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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0371994-04-26026 April 1994 LER 94-004-00:on 940324,found Five Slow Rods While Scram Time Testing Was Being Performed.Caused by Contamination of Internal Scram Solenoid Pilot Valve Head Assemblies. Corrective Action:Install New Head assemblies.W/940426 Ltr ML20046C3991993-08-0606 August 1993 LER 92-009-01:on 920509,observed That Some of Fuel Rod Compression Springs Compressed More than Expected for Assembly Exposure Achieved.Max Envelope Size of Lower Tie Plate Will Be reduced.W/930806 Ltr ML20045G7911993-07-0808 July 1993 LER 93-005-00:on 930608,indicated That Response Time Test for RCIC Low Steam Pressure Isolation Instrumentation Invalid.Caused by Inappropriate Test Method.Procedures Governing Method of Testing Will Be revised.W/930708 Ltr ML20045E9601993-06-30030 June 1993 LER 92-017-02:on 920804,reactor Scrammed Due to Low Primary Water Tank Level Signal.Implemented Minor Change Package Which Will Install DC to DC Converter Between 24 Volt DC Power Supply & Pw Tank Level transmitters.W/930630 Ltr ML20045C5261993-06-16016 June 1993 LER 93-004-00:on 930517,inboard Containment Isolation Valve Which Supplies Steam to RCIC Sys Automatically Isolated Due to Topaz Inverter Failure.Calibr Instructions & PM Program Will Be reviewed.W/930616 Ltr ML20045A0151993-05-28028 May 1993 LER 92-011-02:on 920608,determined That Design Inadequacies Could Result in Exceeding 10CFR100 Limits.Caused by Failure of Original Design to Specify leak-tight Const for Fan Housing.Shaft Seal Design installed.W/930528 Ltr ML20024G9701991-05-0606 May 1991 LER 91-002-00:on 910406,operating Module Breaker in Automatic Turbine Tester Circuitry Tripped Open,Deenergizing Control Solenoid for change-over Valve.Caused by Use of Undersized Circuit Breaker.Module replaced.W/910506 Ltr ML20029A3331991-02-13013 February 1991 LER 91-001-00:on 910114,Tech Spec Limiting Condition of Operation Action Was Not Satisfied After DG Removed from Standby Svc to Perform Preventive Maint.Caused by Personnel Error.Procedure Changed to Prevent recurrence.W/910213 Ltr ML20044A6881990-06-25025 June 1990 LER 90-009-00:on 900526,nonlicensed Personnel Performed Step Out of Sequence During Breaker rack-out & Caused LPCS Pump Breaker to Close.Operator Involved Counseled on Failure to Adhere to Breaker Operation procedure.W/900625 Ltr ML20043H2951990-06-15015 June 1990 LER 90-007-00:on 900516,discovered That Actions Taken for Inoperable Reactor Water Level Transmitter Not Adequate to Comply W/Requirements for Tech Spec 3.3.2.Caused by Personnel Error.Meetings Held w/personnel.W/900615 Ltr ML20043C6741990-06-0101 June 1990 LER 90-006-00:on 900502,review of Effluent Sample Analysis Revealed That Turbine Bldg Ventilation Exhaust Had Not Been Analyzed Exceeding Time Limit.Caused by Personnel Error. Training & Counseling conducted.W/900601 Ltr ML20042F2251990-05-0404 May 1990 LER 90-005-00:on 900406,discovered That Current Surveillance Practices for Stroke Testing Fresh Air Makeup Intake Valves Could Have Resulted in Unfiltered Pathway.Administrative Controls Placed on valves.W/900504 Ltr ML20012D8071990-03-22022 March 1990 LER 89-018-01:on 891215,determined That Inappropriate Quality Level Designations Applied to Class 1E Circuits, in Violation of Reg Guide 1.75.Caused by Discrepant Instrument Index Controls.Handswitch replaced.W/900228 Ltr ML20012D4801990-03-16016 March 1990 LER 90-003-00:on 900215,identified Potential Single Failure Scenario That Could Result in Unavailability of Both Core Spray Sys for Long Term post-LOCA Core Cooling.Detailed Heatup Evaluation Performed for Power bundle.W/900316 Ltr ML20012A1661990-02-28028 February 1990 LER 90-002-00:on 900124,discovered That Div II Solenoid Associated W/Secondary Containment Isolation Valve Did Not Operate During Quarterly Valve Stroke Time Tests.Caused by Procedure Inadequacy.Procedures changed.W/900227 Ltr ML20006E4521990-02-15015 February 1990 LER 89-015-01:on 891030,no Data or Evidence Found That Stroke Time Test Performed on Bettis Actuator for Isolation Damper Following Maint.Caused by Programmatic Weaknesses.New Computer Field Data Added to Work orders.W/900215 Ltr ML20006E0461990-02-0909 February 1990 LER 90-001-00:on 900112,determined That Tech Spec Reactor Coolant Cooldown Rate Limit of 100 Degrees F Exceeded in Reactor Bottom Head Drain Pipe.Caused by Programmatic Deficiencies.Incident Rept Form improved.W/900209 Ltr ML20006B8731990-01-29029 January 1990 LER 89-019-00:on 891230,total Loss of Plant Svc Water Experienced Due to Loss of Power to Supply Wells.Caused by Malfunction of Microwave Info & Control Sys.Periodic Microwave Operational Checks established.W/900129 Ltr ML20006B2781990-01-16016 January 1990 LER 89-017-00:on 890718,determined That Isolation for Postulated RWCU Blowdown Line Breaks in Piping Cold Rooms Was 80 S,Causing Plant to Operate in Unanalyzed Condition. Tech Spec Change Request Will Be