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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20029D0371994-04-26026 April 1994 LER 94-004-00:on 940324,found Five Slow Rods While Scram Time Testing Was Being Performed.Caused by Contamination of Internal Scram Solenoid Pilot Valve Head Assemblies. Corrective Action:Install New Head assemblies.W/940426 Ltr ML20046C3991993-08-0606 August 1993 LER 92-009-01:on 920509,observed That Some of Fuel Rod Compression Springs Compressed More than Expected for Assembly Exposure Achieved.Max Envelope Size of Lower Tie Plate Will Be reduced.W/930806 Ltr ML20045G7911993-07-0808 July 1993 LER 93-005-00:on 930608,indicated That Response Time Test for RCIC Low Steam Pressure Isolation Instrumentation Invalid.Caused by Inappropriate Test Method.Procedures Governing Method of Testing Will Be revised.W/930708 Ltr ML20045E9601993-06-30030 June 1993 LER 92-017-02:on 920804,reactor Scrammed Due to Low Primary Water Tank Level Signal.Implemented Minor Change Package Which Will Install DC to DC Converter Between 24 Volt DC Power Supply & Pw Tank Level transmitters.W/930630 Ltr ML20045C5261993-06-16016 June 1993 LER 93-004-00:on 930517,inboard Containment Isolation Valve Which Supplies Steam to RCIC Sys Automatically Isolated Due to Topaz Inverter Failure.Calibr Instructions & PM Program Will Be reviewed.W/930616 Ltr ML20045A0151993-05-28028 May 1993 LER 92-011-02:on 920608,determined That Design Inadequacies Could Result in Exceeding 10CFR100 Limits.Caused by Failure of Original Design to Specify leak-tight Const for Fan Housing.Shaft Seal Design installed.W/930528 Ltr ML20024G9701991-05-0606 May 1991 LER 91-002-00:on 910406,operating Module Breaker in Automatic Turbine Tester Circuitry Tripped Open,Deenergizing Control Solenoid for change-over Valve.Caused by Use of Undersized Circuit Breaker.Module replaced.W/910506 Ltr ML20029A3331991-02-13013 February 1991 LER 91-001-00:on 910114,Tech Spec Limiting Condition of Operation Action Was Not Satisfied After DG Removed from Standby Svc to Perform Preventive Maint.Caused by Personnel Error.Procedure Changed to Prevent recurrence.W/910213 Ltr ML20044A6881990-06-25025 June 1990 LER 90-009-00:on 900526,nonlicensed Personnel Performed Step Out of Sequence During Breaker rack-out & Caused LPCS Pump Breaker to Close.Operator Involved Counseled on Failure to Adhere to Breaker Operation procedure.W/900625 Ltr ML20043H2951990-06-15015 June 1990 LER 90-007-00:on 900516,discovered That Actions Taken for Inoperable Reactor Water Level Transmitter Not Adequate to Comply W/Requirements for Tech Spec 3.3.2.Caused by Personnel Error.Meetings Held w/personnel.W/900615 Ltr ML20043C6741990-06-0101 June 1990 LER 90-006-00:on 900502,review of Effluent Sample Analysis Revealed That Turbine Bldg Ventilation Exhaust Had Not Been Analyzed Exceeding Time Limit.Caused by Personnel Error. Training & Counseling conducted.W/900601 Ltr ML20042F2251990-05-0404 May 1990 LER 90-005-00:on 900406,discovered That Current Surveillance Practices for Stroke Testing Fresh Air Makeup Intake Valves Could Have Resulted in Unfiltered Pathway.Administrative Controls Placed on valves.W/900504 Ltr ML20012D8071990-03-22022 March 1990 LER 89-018-01:on 891215,determined That Inappropriate Quality Level Designations Applied to Class 1E Circuits, in Violation of Reg Guide 1.75.Caused by Discrepant Instrument Index Controls.Handswitch replaced.W/900228 Ltr ML20012D4801990-03-16016 March 1990 LER 90-003-00:on 900215,identified Potential Single Failure Scenario That Could Result in Unavailability of Both Core Spray Sys for Long Term post-LOCA Core Cooling.Detailed Heatup Evaluation Performed for Power bundle.W/900316 Ltr ML20012A1661990-02-28028 February 1990 LER 90-002-00:on 900124,discovered That Div II Solenoid Associated W/Secondary Containment Isolation Valve Did Not Operate During Quarterly Valve Stroke Time Tests.Caused by Procedure Inadequacy.Procedures changed.W/900227 Ltr ML20006E4521990-02-15015 February 1990 LER 89-015-01:on 891030,no Data or Evidence Found That Stroke Time Test Performed on Bettis Actuator for Isolation Damper Following Maint.Caused by Programmatic Weaknesses.New Computer Field Data Added to Work orders.W/900215 Ltr ML20006E0461990-02-0909 February 1990 LER 90-001-00:on 900112,determined That Tech Spec Reactor Coolant Cooldown Rate Limit of 100 Degrees F Exceeded in Reactor Bottom Head Drain Pipe.Caused by Programmatic Deficiencies.Incident Rept Form improved.W/900209 Ltr ML20006B8731990-01-29029 January 1990 LER 89-019-00:on 891230,total Loss of Plant Svc Water Experienced Due to Loss of Power to Supply Wells.Caused by Malfunction of Microwave Info & Control Sys.Periodic Microwave Operational Checks established.W/900129 Ltr ML20006B2781990-01-16016 January 1990 LER 89-017-00:on 890718,determined That Isolation for Postulated