ML19312D496

From kanterella
Jump to navigation Jump to search
LER 80-006/03L-01:on 800111,w/unit in Mode 3,casing Coolant Pump Discharge Valve MOV-RS-100A Was Discovered to Be Inoperable.Caused by Removal of Casing Cooling Tank Level Transmitter LT-RS103A During Execution of Design Change
ML19312D496
Person / Time
Site: North Anna Dominion icon.png
Issue date: 02/08/1980
From:
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19312D493 List:
References
LER-80-006-03L-02, LER-80-6-3L-2, NUDOCS 8003240505
Download: ML19312D496 (1)


Text

.

< CRO FORM 8346 U. S N,) CLEAR R EC.ULATOM CCMMISS.ON

. om

l* g LICENSEE EVENT REPORT CONTROL ELOCK: l l l l l l (PLE ASE PRINT OR TYPE ALL REQUIRED INFORMAT13M lO l a1 9l l V luCEssEE 7

A l NCcot l A l S l 1 l@l 0 l 0 l- luCEut is is 0 l0s l:.0sEml 0 l0 l- l0 l a0 l@l ao 4 u! Ilw.sE1 lT,PE11ail@lsi ur I l se @ l i

COWT lOl11 3,'.$

l L l@l 0 l 5 l 0101013 l3 16 @l 01 11 11 1l 81 ol@ln 19 74 In la le inE3l@

pEaQRTDATE

? 8 60 61 DOCK ET Nuve ER 6e 69 Ewf NT oaf g 7b EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o 121 l On JanuaTv 11. 1980. vith the unit in %do 1. ensf~ cnn14 g ~,-,/4c4,3. ,1 o un" _l

[OE I RS-100A was discovered to be inocerable and would have been unnhie en nean in tha a . - -I l o 141 l of a CDA. Because the "A" casine cooline subsvsten was restorad en nnar,hla e*,*.e I O 5 I vithin the 7 day tire limit allowed by the applicable Technical Scacific1tinn Actinn I l o is i l statecent, the health and sa fety of the ceneral nubife vara nn+ a f far

  • ad - u n-*,kia l ITJTl ipursuant to T.S. 6.9.1.9.b. l ITTTII I SY3 TEM CAL 7E CAUSE COv P. VALVE CODE CODE SUSCODE COvPONENT CODE SUBCODE SUSCOct

. lTTil 7 s B l BIO LA_J@ LE_jh l V l A l I, b k k lh [_jh $_j h 9 to 12 18 20 11 13 19

,,,,, SE QUENTI AL OCCURRENCE REPORT REVISION L EVENT YE AR REPORT NO. COOE TYPE NO.

@ ,a=E R 'R1810l O [__J 0101 8 Ld I of 31 Lt_.J 1--J l 01

,,,,. 2 5 22 23 24 26 27 28 29 30 31 32

  • ACTION SUTURE EPPECT SHUTDOWN
  • ATTACPUENT NPRO-4 PRlYE COMP, CCY'ONENT TAKEN ACTION ON PLANT METHOD HOURS SUBuITTED PORM bu8. $VPPLiER , M ANUP ACTt'RER I l 33 gl 34 Zi@ W@ W@ l 0l 0l 0l 35 36 37 40 l [ Y_j @

43 lNl@

42

]@

43 l A l 2 l 0 l 047l@

44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h ,

li 101 ]The valve was rendered inoperable due to the removal of easina cooline tank level traml-i i lmitter LT-RS103A d'uring the implementation of a desien chance. With LT-R9101 A n n e _l L'_12_1.lterminated, a low level signal resulted which in turn imposed a close stenal on MOV-Rs i i 3 1100A 'and prevented it from opening if required. LT-RS103A vas imediatelv reinst, tiled 1 g twhich restored level indication and proper valve operation. I 7 a9 a0 5A  % POWER OTH ER STATUS 01 O R DISCOVERY DESCRIPTIC 4 i s (Cj@ l 0 l 0 l O l@lNA l lA l@DperatorObservation l A TivtTY CO TENT AMOUNTOF ACTivlTY LOCATION CF RELEASE 1 6 (Z,,j rELE lZ ASE@D NA OF RELEASE l@l l l NA l 7 8 9 . 10 tt 44 46 80 PERSONNEL EXPOSURES NUVSER TYPE DESCRIPTION

[TlT) l 0 l 0 l 0 l@l Z l@l NA j PERSONNELINJU IES NUMSER DESCRIPTION m 101010 7 8 9 l@l 11 12 NA 80 l

LOSS OF OR DAMACE TO FACILITY 8 lZ.J@l TYPE DESCRIPTION NA o nnq 84 0 5

7 8 9 10 80 PUBLICITY NRC USE ONLY

  • ISSUED - .

2 o [N_jh]DE5CRIPTION NA l llIlllliII11li

.7 o9 30 6s s9 so.;

t- o 2,*

Naesg og oogogogo , , ,, e , c,3, ,, g , qt g Ow og g. a_g n m en , p,oc_ &