing Charcoal Samples Contrary to TS Could Not Be Determined.All Future Analysis Will Be Performed IAW ASTM D3803-1989,per GL 99-02
05000382/LER-1999-007-01, :on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff1999-07-23023 July 1999
- on 990625,operation Outside Tornado Missile Protection Licensing Basis for turbine-driven EFW Pump & Steam Supply Piping,Was Discovered.Caused Indeterminent. Entergy Will Submit 10CFR50.90 to NRC Staff
ML20210D8951999-07-23023 July 1999 Safety Evaluation Accepting First 10-yr Interval Inservice Insp Plan Requests for Relief ISI-018 - ISI-020 05000382/LER-1999-006-01, :on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With1999-07-14014 July 1999
- on 990614,plant Experienced Automatic Reactor Trip Following Loss of 7kV Bus.Caused by Spurious Actuation of Relay on Either RCP 1A or 2A.Personnel Performed Final Switchgear Walkdown with Indications Normal.With
ML20209H3781999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Waterford 3 Ses. with 05000382/LER-1999-005-01, :on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested1999-06-24024 June 1999
- on 980702,determined That Four Contacts in Control Circuits of EFW Control Valves Were Untested.Caused by Personnel Error.Untested Contacts Have Been Tested
ML20195J8951999-06-17017 June 1999 Safety Evaluation Granting Relief for Listed ISI Parts for Current Interval,Per 10CFR50.55a(g)(5)(iii) ML20195J9741999-06-16016 June 1999 Safety Evaluation Supporting Amend 152 to License NPF-38 ML20207E8631999-06-0303 June 1999 Safety Evaluation Accepting Licensee 990114 Submittal of one-time Request for Relief from ASME B&PV Code IST Requirements for Pressure Safety Valves at Plant,Unit 3 ML20195D5491999-06-0303 June 1999 Safety Evaluation Supporting Amend 151 to License NPF-38 ML20195K3391999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Waterford 3 Ses.With ML20195C3041999-05-28028 May 1999 Annual Rept on ABB CE ECCS Performance Evaluation Models 05000382/LER-1999-004-02, :on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing1999-05-14014 May 1999
- on 990415,discovered That Complete Response Time for ESFAS Containment Cooling Function Had Not Been Performed.Caused by Response Time Testing Deficiency. Procedures Will Be Revised to Include Subject Testing
ML20206S7401999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Waterford 3.With ML20205T2621999-04-22022 April 1999 LER 99-S02-00:on 990216,contract Employee Inappropriately Granted Unescorted Access to Plant Protected Area.Caused by Personnel Error.Security Personnel Performed Review of Work & Work Area That Individual Was Involved with ML20206A9641999-04-21021 April 1999 Safety Evaluation Supporting Amend 150 to License NPF-38 05000382/LER-1999-003-02, :on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With1999-04-0909 April 1999
- on 990311,determined That Four Containment Vacuum Relief valves,CVR-101,CVR-201,CVR-102 & CVR-202,were Not Tested.Caused by Contractor Supply of Misinformation. Details of Event Discussed with Contractor.With
ML20205N9671999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Waterford 3 Ses.With ML20205E8531999-03-30030 March 1999 Corrected Pages COLR 3/4 1-4 & COLR 3/4 2-6 to Rev 1, Cycle 10, Colr ML20205A6331999-03-25025 March 1999 SER Accepting Request to Use Mechanical Nozzle Seal Assemblies as an Alternative Repair Method,Per 10CFR50.55a(a)(3)(i) for Reactor Coolant Sys Applications at Plant,Unit 3 05000382/LER-1999-002-03, :on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired1999-03-25025 March 1999
- on 990225,discovered RCS Pressure Boundary Leakage on Two Inconel 600 Instrument Nozzles.Caused by Axial Cracks Near HAZ of Nozzle Partial Penetration Welds Resulting from Pwscc.Leaking Nozzles Have Been Repaired