RWCU Blowdown Line Breaks in Piping Cold Rooms Was 80 S,Causing Plant to Operate in Unanalyzed Condition. Tech Spec Change Request Will Be submitted.W/900116 Ltr ML20005G2121990-01-12012 January 1990 LER 89-007-01:on 890508,RWCU Sys Isolated on Leak Detection Differential Flow Signal While Shifting RWCU Operation from pre-pump to post-pump Mode.Probably Caused by Inadequate Reactor Pressure.Procedure revised.W/900112 Ltr ML20005G2071990-01-12012 January 1990 LER 89-018-00:on 891215,design Basis Review of Instrumentation Determined That 71 Devices,Classified as nonsafety-related,contained in Class 1E Circuits.Caused by Level of Control on Instrument index.W/900112 Ltr ML20005D7411989-12-0606 December 1989 LER 89-016-00:on 891107,during Severe Thunderstorm,Lightning Struck Site,Causing Scram & HPCS Low Water Level Channels to Trip.Design Change Package Issued to Install Lightning Dissipation Sys on Vulnerable structures.W/891206 Ltr ML19332F0731989-11-29029 November 1989 LER 89-015-00:on 891030,no Data or Evidence Found for Stroke Time Test Required to Be Performed Following Maint on Bettis Actuator for Isolation Damper QSZ51F001.Caused by Personnel Error.Programmatic Enhancements initiated.W/891129 Ltr ML19325E6971989-10-31031 October 1989 LER 89-008-02:on 890523,two Redundant Secondary Containment Isolation Dampers Failed to Close within 4 Time Limit of Tech Spec 3.6.6.2.Caused by Malfunction of Exhaust Valves. Exhaust Valve replaced.W/891031 Ltr ML19325E6331989-10-27027 October 1989 LER 89-014-00:on 890929,RWCU Sys Isolated on Simulated Steam Line Tunnel High Temp Signal.Caused by Operator Failure to Perform self-verification Prior to Moving Bypass Switch. General Manager Held Briefings w/personnel.W/891027 Ltr ML20024F4561983-08-31031 August 1983 Updated LER 83-001/01X-2:on 830107,electrician Preparing to Route Cable Noticed Two Wall Penetrations Had Been Opened. Because Control Room Not Notified of Work,No Fire Watch in Effect.Caused by Personnel error.W/830831 Ltr ML20024E8741983-08-31031 August 1983 LER 83-108/01T-0:on 830817,radiation Monitor B Trip Setpoint Found High & Grab Samples & Analyses Started Late.Caused by Personnel Error.Personnel counseled.W/830831 Ltr ML20024E9111983-08-30030 August 1983 Updated LER 83-097/03X-1:on 830720,reactor Water Cleanup Auto Isolation Occurred.Caused by Delta Temp Channel B Indicating Temp Above Trip Point Limit.Investigation continuing.W/830830 Ltr ML20024F5091983-08-29029 August 1983 LER 83-112/03L-0:on 830730,while Troubleshooting Initiation Circuitry to Find Reason for Improper Operation of E12F087B & F025B,partial LOCA Signal Occurred.Caused by Error in Work Order.Administrative Fix underway.W/830829 Ltr ML20024F2091983-08-29029 August 1983 LER 83-111/03L-0:on 830730,during Performance of Work Order to Correct Malfunction W/Div I Isolation Reset Status lights,amphenol-type Signal Cable Connector in C/R Panel Disconnected.Caused by Personnel error.W/830829 Ltr ML20024E9311983-08-29029 August 1983 Updated LER 83-002/01X-1:on 830114,personnel Discovered Heat Detectors in Control Room Standby Fresh Air Sys Not Functionally Tested.Caused by Lack of Proper Procedure. Procedure rewritten.W/830829 Ltr ML20024F6131983-08-29029 August 1983 Updated LER 83-010/99X-2:on 830105,fire Protection Deficiencies on Redundant Raceways/Cables Discovered in Auxiliary,Turbine & Control Bldgs.Caused by Incomplete Const.Maint Work Now complete.W/830829 Ltr ML20024F6071983-08-29029 August 1983 Updated LER 82-050/99X-1:on 820806,Fire Detection Zone 2-10 Went Into Alarm Condition & Would Not Clear.Caused by Diesel Exhaust Fumes Drifting Into Corridor.Detectors Cleaned. Design Change submitted.W/830829 Ltr ML20024D8781983-07-29029 July 1983 LER 83-078/03L-0:on 830701,control Room Operators Unable to Maintain Air Receiver Pressure for Diesel Generator 11. Caused by Setpoint Drift on Relief Valves for diesel-driven & Electric motor-driven Air compressors.W/830729 Ltr ML20024D0891983-07-25025 July 1983 LER 83-079/03L-0:on 830625,auxiliary Trip Unit for High Drywell Pressure Indicated Trip Condition Yet No Reactor Protection Sys Trip Occurred.Caused by Defective Rosemount Auxiliary Trip Unit.Trip Unit replaced.W/830725 Ltr ML20024D0761983-07-25025 July 1983 LER 83-080/03L-0:on 830626,control Room Operators Experienced Problems W/Hvac Sys Involving Inadequate Cooling Capacity & Sys Losses.Partially Caused by Malfunctioning Condenser Cooling Water Flow Control valve.W/830725 Ltr ML20024B9941983-06-29029 June 1983 LER 83-072/01T-0:on 830615,operations Shift Supervisor Discovered Some Continuous Fire Watches Not Performed on 830614.Caused by Personnel Error.Personnel Reinstructed Not to Pull Fire Watch W/O approval.W/830629 Ltr ML20024C4031983-06-27027 June 1983 LER 83-071/03L-0:on 830607,RHR Shutdown Cooling Mode Isolated When Valve E12-F009 Closed.Caused by Blown Fuse. Fuse