Letter Sequence RAI |
|---|
|
Results
Other: ML13212A367, ML14050A304, ML14071A620, ML14072A369, ML14092A346, ML14177A430, ML14238A691, ML14245A371, ML14300A218, ML14317A783, ML15027A196, ML15098A181, ML15106A736, RS-14-183, Updated Responses to NRC Set 14 Requests for Additional Information, Related License Renewal Application, RS-14-249, Results of Detailed Review Performed in Response to Request 1 of NRC RAI B.2.1.7-7 from Set 17, Related to License Renewal Application, RS-15-049, Units 1 and 2 - LRA Impact Assessment Associated with Earlier Responses to Set 29 RAI B.2.1 .5-1a, Related to the License Renewal Application, ULNRC-06118, Updated RAI Response to the License Renewal Application, Enclosures 1 and 2
|
MONTHYEARML13212A3672013-08-12012 August 2013 Plan for the Aging Management Program Regulatory Audits Regarding the Byron and Braidwood Nuclear Stations License Renewal Application Review Project stage: Other ML13262A0352013-10-0707 October 2013 Requests for Additional Information for the Review of the Byron Nuclear Station, Units 1 and 2, and Braidwood Nuclear Station, Units 1 and 2, License Renewal Application -Aging Management, Set 1 Project stage: RAI ML13281A5572013-10-28028 October 2013 Summary of Telephone Conference Call Held on September 25, 2013 Between the U.S. Nuclear Regulatory Commission and Exelon Generation Company, LLC, Concerning RAIs Pertaining to the Byron-Braidwood License Renewal Application (TAC Nos. MF187 Project stage: RAI ML13303B4632013-11-25025 November 2013 Summary of Telephone Conference Call Held on October 22, 2013, Between the U.S. Nuclear Regulatory Commission and Exelon Generation Company, LLC, Concerning RAI Set 3 for the Byron-Braidwood LRA Project stage: RAI ML13281A5742013-11-25025 November 2013 Requests for Additional Information for the Review of the Byron Nuclear Station, Units 1 and 2, and Braidwood Nuclear Station, Units 1 and 2, License Renewal Application - Aging Management, Set 3 (TAC Nos. MF1879, MF1880, MF1881, and MF1882 Project stage: RAI ML13281A5692013-12-12012 December 2013 Request for Additional Information for the Review of the Byron Nuclear Station Units 1 and 2, and the Braidwood Nuclear Station Units 1 and 2, LRA - Aging Management, Set 4 Project stage: RAI ML13282A3692013-12-13013 December 2013 Requests for Additional Information for the Review of the Byron Nuclear Station, Units 1 and 2, and Braidwood Nuclear Station, Units 1 and 2, License Renewal Application - Aging Management, Set 2 Project stage: RAI RS-13-273, Responses to NRC Requests for Additional Information, Set 3, Dated November 25, 2013, Related to the License Renewal Application2013-12-17017 December 2013 Responses to NRC Requests for Additional Information, Set 3, Dated November 25, 2013, Related to the License Renewal Application Project stage: Response to RAI RS-13-274, Response to NRC Requests for Additional Information, Set 5, Dated November 22, 2013, Related to License Renewal Application2013-12-19019 December 2013 Response to NRC Requests for Additional Information, Set 5, Dated November 22, 2013, Related to License Renewal Application Project stage: Response to RAI ML13317A0752014-01-13013 January 2014 Requests for Additional Information for Review of Byron, Units 1 & 2, and Braidwood, Units 1 & 2, License Renewal Applications, Set 6 Project stage: RAI RS-14-003, Bryon, Units 1 and 2, Response to NRC Requests for Additional Information, Set 2, Dated December 13, 2013, Related to the License Renewal Application2014-01-13013 January 2014 Bryon, Units 1 and 2, Response to NRC Requests for Additional Information, Set 2, Dated December 13, 2013, Related to the License Renewal Application Project stage: Response to RAI ML14017A0072014-01-16016 January 2014 Enclosure 1 to ULNRC-06072, Callaway Plant, Unit 1, Responses to Request for Additional Information (RAI) Sets 29 and 27 (RAI B2.1.6-4b) Project stage: Response to RAI ML14007A6582014-01-22022 January 2014 Requests for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 9 Project stage: RAI ML13309A9322014-01-23023 January 2014 Summary of Telephone Conference Call Held on October 31, 2013, Between the U.S. Nuclear Regulatory Commission and Exelon Generation Company, LLC, Concerning Draft Requests for Additional Information Pertaining to the Byron Station and Braid Project stage: Draft RAI ML13330A9322014-01-23023 January 2014 Bbs Record of Conference Call-Regarding-RAI