submitted.W/900116 Ltr ML20005G2121990-01-12012 January 1990 LER 89-007-01:on 890508,RWCU Sys Isolated on Leak Detection Differential Flow Signal While Shifting RWCU Operation from pre-pump to post-pump Mode.Probably Caused by Inadequate Reactor Pressure.Procedure revised.W/900112 Ltr ML20005G2071990-01-12012 January 1990 LER 89-018-00:on 891215,design Basis Review of Instrumentation Determined That 71 Devices,Classified as nonsafety-related,contained in Class 1E Circuits.Caused by Level of Control on Instrument index.W/900112 Ltr ML20005D7411989-12-0606 December 1989 LER 89-016-00:on 891107,during Severe Thunderstorm,Lightning Struck Site,Causing Scram & HPCS Low Water Level Channels to Trip.Design Change Package Issued to Install Lightning Dissipation Sys on Vulnerable structures.W/891206 Ltr ML19332F0731989-11-29029 November 1989 LER 89-015-00:on 891030,no Data or Evidence Found for Stroke Time Test Required to Be Performed Following Maint on Bettis Actuator for Isolation Damper QSZ51F001.Caused by Personnel Error.Programmatic Enhancements initiated.W/891129 Ltr ML19325E6971989-10-31031 October 1989 LER 89-008-02:on 890523,two Redundant Secondary Containment Isolation Dampers Failed to Close within 4 Time Limit of Tech Spec 3.6.6.2.Caused by Malfunction of Exhaust Valves. Exhaust Valve replaced.W/891031 Ltr ML19325E6331989-10-27027 October 1989 LER 89-014-00:on 890929,RWCU Sys Isolated on Simulated Steam Line Tunnel High Temp Signal.Caused by Operator Failure to Perform self-verification Prior to Moving Bypass Switch. General Manager Held Briefings w/personnel.W/891027 Ltr ML20024F4561983-08-31031 August 1983 Updated LER 83-001/01X-2:on 830107,electrician Preparing to Route Cable Noticed Two Wall Penetrations Had Been Opened. Because Control Room Not Notified of Work,No Fire Watch in Effect.Caused by Personnel error.W/830831 Ltr ML20024E8741983-08-31031 August 1983 LER 83-108/01T-0:on 830817,radiation Monitor B Trip Setpoint Found High & Grab Samples & Analyses Started Late.Caused by Personnel Error.Personnel counseled.W/830831 Ltr ML20024E9111983-08-30030 August 1983 Updated LER 83-097/03X-1:on 830720,reactor Water Cleanup Auto Isolation Occurred.Caused by Delta Temp Channel B Indicating Temp Above Trip Point Limit.Investigation continuing.W/830830 Ltr ML20024F5091983-08-29029 August 1983 LER 83-112/03L-0:on 830730,while Troubleshooting Initiation Circuitry to Find Reason for Improper Operation of E12F087B & F025B,partial LOCA Signal Occurred.Caused by Error in Work Order.Administrative Fix underway.W/830829 Ltr ML20024F2091983-08-29029 August 1983 LER 83-111/03L-0:on 830730,during Performance of Work Order to Correct Malfunction W/Div I Isolation Reset Status lights,amphenol-type Signal Cable Connector in C/R Panel Disconnected.Caused by Personnel error.W/830829 Ltr ML20024E9311983-08-29029 August 1983 Updated LER 83-002/01X-1:on 830114,personnel Discovered Heat Detectors in Control Room Standby Fresh Air Sys Not Functionally Tested.Caused by Lack of Proper Procedure. Procedure rewritten.W/830829 Ltr ML20024F6131983-08-29029 August 1983 Updated LER 83-010/99X-2:on 830105,fire Protection Deficiencies on Redundant Raceways/Cables Discovered in Auxiliary,Turbine & Control Bldgs.Caused by Incomplete Const.Maint Work Now complete.W/830829 Ltr ML20024F6071983-08-29029 August 1983 Updated LER 82-050/99X-1:on 820806,Fire Detection Zone 2-10 Went Into Alarm Condition & Would Not Clear.Caused by Diesel Exhaust Fumes Drifting Into Corridor.Detectors Cleaned. Design Change submitted.W/830829 Ltr ML20024D8781983-07-29029 July 1983 LER 83-078/03L-0:on 830701,control Room Operators Unable to Maintain Air Receiver Pressure for Diesel Generator 11. Caused by Setpoint Drift on Relief Valves for diesel-driven & Electric motor-driven Air compressors.W/830729 Ltr ML20024D0891983-07-25025 July 1983 LER 83-079/03L-0:on 830625,auxiliary Trip Unit for High Drywell Pressure Indicated Trip Condition Yet No Reactor Protection Sys Trip Occurred.Caused by Defective Rosemount Auxiliary Trip Unit.Trip Unit replaced.W/830725 Ltr ML20024D0761983-07-25025 July 1983 LER 83-080/03L-0:on 830626,control Room Operators Experienced Problems W/Hvac Sys Involving Inadequate Cooling Capacity & Sys Losses.Partially Caused by Malfunctioning Condenser Cooling Water Flow Control valve.W/830725 Ltr ML20024B9941983-06-29029 June 1983 LER 83-072/01T-0:on 830615,operations Shift Supervisor Discovered Some Continuous Fire Watches Not Performed on 830614.Caused by Personnel Error.Personnel Reinstructed Not to Pull Fire Watch W/O approval.W/830629 Ltr ML20024C4031983-06-27027 June 1983 LER 83-071/03L-0:on 830607,RHR Shutdown Cooling Mode Isolated When Valve E12-F009 Closed.Caused by Blown Fuse. Fuse replaced.W/830627 Ltr ML20024B9981983-06-24024 June 1983 LER 83-070/03L-0:on 830525,reactor Water Cleanup Sys Isolated When Standby Liquid Control Pump B Breaker Closed. Caused by Personnel Error.Isolation Signal reset.W/830624 Ltr ML20024C3121983-06-22022 June 1983 