Letter Sequence Request |
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Initiation
- Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request, Request
- Acceptance...
Results
Other: ML13302A354, ML13302A367, ML13311A220, ML13311B020, ML13311B023, ML13311B024, ML13311B025, ML13311B028, ML13316A522, ML13316A524, ML13316A713, ML13316B729, ML13316B742, ML13316B758, ML13316B810, ML13317A151, ML13317A158, ML13317A160, ML13317A256, ML13317A368, ML13317A479, ML13317A535, ML13317A553, ML13317A700, ML13317A778, ML13317A851, ML13317B031, ML13317B095, ML13317B109, ML13319A212, ML13319A216, ML13322A697, ML13324A846, ML13324A913, ML13326A720, ML13329A100, ML13330A038, ML13330A130, ML13330A153, ML13330A184, ML13330A214, ML13330A241, ML13330A283, ML13331B423, ML13333A455, ML13333A465, ML13333A468, ML13333A473, ML13333A475, ML13333A498... further results
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MONTHYEARML19261E3241979-05-13013 May 1979 Requests Time & Distance Parameters for Emergency Planning Project stage: Request IR 05000361/19790151979-06-25025 June 1979 IE Insp Rept 50-361/79-15 & 50-362/79-15 on 790529-0601.No Noncompliance Noted.Major Areas Inspected:Const Activities Involving License Actions on Previous Insp Findings, Preservice Insp,Instrumentation & safety-related Pipe Welds Project stage: Request ML13304A5631979-06-29029 June 1979 Notifies That NRC Will Not Respond to Applicant 790619 Response & Objections to Document Requests from Intervenors Friends of the Earth.Matter Relates Solely to Discovery Between Intervenors & Applicants Project stage: Request ML13333A5521979-10-17017 October 1979 Forwards Responses to NRC Requirements Established to Date Following TMI Accident, in Response to NRC 790913 Request. Includes Commitments to Actions Set Forth in NUREG-0578 Project stage: Other ML13329A1001979-10-31031 October 1979 Responses to NRC Requirements Established to Date Following TMI Accident Project stage: Other ML13308A6511979-10-31031 October 1979 Nuclear Power Reactors in Us Project stage: Request IR 05000361/19790271979-11-15015 November 1979 IE Insp Repts 50-361/79-27 & 50-362/79-25 on 791001-05.No Noncompliance Noted.Major Areas Inspected:Allegation Re Factory Splices in GE Class IE Electrical Cable Installed at Facilities Project stage: Request ML13333A4551979-11-15015 November 1979 Forwards NRC Generic & plant-specific Requirements for Auxiliary Feedwater Sys.Designs & Procedures of Facility Should Be Evaluated Against Requirements to Determine Degree of Conformity Project stage: Other ML13319A2121979-11-21021 November 1979 Submits Addl Info in Support of 791017 Responses to NUREG-0578 Requirements.Forwards Two Oversize Drawings, Available in Central Files Only Project stage: Other ML13333A4561979-12-14014 December 1979 Responds to NRC Re Operation of Containment Purge & Vent Valves Pending Resolution of Isolation Valve Operability.Purge Valves Closed During Reactor Operation Until Operability Under Design Basis LOCA Is Proven Project stage: Request IR 05000206/19790011979-12-21021 December 1979 IE Insp Rept 50-206/79-01 on 790205-16.Noncompliance Noted: Failure to Issue Procedures,Failure of Offsite Committee to Perform Required Audits & Failure to Issue Corrective Action Request Project stage: Request ML13333A4651980-01-0202 January 1980 Notifies of Intent to Respond to NRC by 800110, Requesting Addl Info Re Auxiliary Feedwater Sys.Response to May Require Six to Eight Months.Util Is Consulting W/Westinghouse Project stage: Other ML13333A4681980-01-14014 January 1980 Responds to NRC 800102 Show Cause Order Re NUREG-0578 & 800104 Request Re Power Reliability.Seeks Aid in Preparing Response.Forwards Analysis of Reliability Impacts Resulting from Facility TMI Backfit Outage. W/O Encl Project stage: Other ML13333A4731980-01-16016 January 1980 Submits Addl Info Requested by NRC Re Auxiliary Feedwater Sys Flow Requirements.Provides Completion Schedule of Six to Eight Months for Requested Info Project stage: Other ML13311B0321980-01-16016 January 1980 Forwards Lists of CA Resident Petitions Re Seismic Conditions at Facility.Petitioners Have Received Fr Notice Re Receipt of Petition Under 10CFR2.206 Project stage: Request ML13311A2201980-01-17017 January 1980 Forwards Addl Info in Response to TMI Lessons Learned Task Force