ML102170525

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IR 05000298-10-003; 03/25/2010 - 06/23/2010; Cooper Nuclear Station, Integrated Resident and Regional Report; Equipment Alignments, Maintenance Effectiveness, Event Follow-up, Other Activities
ML102170525
Person / Time
Site: Cooper Entergy icon.png
Issue date: 08/04/2010
From: Vincent Gaddy
NRC/RGN-IV/DRP/RPB-C
To: O'Grady B
Nebraska Public Power District (NPPD)
References
IR-10-003
Download: ML102170525 (41)


See also: IR 05000298/2010003

Text

UNITED STATES

NU C LE AR RE G UL AT O RY C O M M I S S I O N

REGION IV

6 12 EAST LAMAR BL VD , S U I T E 4 0 0

A R L I N G T O N , T E X A S 7 6 0 1 1 -41 25

August 4, 2010

Brian J. OGrady, Vice President-Nuclear

and Chief Nuclear Officer

Nebraska Public Power - Cooper

Nuclear Station

72676 648A Avenue

Brownville, NE 68321

Subject: COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT

05000298/2010003

Dear Mr. OGrady:

On June 23, 2010, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Cooper Nuclear Station. The enclosed integrated inspection report documents the

inspection findings, which were discussed on July 1, 2010, with Brian OGrady, Vice President

and Chief Nuclear Officer, and other members of your staff.

The inspections examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents two NRC-identified violations, one self-revealing violation and one self-

revealing finding of very low safety significance (Green). Three of these findings were

determined to involve violations of NRC requirements. However, because of the very low safety

significance and because they are entered into your corrective action program, the NRC is

treating these findings as a noncited violations, consistent with Section VI.A.1 of the NRC

Enforcement Policy. If you contest the violations or the significance of the noncited violations,

you should provide a response within 30 days of the date of this inspection report, with the basis

for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission, Region IV, 612 E. Lamar Blvd, Suite 400, Arlington, Texas,

76011-4125; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Cooper Nuclear Station

facility. In addition, if you disagree with the crosscutting aspect assigned to any finding in this

report, you should provide a response within 30 days of the date of this inspection report, with

the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC

Resident Inspector at Cooper Nuclear Station.

Nebraska Public Power District -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, and its

enclosure, will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room).

Sincerely,

/RA/

Vince Gaddy, Chief

Project Branch C

Division of Reactor Projects

Docket: 50-298

License: DRP-46

Enclosure:

NRC Inspection Report 05000298/2010003

w/Attachment: Supplemental Information

cc w/Enclosure:

Gene Mace Michael J. Linder, Director

Nuclear Asset Manager Nebraska Department of

Nebraska Public Power District Environmental Quality

P.O. Box 98 P.O. Box 98922

Brownville, NE 68321 Lincoln, NE 68509-8922

John C. McClure, Vice President Randy Rohrs, Chairman

and General Counsel Nemaha County Board of Commissioners

Nebraska Public Power District Nemaha County Courthouse

1414 15th Street 1824 N Street, Suite 201

P.O. Box 499 Auburn, NE 68305

Columbus, NE 68601

Julia Schmitt, Manager

David Van Der Kamp Nebraska Department of Health

Licensing Manager and Human Services

Nebraska Public Power District Division of Public Health

P.O. Box 98 Nebraska State Office Building, 3rd Fl

Brownville, NE 68321 Lincoln, NE 68509-5026

Deputy Director for Policy

Missouri Department of Natural Resources

P.O. Box 176

Jefferson City, MO 65102-0176

Nebraska Public Power District -3-

Director, Missouri State Emergency Keith G. Henke, Planner

Management Agency Division of Community and Public Health

P.O. Box 116 Office of Emergency Coordination

Jefferson City, MO 65102-0116 P.O. Box 570

Jefferson City, MO 65102

Chief, Radiation and Asbestos

Control Section Art Zaremba

Kansas Department of Health Director of Nuclear Safety Assurance

and Environment Nebraska Public Power District

Bureau of Air and Radiation P.O. Box 98

1000 SW Jackson, Suite 310 Brownville, NE 68321

Topeka, KS 66612-1366

Ronald D. Asche, President

Melanie Rasmussen, State Liaison Officer/ and Chief Executive Officer

Radiation Control Program Director Nebraska Public Power District

Bureau of Radiological Health 1414 15th Street

Iowa Department of Public Health Columbus, NE 68601

Lucas State Office Building, 5th Floor

321 East 12th Street Chief, Technological Hazards

Des Moines, IA 50319 Branch

FEMA, Region VII

John F. McCann, Director, Licensing 9221 Ward Parkway

Entergy Nuclear Northeast Suite 300

Entergy Nuclear Operations, Inc. Kansas City, MO 64114-3372

440 Hamilton Avenue

White Plains, NY 10601-1813

Nebraska Public Power District -4-

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

Acting DRP Director (Anton.Vegel@nrc.gov)

Acting DRP Deputy Director (Troy.Pruett@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

Acting DRS Deputy Director (Jeff.Clark@nrc.gov)

Senior Resident Inspector (Nick.Taylor@nrc.gov)

Resident Inspector (Michael.Chambers@nrc.gov)

Branch Chief, DRP/C (Vincent.Gaddy@nrc.gov)

Senior Project Engineer, DRP/C (Bob.Hagar@nrc.gov)

CNS Administrative Assistant (Amy.Elam@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Public Affairs Officer (Lara.Uselding@nrc.gov)

Project Manager (Lynnea.Wilkins@nrc.gov)

Branch Chief, DRS/TSB (Michael.Hay@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Regional Counsel (Karla.Fuller@nrc.gov)

Congressional Affairs Officer (Jenny.Weil@nrc.gov)

OEMail Resource

ROPreports

DRS/TSB STA (Dale.Powers@nrc.gov)

OEDO RIV Coordinator (Margie.Kotzalas@nrc.gov)

ADAMS: No x Yes SUNSI Review Complete Reviewer Initials: VGG

x Publicly Available x Non-Sensitive

Non-publicly Available Sensitive

RI:DRP/C SRI:DRP/C C:DRS/EB1 S:DRS/TSB C:DRS/EB2

MLChambers NHTaylor TRFarnholtz MCHay NFOKeefe

/RA/ /RA/ /RA/ /RA/ /RA/

8/4/10 88/3/10 7/27/10 8/2/10 7/28/10

C:DRS/OB C:DRS/PSB1 C:DRS/PSB2 C:DRP/C

MHaire MPShannon GEWerner VGGaddy

/RA/BRL for /RA/ /RA/ /RA/

7/28/10 7/28/10 7/28/10 8/4/10

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-298

License: DRP-46

Report: 05000298/2010003

Licensee: Nebraska Public Power District

Facility: Cooper Nuclear Station

Location: 72676 648A Ave

Brownville, NE 68321

Dates: March 25 through June 23, 2010

Inspectors: N. Taylor, Senior Resident Inspector

M. Chambers, Resident Inspector

R. Hagar, Senior Project Engineer

R. Kumana, Project Engineer

Approved By: Vince Gaddy, Chief, Project Branch C

Division of Reactor Projects

-1- Enclosure

SUMMARY OF FINDINGS

IR 05000298/2010003; 03/25/2010 - 06/23/2010; Cooper Nuclear Station, Integrated Resident

and Regional Report; Equipment Alignments, Maintenance Effectiveness, Event Follow-up,

Other Activities

The report covered a 3-month period of inspection by resident inspectors. Four Green findings

were identified. The significance of most findings is indicated by their color (Green, White,

Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process.

Findings for which the significance determination process does not apply may be Green or be

assigned a severity level after NRC management review. The NRC's program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Initiating Events

Green. A self-revealing noncited violation of 10 CFR 50.54.j was identified when

the licensee failed to ensure that mechanisms which may affect reactivity are

manipulated only with the knowledge and consent of a licensed operator at the

controls. Specifically, a work planner caused a feedwater heater trip by touching a

pressure regulating valve without the knowledge of the control room. This action

resulted in a feedwater transient. A subsequent reactivity increase occurred due to

the change in feedwater temperature causing the reactor to exceed the licensed

thermal power limit of 2419 MWt until reactor operators reduced power. The

licensee immediately reduced power using the recirculation pumps. The licensee

entered this issue in their corrective action program as CR-CNS-2010-03091.

The finding was more than minor because the performance deficiency could be

reasonably viewed as a precursor to a significant event in that a reactor power

transient was initiated without the knowledge of the control room. This finding was

characterized under the significance determination process as having very low

safety significance because while the finding degraded the transient initiator

contributor function of the initiating events cornerstone, it did not contribute to both

the likelihood of a reactor trip and the likelihood that mitigation equipment or

functions will not be available. The inspectors determined that this finding has a

crosscutting aspect in the area of human performance associated with the work

practices component because the work planner proceeded in the face of

unexpected circumstances by exceeding the scope of the job when he found the

leak was greater than expected H.4(a) (Section 4OA3).