LER 83-069/03L-0:on 830523,during Attempt to Reenergize Div II Motor Operated Valves,Shutdown Cooling Mode of RHR Sys & Reactor Water Cleanup Sys Isolated.Caused by Failure to Install Power Fuses.Fuses installed.W/830622 Ltr ML20023E0441983-05-27027 May 1983 Updated LER 83-058/01X-1:on 830311,discovered That Fire Watches Not Conducted in Two Areas of Fire Detection Zone 2-19.Limiting Conditions for Operation Entered on 830227. Caused by Personnel Oversight.Zone restored.W/830527 Ltr ML20023D4331983-05-12012 May 1983 LER 83-046/03L-0:on 830412,monthly Functional Surveillance for Div I Chlorine Detection Sys Not Performed by 830410. Caused by Personnel Error ML20023D4771983-05-11011 May 1983 LER 83-052/03L-0:on 830411,while Reviewing Vessel Head Installation Work Package,Discovered Head Flange/Vessel Flange Thermocouples Not Physically Reinstalled During Insulation Installation.Cause Under Evaluation ML20023C5591983-05-0909 May 1983 Updated LER 83-031/99X-1:on 830113,fire Rated Door OC104 Blocked Open to Route Temporary Discharge Hose from Hot Machine Shop Sump to Turbine Bldg Floor Drain Sys.Caused by Inadequacy of Present Sys.Mod to Be Completed by Sept 1983 ML20023D2511983-05-0909 May 1983 LER 83-049/03L-0:on 830409,during Cold Shutdown,Diesel Generator 12 Auto Start Not Available When Alarm Actuated. Caused by Condensate Drain Valve Downstream of Tank C Not Fully Closed.Compressors Reworked ML20023C5611983-05-0909 May 1983 Updated LER 83-004/01T-1:on 830110,penetration AP-72B Found Open & Had Been Open Since 821213.Caused by Planned Maint Work & Personnel Error.Hourly Fire Watch Established. Penetration to Be Resealed by 830630 ML20023C5511983-05-0909 May 1983 LER 83-048/01T-0:on 830423,suppression Pool Level Instrumentation Discovered Not Functionally Tested Since 830409.Cause Under Investigation.Instrumentation Tested Satisfactorily within 8 H ML20023B5541983-04-28028 April 1983 LER 83-060/03L-0:on 830329,during Cold Shutdown,Load Shedding & Div I LSS Sequencing Panel Failure Alarm Actuated.Caused by Failure of 15-volt Dc Power Supply Used to Power Solid State Electronics for Sys Logic ML20023B6731983-04-27027 April 1983 LER 83-061/03L-0:on 830328,one Solenoid Operated Freon Valve Found W/Blown Gasket.Caused by Defective Alco Controls Solenoid Operated Gasket.Valve Reworked W/Valve Repair Kit & New Gasket Installed ML20028G6031983-02-11011 February 1983 LER 83-019/03L-0:on 830112 & 20,one Smoke Detector in Zone 1-15 & Eight Detectors in Zone 2-18 Covered During Planned Maint Functions to Prevent False Alarms or Damage to Unit. Detectors Uncovered After Maint Completed 1994-04-26
[Table view] Category:RO)
MONTHYEARML20029D0371994-04-26026 April 1994 LER 94-004-00:on 940324,found Five Slow Rods While Scram Time Testing Was Being Performed.Caused by Contamination of Internal Scram Solenoid Pilot Valve Head Assemblies. Corrective Action:Install New Head assemblies.W/940426 Ltr ML20046C3991993-08-0606 August 1993 LER 92-009-01:on 920509,observed That Some of Fuel Rod Compression Springs Compressed More than Expected for Assembly Exposure Achieved.Max Envelope Size of Lower Tie Plate Will Be reduced.W/930806 Ltr ML20045G7911993-07-0808 July 1993 LER 93-005-00:on 930608,indicated That Response Time Test for RCIC Low Steam Pressure Isolation Instrumentation Invalid.Caused by Inappropriate Test Method.Procedures Governing Method of Testing Will Be revised.W/930708 Ltr ML20045E9601993-06-30030 June 1993 LER 92-017-02:on 920804,reactor Scrammed Due to Low Primary Water Tank Level Signal.Implemented Minor Change Package Which Will Install DC to DC Converter Between 24 Volt DC Power Supply & Pw Tank Level transmitters.W/930630 Ltr ML20045C5261993-06-16016 June 1993 LER 93-004-00:on 930517,inboard Containment Isolation Valve Which Supplies Steam to RCIC Sys Automatically Isolated Due to Topaz Inverter Failure.Calibr Instructions & PM Program Will Be reviewed.W/930616 Ltr ML20045A0151993-05-28028 May 1993 LER 92-011-02:on 920608,determined That Design Inadequacies Could Result in Exceeding 10CFR100 Limits.Caused by Failure of Original Design to Specify leak-tight Const for Fan Housing.Shaft Seal Design installed.W/930528 Ltr ML20024G9701991-05-0606 May 1991 LER 91-002-00:on 910406,operating Module Breaker in Automatic Turbine Tester Circuitry Tripped Open,Deenergizing Control Solenoid for change-over Valve.Caused by Use of Undersized Circuit Breaker.Module replaced.W/910506 Ltr ML20029A3331991-02-13013 February 1991 LER 91-001-00:on 910114,Tech Spec Limiting Condition of Operation Action Was Not Satisfied After DG Removed from Standby Svc to Perform Preventive Maint.Caused by Personnel Error.Procedure Changed to Prevent recurrence.W/910213 Ltr ML20044A6881990-06-25025 June 1990 LER 90-009-00:on 900526,nonlicensed Personnel Performed Step Out of Sequence During Breaker rack-out & Caused LPCS Pump Breaker to Close.Operator Involved Counseled on Failure to Adhere to Breaker Operation procedure.W/900625 Ltr ML20043H2951990-06-15015 