short-term Requirements Re Emergency Power Supply for Pressurizer Heaters & Relief & Block Valves.Seven Regular Size Drawings & 32 Oversize Drawings Encl Project stage: Other ML13311B0281980-01-18018 January 1980 Affidavit Attesting That Delay Until After 800601 in Implementation of long-term Mods to Provide Reset/Override Ability for All Automaticaly Isolated Valves Does Not Cause Undue Risk to Public Health & Safety Project stage: Other ML13311B0251980-01-18018 January 1980 Affidavit Attesting That Shutdown of Facility During Feb 1980 Will Adversely Impact Reliability in State of Ca. Analysis of Reliability Impacts Resulting from TMI Backfit Outage Encl Project stage: Other ML13311B0241980-01-18018 January 1980 Affidavit Attesting to Inability to Complete Implementation of Mods to Provide Capability for Individual Valve Operability After Containment Isolation Signal Reset &/Or Override Project stage: Other ML13311B0231980-01-18018 January 1980 Answer to NRC 800102 Order to Show Cause Why Licensee Should Not Implement Category a TMI Lessons Learned Task Force short-term Requirements by 800131.Requests Relief Due to Difficulty in Obtaining Equipment.W/Certificate of Svc Project stage: Other ML13311B0201980-01-20020 January 1980 Forwards Response to NRC 800102 Order to Show Cause Why Licensee Should Not Implement Category a TMI Lessons Learned Task Force short-term Requirements by 800131 Project stage: Other ML13333A4751980-01-23023 January 1980 Forwards Response to short-term & long-term Recommendations in Encl 1 of NRC Re Evaluation of Auxiliary Feedwater Sys.Five Drawings in Central Files Only Project stage: Other ML13322A6971980-01-31031 January 1980 Reload Safety Evaluation,Unit 1,Cycle 8 Project stage: Other ML13333A4981980-02-0808 February 1980 Submits Addl Info Re Commitment Schedule for short-term Lessons Learned Task Force Requirements.Circuitry to Close Auxiliary Feedwater Motor Operated Discharge Valve Will Be Installed During Apr 1980 Refueling Outage Project stage: Other ML19296C2141980-02-0808 February 1980 Forwards IE Bulletin 80-04, Analysis of PWR Main Steam Line Break W/Continued Feedwater Addition. No Written Response Required Project stage: Other ML13322A6931980-02-0808 February 1980 Amend 88 to Ol,Consisting of Proposed Changes 86,87,88 & 90 to Tech Specs.Certificate of Svc Encl Project stage: Request ML13322A6961980-02-0808 February 1980 Proposed Changes 86,87,88 & 90 to App a Tech Specs Re Auxiliary Feedwater Sys,Control Group Insertion Limits & Containment Integrity & App B Tech Specs Re Plankton Studies Project stage: Request ML13322A6911980-02-0808 February 1980 Forwards Amend 88 to Ol,Consisting of Proposed Changes 86, 87,88 & 90 to Tech Specs.Nrc Review of Proposed Change 88, Supporting Documentation Requested Prior to Resumption of Power Operation & Fee Encl Project stage: Request ML13333A5071980-02-14014 February 1980 Forwards Addl Info Re Conditions & Results of Endurance Testing Performed on Auxiliary Feedwater Sys Pumps in Support of Responses to NRC Lessons Learned Task Force Requirements Project stage: Other ML14107A2611980-04-18018 April 1980 Provides Preliminary Info Re Impact of Auxiliary Feedwater Sys Automation on Main Steam Line Break Safety Analysis,In Response to NRC 791221 Request.Revised Scoping Studies Will Be Completed by 800516 Project stage: Other IR 05000206/19800051980-04-18018 April 1980 IE Insp Rept 50-206/80-05 on 800310-13.No Noncompliance Noted.Major Areas Inspected:Document Control & Records Programs Project stage: Request ML13330A0381980-04-29029 April 1980 Responds to NRC Re Item 2.1.7.a,NUREG-0578, Automatic Initiation of Auxiliary Feedwater Sys. Commits to Installation of safety-grade Sys During Outage on or After 810101 Project stage: Other ML13302A3541980-05-12012 May 1980 Forwards Amend to OL Application,Consisting of Amend 18 to FSAR & Amend 3 to Fire Protection Plan Project stage: Other ML13316B7421980-05-12012 May 1980 Responds to IE Bulletin 80-04, Analysis of PWR Main Steam Line Break W/Continued Feedwater Addition. Scoping Studies Will Be Completed by 800513.Studies Include Effect of Auxiliary Feedwater Runout & Impact of Other Energy Sources Project stage: Other ML13316B7291980-05-19019 May 1980 Provides Addl Info to 800512 Responses to IE Bulletin 80-04. Evaluation