Set 4 110513 Project stage: RAI ML13318A4152014-01-23023 January 2014 November 12, 2013, Summary of Telephone Conference Call Held Between the U.S. Nuclear Regulatory Commission and Exelon Generation Company, LLC, Concerning Draft Requests for Additional Information Pertaining to the Byron Station and Braidwo Project stage: Draft RAI RS-14-030, Response to NRC Requests for Additional Information, Set 6, Dated January 13, 2014, Related to License Renewal Application2014-02-0404 February 2014 Response to NRC Requests for Additional Information, Set 6, Dated January 13, 2014, Related to License Renewal Application Project stage: Response to RAI ML14006A0212014-02-0606 February 2014 Requests for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application- Aging Management, Set 8 Project stage: RAI ML14023A5642014-02-0707 February 2014 RAI for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 13 Project stage: RAI ML14030A5962014-02-10010 February 2014 Requests for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 12 Project stage: RAI ML14007A6032014-02-18018 February 2014 Request for Additional Information for the Review of the Byron Nuclear Station, Units 1 and 2, and Braidwood Nuclear Station, Units 1 and 2, LRA - Aging Management - Set 17 Project stage: RAI ML14034A0682014-02-18018 February 2014 Request for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 11 Project stage: RAI ML14035A5342014-02-20020 February 2014 January 22, 2014, Summary of Telephone Conference Call Held Between NRC and Exelon Generation Company, Llc., Concerning Draft Requests for Additional Information Pertaining to the Byron Station and Braidwood Station, License Renewal Applica Project stage: Draft RAI ML14035A1892014-02-20020 February 2014 Summary of Telephone Conference Call Held on January 30, 2014, Between the U.S. Nuclear Regulatory Commission and Exelon Generation Company, LLC, Concerning Draft Request for Additional Information Pertaining to the Byron Station and Braidw Project stage: Draft RAI ML14050A1222014-02-24024 February 2014 Summary of Telephone Conference Call Held on January 16, 2014, Between the U.S. Nuclear Regulatory Commission and Exelon Generation Company, LLC, Concerning RAI Set 7, Tor the Byron-Braidwood License Renewal Application (TAC Nos. MF1879, Mf Project stage: RAI ML14038A3362014-02-26026 February 2014 Request for Additional Information for the Review of the Byron Nuclear Station, Units 1 and 2, and Braidwood Nuclear Station, Units 1 and 2, License Renewal Application - Aging Management - Set 10 Project stage: RAI RS-14-051, Response to NRC Requests for Additional Information, Set 8, Dated February 6, 2014 Related to the License Renewal Application2014-02-27027 February 2014 Response to NRC Requests for Additional Information, Set 8, Dated February 6, 2014 Related to the License Renewal Application Project stage: Response to RAI ML14063A4952014-03-0404 March 2014 Response to NRC Requests for Additional Information, Set 13, Dated February 7, 2014 Re License Renewal Application Project stage: Response to RAI ML14051A4312014-03-0404 March 2014 Summary of Telephone Conferene Call Held on January 29, 2014, Between the NRC and Exelon Generating Company, Llc., Concerning RAI Set 10, for the Byron and Braidwood Station License Renewal Application (TAC Nos. MF1879, MF1880, MF1881, and Project stage: RAI ML14036A3102014-03-0404 March 2014 Summary of Telephone Conference Call Held on January 28, 2014, Between NRC and Exelon, Concerning RAI Set 10, for the Byron and Braidwood Station, LRA Project stage: RAI ML14050A1672014-03-0404 March 2014 Summary of Telephone Conference Call on January 23, 2014, Between U.S. Nuclear Regulatory Commission and Exelon Generation Company, LLC, Concerning RAI Set 11, for Byron-Braidwood License Renewal Application (TAC Nos. MF1879, MF1880, MF1881 Project stage: RAI ML14051A4282014-03-0606 March 2014 January 13, 2014, Summary of Telephone Conference Call Held Between the NRC and Exelon RAI Set 8, for the Byron and Braidwood Station LRA Project stage: RAI ML14050A0812014-03-0707 March 2014 Correction to Request for Additional Information B.2.1.10-1, Letter Dated February 7, 2014, for the Review of the Byron Station and Braidwood Station, Units 1 and 2, LRA Set 13 Project stage: RAI ML14064A3912014-03-11011 March 2014 Request for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 15 Project stage: RAI