Green. A self-revealing finding was identified for the licensees failure to

implement the preventive maintenance requirements of the vendor manual for the

plant traveling water screens. Specifically, Vendor Manual 140, Traveling Water

Screen, Revision 35, contained daily and weekly routine maintenance

requirements to open the channel-flushing valve to clear any accumulated debris

-2- Enclosure

from the screens. Despite the fact that the licensee incorporated this vendor

manual into their preventive maintenance system, this maintenance requirement

was overlooked. The failure to perform this maintenance task led to the trip of the

A1 and A2 traveling water screens on May 1, 2010, and required an emergent

power reduction. The licensee entered this issue in their corrective action program

as Condition Report CR-CNS-2010-03195, and implemented daily checks of the

traveling water screens and daily flushing of the screen debris troughs.

The finding was more than minor because it affected the equipment performance

attribute of the initiating events cornerstone, and adversely affected the

cornerstone objective to limit the likelihood of those events that upset plant stability

and challenge critical safety functions during shutdown as well as power

operations. This finding was characterized under the significance determination

process as having very low safety significance because it did not contribute to both

the likelihood of a reactor trip and the likelihood that mitigation functions would be

unavailable. The inspectors determined that no crosscutting aspect was

applicable to this finding because the performance deficiency was not reflective of

current performance (Section 4OA5).

Cornerstone: Mitigating Systems

Green. The inspectors identified a noncited violation of 10 CFR 50 App B

Criterion III, Design Control, in which the licensee failed to maintain

accurate design drawings of the service water system discharge piping.

Specifically, Drawing BR 2120, Yard Circ. & Service Water Piping Plan &

Sections, Revision 14 incorrectly identified the as-built configuration of the

service water system discharge piping, and was used as a design input to

numerous essential calculations. The licensee completed an operability

evaluation that demonstrated that the service water was operable despite the

condition. The licensee entered this issue in their corrective action program as

Condition Report CR-CNS-2010-03689.

The finding was more than minor because it affected the design control attribute of

the mitigating systems cornerstone, and adversely affected the cornerstone

objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core

damage). This finding was characterized under the significance determination

process as having very low safety significance because all of the screening

questions in the Manual Chapter 0609, Attachment 4, Initial Screening and

Characterization of Findings Phase 1 screening table were answered in the

negative. The inspectors determined that no cross cutting aspect was applicable

to this finding due to the age of the performance deficiency and the lack of recent

identification opportunities. (Section 1R04).

Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(2),

requirements for monitoring the effectiveness of maintenance at nuclear power

plants, for failure to demonstrate that the performance of the essential 4160 volt

-3- Enclosure

alternating current power system was effectively controlled through appropriate

preventive maintenance. As a result, the licensee did not establish goals or

monitor the performance of the essential power system Agastat relays per

10 CFR 50.65 (a)(1) to ensure appropriate corrective actions were initiated

when a revised evaluation of a Agastat time delay relay failure incorrectly

changed the initial functional failure determination. Incorrectly changing this

maintenance preventable functional failure resulted in the affected function,

EE-PF03A, not reaching the licensees maintenance rule (a)(1) threshold.

The licensee entered this issue in their corrective action program as

Condition Report CR-CNS-2008-07910.

This finding is more than minor because it affected the reliability objective of the

Equipment Performance attribute under the Mitigating Systems Cornerstone. The

inspectors determined that this performance deficiency was an additional, but

separate consequence of the degraded performance of the essential 4160 volt

alternating current system Agastat relays. Following the guidance of Appendix B

to MC0612 and Appendix D to IP 71111.12, the inspectors determined that this

finding occurred as a consequence of actual problems with the Agastat relays, and

that those actual problems were not attributable to this finding. This finding

therefore cannot be processed through the significance determination process,

and is considered to be Green by NRC staff review. The finding has a crosscutting

aspect in the area of human performance associated with decision-making

because the licensee did not use conservative assumptions in the functional failure

evaluation of a Agastat relay failure H.1(b) (Section 1R12).

B. Licensee-Identified Violations

None

-4- Enclosure

REPORT DETAILS

Summary of Plant Status

Cooper Nuclear Station began the inspection period at full power on March 24, 2010. On

May 1, 2010, the plant reduced power to 70 percent in response to a loss of a circulating water

pump due to intake screen fouling. The licensee cleared the screen and returned to

100 percent power later that day. On May 7, 2010, the licensee reduced power to 70 percent

for scheduled surveillance testing and returned to 100 percent power On June 4, 2010, the

licensee reduced power to 36 percent for scheduled maintenance on the recirculation pump

motor generator B. The plant returned to full power on June 10, 2010, where it remained for the

rest of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 Summer Readiness for Offsite and Alternate-ac Power

a. Inspection Scope

The inspectors performed a review of preparations for summer weather for selected

systems, including conditions that could lead to loss-of-offsite power and conditions that

could result from high temperatures. The inspectors reviewed the procedures affecting

these areas and the communications protocols between the transmission system

operator and the plant to verify that the appropriate information was being exchanged

when issues arose that could affect the offsite power system. Examples of aspects

considered in the inspectors review included:

The coordination between the transmission system operator and the plants

operations personnel during off-normal or emergency events

The explanations for the events

The estimates of when the offsite power system would be returned to a normal

state

The notifications from the transmission system operator to the plant when the

offsite power system was returned to normal

During the inspection, the inspectors focused on plant-specific design features and the

procedures used by plant personnel to mitigate or respond to adverse weather

conditions. Additionally, the inspectors reviewed the UFSAR and performance

requirements for systems selected for inspection, and verified that operator actions were

-5- Enclosure

appropriate as specified by plant-specific procedures. Specific documents reviewed

during this inspection are listed in the attachment. The inspectors also reviewed

corrective action program items to verify that the licensee was identifying adverse

weather issues at an appropriate threshold and entering them into their corrective action

program in accordance with station corrective action procedures. The inspectors

reviews focused specifically on the following plant systems:

Alternate AC readiness and service water systems

These activities constitute completion of one readiness for summer weather affect on

offsite and alternate-ac power sample as defined in Inspection Procedure 71111.01-05.

b. Findings

No findings were identified.

.2 Readiness to Cope with External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The evaluation included a review to check

for deviations from the descriptions provided in the Updated Final Safety Analysis Report

for features intended to mitigate the potential for flooding from external factors. As part

of this evaluation, the inspectors checked for obstructions that could prevent draining,

checked that the roofs did not contain obvious loose items that could clog drains in the

event of heavy precipitation, and determined that barriers required to mitigate the flood

were in place and operable. Additionally, the inspectors performed an inspection of the

protected area to identify any modification to the site that would inhibit site drainage

during a probable maximum precipitation event or allow water ingress past a barrier.

The inspectors also reviewed the abnormal operating procedure for mitigating the design

basis flood to ensure it could be implemented as written. Specific documents reviewed

during this inspection are listed in the attachment.

These activities constitute completion of one external flooding sample as defined in

Inspection Procedure 71111.01-05.

b. Findings

No findings were identified.

-6- Enclosure

1R04 Equipment Alignments (71111.04)

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

April 14, 2010, Core spray A

May 19, 2010, High pressure coolant injection

May 26, 2010, 69kV and 12.5kV switchyard alignment

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could affect the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, Updated Final Safety Analysis Report, technical specification

requirements, administrative technical specifications, outstanding work orders, condition

reports, and the impact of ongoing work activities on redundant trains of equipment in

order to identify conditions that could have rendered the systems incapable of

performing their intended functions. The inspectors also inspected accessible portions

of the systems to verify system components and support equipment were aligned

correctly and operable. The inspectors examined the material condition of the

components and observed operating parameters of equipment to verify that there were

no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program with the appropriate significance characterization. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of three partial system walkdown samples as

defined in Inspection Procedure 71111.04-05.

b. Findings

Introduction. The inspectors identified a Green noncited violation of 10 CFR 50 App B

Criterion III, Design Control, in which the licensee failed to maintain accurate design

drawings of the service water system discharge piping. Specifically, Drawing BR 2120,

Yard Circ. & Service Water Piping Plan & Sections, Revision 14 incorrectly identified

the as-left configuration of the service water system discharge piping, and was used as a

design input to numerous essential calculations.