of Scoping Studies Will Be Completed by Approx 800523 W/Full Response to Item 1 Provided by 801001.Review of Westinghouse Input Re Item 2 to Be Completed by 800701 Project stage: Other ML13303A7821980-05-19019 May 1980 Notification of 800520 Meeting W/Usgs & Util in Bethesda,Md to Discuss Need for Addl Offshore Seismic Profiles Near Site Project stage: Request 05000206/LER-1980-026-01, /01T-0:on 800609,preliminary Results of Main Steam Line Break Accident Scenarios to Determine Containment Response Required Corrective Actions to Reduce Calculated Peak Containment Pressures.Rept Re 800513 Meeting Encl1980-06-0909 June 1980 /01T-0:on 800609,preliminary Results of Main Steam Line Break Accident Scenarios to Determine Containment Response Required Corrective Actions to Reduce Calculated Peak Containment Pressures.Rept Re 800513 Meeting Encl Project stage: Meeting 05000206/LER-1980-026, Forwards LER 80-026/01T-0 & Rept Re Automatic Initiation of Auxiliary Feedwater Sys,Per 800513 Meeting W/Nrc1980-06-10010 June 1980 Forwards LER 80-026/01T-0 & Rept Re Automatic Initiation of Auxiliary Feedwater Sys,Per 800513 Meeting W/Nrc Project stage: Meeting ML13316B7581980-07-16016 July 1980 Reschedules Response to Item 2 of IE Bulletin 80-04, Analysis of PWR Main Stream Line Break W/Continued Feedwater Addition. Response Will Be Forwarded by 800801, Pending MSLB Core Response Reanalysis Project stage: Other ML13331B4231980-08-0404 August 1980 Provides Response to IE Bulletin 80-04,Item 2,per 800716 Commitment.Westinghouse Reviewed Previous Analysis of Core Response Following Main Steam Line Break.Results Indicated No Main or Auxiliary Feedwater Assumed in Previous Analysis Project stage: Other ML13302A3671980-08-13013 August 1980 Forwards Amend to OL Application,Consisting of Amend 19 to Fsar.Amend Provides Open Item Responses Requested by NRC & Miscellaneous Corrections,Clarifications & Additions. Repts & Oversize Drawings Available in Central Files Only Project stage: Other ML13302A4711980-10-0606 October 1980 Forwards Responses to NRC Questions & Revised FSAR Sections Re Preservice & Inservice Insp & Testing Project stage: Request ML13330A1301980-10-0606 October 1980 Notifies That Date for Submittal of Info Re Analyses of Main Steam Line or Feedwater Line Break Assuming Early Initiation of Auxiliary Feedwater Flow Has Been Rescheduled for 801201.Ltr Re TMI Lessons Learned Requirement Mods Encl Project stage: Other ML13302A8501980-10-16016 October 1980 Summary of 800923 Meeting W/Consultants,Usgs,Util & CA Div of Mines & Geology in Menlo Park,Ca Re Plant Seismology & Geology.Attendee List,Agenda & Util Conclusions Encl Project stage: Request ML13319A2161980-10-16016 October 1980 Forwards Design Details for Automated Auxiliary Feedwater Sys & RCS to Be Installed Per TMI Lessons Learned Requirements.Info Provided Supersedes Info in . Drawings in Central Files.Aperture Cards in PDR Project stage: Other ML13316A5241980-10-31031 October 1980 Fatigue Crack Growth Evaluation for San Onofre Unit 1 Main Steam Line Pipe Project stage: Other ML13316A5221980-11-30030 November 1980 Mechanistic Fracture Evaluation of San Onofre Unit 1 Main Steam Line Pipe Containing Postulated Through-Wall Crack Project stage: Other ML13330A1531980-12-0505 December 1980 Requests Extension Until 810201 to Evaluate Impact of Automating Auxiliary Feedwater Sys on Existing Safety Analysis & Extension Until 810115 to Provide Info Re Main Steam Line Piping Integrity Evaluation Project stage: Other ML13316B8101981-01-0505 January 1981 Confirms Implementation Dates for Approved TMI-related Items Contained in NUREG-0737 W/Exceptions Listed.Procurement or Const Activities Will Not Be Initiated Until NRC Review & Concurrence.Mods Targeted for Completion 830101 Project stage: Other ML13330A1841981-01-14014 January 1981 Forwards Westinghouse WCAP-9832 & WCAP-9808 Re Main Steam Line Integrity Evaluation.Crack Appearing Instantaneously Would Be Stable Both Globally & Locally.Initial Circumferential Flaw Would Show Negligible Growth Project stage: Other 1980-10-16
[Table View] |
Text
REGULATORNFORMATION DISTRIBUTION
ACCESSION NBR:8608250043 DOC.DATE: 86/08/21 NOTARIZED: NO DOCKET #
FACIL:50-206 San Onofre Nuclear Station, Unit 1, Southern Californ 05000206 AUTH.NAME AUTHOR AFFILIATION MEDFORD,M.O.