replaced.W/830627 Ltr ML20024B9981983-06-24024 June 1983 LER 83-070/03L-0:on 830525,reactor Water Cleanup Sys Isolated When Standby Liquid Control Pump B Breaker Closed. Caused by Personnel Error.Isolation Signal reset.W/830624 Ltr ML20024C3121983-06-22022 June 1983 LER 83-069/03L-0:on 830523,during Attempt to Reenergize Div II Motor Operated Valves,Shutdown Cooling Mode of RHR Sys & Reactor Water Cleanup Sys Isolated.Caused by Failure to Install Power Fuses.Fuses installed.W/830622 Ltr ML20023E0441983-05-27027 May 1983 Updated LER 83-058/01X-1:on 830311,discovered That Fire Watches Not Conducted in Two Areas of Fire Detection Zone 2-19.Limiting Conditions for Operation Entered on 830227. Caused by Personnel Oversight.Zone restored.W/830527 Ltr ML20023D4331983-05-12012 May 1983 LER 83-046/03L-0:on 830412,monthly Functional Surveillance for Div I Chlorine Detection Sys Not Performed by 830410. Caused by Personnel Error ML20023D4771983-05-11011 May 1983 LER 83-052/03L-0:on 830411,while Reviewing Vessel Head Installation Work Package,Discovered Head Flange/Vessel Flange Thermocouples Not Physically Reinstalled During Insulation Installation.Cause Under Evaluation ML20023C5591983-05-0909 May 1983 Updated LER 83-031/99X-1:on 830113,fire Rated Door OC104 Blocked Open to Route Temporary Discharge Hose from Hot Machine Shop Sump to Turbine Bldg Floor Drain Sys.Caused by Inadequacy of Present Sys.Mod to Be Completed by Sept 1983 ML20023D2511983-05-0909 May 1983 LER 83-049/03L-0:on 830409,during Cold Shutdown,Diesel Generator 12 Auto Start Not Available When Alarm Actuated. Caused by Condensate Drain Valve Downstream of Tank C Not Fully Closed.Compressors Reworked ML20023C5611983-05-0909 May 1983 Updated LER 83-004/01T-1:on 830110,penetration AP-72B Found Open & Had Been Open Since 821213.Caused by Planned Maint Work & Personnel Error.Hourly Fire Watch Established. Penetration to Be Resealed by 830630 ML20023C5511983-05-0909 May 1983 LER 83-048/01T-0:on 830423,suppression Pool Level Instrumentation Discovered Not Functionally Tested Since 830409.Cause Under Investigation.Instrumentation Tested Satisfactorily within 8 H ML20023B5541983-04-28028 April 1983 LER 83-060/03L-0:on 830329,during Cold Shutdown,Load Shedding & Div I LSS Sequencing Panel Failure Alarm Actuated.Caused by Failure of 15-volt Dc Power Supply Used to Power Solid State Electronics for Sys Logic ML20023B6731983-04-27027 April 1983 LER 83-061/03L-0:on 830328,one Solenoid Operated Freon Valve Found W/Blown Gasket.Caused by Defective Alco Controls Solenoid Operated Gasket.Valve Reworked W/Valve Repair Kit & New Gasket Installed ML20028G6031983-02-11011 February 1983 LER 83-019/03L-0:on 830112 & 20,one Smoke Detector in Zone 1-15 & Eight Detectors in Zone 2-18 Covered During Planned Maint Functions to Prevent False Alarms or Damage to Unit. Detectors Uncovered After Maint Completed 1994-04-26
[Table view] Category:RO)
MONTHYEARML20029D0371994-04-26026 April 1994 LER 94-004-00:on 940324,found Five Slow Rods While Scram Time Testing Was Being Performed.Caused by Contamination of Internal Scram Solenoid Pilot Valve Head Assemblies. Corrective Action:Install New Head assemblies.W/940426 Ltr ML20046C3991993-08-0606 August 1993 LER 92-009-01:on 920509,observed That Some of Fuel Rod Compression Springs Compressed More than Expected for Assembly Exposure Achieved.Max Envelope Size of Lower Tie Plate Will Be reduced.W/930806 Ltr ML20045G7911993-07-0808 July 1993 LER 93-005-00:on 930608,indicated That Response Time Test for RCIC Low Steam Pressure Isolation Instrumentation Invalid.Caused by Inappropriate Test Method.Procedures Governing Method of Testing Will Be revised.W/930708 Ltr ML20045E9601993-06-30030 June 1993 LER 92-017-02:on 920804,reactor Scrammed Due to Low Primary Water Tank Level Signal.Implemented Minor Change Package Which Will Install DC to DC Converter Between 24 Volt DC Power Supply & Pw Tank Level transmitters.W/930630 Ltr ML20045C5261993-06-16016 June 1993 LER 93-004-00:on 930517,inboard Containment Isolation Valve Which Supplies Steam to RCIC Sys Automatically Isolated Due to Topaz Inverter Failure.Calibr Instructions & PM Program Will Be reviewed.W/930616 Ltr ML20045A0151993-05-28028 May 1993 LER 92-011-02:on 920608,determined That Design Inadequacies Could Result in Exceeding 10CFR100 Limits.Caused by Failure of Original Design to Specify leak-tight Const for Fan Housing.Shaft Seal Design installed.W/930528 Ltr ML20024G9701991-05-0606 May 1991 LER 91-002-00:on 910406,operating Module Breaker in Automatic Turbine Tester Circuitry Tripped Open,Deenergizing Control Solenoid for change-over Valve.Caused by Use of Undersized Circuit Breaker.Module replaced.W/910506 Ltr ML20029A3331991-02-13013 February 1991 LER 91-001-00:on 910114,Tech Spec Limiting Condition of Operation Action Was Not Satisfied After DG Removed from