Description. During followup of degraded service water system performance from

Refueling Outage 25 that occurred in October 2009, the licensee discovered that the

configuration of the combined service water/circulating water common discharge lines

was not as depicted on Drawing BR 2120, Yard Circ. & Service Water Piping Plan &

Sections, Revision 14. Specifically, BR 2120 showed that the two divisional pipes

-7- Enclosure

terminated 24 feet apart, protruding from the west bank of the plant discharge canal a

few feet below the waterline. In contrast, divers discovered that the pipes instead

terminated at the bottom of the discharge canal only 6 inches apart.

Inspectors learned that the as-found piping configuration was meant by the Architect-

engineer to be an interim step in the fabrication process. Drawing BR 2120 was

developed during plant construction and was revised regularly as the service water

system and circulating water system were constructed. The service water discharge

piping first appears in the drawing in Revision 7, dated March 5, 1968. In this drawing,

the as-found piping configuration was depicted (pipes terminated at the bottom of the

canal, 6 inches apart). The architect-engineer then performed an options analysis of

different piping configurations in an effort to reduce the impact of siltation on the service

water piping, resulting in the recommendation that Nebraska Public Power District

separate the pipes by 24 feet and move their termination point to high on the west bank

of the discharge canal to avoid siltation and the likelihood of common mode failure. This

recommendation was reflected in BR 2120 Revision 13, July 12, 1970. The change

notes on the drawing indicated that the purpose of the revision was changed

termination point of 24 SW-2/CW-2 lines.

The licensees decision regarding this option was documented in Burns and Roe Design

Information Notice 2978-02, July 31, 1973, which states the following:

NPPD has approved the revised SW-2/CW-2 discharge piping into the circ water

discharge canal generally as shown in study dwg 264. Please show the revised

piping such that the 24 CW-2 discharges through the side of the canal rip rap at

center line elevation 867, approximately 2 feet past the rip rap.

Based on this discussion, BR 2120 was updated in Revision 14 to label BR 2120 as a

construction document versus a design sketch. A subsequent Burns and Roe

memorandum dated August 2, 1973, however, documents the following:

The service water piping into the discharge canal has been modified to prevent

silt blockage of the exit piping by rerouting piping through the side of the

discharge canal at an elevation 7 feet above the bottom of the canal. This is

being held in abeyance by NPPD.

The memo contained no discussion of why the design change was being held in

abeyance. The licensee was unable to find any records to help understand the rationale

for not implementing the design change. The net result is that BR 2120 reflected a

planned, but never implemented, design change to the service water system discharge

piping. No further changes were made for BR 2120 until after the discovery of the

configuration error in October 2009.

Although the licensee identified that the discharge lines were not depicted on Drawing

BR 2120, the inspectors added value by identifying that BR 2120 had been used as a

design input into NEDC 92-034, Water Hammer Analysis of Service Water System.

NEDC 92-034 is a design basis calculation that was performed to document the

-8- Enclosure

response of the service water system to potential water hammer affects during design

basis events. This calculation depended on an analytical model of the service water

system that was developed based upon available drawings, one of which was BR 2120;

however, BR 2120 contained substantial errors in that it documented the wrong

elevation of the discharge point and did not include several ninety degree pipe bends

that exist in the as-built piping. As a result, the calculation result was called into

question by the inspectors.

In response to this question, the licensee initiated CR-CNS-2010-03689 and completed

an operability evaluation that demonstrated that the service water system was operable

despite this unanalyzed condition. Additional corrective actions have since been

identified, including an action to re-perform the affected calculation. Additionally, an

extent of condition review by the licensee identified five other calculations that appear to

have used BR 2120 as a design input.

The inspectors determined that this represented a failure to document the plant design in

applicable drawings. Reviews by the inspectors did not identify any recent opportunities

to discover the error prior to October 2009.

Analysis. The inspectors determined that the finding is a performance deficiency in that

the licensee failed to maintain accurate design drawings of the service water system

discharge piping. The finding was more than minor because it affected the design

control attribute of the mitigating systems cornerstone, and adversely affected the

cornerstone objective to ensure the availability, reliability, and capability of systems that

respond to initiating events to prevent undesirable consequences (i.e., core damage).

This finding was characterized under the significance determination process as having

very low safety significance because all of the screening questions in the Manual

Chapter 0609, Attachment 4, Initial Screening and Characterization of Findings

Phase 1 screening table were answered in the negative. The inspectors determined that

no cross cutting aspect was applicable to this finding due to the age of the performance

deficiency and the lack of recent identification opportunities.

Enforcement. 10 CFR 50 Appendix B, Criterion III, Design Control, requires, in part,

that measures shall be established to assure that the design basis for structures,

systems, and components that could prevent or mitigate the consequences of postulated

accidents are correctly translated into drawings. Contrary to this requirement, from the

beginning of power operations on January 18, 1974, to present, the plant drawings used

to document the design of the service water discharge piping were incorrect. As a

result, incorrect information was used as in input to numerous essential calculations and

analyses. Because the finding is of very low safety significance and has been entered

into the licensees corrective action program as CR-CNS-2010-03689, this violation is

being treated as an NCV consistent with Section VI.A of the Enforcement Policy:

NCV 05000298/2010003-01, "Failure to Document Design of Service Water Discharge

Piping in Plant Drawings.

-9- Enclosure

.2 Complete Walkdown

a. Inspection Scope

On April 14, 2010, the inspectors performed a complete system alignment inspection of

the Reactor Core Isolation Cooling system to verify the functional capability of the

system. The inspectors selected this system because it was considered both safety

significant and risk significant in the licensees probabilistic risk assessment. The

inspectors inspected the system to review mechanical and electrical equipment line ups,

electrical power availability, system pressure and temperature indications, as

appropriate, component labeling, component lubrication, component and equipment

cooling, hangers and supports, operability of support systems, and to ensure that

ancillary equipment or debris did not interfere with equipment operation. The inspectors

reviewed a sample of past and outstanding work orders to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the corrective action program database to ensure that system equipment-

alignment problems were being identified and appropriately resolved. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one complete system walkdown sample as

defined in Inspection Procedure 71111.04-05.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05)

Quarterly Fire Inspection Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

April 7, 2010, Diesel generator 1B room, Zone 14B

April 7, 2010, Diesel generator 1B diesel oil day tank room, Zone 14D

April 14, 2010, Reactor building 859 feet 9 inch level, Zone 1B

April 14, 2010, Hydraulic drive pump room, Zone 1G

The inspectors reviewed areas to assess if licensee personnel had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant; effectively maintained fire detection and suppression capability; maintained

passive fire protection features in good material condition; and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features, in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

- 10 - Enclosure

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to affect equipment that could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed; that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees corrective action program.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four quarterly fire-protection inspection samples

as defined in Inspection Procedure 71111.05-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

a. Inspection Scope

On April 13, 2010, and June 9, 2010, the inspectors observed a crew of licensed

operators in the plants simulator to verify that operator performance was adequate,

evaluators were identifying and documenting crew performance problems, and training

was being conducted in accordance with licensee procedures. The inspectors evaluated

the following areas:

Licensed operator performance

Crews clarity and formality of communications

Crews ability to take timely actions in the conservative direction

Crews prioritization, interpretation, and verification of annunciator alarms

Crews correct use and implementation of abnormal and emergency procedures

Control board manipulations

Oversight and direction from supervisors

Crews ability to identify and implement appropriate technical specification

actions and emergency plan actions and notifications

- 11 - Enclosure

The inspectors compared the crews performance in these areas to pre-established

operator action expectations and successful critical task completion requirements.

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of two quarterly licensed-operator requalification

program samples as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

April 25, 2010, Barksdale pressure switch failures

May 12, 2010, Extent of condition review of RHR-MOV functional failure

evaluations

May 13, 2010, Safety relief pilot valve test failures

June 3, 2010, RHR-MO-15D valve failure to open functional failure evaluations

The inspectors reviewed events such as where ineffective equipment maintenance has

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

Implementing appropriate work practices

Identifying and addressing common cause failures

Scoping of systems in accordance with 10 CFR 50.65(b)

Characterizing system reliability issues for performance

Charging unavailability for performance

Trending key parameters for condition monitoring

Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or -(a)(2)

Verifying appropriate performance criteria for structures, systems, and

components classified as having an adequate demonstration of performance

- 12 - Enclosure

through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as

requiring the establishment of appropriate and adequate goals and corrective

actions for systems classified as not having adequate performance, as described

in 10 CFR 50.65(a)(1)

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of four quarterly maintenance effectiveness

samples as defined in Inspection Procedure 71111.12-05.

b. Findings

Introduction. The inspectors identified a Green noncited violation of 10 CFR 50.65(a)(2),

requirements for monitoring the effectiveness of maintenance at nuclear power plants,

for failure to demonstrate that the performance of the essential 4160 volt alternating

current power system was effectively controlled through appropriate preventive

maintenance. As a result, the licensee did not establish goals or monitor the

performance of the essential power system Agastat relays per 10 CFR 50.65(a)(1) to

ensure appropriate corrective actions were initiated when a revised evaluation of a

Agastat time delay relay failure incorrectly changed the initial functional failure

determination. Incorrectly changing this maintenance preventable functional failure

resulted in the affected function, EE-PF03A, not reaching the licensees maintenance

rule (a)(1) threshold.