Southern California Edison Co.
RECIP.NAME RECIPIENT AFFILIATION LEARG.E.
PWR Project Directorate 1
SUBJECT:
Forwards Proposed Change 165 to Tech Specsurequiring that lower pressurizer level trip setpoint be maintained until mods to mismatch trip completedper NRC 860813 request.
Formal amend application will be submitted later.
DISTRIBUTION CODE: AOO1D COPIES RECEIVED:LTR I ENCL 1 SIZE:
TITLE: OR Submittal: General Distribution NOTES:License Exp date in accordance with 10CFR2,2.109.
05000206 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PWR--A EB 1
1 PWR-A EICSB 2
2 PWR-A FOB 1
1 PWR-A PD1 LA 1
0 PWR-A PD1 PD 01 5
5 DUDLEYR 1
1 PWR-A PSB 1
1 PWR-A RSB 1
1 INTERNAL: ADMILFMB 1
0 1
0 NRR/ORAS 1
0 04 1
1 RGN5 1
1 EXTERNAL: EG&G BRUSKE,S 1
1 LPDR 03 1
1 NRC PDR 02 1
1 NSIC 05 1
1 TOTAL NUMBER OF COPIES REGUIRED: LTTR 22 ENCL 18
Southern California Edison Company P. 0. BOX 800 2244 WALNUT GROVE AVENUE ROSEMEAD, CALIFORNIA 91770 M. 0.
MEDFORD TELEPHONE MANAGER. NUCLEAR LICENSING (618) 302-1749 August 21, 1986 Director, Office of Nuclear Reactor Regulation Attention: G. E. Lear, Director PWR Project Directorate No., 1 U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Gentlemen:
Subject:
Docket No. 50-206 Proposed Change No. 165 San Onofre Nuclear Generating Station Unit 1 The failure of pressure transmitter PT-459 was reported to the NRC, (by red phone) pursuant to 10 CFR 50.72 on July 29, 1986. The SCE review"of this failure and its consequences has identified a deficiency in the design, of the Steam/Feedwater Flow Mismatch Reactor Trip System. This deficiency has been the subject of several telephone discussions with the NRC staff during the past two weeks. The identified design deficiency can, due to a single failure, prevent the mismatch trip from occurring when required. This single failure therefore impacts the safety analyses for the Loss of Main Feedwater and Feedline Break transients since credit is taken for this trip in these two events.
As previously discussed with the NRC staff, immediate compensatory measures were instituted following identification of the problem. In addition, the affected safety analyses were reanalyzed without credit for the mismatch trip. The results of these analyses required that the Pressurizer High Level Trip setpoint be lowered to 50% (for Loss of Main Feedwater only) from the then existing 70% level in order to provide a transient response within the acceptance criteria previously committed. These analyses are provided as Enclosure 1. The lower pressurizer level trip is at the present time required by administrative controls, to be maintained until corrective actions are completed to assure that the mismatch trip is single failure proof.
During the telephone discussion of August 13, 1986, the NRC staff requested that the administrative controls be formalized by submitting a revision to Technical Specification 2.1 which required that the lower,
pressurizer level trip setpoint be maintained until modifications to the mismatch trip are completed. Accordingly, Enclosure 2 providis A preliminary copy of Proposed Change No. 165 to the SONGS 1 Technical Specifications.
PPDR 60LOB250043 86082 PDR
e 0
Mr. G.
August 21, 1986 This preliminary copy is provided in conjunction with the safety analyses of in order to assist the NRC staff in their request to expedite the issuance of this proposed change. The formal submittal in the form of a License Amendment Application will be provided shortly, following the required safety review and approval.
If you have any questions or desire additional information, please contact me.