Standby Svc to Perform Preventive Maint.Caused by Personnel Error.Procedure Changed to Prevent recurrence.W/910213 Ltr ML20044A6881990-06-25025 June 1990 LER 90-009-00:on 900526,nonlicensed Personnel Performed Step Out of Sequence During Breaker rack-out & Caused LPCS Pump Breaker to Close.Operator Involved Counseled on Failure to Adhere to Breaker Operation procedure.W/900625 Ltr ML20043H2951990-06-15015 June 1990 LER 90-007-00:on 900516,discovered That Actions Taken for Inoperable Reactor Water Level Transmitter Not Adequate to Comply W/Requirements for Tech Spec 3.3.2.Caused by Personnel Error.Meetings Held w/personnel.W/900615 Ltr ML20043C6741990-06-0101 June 1990 LER 90-006-00:on 900502,review of Effluent Sample Analysis Revealed That Turbine Bldg Ventilation Exhaust Had Not Been Analyzed Exceeding Time Limit.Caused by Personnel Error. Training & Counseling conducted.W/900601 Ltr ML20042F2251990-05-0404 May 1990 LER 90-005-00:on 900406,discovered That Current Surveillance Practices for Stroke Testing Fresh Air Makeup Intake Valves Could Have Resulted in Unfiltered Pathway.Administrative Controls Placed on valves.W/900504 Ltr ML20012D8071990-03-22022 March 1990 LER 89-018-01:on 891215,determined That Inappropriate Quality Level Designations Applied to Class 1E Circuits, in Violation of Reg Guide 1.75.Caused by Discrepant Instrument Index Controls.Handswitch replaced.W/900228 Ltr ML20012D4801990-03-16016 March 1990 LER 90-003-00:on 900215,identified Potential Single Failure Scenario That Could Result in Unavailability of Both Core Spray Sys for Long Term post-LOCA Core Cooling.Detailed Heatup Evaluation Performed for Power bundle.W/900316 Ltr ML20012A1661990-02-28028 February 1990 LER 90-002-00:on 900124,discovered That Div II Solenoid Associated W/Secondary Containment Isolation Valve Did Not Operate During Quarterly Valve Stroke Time Tests.Caused by Procedure Inadequacy.Procedures changed.W/900227 Ltr ML20006E4521990-02-15015 February 1990 LER 89-015-01:on 891030,no Data or Evidence Found That Stroke Time Test Performed on Bettis Actuator for Isolation Damper Following Maint.Caused by Programmatic Weaknesses.New Computer Field Data Added to Work orders.W/900215 Ltr ML20006E0461990-02-0909 February 1990 LER 90-001-00:on 900112,determined That Tech Spec Reactor Coolant Cooldown Rate Limit of 100 Degrees F Exceeded in Reactor Bottom Head Drain Pipe.Caused by Programmatic Deficiencies.Incident Rept Form improved.W/900209 Ltr ML20006B8731990-01-29029 January 1990 LER 89-019-00:on 891230,total Loss of Plant Svc Water Experienced Due to Loss of Power to Supply Wells.Caused by Malfunction of Microwave Info & Control Sys.Periodic Microwave Operational Checks established.W/900129 Ltr ML20006B2781990-01-16016 January 1990 LER 89-017-00:on 890718,determined That Isolation for Postulated RWCU Blowdown Line Breaks in Piping Cold Rooms Was 80 S,Causing Plant to Operate in Unanalyzed Condition. Tech Spec Change Request Will Be submitted.W/900116 Ltr ML20005G2121990-01-12012 January 1990 LER 89-007-01:on 890508,RWCU Sys Isolated on Leak Detection Differential Flow Signal While Shifting RWCU Operation from pre-pump to post-pump Mode.Probably Caused by Inadequate Reactor Pressure.Procedure revised.W/900112 Ltr ML20005G2071990-01-12012 January 1990 LER 89-018-00:on 891215,design Basis Review of Instrumentation Determined That 71 Devices,Classified as nonsafety-related,contained in Class 1E Circuits.Caused by Level of Control on Instrument index.W/900112 Ltr ML20005D7411989-12-0606 December 1989 LER 89-016-00:on 891107,during Severe Thunderstorm,Lightning Struck Site,Causing Scram & HPCS Low Water Level Channels to Trip.Design Change Package Issued to Install Lightning Dissipation Sys on Vulnerable structures.W/891206 Ltr ML19332F0731989-11-29029 November 1989 LER 89-015-00:on 891030,no Data or Evidence Found for Stroke Time Test Required to Be Performed Following Maint on Bettis Actuator for Isolation Damper QSZ51F001.Caused by Personnel Error.Programmatic Enhancements initiated.W/891129 Ltr ML19325E6971989-10-31031 October 1989 LER 89-008-02:on 890523,two Redundant Secondary Containment Isolation Dampers Failed to Close within 4 Time Limit of Tech Spec 3.6.6.2.Caused by Malfunction of Exhaust Valves. Exhaust Valve replaced.W/891031 Ltr ML19325E6331989-10-27027 October 1989 LER 89-014-00:on 890929,RWCU Sys Isolated on Simulated Steam Line Tunnel High Temp Signal.Caused by Operator Failure to Perform self-verification Prior to Moving Bypass Switch. General Manager Held Briefings w/personnel.W/891027 Ltr ML20024F4561983-08-31031 August 1983 Updated LER 83-001/01X-2:on 830107,electrician Preparing to Route Cable Noticed Two Wall Penetrations Had Been Opened. Because Control Room Not Notified of Work,No Fire Watch in Effect.Caused by Personnel error.W/830831 Ltr ML20024E8741983-08-31031 August 1983 