June 1990 LER 90-007-00:on 900516,discovered That Actions Taken for Inoperable Reactor Water Level Transmitter Not Adequate to Comply W/Requirements for Tech Spec 3.3.2.Caused by Personnel Error.Meetings Held w/personnel.W/900615 Ltr ML20043C6741990-06-0101 June 1990 LER 90-006-00:on 900502,review of Effluent Sample Analysis Revealed That Turbine Bldg Ventilation Exhaust Had Not Been Analyzed Exceeding Time Limit.Caused by Personnel Error. Training & Counseling conducted.W/900601 Ltr ML20042F2251990-05-0404 May 1990 LER 90-005-00:on 900406,discovered That Current Surveillance Practices for Stroke Testing Fresh Air Makeup Intake Valves Could Have Resulted in Unfiltered Pathway.Administrative Controls Placed on valves.W/900504 Ltr ML20012D8071990-03-22022 March 1990 LER 89-018-01:on 891215,determined That Inappropriate Quality Level Designations Applied to Class 1E Circuits, in Violation of Reg Guide 1.75.Caused by Discrepant Instrument Index Controls.Handswitch replaced.W/900228 Ltr ML20012D4801990-03-16016 March 1990 LER 90-003-00:on 900215,identified Potential Single Failure Scenario That Could Result in Unavailability of Both Core Spray Sys for Long Term post-LOCA Core Cooling.Detailed Heatup Evaluation Performed for Power bundle.W/900316 Ltr ML20012A1661990-02-28028 February 1990 LER 90-002-00:on 900124,discovered That Div II Solenoid Associated W/Secondary Containment Isolation Valve Did Not Operate During Quarterly Valve Stroke Time Tests.Caused by Procedure Inadequacy.Procedures changed.W/900227 Ltr ML20006E4521990-02-15015 February 1990 LER 89-015-01:on 891030,no Data or Evidence Found That Stroke Time Test Performed on Bettis Actuator for Isolation Damper Following Maint.Caused by Programmatic Weaknesses.New Computer Field Data Added to Work orders.W/900215 Ltr ML20006E0461990-02-0909 February 1990 LER 90-001-00:on 900112,determined That Tech Spec Reactor Coolant Cooldown Rate Limit of 100 Degrees F Exceeded in Reactor Bottom Head Drain Pipe.Caused by Programmatic Deficiencies.Incident Rept Form improved.W/900209 Ltr ML20006B8731990-01-29029 January 1990 LER 89-019-00:on 891230,total Loss of Plant Svc Water Experienced Due to Loss of Power to Supply Wells.Caused by Malfunction of Microwave Info & Control Sys.Periodic Microwave Operational Checks established.W/900129 Ltr ML20006B2781990-01-16016 January 1990 LER 89-017-00:on 890718,determined That Isolation for Postulated RWCU Blowdown Line Breaks in Piping Cold Rooms Was 80 S,Causing Plant to Operate in Unanalyzed Condition. Tech Spec Change Request Will Be submitted.W/900116 Ltr ML20005G2121990-01-12012 January 1990 LER 89-007-01:on 890508,RWCU Sys Isolated on Leak Detection Differential Flow Signal While Shifting RWCU Operation from pre-pump to post-pump Mode.Probably Caused by Inadequate Reactor Pressure.Procedure revised.W/900112 Ltr ML20005G2071990-01-12012 January 1990 LER 89-018-00:on 891215,design Basis Review of Instrumentation Determined That 71 Devices,Classified as nonsafety-related,contained in Class 1E Circuits.Caused by Level of Control on Instrument index.W/900112 Ltr ML20005D7411989-12-0606 December 1989 LER 89-016-00:on 891107,during Severe Thunderstorm,Lightning Struck Site,Causing Scram & HPCS Low Water Level Channels to Trip.Design Change Package Issued to Install Lightning Dissipation Sys on Vulnerable structures.W/891206 Ltr ML19332F0731989-11-29029 November 1989 LER 89-015-00:on 891030,no Data or Evidence Found for Stroke Time Test Required to Be Performed Following Maint on Bettis Actuator for Isolation Damper QSZ51F001.Caused by Personnel Error.Programmatic Enhancements initiated.W/891129 Ltr ML19325E6971989-10-31031 October 1989 LER 89-008-02:on 890523,two Redundant Secondary Containment Isolation Dampers Failed to Close within 4 Time Limit of Tech Spec 3.6.6.2.Caused by Malfunction of Exhaust Valves. Exhaust Valve replaced.W/891031 Ltr ML19325E6331989-10-27027 October 1989 LER 89-014-00:on 890929,RWCU Sys Isolated on Simulated Steam Line Tunnel High Temp Signal.Caused by Operator Failure to Perform self-verification Prior to Moving Bypass Switch. General Manager Held Briefings w/personnel.W/891027 Ltr ML20024F4561983-08-31031 August 1983 Updated LER 83-001/01X-2:on 830107,electrician Preparing to Route Cable Noticed Two Wall Penetrations Had Been Opened. Because Control Room Not Notified of Work,No Fire Watch in Effect.Caused by Personnel error.W/830831 Ltr ML20024E8741983-08-31031 August 1983 LER 83-108/01T-0:on 830817,radiation Monitor B Trip Setpoint Found High & Grab Samples & Analyses Started Late.Caused by Personnel Error.Personnel counseled.W/830831 Ltr ML20024E9111983-08-30030 August 1983 Updated LER 83-097/03X-1:on 830720,reactor Water Cleanup Auto Isolation Occurred.Caused by Delta Temp Channel B Indicating Temp Above Trip Point Limit.Investigation continuing.W/830830 Ltr ML20024F5091983-08-29029 August 1983 LER 83-112/03L-0:on 830730,while Troubleshooting Initiation Circuitry to Find Reason for Improper