05000318/LER-1979-016-03, /03L-0 on 790520:while Inserting Group 5 Control Element Assemblies,Cea 36 Dropped to Bottom of Core.Caused by Spike in 15 Volt Power Supply.Design Mod to Be Installed During Next Refueling Outage

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/03L-0 on 790520:while Inserting Group 5 Control Element Assemblies,Cea 36 Dropped to Bottom of Core.Caused by Spike in 15 Volt Power Supply.Design Mod to Be Installed During Next Refueling Outage
ML19270G039
Person / Time
Site: Calvert Cliffs Constellation icon.png
Issue date: 05/25/1979
From: Davis S, Miernicki M
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19270G034 List:
References
LER-79-016-03L-01, LER-79-16-3L-1, NUDOCS 7906010207
Download: ML19270G039 (1)


LER-1979-016, /03L-0 on 790520:while Inserting Group 5 Control Element Assemblies,Cea 36 Dropped to Bottom of Core.Caused by Spike in 15 Volt Power Supply.Design Mod to Be Installed During Next Refueling Outage
Event date:
Report date:
3181979016R03 - NRC Website

text

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8 60 61 DOCK ET NUYBER 68 69 EVENT CATE 74 75 HEPORT DATE 50 EVENT DESCRIPTION AND PROBABLE CONSEGUENCES h At 1142 while insertino aroun 5 control eierent assemblies (CEA's), CEA 36 I

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drocoed to the botton of the core.

In accordance wi th T.S. 3.1.3.1.f, i

I reactor cower was reduced to less than 70% at 1222.

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withdrawn and realigned with its grouo.

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