LER 83-108/01T-0:on 830817,radiation Monitor B Trip Setpoint Found High & Grab Samples & Analyses Started Late.Caused by Personnel Error.Personnel counseled.W/830831 Ltr ML20024E9111983-08-30030 August 1983 Updated LER 83-097/03X-1:on 830720,reactor Water Cleanup Auto Isolation Occurred.Caused by Delta Temp Channel B Indicating Temp Above Trip Point Limit.Investigation continuing.W/830830 Ltr ML20024F5091983-08-29029 August 1983 LER 83-112/03L-0:on 830730,while Troubleshooting Initiation Circuitry to Find Reason for Improper Operation of E12F087B & F025B,partial LOCA Signal Occurred.Caused by Error in Work Order.Administrative Fix underway.W/830829 Ltr ML20024F2091983-08-29029 August 1983 LER 83-111/03L-0:on 830730,during Performance of Work Order to Correct Malfunction W/Div I Isolation Reset Status lights,amphenol-type Signal Cable Connector in C/R Panel Disconnected.Caused by Personnel error.W/830829 Ltr ML20024E9311983-08-29029 August 1983 Updated LER 83-002/01X-1:on 830114,personnel Discovered Heat Detectors in Control Room Standby Fresh Air Sys Not Functionally Tested.Caused by Lack of Proper Procedure. Procedure rewritten.W/830829 Ltr ML20024F6131983-08-29029 August 1983 Updated LER 83-010/99X-2:on 830105,fire Protection Deficiencies on Redundant Raceways/Cables Discovered in Auxiliary,Turbine & Control Bldgs.Caused by Incomplete Const.Maint Work Now complete.W/830829 Ltr ML20024F6071983-08-29029 August 1983 Updated LER 82-050/99X-1:on 820806,Fire Detection Zone 2-10 Went Into Alarm Condition & Would Not Clear.Caused by Diesel Exhaust Fumes Drifting Into Corridor.Detectors Cleaned. Design Change submitted.W/830829 Ltr ML20024D8781983-07-29029 July 1983 LER 83-078/03L-0:on 830701,control Room Operators Unable to Maintain Air Receiver Pressure for Diesel Generator 11. Caused by Setpoint Drift on Relief Valves for diesel-driven & Electric motor-driven Air compressors.W/830729 Ltr ML20024D0891983-07-25025 July 1983 LER 83-079/03L-0:on 830625,auxiliary Trip Unit for High Drywell Pressure Indicated Trip Condition Yet No Reactor Protection Sys Trip Occurred.Caused by Defective Rosemount Auxiliary Trip Unit.Trip Unit replaced.W/830725 Ltr ML20024D0761983-07-25025 July 1983 LER 83-080/03L-0:on 830626,control Room Operators Experienced Problems W/Hvac Sys Involving Inadequate Cooling Capacity & Sys Losses.Partially Caused by Malfunctioning Condenser Cooling Water Flow Control valve.W/830725 Ltr ML20024B9941983-06-29029 June 1983 LER 83-072/01T-0:on 830615,operations Shift Supervisor Discovered Some Continuous Fire Watches Not Performed on 830614.Caused by Personnel Error.Personnel Reinstructed Not to Pull Fire Watch W/O approval.W/830629 Ltr ML20024C4031983-06-27027 June 1983 LER 83-071/03L-0:on 830607,RHR Shutdown Cooling Mode Isolated When Valve E12-F009 Closed.Caused by Blown Fuse. Fuse replaced.W/830627 Ltr ML20024B9981983-06-24024 June 1983 LER 83-070/03L-0:on 830525,reactor Water Cleanup Sys Isolated When Standby Liquid Control Pump B Breaker Closed. Caused by Personnel Error.Isolation Signal reset.W/830624 Ltr ML20024C3121983-06-22022 June 1983 LER 83-069/03L-0:on 830523,during Attempt to Reenergize Div II Motor Operated Valves,Shutdown Cooling Mode of RHR Sys & Reactor Water Cleanup Sys Isolated.Caused by Failure to Install Power Fuses.Fuses installed.W/830622 Ltr ML20023E0441983-05-27027 May 1983 Updated LER 83-058/01X-1:on 830311,discovered That Fire Watches Not Conducted in Two Areas of Fire Detection Zone 2-19.Limiting Conditions for Operation Entered on 830227. Caused by Personnel Oversight.Zone restored.W/830527 Ltr ML20023D4331983-05-12012 May 1983 LER 83-046/03L-0:on 830412,monthly Functional Surveillance for Div I Chlorine Detection Sys Not Performed by 830410. Caused by Personnel Error ML20023D4771983-05-11011 May 1983 LER 83-052/03L-0:on 830411,while Reviewing Vessel Head Installation Work Package,Discovered Head Flange/Vessel Flange Thermocouples Not Physically Reinstalled During Insulation Installation.Cause Under Evaluation ML20023C5591983-05-0909 May 1983 Updated LER 83-031/99X-1:on 830113,fire Rated Door OC104 Blocked Open to Route Temporary Discharge Hose from Hot Machine Shop Sump to Turbine Bldg Floor Drain Sys.Caused by Inadequacy of Present Sys.Mod to Be Completed by Sept 1983 ML20023D2511983-05-0909 May 1983 LER 83-049/03L-0:on 830409,during Cold Shutdown,Diesel Generator 12 Auto Start Not Available When Alarm Actuated. Caused by Condensate Drain Valve Downstream of Tank C Not Fully Closed.Compressors Reworked ML20023C5611983-05-0909 May 1983 Updated LER 83-004/01T-1:on 830110,penetration AP-72B Found Open & Had Been Open Since 821213.Caused by Planned Maint Work & Personnel Error.Hourly Fire Watch Established. Penetration to Be Resealed by 830630 ML20023C5511983-05-0909 May 1983 LER 83-048/01T-0:on 830423,suppression Pool Level Instrumentation Discovered