Operation of E12F087B & F025B,partial LOCA Signal Occurred.Caused by Error in Work Order.Administrative Fix underway.W/830829 Ltr ML20024F2091983-08-29029 August 1983 LER 83-111/03L-0:on 830730,during Performance of Work Order to Correct Malfunction W/Div I Isolation Reset Status lights,amphenol-type Signal Cable Connector in C/R Panel Disconnected.Caused by Personnel error.W/830829 Ltr ML20024E9311983-08-29029 August 1983 Updated LER 83-002/01X-1:on 830114,personnel Discovered Heat Detectors in Control Room Standby Fresh Air Sys Not Functionally Tested.Caused by Lack of Proper Procedure. Procedure rewritten.W/830829 Ltr ML20024F6131983-08-29029 August 1983 Updated LER 83-010/99X-2:on 830105,fire Protection Deficiencies on Redundant Raceways/Cables Discovered in Auxiliary,Turbine & Control Bldgs.Caused by Incomplete Const.Maint Work Now complete.W/830829 Ltr ML20024F6071983-08-29029 August 1983 Updated LER 82-050/99X-1:on 820806,Fire Detection Zone 2-10 Went Into Alarm Condition & Would Not Clear.Caused by Diesel Exhaust Fumes Drifting Into Corridor.Detectors Cleaned. Design Change submitted.W/830829 Ltr ML20024D8781983-07-29029 July 1983 LER 83-078/03L-0:on 830701,control Room Operators Unable to Maintain Air Receiver Pressure for Diesel Generator 11. Caused by Setpoint Drift on Relief Valves for diesel-driven & Electric motor-driven Air compressors.W/830729 Ltr ML20024D0891983-07-25025 July 1983 LER 83-079/03L-0:on 830625,auxiliary Trip Unit for High Drywell Pressure Indicated Trip Condition Yet No Reactor Protection Sys Trip Occurred.Caused by Defective Rosemount Auxiliary Trip Unit.Trip Unit replaced.W/830725 Ltr ML20024D0761983-07-25025 July 1983 LER 83-080/03L-0:on 830626,control Room Operators Experienced Problems W/Hvac Sys Involving Inadequate Cooling Capacity & Sys Losses.Partially Caused by Malfunctioning Condenser Cooling Water Flow Control valve.W/830725 Ltr ML20024B9941983-06-29029 June 1983 LER 83-072/01T-0:on 830615,operations Shift Supervisor Discovered Some Continuous Fire Watches Not Performed on 830614.Caused by Personnel Error.Personnel Reinstructed Not to Pull Fire Watch W/O approval.W/830629 Ltr ML20024C4031983-06-27027 June 1983 LER 83-071/03L-0:on 830607,RHR Shutdown Cooling Mode Isolated When Valve E12-F009 Closed.Caused by Blown Fuse. Fuse replaced.W/830627 Ltr ML20024B9981983-06-24024 June 1983 LER 83-070/03L-0:on 830525,reactor Water Cleanup Sys Isolated When Standby Liquid Control Pump B Breaker Closed. Caused by Personnel Error.Isolation Signal reset.W/830624 Ltr ML20024C3121983-06-22022 June 1983 LER 83-069/03L-0:on 830523,during Attempt to Reenergize Div II Motor Operated Valves,Shutdown Cooling Mode of RHR Sys & Reactor Water Cleanup Sys Isolated.Caused by Failure to Install Power Fuses.Fuses installed.W/830622 Ltr ML20023E0441983-05-27027 May 1983 Updated LER 83-058/01X-1:on 830311,discovered That Fire Watches Not Conducted in Two Areas of Fire Detection Zone 2-19.Limiting Conditions for Operation Entered on 830227. Caused by Personnel Oversight.Zone restored.W/830527 Ltr ML20023D4331983-05-12012 May 1983 LER 83-046/03L-0:on 830412,monthly Functional Surveillance for Div I Chlorine Detection Sys Not Performed by 830410. Caused by Personnel Error ML20023D4771983-05-11011 May 1983 LER 83-052/03L-0:on 830411,while Reviewing Vessel Head Installation Work Package,Discovered Head Flange/Vessel Flange Thermocouples Not Physically Reinstalled During Insulation Installation.Cause Under Evaluation ML20023C5591983-05-0909 May 1983 Updated LER 83-031/99X-1:on 830113,fire Rated Door OC104 Blocked Open to Route Temporary Discharge Hose from Hot Machine Shop Sump to Turbine Bldg Floor Drain Sys.Caused by Inadequacy of Present Sys.Mod to Be Completed by Sept 1983 ML20023D2511983-05-0909 May 1983 LER 83-049/03L-0:on 830409,during Cold Shutdown,Diesel Generator 12 Auto Start Not Available When Alarm Actuated. Caused by Condensate Drain Valve Downstream of Tank C Not Fully Closed.Compressors Reworked ML20023C5611983-05-0909 May 1983 Updated LER 83-004/01T-1:on 830110,penetration AP-72B Found Open & Had Been Open Since 821213.Caused by Planned Maint Work & Personnel Error.Hourly Fire Watch Established. Penetration to Be Resealed by 830630 ML20023C5511983-05-0909 May 1983 LER 83-048/01T-0:on 830423,suppression Pool Level Instrumentation Discovered Not Functionally Tested Since 830409.Cause Under Investigation.Instrumentation Tested Satisfactorily within 8 H ML20023B5541983-04-28028 April 1983 LER 83-060/03L-0:on 830329,during Cold Shutdown,Load Shedding & Div I LSS Sequencing Panel Failure Alarm Actuated.Caused by Failure of 15-volt Dc Power Supply Used to Power Solid State Electronics for Sys Logic ML20023B6731983-04-27027 April 1983 LER 83-061/03L-0:on 830328,one Solenoid Operated Freon Valve Found W/Blown Gasket.Caused by Defective Alco Controls Solenoid Operated Gasket.Valve Reworked W/Valve Repair Kit & New Gasket Installed ML20028G6031983-02-11011 February 1983 LER 83-019/03L-0:on 830112 & 20,one