ML19261B191

From kanterella
Jump to navigation Jump to search
LER 79-001/03L-0 on 790104:during Monthly Operability Test, Inlet Air Heater on a Standby Gas Treatment Sys Was Found Inoperable.Caused by Setpoint Drift of Flow Switch 1/2-7541-8A
ML19261B191
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 01/25/1979
From: Kooi M
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19261B184 List:
References
LER-79-001-03L-01, LER-79-1-3L-1, NUDOCS 7902140151
Download: ML19261B191 (2)


Text

. . . .~

17 7/)

LICENSEE EVENT REPORT CONTPpL BLOCK: l l l l l l l (PLEASE PRINT OR TYF'E ALL REQUIRED INFoRMATioN) i e

[O hJ j i L l Q l A l D 2 14 l@! 0 l 0 0l-l0l0l0l- 0 l0 l0 l@!4l1l1 15 LICEr.St NUr/CEri 23 2d l1 l1 !@!57 CATE8 LICENSE TYPE JO l l@

l *6 9 llCtNSEE CGr)E COTT 7

o i 8

SfAT 60 L l@l 0 l 5 l 0 l 0 l 0 l 2 l636 l635 l@[0 01 DOC < E T P.VMelE H l1ATEl0 l4 74l7 l9 }@[

EVENT C 75 0 lC 1 REPOHT ATEl2 l5 83 l7 19 l@

EVENT DESCRIPTION AND PRO 3ABLE CONSEQUENCES h '

O 2 While performing monthly operability test, procedure QOS 7500-5, it was discovered l

,gg3; [

that the inlet air heater on the "A" Standby Gas Treatment (SBGT) system was not [

p) g operating. The temperature switch was reset and the operability test was successfully l l g y ,, y completed. The next day, the heater again failed and additional investigation of the g failure was begun. In accordance with Technical Specification 3.7.B.1.a, the g g g g , g redundant SBGT System was operable during each of the above failures.  ;

I

[o a l 83

$YS TE M CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE lo[9] lS lC l@ W@ lE l@ l 1l N 12 13 S l T l R l U l@

18 19 S l@ W @ 20 7 8 9 to 11 OCCURRENCE REPORT REVISION SEQUEN TI AL EVENT YEAR REPOR T NO. CODE TYPE N O.

@ , REP g LE R/RO

[_j l0 l0 l1 l y l0 3 lLl [.-_j [0l 32_

_ l217l9l 22 23 24 2G 27 28 29 30 31 HOURS 22 F R UB. SUPPLI ER MAN FACTURER 1E A ON ON PL T E S BP 1 E

[EjglJ4Z 33_

jg l3SZ[@

y@

36 l0l0l0l 31 l

40 lY l@

41 U@ W@ ltil2l3l5l@

42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l The cause of the failure was due to setpoint dri f t of flow switch 1/2-7541-8A. This I i i switch actuates the heater when flow is present in the SBGT train. The flow swi tch I was calibrated and the "A" SBGT was tested satisfactorily. The heater itself was [

not failed. l

, 3 l

t 4 1 go 7 8 9 ST S  % POWER OTHER ST ATUS bl5 O RY DiSCOVEf tY DESCRIPTION 1 5 l F l@ l ' 0 l 8 l 8' l@l" NA l lBl@l Routine Test l Alnvi rY CON T E NT AMOUNT OF ACTIVITY LOC ATION OF HELE ASE en E ASE O OF REL E ASE l

1 6 y @ [_Z_j@l NA 44 l l 45 NA

+0 1 8 9 10 11 PERSONNEL E XPO5URES NUMGEH TYPE DESCRIPTION -

1 ,

g l 0 l0 l@l Zl@l NA l

' u nSO w d'iN3 3,ES NUs.s E n

[Lif._] I o l o l o l@l12 OtSCn.P nON@N A l SO 8 9 11 L OSS Or 09 O A*/ AGE T O F A0!LITY -

I T 'E DE SCm p TION q , NA l f1 l o P. s ,a FUhlCITY NRC USE ONLY

'J I; O NA l

[jlllllllllll%;

{ /h) b(5h,l ESCHiPTION 0 es e, o.s 309-654-2241, ext. 252 7 5 0 2 I dt*o 5r(2nr n ti . K i e

p. PHONE: 3
1. LER NUMBER: LER/R0 79-01/03L-0 ll. LICENSEE NAME: Commonwealth Edison Company Quad-Cities Nuclear Power Station 111. FACILITY NAME: Unit Two IV. DOCKET NUMBER: 050-265 V. EVENT DESCRIPTION:

On January 4, 1979, at 10:30 a.m. , while performing the monthly operability test, procedure QOS 7500-5, it was discovered that the inlet air heater on "A" Standby Gas Treatment (SBGT)

System was r.ot operating. The "A" SBGT System was immediately declarcJ inoperable. Since the operability test on "B" SBGT System had been completed just prior to this event, the require-ments of Technical Specification 3.7.B.I.a. were satisfied.

Immediate investigation of the failure revealed that temperature switch 1/2-7541-11A in the heater control circuit had tripped.

The switch was reset and the operability test on "A" SBGT System was successfully completed. At 1:00 p.m. the next day, "A" SBGT System was put on and the heater again failed to operate. An operability test on "B" SBGT System was subsequently completed and an investigation of the failure was begun.

VI. PROBABLE CONSEQUENCES OF THE OCCURRENCE:

Both SBGT Systems had been proven operable on December 4, 1978. The redundant "B" SBGT System was operable during this occurrence. Also, the filters, demister, fan, and dampers for the "A" SBGT train were operable. Consequently no adverse safety implications were presented by this event.

Vll. CAUSE The cause of the failure was due to setpoint drif t of flow switch 1/2-7541-8A. This switch actuates the "A" SBGT system heater when flow is present in the SBGT train. The flow switch had failed in the closed position, thus energizing the heater. Since no cooling flow was available, temperature switch 1/2-7541-11A then tripped the heater when the 200 F0 setpoint temperature was reached. When the temperature switch was reset and flow was initiated, the heater remained on until the air flow ceased and the temperature switch again tripped the heater due to high temperature. Flow switch 1/2-7541-8A is model number DA-5333 manufactured by Mercold Corp.

Vill. CORRECTIVE ACTION:

The flow switch was calibrated and the "A" SBGT was tested satisfactorily. Since this is the first failure of this type, thus corrective action is considered sufficient.