ML14064A4032014-03-11011 March 2014 Summary of Telephone Conference Call on February 27, 2014, Between U.S. Nuclear Regulatory Commission & Exelon Generation Company, LLC Concerning Draft Request for Additional Information Re Byron Station & Braidwood Station License Renewal Project stage: Draft RAI ML14058B1802014-03-11011 March 2014 Summary of Telephone Conference Call on February 18, 2014, Between U.S. Nuclear Regulatory Commission & Exelon Generation Company, LLC Concerning Draft Request for Additional Information Regarding Byron & Braidwood Stations, License Renewal Project stage: Draft RAI ML14072A3692014-03-13013 March 2014 AMP Audit Enclosure (3) Project stage: Other ML14071A6202014-03-13013 March 2014 Aging Management Programs Audit Report Regarding the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2 (Tac Nos. MF1879, MF1880, MF1881, and MF1882) Project stage: Other ML14050A3042014-03-14014 March 2014 Scoping and Screening Methodology Audit Report Regarding the Byron Station, and Braidwood Station, Units 1 and 2, LRA Project stage: Other ML14058B1822014-03-18018 March 2014 Request for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 14 Project stage: RAI ML14051A5032014-03-20020 March 2014 Request for Additional Information for the Review of the Byron Nuclear Station Units 1 and 2, and Braidwood Nuclear Station, Units 1 and 2, License Renewal Application - Set 17 Project stage: RAI RS-14-084, Responses to NRC Requests for Additional Information, Set 10, Dated February 26, 2014 Related to the License Renewal Application2014-03-28028 March 2014 Responses to NRC Requests for Additional Information, Set 10, Dated February 26, 2014 Related to the License Renewal Application Project stage: Response to RAI ML14073A7052014-04-0303 April 2014 Summary of Telephone Conference Call Held on February 12, 2014, Between the NRC and Exelon, Concerning Drais Pertaining to the Byron and Braidwood Station, LRA Project stage: RAI ML14084A3352014-04-0303 April 2014 Request for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 16 Project stage: RAI ML14084A4882014-04-0707 April 2014 Summary of Telephone Conference Call Held Between NRC and Exelon Generation Company, LLC, Concerning Draft Request for Additional Information Pertaining to the Byron and Braidwood License Renewal Application Set 16 Project stage: Draft RAI ML14092A2612014-04-0707 April 2014 Request for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 20 Project stage: RAI ML14092A3462014-04-0707 April 2014 Project Manager Change for the License Renewal of Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2 Project stage: Other ML14094A3662014-04-0808 April 2014 Request for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 19 Project stage: RAI ML14093B2472014-04-10010 April 2014 Request for Additional Information for the Review of the Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, License Renewal Application, Set 18 Project stage: RAI ML14099A4852014-04-17017 April 2014 Request for Additional Information for the Review of the Byron Station, Units 1 & 2, and Braidwood Station, Units 1 & 2, License Renewal Application, Set 21, Project stage: RAI 2014-02-27
[Table View] |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 April 2, 2015 Mr. Michael P. Gallagher Vice President, License Renewal Projects Exelon Generation Company, LLC 200 Exelon Way Kennett Square, PA 19348
SUBJECT:
REQUEST FOR ADDITIONAL INFORMATION FOR THE REVIEW OF THE BYRON STATION, UNITS 1 AND 2, AND BRAIDWOOD STATION, UNITS 1 AND 2, LICENSE RENEWAL APPLICATION - SET 48 (TAC NOS. MF1879, MF1880, MF1881, AND MF1882)
Dear Mr. Gallagher:
By letter dated May 29, 2013, Exelon Generation Company, LLC, submitted an application pursuant to Title 10 of the Code of Federal Regulations Part 54, to renew operating licenses NPF-37, NPF-66, NPF-72, and NPF-77 for Byron Station, Units 1 and 2, and Braidwood Station, Units 1 and 2, respectively, for review by the U.S. Nuclear Regulatory Commission staff. The staff is reviewing the information contained in the license renewal application and has identified, in the enclosure, areas where additional information is needed to complete the review.
These requests for additional information were discussed with John Hufnagel, and a mutually agreeable date for the response is by April 17, 2015. If you have any questions, please contact me at 301-415-3873 or by e-mail at john.daily@nrc.gov.