ML20204H1401999-03-23023 March 1999 Rev 1 to Engineering Rept C-NOME-ER-0120, Design Evaluation of Various Applications at Waterford Unit 3 ML20204H1231999-03-22022 March 1999 Rev 1 to Design Rept C-PENG-DR-006, Addendum to Cenc Rept 1444 Analytical Rept for Waterford Unit 3 Piping ML20204H2451999-03-22022 March 1999 Rev 2 to C-NOME-SP-0067, Design Specification for Mechanical Nozzle Seal Assembly (Mnsa) Waterford Unit 3 ML20204F0791999-03-17017 March 1999 Rev 1 to Waterford 3 COLR for Cycle 10 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207F3491999-03-0505 March 1999 LER 99-S01-00:on 990203,contraband Was Discovered in Plant Protected Area.Bottle Was Determined to Have Been There Since Original Plant Construction.Bottle Was Removed & Security Personnel Performed Search of Area.With ML20204B5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Waterford 3.With ML20203H8151999-02-17017 February 1999 Safety Evaluation Supporting Amend 149 to License NPF-38 ML20203H8591999-02-17017 February 1999 Safety Evaluation Accepting Licensee Second Ten Year ISI Program & Associated Relief Requests for Plant,Unit 3 05000382/LER-1999-001, :on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With1999-02-0404 February 1999
- on 990105,TS 3.0.3 Was Entered.Caused by Less than Adequate Chiller Thermostat Control.Placed Tamper Seal on Chiller Thermostat.With
ML20202H9161999-02-0202 February 1999 Safety Evaluation Supporting Amend 148 to License NPF-38 ML20199H6261999-01-21021 January 1999 Safety Evaluation Accepting Classification of Instrument Air Tubing & Components for Safety Related Valve Top Works.Staff Recommends That EOI Revise Licensing Basis to Permit Incorporation of Change 05000382/LER-1998-020, :on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With1998-12-31031 December 1998
- on 981204,determined That Certain Core Power Distribution SRs Had Been Incorrectly Scheduled.Caused by TS Change Implementation Error.Will Perform Final Review of TS SRs with 4.0.4 Exemption.With
ML20199C9101998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Waterford 3.With ML20198F4691998-12-21021 December 1998 Safety Evaluation Supporting Amend 147 to License NPF-38 ML20196F4911998-12-0101 December 1998 SER Accepting Request for Relief ISI2-09 for Waterford Steam Electric Station,Unit 3 & Arkansas Nuclear One,Unit 2 ML20206N4131998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Waterford 3.With ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program 1999-09-30
[Table view] |
Text
-
a J.,
ATTACHMENT 1 SECTION 6.0 0F ABB' COMBUSTION ENGINEERING NUCLEAR SERVICES REPORT C-MECH-ER-021 DATED OCTOBER 11, 1993 I
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- 6.0 SURVEILLANCE CAPSULE WITHDRAWAL SCHEDULE The Waterford 3 reactor has 6 surveillance capsules designed to monitor the changes.
in beltline material propenies (Ref. 21). The governing withdrawal schedule for these capsules as required by 10 CFR 50, Appendix H, is defined in Table 5.3-10 of the Waterford 3 Final Safety Analysis Report (FSAR) (Ref. 22). This current withdrawal schedule is presented in Table 7 along with the capsule identification number and original target fluence as presented in Reference 3.
Capsule 2, located at the 97 degree position. (also referred to as capsule W-97) was removed, and the encapsulated specimens were tested.. A major result in the W-97 l capsule repon peninent to the capsule removal schedule was a change in the capsule lead factors. The lead factor is defined as the ratio of neutron flux density at the
[
location of the specimens in a surveillance capsule to the neutron flux density of the.
-i inside surface at the peak fluence location (Ref. 23). For capsules W-104 and W-284-i the lead factor was revised from 1.5 to 0.81 (Ref. 3) and for the remaining capsules (W-83, W-97, W-263 and W-277) the lead factor was revised from 1.5 to 1.26 in Reference 3.
A revised schedule was developed using the lead factors provided by Reference 3 and the guidance of ASTM E185-82 in accordance with current 10 CFR. 50, Appendix H requirements. Factors external to the ASTM E185-82 procedure that were also considered included:
1.