Description. The licensee had two functional failures associated with the 4160 volt

essential power supply function EE-PF03A in 2008. EE-PF03As function is to provide

essential 4160 volt alternating current power to the Division 1 critical station electrical

auxiliary loads. These two functional failures exceeded the threshold to perform a

maintenance rule (a)(1) evaluation to determine if system performance was effectively

controlled through appropriate maintenance.

The first functional failure occurred March 3, 2008, when an Agastat time delay relay

failed repeated attempts to calibrate. This relay is required to open the Division 1 critical

feeder breaker on low voltage prior to the low voltage condition damaging essential

equipment such as the motors on emergency core cooling pumps. This was related to a

long standing problem with Agastat time delay relays having foreign material introduced

during manufacturing that introduced random changes in the timers countdown

performance. The licensee had been handling this issue for several years by frequent

preventative maintenance to monitor Agastat relays for normal wear and indications of

foreign material degraded performance. Therefore, this was a maintenance preventable

functional failure. Condition Report CR-CNS-2008-01352 was initiated to resolve this

problem.

- 13 - Enclosure

The second functional failure occurred October 28, 2008, when an essential service

water pump supply breaker failed to close and start the pump when loose screws on the

breakers micro switch prevented it from functioning. The loose screws were due to

inadequate oversight of the breaker refurbishment process and therefore, a maintenance

preventable functional failure. Condition Report CR-CNS-2008-07910 was initiated to

resolve this problem.

A December 23, 2008, licensees maintenance rule expert panel meeting determined

that these two maintenance rule preventable failures required placing the function

EE-PR03A in (a)(1) status to monitor the performance of the Division 1 essential

4160 volt alternating current supply against goals to ensure this system is capable of

fulfilling its function. Several months passed while the licensee attempted to determine

what would be the appropriate goals and corrective actions to address these functional

failures.

On March 23, 2009, the maintenance rule expert panel returned the function EE-PF03A

to (a)(2) status based on a revision of the March 3, 2008, Agastat relay functional failure

evaluation. This revised evaluation determined that the Agastat relay failure was not a

maintenance rule functional failure due to the failed relay timer results being less than

the design function time requirement of 17 seconds by 0.3 seconds. The 17 seconds is

the design basis time exposure below which essential motors are assumed to not be

damaged by undervoltage conditions. Based on this revised functional failure evaluation

conclusion, the relay was capable of providing adequate control for the associated

essential equipment and was not a functional failure. This lowered the EE-PF03A

function failures below the threshold that required meeting 10CFR50.65.(a)(1)

requirements. However, the inspectors identified that this evaluation used an invalid

assumption. It used data from the four failed attempts to calibrate an Agastat relay that

was operating unpredictably and required replacement. The use of this data was

determined to be unacceptable because it was obtained from a relay that was operating

unpredictably and required subsequent replacement. As such, the inspectors

determined that the revised functional failure was not valid. 10 CFR 50.65 (a)(2)

requires that the function EE-PR03A performance be effectively controlled through the

performance of appropriate preventative maintenance. The two functional failures

demonstrate that the requirements of (a)(2) were not being met. Therefore, the incorrect

assumption used in the revised fictional failure evaluation resulted in the Cooper Station

being in violation of 10 CFR 50.65(a)(2).

A problem identification and resolution inspection team noted similar issues with other

Agastat time delay relays during an inspection in March and April 2009. The results of

the teams finding is documented in Inspection Report 05000298/2009007 as a noncited

violation for the licensees failure to perform adequate operability determinations of

degraded and potentially degraded conditions associated with essential Agastat time

delay relays with internal foreign material contamination. One of the licensees

corrective actions was to implement a design change to replace 22 time critical Agastat

relays with digital time relays. The relay associated with the March 3, 2008, functional

failure was replaced with the digital upgrade in October 2009. The effectiveness of this

corrective action is monitored by the licensees corrective action program.

- 14 - Enclosure

Following the guidance of Appendix B to MC 0612 this finding is more than minor

because failure to monitor the effectiveness of the Division 1 essential 4160 volt

alternating current supply system affects the reliability objective of the Equipment

Performance attribute under the Mitigating Systems Cornerstone. This issue was

screened with the assistance of Inspection Procedure 71111.12, Maintenance

Effectiveness, Appendix D, Regulatory Review, that supplements the general

guidance of IMCs 0612 and 0609 by providing specific guidance on the disposition of

maintenance effectiveness issues. This is a Category II maintenance effectiveness

issue in that this failure to establish goals and monitoring for the essential 4160 volt

alternating current supply system is not attributable to poor Agastat relay performance

but a result of an inadequate licensee functional failure evaluation. Since the equipment

reliability problems were corrected by the licensees corrective action program via a

design change and the maintenance rule violation has occurred as a separate

consequence of the Agastat relay problems, this cannot be processed through the

significance determination process.

Analysis. The inspectors determined that the failure by licensee personnel to correctly

determine that the maintenance rule (a)(1) threshold had been reached was a

performance deficiency. This finding is more than minor because failure to monitor the

effectiveness of the essential 4160 volt alternating current function, EE-PF03A, affects

the reliability objective of the Equipment Performance attribute under the Mitigating

Systems Cornerstone. The inspectors determined that this performance deficiency was

an additional, but separate consequence of the degraded performance of the essential

4160 volt alternating current system Agastat relays. Following the guidance of

Appendix B to MC0612 and Appendix D to IP 71111.12, the inspectors determined that

this finding occurred as a consequence of actual problems with the Agastat relays, and

that those actual problems were not attributable to this finding. This finding therefore

cannot be processed through the significance determination process, and is considered

to be Green by NRC staff review. The finding has a crosscutting aspect in the area of

human performance associated with decision-making because the licensee did not use

conservative assumptions in the functional failure evaluation of a Agastat relay

failure H.1(b).

Enforcement. Title 10 CFR 50.65(a)(1) requires, in part, that holders of an operating

license shall monitor the performance or condition of structures, systems and

components within the scope of the rule as defined by 10 CFR 50.65(b), against

licensee-established goals, in a manner sufficient to provide reasonable assurance that

such structures, systems, and components are capable of fulfilling their intended safety

functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in

10 CFR 50.65(a)(1) is not required where it has been demonstrated that the

performance or condition of an system is being effectively controlled through the

performance of appropriate preventive maintenance, such that the system remains

capable of performing its intended function. Contrary to this requirement, from

December 28, 2008, to the present, the licensee did not demonstrate that the

performance of the 4160 volt alternating current system had been effectively controlled

through appropriate preventative maintenance and did not monitor against

- 15 - Enclosure

licensee-established goals in a manner sufficient to provide reasonable assurance that

the essential electrical supply system was capable of fulfilling its intended safety

functions. Specifically, the licensee failed to identify and properly account for

maintenance preventable functional failures that occurred March 3, 2008 and

October 28, 2008, that demonstrated that the performance of the Division 1 essential

4160 volt alternating current system was not being effectively controlled through the

performance of appropriate preventative maintenance and, as a result, that goal setting

and monitoring was required. Because the finding is of very low safety significance and

has been entered into the licensees corrective action program as CR-CNS-2010-5587,

this violation is being treated as a noncited violation consistent with Section VI.A.1 of the

NRC Enforcement Policy: NCV 05000298/2010003-02, Failure to Place the essential

4160 volt alternating current system Agastat relays in (a)(1).

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed licensee personnel's evaluation and management of plant risk

for the maintenance and emergent work activities affecting risk-significant and safety-

related equipment listed below to verify that the appropriate risk assessments were

performed prior to removing equipment for work:

April 6, 2010, Diesel generator 1 work window

May 11, 2010, High pressure coolant injection filter inspection

June 3, 2010, Diesel generator 2 walkdown without Control Room notification

during Yellow window with diesel generator 1 I lockout

June 8-9, 2010, Reactor recirculation motor generator pump B maintenance and

return to service

The inspectors selected these activities based on potential risk significance relative to

the reactor safety cornerstones. As applicable for each activity, the inspectors verified

that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)

and that the assessments were accurate and complete. When licensee personnel

performed emergent work, the inspectors verified that the licensee personnel promptly

assessed and managed plant risk. The inspectors reviewed the scope of maintenance

work, discussed the results of the assessment with the licensee's probabilistic risk

analyst or shift technical advisor, and verified plant conditions were consistent with the

risk assessment. The inspectors also reviewed the technical specification requirements

and inspected portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Specific

documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four maintenance risk assessments and

emergent work control inspection samples as defined in Inspection

Procedure 71111.13-05.