Sincerely,
/RA/
John W. Daily, Senior Project Manager Projects Branch 1 Division of License Renewal Office of Nuclear Reactor Regulation Docket Nos. 50-454, 50-455, 50-456, and 50-457
Enclosure:
As stated cc w/encl: Listserv
ML15089A110
- concurrence via email OFFICE PM: DLR/RPB1 LA: DLR/RPB1 BC: DLR/RPB1 PM: DLR/RPB1 NAME JDaily YDiaz-Sanabria JDaily DATE 3/31/15 3/31/15 3/31 /15 4/ 2/15
ENCLOSURE BYRON STATION, UNITS 1 AND 2 AND BRAIDWOOD STATION, UNITS 1 AND 2 REQUEST FOR ADDITIONAL INFORMATION - SET 48 (TAC NOS. MF1879, MF1880, MF1881, AND MF1882)
RAI B.2.24-1c, Flux Thimble Tube Inspection follow-up Applicability: Braidwood Station (Braidwood), Units 1 and 2 Note: This RAI is composed of three sections (1-3), each of which deals with a background, issue, and request.
Background 1:
In its response dated February 23, 2015, the applicant stated that historical flux thimble tube wear experienced at Braidwood is bounded by industry operating experience for which the GALL Report AMP was evaluated. The applicant further stated that a plant-specific AMP is not necessary, since its plant-specific condition and age-related operating experience is bounded by the conditions and operating experience for which GALL Report AMP XI.M37 was evaluated.
In its RAI response dated October 31, 2014, the applicant stated that widespread inability to obtain flux thimble tube eddy current data occurred suddenly at Braidwood Station, Units 1 and 2 and involved flux thimble tubes of various in-service times. The applicant also stated that while Byron, Units 1 and 2 and Braidwood, Units 1 and 2 have the same basic flux thimble tube design (i.e., dimensions), the Byron Units have not had significant difficulty completing eddy current examinations.
In its October 31, 2014 response, the applicant stated that causal factors which include moisture and lubricant could account for the difficulties getting eddy current data, and it would consider activities to mitigate this issue. In its response dated February 23, 2015, the applicant stated that moisture and lubricant were not likely the causal factors and that deformation of the flux thimble tubes such that the internal dimension of the tubes is affected could prevent the eddy current probe from being fully inserted. The applicant also stated that deformation could occur because of mishandling, and is unlikely to result in deformation of all 58 flux thimble tubes. The applicant concluded that the most logical scenario is that the eddy current testing equipment or testing process is the likely cause of the recent issues related to obtaining eddy current testing data.
Issue 1:
The staff noted from the applicants responses that its program failed to obtain useful data from most of its flux thimble tubes during the recent outage inspections since 2012, due to restrictions inside the flux thimble tubes. The staff is concerned that the applicant has yet to identify the root cause and, as a result, is not able to implement effective corrective actions to resolve the problem.
The staff performed an industry operating experience search and did not note occurrences of widespread issues with inability to get eddy current data. In addition, since the 1980s when flux thimble tube wear became an issue, industrys use of chrome plated replacement tubes has greatly reduced wear rates which does not seem to be the case with the chrome plated replacement flux thimble tubes at Braidwood. The staff is also concerned that the increasing trend in the numbers of uninspectable flux thimble tubes, unique to Braidwood, may be due to an age-related deformation of the tubes (i.e., reduction in inside diameter).
Request 1:
(a) Provide technical justification that the operating experience for which the GALL Report AMP was evaluated is applicable to the plant-specific operating experience at Braidwood, considering the high wear rates, and multiple issues with eddy current examinations.
(b) Explain if higher than normal wear rates have been observed with chrome plated replacement tubes.
(c) Provide root cause analysis and corrective actions related to the inability to obtain useful inspection data.
(d) Explain if there is a new age-related mechanism in addition to wear that is causing obstruction of eddy current probe insertion.
(e) If the applicants operating experience is unique and not bounded by the operating experience for which the GALL Report AMP XI.M37 was evaluated, explain why a plant-specific AMP is not required to manage the aging effects during the period of extended operation (PEO).
Background 2:
In the LRA, the applicant described its program as an existing program which is consistent with the GALL Report AMP XI.M37, Flux Thimble Tube Inspection. In its February 23, 2015, response to the staffs follow-up RAI, the applicant described its program elements as will be consistent with the GALL Report AMP XI.M37 program elements.