Coordination with the generation of P-T limits and LTOP evaluation beyond 20 EFPY. - If additional smveillance capsule information is'to be used to i
support the generation of P-T limits and an LTOP evaluation beyond 20 -
EFPY, the next capsuir withdrawal must allow for enough time to analyze the encapsulated materials as well as develop new P-T limits and LTOP requirements prior to 20 EFPY.
2.
Potential for we of Position 2 of Regulatory Guide 1.99, Rev. 2 - Surveillance-capsule data may be used in conjunction with Position 2 of R.G.1.99, Revi 2 to predict mean shift in reference temperature (ARTm) and decrease'in upper 3
shelf energy (USE) once credible surveillance data is obtained, One requirement for credibility is that, "the surveillance data for the correlation c
4 ABB Combustion Engineering Nuclear Services C4fECH-ER-021. Rev. 00 24
~
monitor material in the capsule should fall within the scatter band of the data base for that material" (Reference 8).
Capsule W-97 did not contain correlation material (Ref. 21), so the next capsule withdrawn must contain correlation material in order to allow for the use of Position 2 of R.G.1.99, Rev. 2. The two capsules that contain correlation material are W-104 and W-263 (Ref. 21).
3.
The reactor coolant cold leg temperature for Waterford 3 has been reduced by 8*F from 553*F to 545*F (Ref.13). The effect, if any, of this temperature reduction on the reactor vessel beltline materials must be monitored.
The new operating condition was evaluated, and it was determined that the requirements of 10 CFR 50, Appendix G and 10 CFR 50.61 are not affected.
by the temperature reduction of the cold leg (Ref.13). However, variations in the adjusted reference temperature (ART) and upper shelf energy (USE) of the surveillance material from predicted decreases must be monitored to verify the validity of the previous studies. This evaluation should be made at the time of the second surveillance capsule withdrawal, and modifications to the shift in ART and USE predictions can be made if necessary. The timing of the second capsule withdrawal should be such that significant variations from predictions 1 can be detected early enough to ensure that the P-T limits based on the ART predictions remain conservative.
4.
The surveillance capsule withdrawal schedule should be managed with consideration given to plant license renewal. Enough capsules must be tested to assure confidence in beltline material properties, but capsules should also be conserved to allow for future testing beyond the current design lifetime.
The guidelines provided 'in Section 7. " Irradiation Requirements" and Subsection 7.6,-
" Number of Surveillance Capsules and Withdrawal Schedule" of ASTM E185-82 (Ref. 23) are currently required by 10 CFR 50, Appendix H for establishing.the surveillance capsule withdrawal schedule. A' review of the proposed revised standards (Ref. 24) showed no changes affecting the method for determining the. withdrawal schedule. Therefore, future modifications to 10 CFR 50 Appendix H by reference to this revised ASTM E185-93 standard are not expected to alter the capsule withdrawal ABB Combustion Engineering Nuclear Services C-MECH-ER-02), Rev. 00 25
l requirements.
i According to ASME E185-82 (Ref. 23), the peak vessel inside fluence at EOL and the corresponding transition temperature shift must be estimated to determine the
[
number of capsules required for removal. Waterford 3 has a peak EOL fluence of f
2 2
1 3.69 x'10 n/cm (Ref. 3) and a 1/4t fluence of 2.20 x 10 n/cm. (using equation 3 of R.G.1.9% Rev. 2 to attenuate fluence to the 1/4t location).
a Based on the calculations of RTns (Table 6), the largest shift in reference temperature (ARTsm) at EOL is 59.4*F (note that the method in'10 CFR 50.61 for calculating ARTns and the R.G.1.99, Rev. 2 method for calculating ARTsm produce equivalent results). Using ASTM E185-82, it was determined that 3 capsules must be withdrawn in the following order.
First Capsule: - (Removed and tested)
Second Capsule: At 15 EFPY or at the time when the accumulated neutron fluence of the capsule corresponds to the auproximate EOL fluence at the reactor vessel inner wall location, whichevar comes first.
Third (Final) Capsule: At EOL but not less than once or greater than twice the peak EOL vessel fluence. This may be modified on the basis of previous tests. This capsule may be held without testing following withdrawal.