- 16 - Enclosure

b. Findings

No findings were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed the following issues:

April 9, 2010, Service water discharge piping

April 21, 2010, RHR-MO-15D failure

May 20, 2010, Service water booster pump D water in oil

May 20, 2010, RHR-A motor heater wiring discolored

The inspectors selected these potential operability issues based on the risk significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that technical specification operability was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability and

design criteria in the appropriate sections of the technical specifications and UFSAR to

the licensee personnels evaluations to determine whether the components or systems

were operable. Where compensatory measures were required to maintain operability,

the inspectors determined whether the measures in place would function as intended

and were properly controlled. The inspectors determined, where appropriate,

compliance with bounding limitations associated with the evaluations. Additionally, the

inspectors also reviewed a sampling of corrective action documents to verify that the

licensee was identifying and correcting any deficiencies associated with operability

evaluations. Specific documents reviewed during this inspection are listed in the

attachment.

These activities constitute completion of four operability evaluations inspection

sample(s) as defined in Inspection Procedure 71111.15-04

b. Findings

No findings were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following postmaintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

May 5, 2010, Service water pump C impeller lift

May 7, 2010, Diesel generator fuel oil modification testing

- 17 - Enclosure

May 11, 2010, High pressure coolant injection filter inspection

May 13, 2010, Reactor building crane postmaintenance test

May 20, 2010, H intermediate range monitor post maintenance testing

May 21, 2010, Ronan power supply replacement post maintenance testing

The inspectors selected these activities based upon the structure, system, or

component's ability to affect risk. The inspectors evaluated these activities for the

following (as applicable):

The effect of testing on the plant had been adequately addressed; testing was

adequate for the maintenance performed

Acceptance criteria were clear and demonstrated operational readiness; test

instrumentation was appropriate

The inspectors evaluated the activities against the technical specifications, the Updated

Final Safety Analysis Report, 10 CFR Part 50 requirements, licensee procedures, and

various NRC generic communications to ensure that the test results adequately ensured

that the equipment met the licensing basis and design requirements. In addition, the

inspectors reviewed corrective action documents associated with postmaintenance tests

to determine whether the licensee was identifying problems and entering them in the

corrective action program and that the problems were being corrected commensurate

with their importance to safety. Specific documents reviewed during this inspection are

listed in the attachment.

These activities constitute completion of six postmaintenance testing inspection samples

as defined in Inspection Procedure 71111.19-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and technical specifications to ensure that the surveillance activities listed

below demonstrated that the systems, structures, and/or components tested were

capable of performing their intended safety functions. The inspectors either witnessed

or reviewed test data to verify that the significant surveillance test attributes were

adequate to address the following:

Preconditioning

Evaluation of testing impact on the plant

- 18 - Enclosure

Acceptance criteria

Test equipment

Procedures

Jumper/lifted lead controls

Test data

Testing frequency and method demonstrated technical specification operability

Test equipment removal

Restoration of plant systems

Fulfillment of ASME Code requirements

Updating of performance indicator data

Engineering evaluations, root causes, and bases for returning tested systems,

structures, and components not meeting the test acceptance criteria were correct

Reference setting data

Annunciators and alarms setpoints

The inspectors also verified that licensee personnel identified and implemented any

needed corrective actions associated with the surveillance testing.

April 21, 2010, Residual heat removal pump D, motor operator 15D failure

May 12, 2010, Diesel generator fuel oil special test

May 25, 2010, Performance of offsite AC power alignment to support 6.1DG.301

May 26, 2010, Reactor coolant system leak rate checks

Specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of four surveillance testing inspection samples as

defined in Inspection Procedure 71111.22-05.

b. Findings

No findings were identified.

- 19 - Enclosure

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1 Safety System Functional Failures (MS05)

a. Inspection Scope

The inspectors sampled licensee submittals for the safety system functional failures

performance indicator for the period from the second quarter 2009 through the first

quarter. To determine the accuracy of the performance indicator data reported during

those periods, the inspectors used definitions and guidance contained in NEI Document

99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, and

NUREG-1022, Event Reporting Guidelines 10 CFR 50.72 and 50.73." The inspectors

reviewed the licensees operator narrative logs, operability assessments, maintenance

rule records, maintenance work orders, issue reports, event reports, and NRC integrated

inspection reports for the period of April 2009 through March 2010, to validate the

accuracy of the submittals. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the performance

indicator data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the attachment to this report.

These activities constitute completion of one safety system functional failure sample as

defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.2 Reactor Coolant System Specific Activity (BI01)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system specific

activity performance indicator for the period from the second quarter 2009 through the

second quarter 2010. To determine the accuracy of the performance indicator data

reported during those periods, the inspectors used definitions and guidance contained in

NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline,

Revision 6. The inspectors reviewed the licensees reactor coolant system chemistry

samples, technical specification requirements, issue reports, event reports, and NRC

integrated inspection reports for the period of March 2009 through May 2010, to validate

the accuracy of the submittals. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the performance

indicator data collected or transmitted for this indicator and none were identified. In

addition to record reviews, the inspectors observed a chemistry technician obtain and

analyze a reactor coolant system sample. Specific documents reviewed are described

in the attachment to this report.

- 20 - Enclosure

These activities constitute completion of one reactor coolant system specific activity

samples defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

.3 Reactor Coolant System Leakage (BI02)

a. Inspection Scope

The inspectors sampled licensee submittals for the reactor coolant system leakage

performance indicator for the period from the second quarter 2009 through the second

quarter 2010 To determine the accuracy of the performance indicator data reported

during those periods, the inspectors used definitions and guidance contained in NEI

Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6.

The inspectors reviewed the licensees operator logs, reactor coolant system leakage

tracking data, issue reports, event reports, and NRC integrated inspection reports for the

period of March 2009 through May 2010, to validate the accuracy of the submittals. The

inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the performance indicator data collected or

transmitted for this indicator and none were identified. Specific documents reviewed are

described in the attachment to this report.

These activities constitute completion of one reactor coolant system leakage sample as

defined in Inspection Procedure 71151-05.

b. Findings

No findings were identified.

4OA2 Identification and Resolution of Problems (71152)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical

Protection

Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees corrective action program and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors focused their review on repetitive equipment

issues, but also considered the results of daily corrective action item screening

discussed in Section 4OA2.2, above, licensee trending efforts, and licensee human

performance results. The inspectors nominally considered the 6-month period of

- 21 - Enclosure

October 2009 through March 2010 although some examples expanded beyond those

dates where the scope of the trend warranted.

The inspectors also included issues documented outside the normal corrective action

program in major equipment problem lists, repetitive and/or rework maintenance lists,

departmental problem/challenges lists, system health reports, quality assurance

audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.

The inspectors compared and contrasted their results with the results contained in the

licensees corrective action program trending reports. Corrective actions associated with

a sample of the issues identified in the licensees trending reports were reviewed for

adequacy.

These activities constitute completion of one single semi-annual trend inspection

samples as defined in Inspection Procedure 71152-05.

b. Findings and Observations

No findings were identified. The inspectors evaluated the licensees trending

methodology and observed that the licensee had performed a detailed review. The

licensee routinely review cause codes, involved organizations, key words, and system

links to identify potential trends in their corrective action program data. The inspectors

compared the licensee process results with the results of the inspectors daily screening

and did not identify any discrepancies or potential trends in the corrective action program

data that the licensee had failed to identify. The inspectors did, however, identify

additional insights into several of these issues as documented below:

Human Error Prevention Techniques Substantive Cross-Cutting Issue Review.

The NRC identified a crosscutting theme associated with the work practices component

of the human performance area related to the use of human error prevention techniques

H.4(a) in 2008. Since the licensee recognized the theme and developed corrective

actions, a crosscutting issue was not identified for the 2008 human performance issue.

During the 2009 assessment period seven findings were identified with the crosscutting

aspect related to the use of human error prevention techniques. Five of these occurred

following full implementation of the licensees corrective actions. Based on these

findings with the repeated common theme, the NRC staff identified a substantive

crosscutting issue in the human performance area associated with work practices

related to the use of human error prevention techniques at Cooper Nuclear

Station H.4(a). These findings occurred in initiating events, barrier integrity and

occupational radiation safety cornerstones. This baseline inspection semi annual trend

continues to monitor for sustainable performance improvements as evidenced by

effective implementation of an appropriate corrective action plan that results in no safety

significant inspection findings and a notable reduction in the overall number of inspection

findings with the same common theme.