Not Functionally Tested Since 830409.Cause Under Investigation.Instrumentation Tested Satisfactorily within 8 H ML20023B5541983-04-28028 April 1983 LER 83-060/03L-0:on 830329,during Cold Shutdown,Load Shedding & Div I LSS Sequencing Panel Failure Alarm Actuated.Caused by Failure of 15-volt Dc Power Supply Used to Power Solid State Electronics for Sys Logic ML20023B6731983-04-27027 April 1983 LER 83-061/03L-0:on 830328,one Solenoid Operated Freon Valve Found W/Blown Gasket.Caused by Defective Alco Controls Solenoid Operated Gasket.Valve Reworked W/Valve Repair Kit & New Gasket Installed ML20028G6031983-02-11011 February 1983 LER 83-019/03L-0:on 830112 & 20,one Smoke Detector in Zone 1-15 & Eight Detectors in Zone 2-18 Covered During Planned Maint Functions to Prevent False Alarms or Damage to Unit. Detectors Uncovered After Maint Completed 1994-04-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217F9921999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20212F5641999-09-23023 September 1999 SER Concluding That All of ampacity-related Concerns Have Been Resolved & Licensee Provided Adequate Technical Basis to Assure That All of Thermo-Lag Fire Barrier Encl Cables Operating within Acceptable Ampacity Limits ML20211Q3171999-09-0909 September 1999 Safety Evaluation Accepting BWROG Rept, Prediction of Onset of Fission Gas Release from Fuel in Generic BWR, Dtd July 1996 ML20216E4881999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Grand Gulf Nuclear Station.With ML20211A6921999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20209J1961999-07-12012 July 1999 Special Rept 99-001:on 990528,smoke Detectors Failed to Alarm During Performance of Routine Channel Functional Testing.Applicable TRM Interim Compensatory Measure of Establishing Roving Hourly Fire Patrol Was Implemented ML20196K4981999-07-0101 July 1999 Safety Evaluation Authorizing PRR-E12-01,PRR-E21-01, PRR-P75-01,PRR-P81-01,VRR-B21-01,VRR-B21-02,VRR-E38-01 & VRR-E51-01.Concludes That Alternatives Proposed by EOI Acceptable ML20209G0691999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20196A1161999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Grand Gulf Nuclear Station.With ML20206Q4831999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Grand Gulf Nuclear Station Unit 1.With ML20206J1201999-04-30030 April 1999 Redacted ME-98-001-00, Pressure Locking & Thermal Binding Test Program on Two Gate Valves with Limitorque Actuators ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205P8771999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207K5141999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Grand Gulf Nuclear Station,Unit 1.With ML20206T7991999-01-31031 January 1999 Iodine Revolatizitation in Grand Gulf Loca ML20207A8301998-12-31031 December 1998 1998 Annual Operating Rept for Ggns,Unit 1 ML20206R9501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20206D7721998-12-31031 December 1998 South Mississippi Electric Power Association 1998 Annual Rept ML20198E2481998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20195F4121998-11-13013 November 1998 Rev 16 to GGNS-TOP-1A, Operational QA Manual (Oqam) ML20195C4841998-11-0606 November 1998 SER Accepting QA Program Change to Consolidate Four Existing QA Programs for Arkansas Nuclear One,Grand Gulf Nuclear Station,River Bend Station & Waterford 3 Steam Electric Station Into Single QA Program ML20195C2791998-11-0505 November 1998 BWR Feedwater Nozzle Inservice Insp Summary Rept for GGNS, NUREG-0619-00006 ML20195F4801998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20155C1351998-10-26026 October 1998 Rev B to Entergy QA Program Manual ML20154K2391998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Grand Gulf Nuclear Station Unit 1.With ML20155F1961998-09-0101 September 1998 Engineering Rept for Evaluation of BWR CR Drive Mounting Flange Cap Screw ML20153B2161998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Grand Gulf Nuclear Station,Unit 1.With ML20237B6661998-07-31031 July 1998 Monthly Operating Rept for Jul 1998 for Grand Gulf Nuclear Station,Unit 1 ML20236R0231998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Grand Gulf Nuclear Station,Unit 1 ML20155J0811998-05-31031 May 1998 10CFR50.59 SE for Period Jan 1997 - May 1998 ML20249B1251998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Grand Gulf Nuclear Station,Unit 1 ML20248B6261998-05-11011 May 1998 Rev 6 to Grand Gulf Nuclear Station COLR Safety-Related ML20217Q6701998-05-0606 May 1998 SER Approving Proposed Postponement of Beginning Augmented Exam Requirements of 10CFR50.55a(g)(6)(ii)(A)(2) at Grand Gulf for Circumferential Shell Welds for Two Operating Cycles ML20206J1271998-04-30030 April 1998 Pressure Locking Thrust Evaluation Methodology for Flexible Wedge Gate Valves ML20247F3591998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Grand Gulf Nuclear