The second capsule to be withdrawn could be either W-104 or W-263 to obtain credible surveillance data. However, capsule W-104 has a low lead factor (0.81),
whereas capsule W-263 has a high lead factor (1.26). It is preferred to withdraw capsule W-263 for the second capsule, as the capsule fluence would be greater than the peak surface fluence received by the vessel. Capsule W-263 would be expected to receive a fluence equivalent to the EOL fluence at the reactor vessel inner wall at
]
25.4 EFPY (32 EFPY/1.26).
l ABB Combustion Engineering Nuclear Senices C MECH-ER-021. Rev. 00 26.
Given the criteria for withdrawal of the second capsule (above), capsule W-263 should be withdrawn at 15 EFPY, The capsule fluence corresponding to 15 EFPY 2
was estimated to be 2.18 x 10 n/cm using the lead factor of 1.26 and linear interpolation of the EOL vessel fluence of 3.69 x 10t' n/cm E ven in Reference 3.
2 i Modifying the withdrawal schedule to meet the current edition of ASTM standards calls for the last capsule to be removed between 25.4 and 50.8 EFPY. It 6 suggested that capsule withdrawal occur no later than 32 EFPY because this time correspends to the plant ECL. This will correspond to a capsule fluence of 4.65 x 102' n/cm,
2 Given the requirements of 10 CFR 50, Appendix H and ASTM E185-82 along with the plant-specific considerations for Waterford 3, Table 8 presents the recommended-schedule'for the Waterford 3 reactor vessel surveillance capsule removal program:
This schedule meets ASTM E185-82 requirements for capsule withdrawal (Ref. 23) as currently required by 10 CFR 50, Appendix H. It allows for detection of any effect on ARTsor or decrease in USE which could result from the reduction in cold leg -
temperature. This schedule should make available credible surveillance data for analyses following Position 2 of Regulatory Guide 1.99, Revision 2 (Ref. 8), and it :
provides for capsule withdrawal and testing prior to a P-T limit modification ~
following 20 EFPY. This schedule will also allow for a sufficient number of standby-capsules (3) to be maintained for possible license renewal or tc-provide for other future contingencies.
i
. ABB Combustion Engineering Nuclear Services C-MECH ER-021. Rev. 00 27-
s ATTACHMENT 2 REACTOR VESSEL MATERIAL SURVEILLANCE PROGRAM -
i WITH0RAWAL SCHEDULE r
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TABLE 4.4-5 35
-REACTOR VESSEL MATERIAL SURVEILLANCE PROGRAM - WITH0RAWAL SC
' CAPSULE VESSEL LEAD g' NUMBER LOCATION FACTOR U
WITHORAWAL TIME (EFPY)*
.1 83*
w 1.50 Standby 2
97*
1.50 4.0 EFPY 3
lu4*
1.50 11.0 EFPY 6
284*
1.50 18.0 EFPY 4
263*
1.50
$5 Standby 277*
1.50 Standby
+
b
.t t
a
.if
- Withdrawal time may be modified to coincide.with those refueling outages or plant shutdowns most closely approaching the withdrawal schedule.
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ATTACHMENT 3 REACTOR VESSEL MATERIAL SURVEILLANCE PROGPAM -
WITHDRAWAL. SCHEDULE r
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4 REACTOR VESSEL MATERIAL SURVEILLANCE PROGRAM -
WITHDRAWAL SCHEDULE Capsule Capsule Azimuthal Lead Removal Target Fluence No.
I.D.
Location (deg.)
Factor Time (EFPY)
(n/cm:)
1 W-83 83 1.26 Standby 2*
W-97 97 1.26 4.44 6.47 x 10 8 3
W-104 104 0.81 Standby 4
W-263 263 1.26 15
- 2. i8 x 10
5 W-277 277
.1.26 25.4 3.69 x 10 '
to to 50.8 7.38 x 101' 1
Recommended Recommend d 9
s 32 s4.65 x 17' 6
W-284 284 0.81 Standby
- Values represent actual data on removed capsule.
1 j
i