A comparison of the licensees human performance trends from their condition report

record in 2009 versus the trends from early 2010 was performed. Consequential human

- 22 - Enclosure

errors and non-consequential human errors were higher in 2009 than 2010. The

majority of 2009 errors were during the fall 2009 refueling outage, as expected, due to

the large number of activities performed during an outage versus normal plant operation.

The same effect was noted for procedure quality and adherence issues with an

increasing trend during the fourth quarter 2009 compared to a decreasing trend during

the first quarter 2010.

The licensee improvement plan while mainly implemented has a few actions that are completing

during June and July 2010. This is a non-refueling year for the licensee. The gross number of

maintenance activities is substantially lower and so the opportunities for human performance

errors are correspondingly lower. Based on the lower number of activities performed during full

power operations compared to a refueling outage and the need to allow time to observe the

effectiveness of the licensee improvement plan the NRC will continue to monitor the licensees

progress via the baseline inspection program.

Trend in Inadequate Apparent Cause Reviews:

During routine corrective action program document reviews, the inspectors noted that the

apparent cause evaluation performed under CR-CNS-2010-02875 had been flagged as

inadequate during the licensees effectiveness review. The inspectors noted that Corrective

Action Program Desk Guide #7, Just in Time (JIT) Training for Apparent Causes, Revision 0,

requires apparent cause evaluators to receive just-in-time training prior to performing this

activity. In the case of CR-CNS-2010-02875 the inspectors noted that the apparent cause

evaluator had been exempted from the licensees normal just-in-time training. As a result, the

inspectors reviewed the results of apparent cause effectiveness evaluations for the previous

year and discovered that eleven apparent cause evaluations had been flagged as inadequate.

Four of these were performed by persons who were exempted from the required just-in-time

training. Another five inadequate evaluations were performed by persons who received the

training via a video tape versus in person. Lastly, the inspectors noted that one individual had

been flagged for an inadequate evaluation on three separate occasions in the past year but had

received the initial just in time training prior to performing each of the inadequate evaluations.

The inspectors also noted that the licensee had made no attempt to evaluate this adverse trend

or take any corrective actions to improve performance. The inspectors determined that the

record of inadequate apparent cause evaluations reveals several potential gaps in the

administration of the just-in-time training required by Desk Guide #7.

Trend in Back Leakage into F Sump:

The inspectors reviewed the collection of drywell unidentified leak rate data for adverse trends.

The licensees F sump collects unidentified leakage in the drywell, and a pair of pumps

remove the water by pumping it to the liquid radwaste system. A flow totalizer measures the

total volume of water pumped every eight hours, and from this a measured unidentified leak rate

is determined to satisfy technical specification surveillance requirements. The discharge lines

from each pump contain a check valve to prevent back leakage into the sump from the liquid

radwaste system. These check valves have been historically poor at preventing back leakage.

On at least four occasions in previous twelve months, operators questioned the accuracy of the

- 23 - Enclosure

measured leak rate and isolated the pump discharge lines in order to determine a meaningful

leak rate.

The back leakage problem has routinely caused the measured leak rate to be off by over 0.1

gpm.

The inspectors reviewed Regulatory Guide 1.45, Reactor Coolant Pressure Boundary Leakage

Detection Systems, May 1973, which establishes sensitivity requirements for leak rate sensing

systems of Coopers vintage. Even with the worst case back leakage seen to date, the licensee

still satisfied the required instrument sensitivity of detecting a one gpm leak rate in less than one

hour. The back leakage problem, however, has caused unnecessary entries into Procedure 0-

CNS-OP-109, Drywell Leakage Investigation, to look for leakage that did not exist. Procedural

0-CNS-OP-109 requires operators to begin looking for leak sources when measured leakage

exceeds 0.25 gpm. The back leakage issue has caused operators to question the measured

leak rate and become accustomed to routinely entering Procedure 0-CNS-OP-109. This

effectively desensitizes control room operators to small changes in drywell unidentified leak rate

and could interfere with prompt identification of developing reactor coolant system leakage.

The licensee has a standing maintenance task to replace the leaking check valves each outage,

but this strategy has not been successful in eliminating the back leakage issue. The licensee

has planned a modification to be implemented in Refueling Outage 26, which will replace the

existing valves with a soft-seated design. The inspectors noted that this modification was also

planned for Refueling Outage 25, but was deferred due to having minimal beneficial value as

described in the response to CR-CNS-2009-00003.

4OA3 Event Follow-up (71153)

.1 (Closed) Licensee Event Report 05000298/2010-001-00, Safety Relief Valves Test

Exceeded Technical Specification Limits

a. Inspection Scope

On January 12, 2010, two safety relief valve pilot assemblies as-found pressure

setpoints exceeded the technical specification SR 3.4.3.1 limits when tested in a test

shop. Three safety relief valves and five safety relief valves pilot assemblies were

removed during the licensees fall 2009 refueling outage. The replacement pilot

assemblies installed during the fall 2009 refueling outage were refurbished and certified

to lift within the setpoint acceptance criteria prior to installation. The licensee

investigation determined the failures were due to pilot disc-to-seat corrosion bonding. A

corrective action that has not been fully implemented was developed from previous

failures described in LER 2008-002-00. This action is to submit a technical specification

license amendment to allow one or two failures out of the eight total safety relief valves

without exceeding technical specification limits. No new findings were identified in the

inspectors review. This finding constitutes a minor violation of Technical Specification

Surveillance Requirement 3.4.3.1. that is not subject to enforcement action in

accordance with Section IV of the NRC's Enforcement Policy. This Licensee Event

Report is closed.

- 24 - Enclosure

b. Findings

No findings were identified.

.2 Work Preparation Activities Cause Unplanned Increase in Reactor Power

a. Inspection Scope

On April 28, 2010, a work planner affected a leaking feedwater heater control valve

during a planning walkdown. The reactivity increase due to the change in feedwater

temperature caused the reactor to exceed the licensed thermal power limit of 2419 MWt

until reactor operators reduced power. The event was reviewed by the inspectors and a

green noncited violation was identified for the licensees failure prevent the operation of

plant equipment of which may affect the reactivity or power level of a reactor without the

knowledge and consent of a licensed operator or senior operator present at the controls.

This finding is described below.

b. Findings

Introduction. A Green self-revealing noncited violation of 10 CFR 50.54.j was identified

when a work planner caused a feedwater heater trip by touching a pressure regulating

valve without the knowledge of the control room. The reactivity increase due to the

change in feedwater temperature caused the reactor to exceed the licensed thermal

power limit of 2419 MWt until reactor operators reduced power.

Description. On April 28, 2010, a work planner was preparing a work package for repair

of an air leak on CNS-0-CD-PRV-PRV10, the pressure regulating valve for the

A5 feedwater heater level control valve. While walking down the area of the repair, the

planner observed that the leak was larger than expected. The planner then applied

pressure with his hands around the gasket in the vicinity of the leak. He did not report or

request permission for this action from the control room. When he covered the leak with

his hands, the change in leak rate resulted in a transient of the level control valve signal.

The signal transient caused the level in the A5 heater to drop by dumping condensate to

the A3 heater. The A3 feedwater heater has been operated with the level control valve

in manual since November 30, 2009, due to excessive cycling of the associated level

control valve; therefore, the A3 heater did not automatically respond to the rapid

increase in level. The control room received both the A5 HEATER LOW LEVEL and

A3 HEATER HIGH LEVEL alarm at 8:24 a.m. The A3 HEATER HIGH LEVEL TRIP

alarm came in 1 minute later. Over the next 30 minutes, the operators attempted to

stabilize feedwater heater levels. The feedwater heater trip and level transients resulted

in an approximately 0.8°F drop in feedwater temperature, which caused an increase in

reactor power to 2421 MWt. The operators immediately reduced power with

recirculation pumps to 2419 MWt.

In response to the event, the licensee performed an apparent cause evaluation and a

human performance evaluation. The human performance evaluation indicated that a

two-minute drill had not been performed. In the apparent cause evaluation, the

- 25 - Enclosure

licensee stated the planner had exceeded the scope of job by touching the component

instead of visually inspecting it. The licensee also stated in the evaluation that

interviews with valve team personnel revealed that they had cautioned a non-licensed

operator the previous day about not touching the pressure relief valve due to the

potential to affect the air control signal. The licensees corrective actions included

coaching the work planner, training plant personnel on the potential for causing a plant

transient during system walkdowns, and establishing pre-job briefs for the planning

department. In addition, caution tape was placed around the pressure regulating valve.