Plant,Unit 1 ML20217M8951998-04-30030 April 1998 QA Program Manual ML20217P8281998-04-0707 April 1998 Safety Evaluation Accepting Relief Authorization for Alternative to Requirements of ASME Section Xi,Subarticle IWA-5250 Bolting Exam for Plants,Per 10CFR50.55a(a)(3)(i) ML20217P0381998-04-0606 April 1998 Safety Evaluation Supporting Amend 135 to License NPF-29 ML20217A0291998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Grand Gulf Nuclear Sation,Unit 1 ML20216J4211998-03-18018 March 1998 SER Approving Alternative to Insp of Reactor Pressure Vessel Circumferential Welds for Grand Gulf Nuclear Station ML20216J2021998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Grand Gulf Nuclear Station,Unit 1 ML20203A2891998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Grand Gulf Nuclear Station ML20247B4111997-12-31031 December 1997 1997 Annual Financial Rept for South Mississippi Electric Power Association ML20203H9741997-12-31031 December 1997 1997 Annual Operating Rept, for Ggns,Unit 1 ML20198P1121997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Grand Gulf Nuclear Station,Unit 1 ML20203B5581997-12-0404 December 1997 Special Rept 97-003:on 971111,valid Failure of Div 2 EDG Occurred,Due to Jacket Water Leak.Failure Reported,Per Plant Technical Requirements Manual Section 7.7.2.2 ML20203K4031997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Grand Gulf Nuclear Station,Unit 1 ML20199H3711997-11-19019 November 1997 SER Accepting Approving Request Relief from Requirements of Section XI, Rule for Inservice Insp of NPP Components, of ASME for Current or New 10-year Inservice Insp Interval IAW 50.55(a)(3)(i) of 10CFR50 ML20199F3431997-11-18018 November 1997 SER Accepting Rev 15 of Operational Quality Assurance Manual for Grand Gulf Nuclear Station,Unit 1 1999-09-09
[Table view] |
Text
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Tu 6D14374:09 W. T. Cottle m n, s .y June 15, 1990 m-a '
O.S. Nuclear Regulatory Commission I Mail Station P1-137 -
Washington, D.C. 20555 l Attention: Document Control Desk Gentlemen:
SUBJECT:
Grand Gulf Nuclear Station Unit 1 Docket No. 50-416 :
License No. NPF-29 Failure To Comply With Technical Specifications Due To Personnel Error -
LER 90-007 AECH-90/0109 Attached is Licensee Event Report (LER)90-007 which is a final '
report.
Yours truly, ,
WTC:cg "IO Attachment cc:
Mr. T.D.
Mr. H. C.
Cloninger Hintz(w(w/a) /a)
Mr. J. G. Cesare (w/o) i Mr. R. B. McGehee (w/a)-
Mr.N.S.Reynolds(w/a)
Mr.H.H.
Mr. O. L.
ChristensenThomas (w/o)(w/a)
Mr. Stewart D. Ebneter (w/a)
Regional Administrator U.S. Nuclear Regulatory Commission Region II 101 Marietta St., N.W., Suite 2900 Atlanta, Secrgia 30323 Mr. L. L. Kintner, Project Manager (w/a) l OfficeofNuclearReactorRegulation l U.S. Nuclear Regulatory Commission Mail Stop 11021 / p Washington, D~.C. 20555 /
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. UCENSEE EVENT REPORT (LER) '*'"'8""
i eAciuTY NAME ni poCRt? NUMetR Gi rain m I Grand Gulf Nuclear Station - Unit 1 0 ls l 0 j 010161116 1 l0Fl O l 4 18768 44:
Failure to Comt,1v Vit_h Technical Stiecifications Due to Personnel Error EVENT DAf t tli Lth NUMSERlei REPORT DATE (76 OTHER f ACILITill INvotvt0108 MONY ?AY YEAR YEAR L MONTH DAY YEAR F ACibet v hawlt DOCkti NVM9tRtSt ku#N[R v ,
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O!$ 1l6 9 0 9l0 0 l0 l 7 0 l0 0 l6 1l5 9l 0 0 1 5 l 010 1 0l l 1 opt RATisse THIS RSPORT 68 WOMITTED PURSUANT TO THE REQUIREM6NTS Of 10 CpR O tenece one er n*ere of rae f.newal HH j l N 40116) 20 408tel to.736slGHwi 73.71thi R 30.eseteH1Hil to 304eHil to.73telGHet 73.? Hal n.i u oi n a wnHai
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M 406ta H1 Hell) y 60.73talGHit 90.73 eH2 HoulH Al l 30 408teH1Hivl 60.73toltiital 30.73teH2Henintel 29 4eeleH1Het 90 73telt210nl to.73teH2Hal i LICEN898 CONT ACT FOR TMil LER H2l NiME YtLtPHONE NVM$tR Area COO 4 Ronald Byrd/Licentin; Engineer i 6 l0 i l 4 i 3 i? i ,2 il i 8l2 CoierttTE oNE uNE poR e AggNT AitVRE oleCRino N Twie RteoRT H3, CAust sYtttM ,,,,, ,y,,,, ,,,,,,,,, ss CoMeoNENT *^lW;AC. age,oa,TAggt MANg;Ac. ng,9oRTAgt-I I I I I I I I i 1 1 1 1 I I' I l l l l l l l 1 l 1 i l I SUPPLEMENTAL REPORT ExFICTt0 Het MONTH DAY YEAR Sv0 MIS $10N emo tuacreo spewssioN oares G Yts tar v ~} No l l l AseTRACT<t - , , = .o . - % ar ..u.rr . 4;e ,oei On May 16, 1990, an Operations Shift Supervisor determined that the actions taken by the previous shift for an inoperable reactor water level l
l
' transmitter were not adequate to comply with the requirements of Technical.
Specification 3.3.2 (Isolation Actuation Instrumentation). The level transmitter was inoperable for 10.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />; however, the affected channel was actually in the tripped condition for only 6.6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> during that time.