Smoke Detector in Zone 1-15 & Eight Detectors in Zone 2-18 Covered During Planned Maint Functions to Prevent False Alarms or Damage to Unit. Detectors Uncovered After Maint Completed 1994-04-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F9921999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20212F5641999-09-23023 September 1999 SER Concluding That All of ampacity-related Concerns Have Been Resolved & Licensee Provided Adequate Technical Basis to Assure That All of Thermo-Lag Fire Barrier Encl Cables Operating within Acceptable Ampacity Limits ML20211Q3171999-09-0909 September 1999 Safety Evaluation Accepting BWROG Rept, Prediction of Onset of Fission Gas Release from Fuel in Generic BWR, Dtd July 1996 ML20216E4881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Grand Gulf Nuclear Station.With ML20211A6921999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20209J1961999-07-12012 July 1999 Special Rept 99-001:on 990528,smoke Detectors Failed to Alarm During Performance of Routine Channel Functional Testing.Applicable TRM Interim Compensatory Measure of Establishing Roving Hourly Fire Patrol Was Implemented ML20196K4981999-07-0101 July 1999 Safety Evaluation Authorizing PRR-E12-01,PRR-E21-01, PRR-P75-01,PRR-P81-01,VRR-B21-01,VRR-B21-02,VRR-E38-01 & VRR-E51-01.Concludes That Alternatives Proposed by EOI Acceptable ML20209G0691999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20196A1161999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Grand Gulf Nuclear Station.With ML20206Q4831999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Grand Gulf Nuclear Station Unit 1.With ML20206J1201999-04-30030 April 1999 Redacted ME-98-001-00, Pressure Locking & Thermal Binding Test Program on Two Gate Valves with Limitorque Actuators ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205P8771999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207K5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20206T7991999-01-31031 January 1999 Iodine Revolatizitation in Grand Gulf Loca ML20207A8301998-12-31031 December 1998 1998 Annual Operating Rept for Ggns,Unit 1 ML20206R9501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20206D7721998-12-31031 December 1998 South Mississippi Electric Power Association 1998 Annual Rept ML20198E2481998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20195F4121998-11-13013 November 1998 Rev 16 to GGNS-TOP-1A, Operational QA Manual (Oqam) ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20195C2791998-11-0505 November 1998 BWR Feedwater Nozzle Inservice Insp Summary Rept for GGNS, NUREG-0619-00006 ML20195F4801998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML20154K2391998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Grand Gulf Nuclear Station Unit 1.With ML20155F1961998-09-0101 September 1998 Engineering Rept for Evaluation of BWR CR Drive Mounting Flange Cap Screw ML20153B2161998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20237B6661998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Grand Gulf Nuclear Station,Unit 1 ML20236R0231998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Grand Gulf Nuclear Station,Unit 1 ML20155J0811998-05-31031 May 1998 10CFR50.59 SE for Period Jan 1997 - May 1998 ML20249B1251998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Grand Gulf Nuclear Station,Unit 1 ML20248B6261998-05-11011 May 1998 Rev 6 to Grand Gulf Nuclear Station COLR Safety-Related ML20217Q6701998-05-0606 May 1998 SER Approving Proposed Postponement of Beginning Augmented Exam Requirements of 10CFR50.55a(g)(6)(ii)(A)(2) at Grand Gulf for Circumferential Shell Welds for Two Operating Cycles ML20206J1271998-04-30030 April 1998 Pressure Locking Thrust Evaluation Methodology for Flexible Wedge Gate Valves ML20247F3591998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Grand Gulf Nuclear Plant,Unit 1 ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) ML20217P0381998-04-0606 April 1998 Safety Evaluation Supporting Amend 135 to License NPF-29 ML20217A0291998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Grand Gulf Nuclear Sation,Unit 1 ML20216J4211998-03-18018 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Grand Gulf Nuclear Station ML20216J2021998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Grand Gulf Nuclear Station,Unit 1 ML20203A2891998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Grand Gulf Nuclear Station ML20247B4111997-12-31031 December 1997 1997 Annual Financial Rept for South Mississippi Electric Power Association ML20203H9741997-12-31031 December 1997 1997 Annual Operating Rept, for Ggns,Unit 1 ML20198P1121997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Grand Gulf Nuclear Station,Unit 1 ML20203B5581997-12-0404 December 1997 Special Rept 97-003:on 971111,valid Failure of Div 2 EDG Occurred,Due to Jacket Water Leak.Failure Reported,Per Plant Technical Requirements Manual Section 7.7.2.2 ML20203K4031997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Grand Gulf Nuclear Station,Unit 1 ML20199H3711997-11-19019 November 1997 SER Accepting Approving Request Relief from Requirements of Section XI, Rule for Inservice Insp of NPP Components, of ASME for Current or New 10-year Inservice Insp Interval IAW 50.55(a)(3)(i) of 10CFR50 ML20199F3431997-11-18018 November 1997 SER Accepting Rev 15 of Operational Quality Assurance Manual for Grand Gulf Nuclear Station,Unit 1 1999-09-09