Analysis. The licensee failing to ensure that mechanisms which may affect reactivity

were manipulated only with the knowledge and consent of a licensed operator at the

controls was a performance deficiency. The finding was more than minor because the

performance deficiency could be reasonably viewed as a precursor to a significant event

in that a reactor power transient was initiated without the knowledge of the control room.

Using Manual Chapter 0609.04 this finding was characterized under the significance

determination process as having very low safety significance because while the finding

degraded the transient initiator contributor function of the initiating events cornerstone, it

did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation

equipment or functions will not be available. The inspectors determined that this finding

has a crosscutting aspect in the area of human performance associated with the work

practices component because the work planner proceeded in the face of unexpected

circumstances by exceeding the scope of the job when he found the leak was greater

than expected H.4(a).

Enforcement. 10 CFR 50.54.j requires, in part, that apparatus and mechanisms other

than controls, the operation of which may affect the reactivity or power level of a reactor,

shall be manipulated only with the knowledge and consent of a licensed operator or

senior operator present at the controls. Contrary to the above, on April 28, 2010, a work

planner manipulated the instrument air system, without the knowledge and consent of a

licensed operator or senior operator present at the controls, causing a feedwater

transient and reactivity change. However, because this inspection finding was

characterized by the significance determination process as having very low risk

significance (Green) and has been entered in the licensees corrective action program as

CR CNS-2010-03091, this violation is being treated as a noncited violation, consistent

with Section IV.A.1 of the NRC Enforcement Policy: NCV 05000298/2010003-03, Work

Preparation Activities Cause Unplanned Increase in Reactor Power.

4OA5 Other Activities

Failure to Perform Required Maintenance Causes Unplanned Down Power

a. Inspection Scope

On May 1, 2010, control room operators initiated a rapid power reduction after receiving

trip alarms on the A1 and A2 traveling water screens and subsequent loss of vacuum on

the main condenser. After stabilizing power below the capacity of two circulating water

pumps, operators tripped the A circulating water pump. The licensees investigation

determined that the cause of the traveling water screen trip was accumulated debris in

- 26 - Enclosure

the screen debris trough as a result of failing to perform the required routine

maintenance on the traveling water screens.

b. Findings

Introduction. A Green self-revealing finding was identified for the licensees failure to

implement the preventive maintenance requirements of the vendor manual for the plant

traveling water screens. Specifically, Vendor Manual 140, Traveling Water Screen,

Revision 35, contained daily and weekly routine maintenance requirements to open the

channel-flushing valve to clear any accumulated debris from the screens. Despite the

fact that the licensee incorporated this vendor manual into their preventive maintenance

system, this maintenance requirement was overlooked. The failure to perform this

maintenance task led to the trip of the A1 and A2 traveling water screens on

May 1, 2010, and required an emergent power reduction.

Description. On May 1, 2010, the Missouri River was in the midst of a level transient,

during which a large amount of debris was entering the intake structure and was being

removed by the traveling water screens. At the time of the event, only three of the

plants four circulating water pumps were available due to maintenance activities

affecting the fourth pump. Each circulating water pump can draw its required flow from

one of two traveling water screens (there are two dedicated screens per pump).

The event began when control room operators received alarms suggesting that the A1

traveling water screen had tripped, followed shortly by similar alarms for the A2 screen.

Operators made a failed attempt to restart the tripped screens but were unsuccessful.

Operators entered Abnormal Operating Procedure 2.4VAC and recognized degrading

vacuum on the main condenser. As a result, operators began a rapid power reduction to

avoid a low-vacuum turbine trip. After reducing power to approximately seventy percent

(within the capacity of two circulating water pumps), operators tripped the A circulating

water pump from the control room.

Operators immediately inspected the A1 and A2 screens, and found an accumulation of

river debris inside the debris flushing trough. The debris created drag on the screen

baskets. This increased drag had caused the A1 screen to trip. When the full flow of

the A circulating water pump was then diverted to the A2 screen, the high debris loading

on the screens caused a high differential pressure trip of the A2 screen. After clearing

the debris from the A1 screen, operators were again able to restore a two-screen lineup

for the A circulating water pump, start the pump, and return the plant to full power.

In the root cause investigation performed under CR-CNS-2010-03195, the evaluators

identified that the applicable vendor manual had identified a list of routine maintenance

tasks. The evaluators identified the following daily maintenance task that was never

incorporated into the licensees preventive maintenance program or system operating

procedures:

Check that debris is being washed off the screen into the debris channel and

that the channel is clear. Briefly open the channel-flushing valve if necessary.

- 27 - Enclosure

Additionally, the following weekly task was also omitted:

Open the flushing valves on the wash water jet pipes for approximately fifteen

(15) seconds to clear any accumulated debris.

The inspectors reviewed Change Evaluation Document 6014001, Traveling Water

Screens Replacement, April 19, 2005, and learned that the modification package

incorporated most of the maintenance tasks from the vendor manual, but was silent on

operation of the channel-flushing valve. Interviews with licensee personnel suggested

that this may have been due to a misunderstanding of the normal system lineup, or just

an oversight on the part of the evaluator. Regardless of the cause, the net effect was

that the design process never identified the need to routinely open the channel-flushing

valve and led directly to the screen failure on May 1, 2010.

The inspectors determined that the age of the performance deficiency and lack of recent

opportunities to discover this error suggested that this performance deficiency is not

indicative of current performance.

In response to this event, the licensee performed a review of the applicable vendor

manual preventive maintenance and instituted a nightly task to inspect the debris

channel and cycle the channel flushing valves for each traveling water screen. The

licensee also initiated actions to perform an extent of cause check of other important

equipment that had been recently installed to ensure appropriate vendor recommended

maintenance requirements have been implemented.

Analysis. The licensees failure to implement the required routine maintenance for the

traveling water screens is a performance deficiency. The finding was more than minor

because it affected the equipment performance attribute of the initiating events

cornerstone, and adversely affected the cornerstone objective to limit the likelihood of

those events that upset plant stability and challenge critical safety functions during

shutdown as well as power operations. Using Manual Chapter 0609.04 this finding was

characterized under the significance determination process as having very low safety

significance because it did not contribute to both the likelihood of a reactor trip and the

likelihood that mitigation functions would be unavailable. The inspectors determined that

no crosscutting aspect was applicable to this finding because the performance

deficiency was not reflective of current performance.

Enforcement. Enforcement action does not apply because the performance deficiency

did not involve a violation of a regulatory requirement. Because this finding does not

involve a violation of regulatory requirements and has very low safety significance, it is

identified as FIN 05000298/2010003-04, "Failure to Perform Required Maintenance

Causes Unplanned Down Power.

- 28 - Enclosure

4OA6 Meetings

Exit Meeting Summary

On July 1, 2010, the inspectors presented the inspection results to Mr. Brian OGrady, and other

members of the licensee staff. The licensee acknowledged the issues presented. The

inspector asked the licensee whether any materials examined during the inspection should be

considered proprietary. No proprietary information was identified.

On July 12, 2010, the inspectors conducted a telephonic exit meeting to present changes in the

inspection results to Mr. Dave VanDerKamp. The licensee acknowledged the changes to the

issues presented. The inspector asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

- 29 - Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

A. Able, Instrument & Control Engineering Supervisor, Design Engineering Department

D. Anderson, Supervior, ALARA

J. Austin, Manager, Emergency Preparedness

D. Buman, Director of Engineering

B. Chapin, Manager, Outage

S. Charbonnet, NPPD ESD Lead

R. Dewhirst, Senior Project Manager

R. Estrada, Manager, Design Engineering

K. Fike, Plant Chemist, Chemistry Department

J. Flaherty, Licensing

S. Freborg, ESD Mechanical Programs Supervisor

G. Gardner, NSSS Supervisor, System Engineering Department

K. Gehring-Ohrablo, Chem Tech, Chemistry Department

T. Hough, Maintenance Rule Coordinator

N. Joergensen, Design Engineer

L. Keiser, SW and RHR System Engineer

D. Kirkpatrick, Technician, Radiation Protection

P. Leininger, Erosion/Corrosion Program Engineer

D. McMahon, REC System Engineer

A. Meinke, Chemistry Engineer, Chemistry Department

M. Metzger, System Engineer

D. Madsen, Licensing

D. Parker, Manager, Maintenance

R. Penfield, Manager, Operations

A. Sarver, BOP/Elect/I&C Supervisor, System Engineering Department

K. Tanner, Supervisor, Radiation Protection

J. Teten, Chemistry Supervisor

D. VanDerKamp, Licensing Manager

J. Webster, Director of Projects, Project Department

R. Wulf, SED Manager

A. Zaremba, Director Nuclear Safety Assurance

NRC Personnel

Runyan, Mike, Senior Risk Analyst

A-1 Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

Failure to Document Design of Service Water Discharge Piping in

05000298/2010003-01 NCV

Plant Drawings

Failure to Place the Essential 4160 Volt Alternating Current

05000298/2010003-02 NCV

System Agastat Relays in (a)(1)