Issue 2:
The staff reviewed the applicants claim of program consistency by comparing the applicants program with the GALL program. The staff noted that several program elements in the applicants program are not consistent with those of the GALL program. Specifically, the applicants program failed to obtain useful data from most of its flux thimble tubes during the recent outage inspections since 2012, and proposes an enhancement to replace its tubes every three cycles if flux thimble tube inspection data cannot be obtained. Based on the applicants existing operating experience, there is a possibility that the issues with the eddy current examinations will recur during the PEO. Based on this, the applicant will be replacing the flux thimble tubes at an acceptable frequency instead of inspecting them. In such a case, the applicants program would have exceptions to the following elements of the GALL AMP:
Element 3. Parameters Monitored/Inspected. GALL Guidance recommends that flux thimble tube wall thickness is monitored to detect loss of material from the flux thimble tubes. The applicants program would not be able to monitor material loss, or wear.
Element 4. Detection of Aging Effects. GALL Guidance recommends an inspection methodology (such as eddy current testing) used to detect loss of material. The applicants program would not be able to detect the aging effect of wear.
Element 5. Monitoring and Trending. GALL Guidance recommends that flux thimble tube wall thickness measurements are trended and wear rates are calculated and projected based on plant-specific data. The applicants program would not be able to provide trending and monitoring.
Request 2:
Identify all of the programs exceptions to GALL Report AMP XI.M37, Flux Thimble Tube Inspection when flux thimble tube inspection data cannot be obtained. Discuss how the proposed enhancement, to replace tubes at an acceptable frequency, will address the exceptions. Revise the program accordingly.
Background 3:
In its response dated February 23, 2015, the applicant stated multiple times that No flux thimble tube has been replaced due to age-related degradation in less than four (4) cycles, and that None of the 116 flux thimble tubes were required to be replaced due to age-related degradation in less than four (4) refueling cycles.
In its response, the applicant also stated multiple times that plant-specific historical wear rates were used to project tube wear and were applicable. The applicant further stated that industry operating experience indicates that flux thimble tube wear decreases over the flux thimble tube service life. In addition, the applicant provided an enhancement to its AMP to replace flux thimble tubes every three cycles when inspection data cannot be obtained.
Issue 3:
In Table 2, on Page 13 of its response, the applicant indicated that three tubes had to be replaced after only one cycle of service due to wear, which the staff considers to be age-related.
This appears to contradict the applicants statement that No flux thimble tube has been replaced due to age-related degradation in less than four (4) cycles.
The applicants justification for the enhancement does not consider worst case wear scenarios.
For example, it had experienced higher than expected wear rates but does not consider high wear rates in consecutive cycles. The applicant cited industry operating experience that wear rates decrease following high wear in earlier cycles. The staff noted that the applicant also experienced an increase in wear rates following cycles of low wear rates.
In addition, during its review of industry operating experience, the staff noted that there is industry operating experience which indicates that high wear rates may be sustained in multiple cycles. Specifically, the staff noted that a similar plant encountered multiple tube failures prior to the completion of three cycles of operation (LER-272/1981-028). A three-cycle replacement period appears to be inadequate.
Request 3:
a) Explain why initial wear resulting in replacement of three flux thimble tubes after one cycle is not flow related wear and will not recur.
b) Explain why replacing flux thimble tubes every three cycles when examination data are not obtained is adequate, in light of the plant-specific high wear rates, and industry operating experience which indicates that high wear rates could continue into subsequent cycles and result in tube failures in less than three cycles.
Letter to M. Gallagher from John W. Daily dated Month April 2, 2015
SUBJECT:
REQUEST FOR ADDITIONAL INFORMATION FOR THE REVIEW OF THE BYRON NUCLEAR STATION, UNITS 1 AND 2, AND BRAIDWOOD NUCLEAR STATION, UNITS 1 AND 2, LICENSE RENEWAL APPLICATION - SET 48 (TAC NOS. MF1879, MF1880, MF1881, AND MF1882)
DISTRIBUTION:
E-MAIL:
PUBLIC RidsNrrDlr Resource RidsNrrDlrRpb1 Resource RidsNrrDlrRpb2 Resource RidsOgcMailCenter JDaily TTran DMcIntyre, OPA JWiebe, DORL EDuncan, RIII JBenjamin, RIII AGarmoe, RIII SRI, Byron Station, RIII JRobbins, RIII VMitlyng, RIII PChandrathil, RIII