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e Energy ~ Tel 001437 6809 William T. Cottle ,
Vce Presdent I ; Noelcar Operahons i
March 12, 1990 U.S. Nuclear Regulatory Commission Mail Station P1-137 Washington, D.C. 20555 Attention: Document Control Desk Gentlemen:
SUBJECT:
Grand Gulf Nuclear Station Unit 1 Docket No. 50-416 License No. NPF-29 Loss of ESF Division 1 Power Could Effect Long-Term Post-LOCA Core Spray LER 90-003-00 '
AECH-90/0052 Attached is Licenseo Event Report (LER)90-003 which in an Interim report.
Yours truly, wrC%-
WTC:cg
-Attachment cc: Mr. D. C. Illutz (w/a)
Mr. T.11. Cloninger (w/a)
Mr. R. B. McGehee (w/a) gg"g Mr. N. S. Reynolds (w/a)
Mr.11. L. Thomas (w/o) lir. II. O. Christensen (w/a) w Mr. Stewart D. Ebneter (w/a)
F>O@$o Regional Administrator 88 U.S. Nuclear Regulatory Commission
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c;o 101 Marietta St., N.W., Suite 2900 Atlanta, Georgia 30323 om Nr
.g Mr. L. L. Kintner, Project Manager (w/a) orr Of fice of Nuclear Reactor Regulation
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.On February 15, 1990, System Energy Resources, Inc. (SEkI) identified a
! potential single failure scenario that could result in the l- unaval'1 ability of both core spray systems for long term post-LOCA core i cooling.- UFSAR Section 6.3.3.2 states that criterion 5 of 10CFR50.46 is
- l. demonstrated generically for General Electric (GE) BWRs in that the core remains covered to at least the jet pump suction elevation and the uncovered region is cooled by core spray. In a postulated LOCA scenario-where the single failure is the ESF Electrical Division 1, the Low Pressure Core Spray (LPCS) system and the Standby Service Water (SSW)
I "A" system would not be available. This would leave the High Pressure L Core Spray (HPCS) system (ESF Electrical Division 3) the only available l core spray. In the GGNS design, the HPCS service water and the Division 1 service water both return via the SSW "A" spray header. The relatively small return flow of the HPCS service water, without added SSW return flow from Division 1 components, would be insufficient to provide effective spray over the SSW "A" cooling tower fill. After approximately 50 to 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br />, HPCS service water temperature could exceed the 90 degrees F design temperature, and the availability of the HPCS system may not be assured. GE has performed an evaluation which demonstrated ECCS criteria are met assuming no credit for spray cooling after the initial 50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br /> of HPCS operation. SERI considers this evaluation adequate for interim operation and is evaluating the ultimate solution to the condition.
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A. Reportable Occurrence:
On February 15, 1990, System Energy Resources, Inc. (SERI)
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identified a condition that could affect the availability of the High Pressure Core Spray'(llPCS) system (EIIS code: BG).for long term post-LOCA core cooling. This condition is-reported pursuant to 10CFR50.73(a)(2)(v).
B.- Initial Condition:
=The plant was operating at 100 percent power at the time of.
discovery.
C. Description of Occurrence:
Criterion 5 of the acceptance criteria for_ECCS Systems in 10CFR50.46 states, "After any calculated successfully initial operation of the ECCS, the calculated core thermal temperature shall be maintained at an acceptably low value and decay heat .
shall be removed for the extended period of time required by the L long-lived radioactivity remaining in the core." UFSAR Section 6.3.3.2 states that conformance to this criterion is demonstrated
[ generically for General Electric (GE) BWRs in that the core I remains covered to at least the jet pump suction elevation and i the uncovered region is cooled by spray cooling.
1.
During a special review conducted as part of the Technical Specification Improvement Program, SERI design engineers identified a situation in.which the HPCS system could become unavailable after about 50 to 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> of: post-LOCA operation.
In a postulated LOCA scenario where a failure of ESF Electrical Division 1 occurs, the Division 1 Emergency Core Cooling (ECC)-
systems and support systems (Low Pressure Core Spray, Low Pressure Coolant Injection "A", and Standby Service Water "A")
would not be available for long term core cooling, llPCS, which 1- is powered from ESF Electrical Division 3, would be the only available core spray.