Work Preparation Activities Cause Unplanned Increase in

05000298/2010003-03 NCV

Reactor Power

Failure to Perform Required Maintenance Causes Unplanned

05000298/2010003-04 FIN

Down Power

LIST OF DOCUMENTS REVIEWED

Section 1RO1: Adverse Weather Protection

MISCELLANEOUS DOCUMENTS

NUMBER TITLE DATE

EE-SY CNS System Health Report March 2010

Section 1RO1: Adverse Weather Protection

PROCEDURE

NUMBER TITLE REVISION

2.1.14 General Operating Procedure, Seasonal Weather 14

Preparations

5.1FLOOD Emergency Procedure, Flood 7

5.3GRID Emergency Procedure, Degraded Grid Voltage 29

7.0.11 Maintenance Procedure, Flood Control Barriers 9

WORK ORDER 4663687

A-2 Attachment

Section 1RO4: Equipment Alignment

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

Burns and Roe Design Information Notice, Service Water

7/31/73

System Modification Circ. Water Discharge Canal Piping

Core Spray Component Checklist 2

CNS-RCIC-1 Flow Diagram RCIC Turbine Lube Oil Subsystem 3/10/89

NEDC 92-034 Water Hammer Analysis of Service Water System 3C1

2043 Burns & Roe, Flow Diagram Reactor Core Isolation Coolant

NS4

and Reactor Feed Systems Cooper Nuclear Station

2044 Burns & Row, Cooper Nuclear Station Flow Diagram - High

N70

Pressure Coolant Injection and Reactor Feed System

2045 SH1 Core Spray System N58

95516C EG-R Governor Hydraulic System General Electric RCIC 2/08/74

Units

Section 1RO4: Equipment Alignment

PROCEDURE

NUMBER TITLE REVISION

2.2.33A System Operating Procedure, High Pressure Coolant

24

Injection System Component Checklist

2.2.67A CNS Operations Manual System Operating Procedure,

Reactor Core Isolation Cooling System Component 20

Checklist

3.7 Engineering Procedure, Drawing Change Notice 31

3.8 Engineering Procedure, Drawing Control 22

6.EE.610 Surveillance Procedure, Off-Site AC Power Alignment 24

CONDITION REPORT

CR-CNS-2009-02859 CR-CNS-2009-03689

A-3 Attachment

Section 1RO5: Fire Protection

MISCELLANEOUS DOCUMENTS

NUMBER TITLE DATE

FHA FA Drawing, FHA Matrix FA1-FZ1B 2/28/03

FHA FA Drawing, FHA Matrix FA1-FZ1G 2/28/03

93-15 Engineering Evaluation

NFPA 30 Flammable and Combustibles Liquids Code 1973 Edition

Section 1R11: Licensed Operator Requalification Program

LESSON

NUMBER TITLE REVISION

SKL0540132 0

Section 1R11: Licensed Operator Requalification Program

SCENARIO OVERVIEW

Aircraft Threat, Vehicle Accident Breaches Secondary Containment, Spurious Group 1

Isolation, Failure to Scram, Fuel Clad Failure

Section 1R12: Maintenance Effectiveness

NOTIFICATION

NUMBER TITLE

10711374

10727134 Component RHR-MO-MO15D, RHR Pump Shutdown

Cooling Suction Motor Operated Valve Functional Failure

Evaluations for Functions: RHR-PF01B, RHR-PR02B, RHR-

PF03B, RHR-PF04B and RHR-SD1

CONDITION REPORT

CR-CNS-2010-02334 CR-CNS-2010-02355 CR-CNS-2010-02709

A-4 Attachment

Section 1R13: Maintenance Risk Assessment and Emergent Work Controls

PROCEDURE

NUMBER TITLE REVISION

0.40.9 Administrative Procedure Work Activity Risk Management 2

Process

0.49 Administrative Procedure

CONDITION REPORT

CR-CNS-2010-04001

WORK ORDER 4731476 473857

Section 1R15: Operability Evaluations

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION /

DATE

Nebraska Public Power District Letter, Response to Generic January 29,

Letter 89-13 1990

EN-OP-104 Operability Determinations 3

Section 1R15: Operability Evaluations

PROCEDURE

NUMBER TITLE REVISION

0.5.OPS Administrative Procedure, Operations Review of Condition 29

Reports/Operability Determination

2.0.11 Conduct of Operations Procedure, Entering and Exiting 27

Technical Specification/TRM/ODAM LCO Condition(s)

2.0.11.1 Conduct of Operations Procedure, Safety Function 4

Determination Program

CONDITION REPORT

CR-CNS-2006-00471 CR-CNS-2009-08848 CR-CNS-2010-02347 CR-CNS-2010-02529

CR-CNS-2010-02709 CR-CNS-2010-03592 CR-CNS-2010-03641

A-5 Attachment

WORK ORDER 4740871

Section 1R19: Postmaintenance Testing

MISCELLANEOUS DOCUMENTS

NUMBER TITLE REVISION

6.2 IRM.304 IRM Channel Calibration (Mode Switch in Run)(Div 2) 21

NEDC 91-045 Diesel Fuel Transfer Flow Rate with 8 3/8 Pump Impeller 1C1

Section 1R19: Postmaintenance Testing

PROCEDURE

NUMBER TITLE REVISION

3.4.7 Engineering Procedure, Design Calculations 31

6.1DG.401 Surveillance Procedure, Diesel Generator Fuel Oil Transfer 27

Pump IST Flow Test (Div 1)

6.1SW.101 Surveillance Procedure, Service Water Surveilllance 31

Operation (Div 1)(IST)

WORK ORDER 4625372 4656444 4664046 4731476 473857

Section 1R22: Surveillance Testing

PROCEDURE

NUMBER TITLE REVISION

6.EE.610 Surveillance Procedure, Off-Site AC Power Alignment 24

6.LOG.601 Surveillance Procedure, Daily Surveillance Log - Modes 1, 103

2, and 3, Attachment 3 Unidentified Leak Rate and

Attachment 4 Identified and Total Leak Rate Checks

6.1DG.401 Surveillance Procedure, Diesel Generator Fuel Oil Transfer 27

Pump IST Flow Test (Div 1)

6.2RHR.201 Surveillance Procedure, FHR Power Operated Valve 21

Operability test (IST)(Div 2)

A-6 Attachment

CONDITION REPORT

CR-CNS-2010-2709

WORK ORDER 4705353 4705582

Section 4OA1: Performance Indicator Verification

MISCELLANEOUS DOCUMENTS

NUMBER TITLE DATE

8.4.1.1B Chemistry Report, Gamma Detector Nuclide Identification 5/20/10

Sheet for Reactor Iodine

Chemistry Department Dailies and Weeklies Hints Table 11/21/06

Chemistry Measurements Database (Open CDM) Sample 1/4/10-

Pint RX WATER 8.4.1.1.1/8.4.1.1.2/8.4.1.1.3 Dose 5/24/10

Equivalent Iodine 131

Pre-Job Brief worksheet for Reactor Water Sampling

Section 4OA1: Performance Indicator Verification

PROCEDURE

NUMBER TITLE REVISION

6.LOG.601 Surveillance Procedure, Daily Surveillance Log - Modes 1, 103

2, and 3 - Attachment 3 Unidentified Leak Rate Checks

and Attachment 4 Identified and Total Leak Rate Checks

8.4 Chemistry Procedure, Routine Sampling and Sample Valve 30

Control

8.8DWAM Chemistry Procedure, Particulate and Iodine Sample 2

Collection for Drywell Atmosphere Monitor

8.8.1.14 Chemistry Procedure, Radiochemical Iodines Analysis 16

Section 4OA2: Identification and Resolution of Problems

MISCELLANEOUS DOCUMENTS

TITLE

Primary Control Rod System Reports

A-7 Attachment

Section 4OA2: Identification and Resolution of Problems

PROCEDURE

NUMBER TITLE REVISION

6.1SW.101 Surveillance Procedure, Service Water Surveillance 31

Operation (Div 1)(IST)

CONDITION REPORT

CR-CNS-2010-02745 CR-CNS-2010-02875 CR-CNS-2010-02932 CR-CNS-2010-02935

A-8 Attachment