Very trul yo rs, cc:
Mr. A. E. Chaffee, Regulatory Projects Branch, Region V Mr. F. R. Huey, NRC Senior Resident Inspector, SONGS 1, 2 and 3
ENCLOSURE 1 Loss of Normal Feedwater And Main Feedline Rupture Reanalysis San Onofre Unit 1 BACKGROUND The loss of Normal Feedwater (LONF) event and the Main Feedline Rupture (FLB) event were recently analyzed in the Spring of 1986 for Southern California Edison's (SCE) SONGS 1, Reference 1. This analysis showed that for the LONF with loss of reactor coolant pumps (RCPs), an auxiliary feedwater (AFW) flow of 165 gpm to 3 steam generators initiated 30 minutes after reactor trip provides acceptable results.
An AFW flow of 250 gpm to 2 steam generators initiated 20 minutes after reactor trip is adequate to remove decay heat for the FLB with loss of RCPs event. The above conclusions were based on the assumption that reactor trip was provided by the steam flow/feed flow mismatch signal.
Due to concerns raised by SCE regarding the availability of the steam flow/feed flow mismatch reactor trip, SCE has requested Westinghouse to reanalyze the LONF and the FLB events assuming the steam flow/feed flow mismatch reactor trip is not available.
ANALYSIS As in the 1986 LONF and FLB analysis, the LOFTRAN code is used to simulate the transients. The reanalysis consisted of two cases to determine the impact of no steam flow/feed flow mismatch reactor trip for the LONF and FLB events.
Protection is expected to be provided by the high pressurizer pressure, the high pressurizer water level, or the variable low pressurizer pressure reactor trip. The assumptions modelled in this reanalysis are the same assumptions used in the Spring 1986 analysis except as noted below.
- 1. A high pressurizer water level reactor trip setpoint of 50% NRS for the LONF and 70% NRS for the FLB are assumed with a delay time of 2 seconds.
- 2. A high pressurizer pressure reactor trip setpoint of 2260 psia (including uncertainties) is assumed with a delay time of 2 seconds.
- 3. The delay time of the variable low pressurizer pressure reactor trip is assumed to be 2.32 seconds.
- 4. An initial pressurizer water level of 37.5% NRS is modelled which corresponds to the programmed pressurizer level at full power and reduced average temperature.
- 5. For this reanalysis, the unavailability of the steam flow/feed flow reactor trip is assumed to be the single failure. As such, the turbine driven AFW pump is available. The turbine driven AFW pump, which delivers a total of 165 gpm to 3 steam generators, is modelled only for the LONF event. The steam pressure during the FLB event is not expected to be sufficient for the turbine driven AFW pump. A delay of 3 minutes following a low steam generator water level signal is assumed for initiation of the turbine driven AFW pump. For the FLB event, a delay of 15 minutes following a low steam generator water level is assumed for initiation of the motor driven AFW pump followed by a line fill time of approximately 5 minutes. The motor driven AFW pump delivers a total of 250 gpm to 2 steam generators.
RESULTS The results of the transient analysis are shown in the attached figures.
Loss of Normal Feedwater The results show that lowering the high pressurizer water level reactor trip setpoint to 50% prevents the pressurizer from filling. Reactor trip occurs on pressurizer high level at 65.3 seconds.
Peak pressurizer volume of 1092 cubic feet occurs at 1729 seconds.
Feedline Break The results show that the pressurizer fills and hot leg boiling occurs.
Reactor trip occurs on the existing variable low pressure trip at 24.4 seconds. Peak pressurizer pressure of 2204 psia occurs at 1151 seconds.
Peak pressurizer volume of 1316 cubic feet occurs at 1145 seconds.
Detailed calculations showed that the mass relieved through the PORV's between the time of bulk boiling in the primary system and the time that the heat removal capability of the AFW exceeds the core decay heat (turnaround) was not sufficient to uncover the core. As such, the ultimate acceptance criteria for a FLB that the core remains coolable during the transient is shown to be met.
CONCLUSIONS The results of the analysis show that for the LONF with loss of RCPs event, an AFW flow of 165 gpm to 3 steam generators with a 3 minute delay in initiating the turbine driven AFW pump and a pressurizer high water level reactor trip setpoint of 50% NRS provide adequate protection to prevent the pressurizer from filling.
For the FLB with loss of RCPs event, an AFW flow of 250 gpm to 2 steam generators with a 15 minute delay in initiating the motor driven AFW pump and the existing variable low pressure trip are adequate to remove decay heat and keep the core coolable. Hence, the change in the high pressurizer water level trip.is required only for the LONF event.
REFERENCE M. 0. Medford (SCE) to G. E. Lear (NRC) letter dated May 1, 1986 0018P