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D. Apparent'Cause: l i
Conformance to Criterion 5 of 10CFR50.46 was demonstrated generically for GE BWRs in section III. A of NEDO-20566, GE's LOCA Topical Report, submitted August 1974. The GGNS FSAR referenced this Topical Report and stated that the uncovered region of the core could be cooled by core spray and/or steam generated in the covered part of the core. GE identified concerns in 1984 that LPCI injection, inside the shroud, could subcool the water within
, some of the fuel bundles and thereby result in a reduction of long-term steam. cooling capability. The FSAR was then revised to_ '
clarify that core spray was the_only method utilized at GGNS for long-term cooling of the uncovered region of the core.
During- the 1984 reviews of the GE Topical Report and concerns raised by'GE over steam cooling, SERI did not recognize that the spray nozzle distribution concern could adversely affect HPCS.
long-term cooling availability. Thus, core spray with either LPCS or HPCS was deemed an acceptable means of long-term cooling for the uncovered area of the core.
E. Supplemental Corrective Actions:
GE completed'its specific evaluation for Grand Gulf Nuclear Station on February 22, 1990. 'The results of the evaluation confirmed that. adequate _long-term post-LOCA core cooling is assured with the two Division 2 LPCI systems. The GE evaluation demonstrated' compliance with all ECCS criteria using established conservative analytical techniques. .SERI'is investigating alternatives for final resolution of this concern. An update report will be' submitted by April 20, 1990 providing our planned resolution of this concern.
F. Safety Assessment-Thermal hydraulic evaluations performed by GE demonstrate that operation of the two LPCI pumps (LPCI "B" and LPCI "C") for long-term cooling will result in substantial spill over of water into the upper plenum which then drains through the fuel bundles.
This flow rate alone may provide adequate cooling to fuel bundles; however, equal distribution of the flow could not be a demonstrated. A detailed heatup evaluation was performed for '
some high power bundles assuming no cooling water flow from the upper plenum. This evaluation showed that long-term peak cladding temperatures (PCT) and local oxidation values were acceptable under the requirements of 10CFR50.46. Additional conservatism included in the GE evaluation are: a 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> basin g ..
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heatup time was used when a 60 hour6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> heatup time was demonstrated by ,
calculations; no credit was taken for basin cooling capabilities;
- the time limit was set by a 90 degree F llPCS Service Water temperature rather than the ultimate temperature at which equipment is expected to fail; and no credit was taken for lower ,
than the design APLilGR conditions in the upper third of the core.
Long1 term PCT and local oxidation values of approximately 1580 degrees F and 16 percent were obtained. Therefore, compliance with 10CFR50.46 is maintained and thera are no adverse safety consequences that result from the HPCS post-LOCA long-term availability. concerns.
In evaluating long-term post-LOCA core cooling without core
.. spray, GE used the 1979 version of ANSI /ANS 5.1 for calculation of decay heat load. The 1979 ANS 5.1 Decay IIcat Model differs from the previously used 1971 version by a factor of 1.2
-primarily due to differences in the decay heat uncertainty factors. The use of the 1979 standard is conservative and consistent with 10CFR50.46(a)(1)(1) in that sufficient supporting justification exists to show that the analytical technique realistically describes the behavior of the system during a LOCA, 10CFR50.46 was amended in 1988 to allow licensees to use either
. Appendix K or a realistic evaluation model (such as the 1979 ANS 5.1 Decay lleat Model). . In addition, Regulatory Guide 1.157 was issued in May, 1989 to describe alternate methods of implementing 10CFR50.46(a)(1). The Regulatory Guide endorses the 1979 edition of ANS 5.1 as-a generically acceptable method of calculating fission product decay heat. SERI. considers the application of the 1979 edition for determining the interim operability of the llPCS system and long-term post-LOCA core cooling capabilities to be acceptable and recognizes that the use of the standard as a licensing basis would have to be further justified to the NRC staff.
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By design, the HPCS service water system (EIIS code: BS) circulates cooling water from the SSW "A" basin through Division 3 components for heat removal and then discharges back into the SSW "A" basin. In the event that a loss of ESF Electrical Division 1 occurs, the relatively small return flow of the HPCS service water, without the added SSW return flow from Division 1 ,
1 components, would be insufficient to provide effective spray over the SSW cooling tower fill.- After a period of time (approximately 50 to 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br />) the HPCS Service Water temperature could exceed the'90' degrees F design temperature. Thus, long-term cooling of the HPCS service water and consequently the availability of the HPCS system may not be assured.
SERI conferred with General Electric after identifying this situation. GE performed an initial evaluation on February,15, 1990, which concluded that long term cooling could be ensured t after 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> without a core spray system based on the availability of the Division 2 Low Pressure Coolant Injection (LPCI) systems.
As GE continued with more specific evaluations to validate the conclusion, SERI developed contingency plans for the aforementioned scenario which will remain in effect until final resolution of the concern. In the event that Division 1 :
Electrical power supplies were unavailable but the distribution system was functional, the Division 3 Diesel Generator would be aligned'to the Division 1 distrib.ution system to utilize the Low Pressure Core Spray (LPCS)' system for core spray. If the Division 1 Electrical distribution system was not functional, measures would be taken to transfer water between the two SSW basins in an attempt to maintain the Division 1 SSW basin as cool as possible. Three different methods judged to be the most viabic in accomplishing the basin water transfer were established which include utilization of either the Division 2 SSW pump or temporary pumps as needed.
These plans were developed as interim and immediate response to the issue until the GE evaluation could be completed. The GE evaluation has been successfully completed and is described in the Safety Assessment below. To provide additional assurance the interim compensatory plans will remain in effect until the concern is resolved.
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