The failure to maintain compliance with the LCO requirements was due to an error by licensed operators. The Technical Specifications placed different LCO time limits on the different functions of the affected instrumentation.
In evaluating options to take advantage of the extended LCO time limits for I the Reactor protection System trip function, the Operations Shift Supervisor i and Shift Superintendent did nct ensure that a detailed technical review was performed to verify that the method of maintaining compliance with the Ghutdown Cooling isolation. function was adequate. ,
Improper assumptions and verbal communications not being fully understood were contributing factors. Meetings were held with all shift SR0s to discuss:
specific duties relative to Technical Specification compliance, the expectations of personnel performing technical reviews, and concise communications.
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A. Reportable Condition On May 16, 1990, licensed operators failed to maintain complianco with the requirements of Technical Specification Action 3.3.2.b for an inoperable isolation actuation instrument (EIIS system code: JM). This condition is reported pursuant to 10CFR50.73(a)(2)(1)(B).
B. Initial Conditions The' plant was operating at approximately 100 percent power at the time of occurrence with the affected isolation valves in the normally closed position.
C. Description of Occurrence On May 16, 1990, a Licensed Shift Supervisor determined that the actions taken by the previous operations shift for an inoperable level transmitter were not adequate to comply with the requirements of Technical Specification 3.3.2. The level transmitter was inoperable'for 10.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. The total time of noncompliance with Limiting Condition for Operation (LCO) was 3.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br />. The following discussion sununarizes the soquence of evnnts leading to the error.
'On May 16,-'1990 at 1144, reactor level transmitter 1B21-N080B was declared inoperable after a special inspection revealed that although it was functional, it did not fully meet environmental qualification requirements. The heat shrink around one of.the transmitter openings.did not completely seal the opening as required.. 'A Limiting Condition for
-Operation (LCO) was entered pursuant to Technical Specifications 3.3.1 and 3.3.2.
Technical Specification 3.3.1 (RPS Instrumentation) states: "With the number of OPERABLE channels less than required by the minimum OPERABLE channels per Trip System requirement (2 per Trip System) for one trip system, place the inoperable channel and/or that trip system in the
-tripped condition within twelve hours."
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% Technical Specification 3.3.2 (Isolation Actuation Instrumentation) k states: "With the number of OPERABLE channels less than required by tho'
$. minimum OPERABLE channels por Trip System requirement (2 per Trip System)
[ , for one trip. system, place the inoperable channel and/or trip system in L the tripped condition within one hour."
The operator's first response was to conservatively place trip unit 1B21-N680B to trip. This provided a "B" channel trip to both the RPS and SDC isolation trip-functions. The Shift Superintendent.then decided to take advantage of the extended LCO thne limit for the inoperable RPS channel to minimize potential plant transients. After confirming that
[ the LCO requirements were met, operators began investigating options for
- - clearing the RPS channel trip.
The Shift Superintendent consulted with operations section supervision on a proposal to remove the trip condition from trip unit B21-N600B, reset the RpS trip logic, and place in effect administrative controls to restrict resetting the SDC isolation logic. This proposal was concurred with by the staff assistant and management.
At 1350 on May 16, Trip unit B21-N680B was removed from the tripped condition and the RPS trip was reset. An information tag was placed on the SDC isolation reset switch prohibiting the reset of the SDC isolation signal. The Shift Superintendent thought that the isolation channel for valve E12-F037B would remain tripped by this-action.
T When the next operations shift. began, the oncoming Shift Supervisor
_ questioned the actions taken for the SDC isolation function. Upon reviewing the isolation logic schematics,,it was realized that the "B" channel isolation logic for valve E12-F037B was not tripped:and that the LCO requirements were not being met. At 1633, handswitch C71-M611B was placed to " TEST" which provided the B channel trip and roostablished Technical Specification compliance.
Level transmitter B21-N080B was resealed and returned to operable status at 2158 on May 16.
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'O. Apparent Cause The Shift Supervisor had performed a preliminary review of logic schematics in developing alternatives for clearing the Rps channel trip, but had not performed a detailed comprehensive review to verify Technical Specification compliance for the particular method chosen. The Shift Superintendent made the decision on the method of Technical Specification compliance based on j his knowledge-of how the system functioned and concurrence from operations section supervision. The Shift Superintendent received this concurrence based on approval of the general method of compliance and not on a detailed technical review.- Through various communications with the staff and ;
management, the Shift Superintendent thought that a technical review had been completed..
The failure to maintain compliance with the LCO requirements was due to an error by licensed operators. The Operations Sh.ift Supervisor and Shift Superintendent did not ensure that a detailed technical review was performed to verify the adequacy of the actions taken. Improper assumptions and verbal communications not being fully understood were contributing factors.
E. Supplemental corrective Action An Incident Review Board (IRB) was convened on May 17 to investigate the incident. In addition, a !!uman Performance Enhancement System (HPES) evaluation was conducted.
The Operations Superintendent counseled the individuals involved and met with all SROs to discuss the event and its causes. These meetings focused on the following matters: the specific responsibilities and duties of the Shift Supervisor and Shift Superintendent relative to Technical Specification compliance and technical verifications, the expectations of personnel performing technical reviews, and concise communications with non-shift resources such that information or requests are clearly understood.
F. Safety Assessment Valve E12-F037B is in the Residual lleat Removal (RHR) discharge line to the upper containment pools. The line is used for emergency inventory makeup to the upper containment pools. The E12-F037B valve is normally closed during plant operation and was maintained closed during this event. The valve does not have an automatic opening feature. Emergency inventory makeup to the upper containment pools is accomplished only by operator actions. Therefore, the event did not compromise plant safety.
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