ML051990328

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IR 05000361-05-003, 05000362-05-003, on 04/08/05 - 06/26/05; San Onofre Nuclear Generating Station, Units 2 & 3; Integrated Resident and Regional Report; Maintenance Effectiveness and Temporary Plant Modifications
ML051990328
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 07/15/2005
From: Troy Pruett
NRC/RGN-IV/DRP/RPB-D
To: Ray H
Southern California Edison Co
References
IR-05-003
Download: ML051990328 (32)


See also: IR 05000361/2005003

Text

July 15, 2005

Harold B. Ray, Executive Vice President

San Onofre, Units 2 and 3

Southern California Edison Co.

P.O. Box 128, Mail Stop D-3-F

San Clemente, CA 92674-0128

SUBJECT: SAN ONOFRE NUCLEAR GENERATING STATION - NRC INTEGRATED

INSPECTION REPORT 05000361/2005003; 050000362/2005003

Dear Mr. Ray:

On June 26, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your San Onofre Nuclear Generating Station, Units 2 and 3 facility. The enclosed integrated

report documents the inspection findings, which were discussed on April 15 and June 24, 2005,

with Dr. R. Waldo and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

This report documents two NRC identified findings of very low safety significance (Green). One

of these findings was determined to involve a violation of NRC requirements; however, because

of the very low safety significance and because it was entered into your corrective action

program, the NRC is treating this finding as a noncited violation (NCV) consistent with

Section VI.A of the NRC Enforcement Policy. If you contest this noncited violation, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-

4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington

DC 20555-0001; and the NRC Resident Inspector at San Onofre Nuclear Generating Station,

Units 2 and 3, facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

Southern California Edison Co. -2-

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Troy W. Pruett, Chief

Project Branch D

Division of Reactor Projects

Dockets: 50-361

50-362

Licenses: NPF-10

NPF-15

Enclosure:

NRC Inspection Report 05000361/2005003; 05000362/2005003

w/Attachment: Supplemental Information

cc w/enclosure:

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, CA 92101

Gary L. Nolff

Power Projects/Contracts Manager

Riverside Public Utilities

2911 Adams Street

Riverside, CA 92504

Eileen M. Teichert, Esq.

Supervising Deputy City Attorney

City of Riverside

3900 Main Street

Riverside, CA 92522

Raymond Waldo, Vice President,

Nuclear Generation

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Southern California Edison Co. -3-

David Spath, Chief

Division of Drinking Water and

Environmental Management

California Department of Health Services

P.O. Box 942732

Sacramento, CA 94234-7320

Michael R. Olson

San Onofre Liaison

San Diego Gas & Electric Company

P.O. Box 1831

San Diego, CA 92112-4150

Ed Bailey, Chief

Radiologic Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

Mayor

City of San Clemente

100 Avenida Presidio

San Clemente, CA 92672

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Douglas K. Porter, Esq.

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, CA 91770

Dwight E. Nunn, Vice President

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Daniel P. Breig, Station Manager

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Southern California Edison Co. -4-

A. Edward Scherer

Southern California Edison

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Brian Katz, Vice President, Nuclear

Oversight and Regulatory Affairs

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Adolfo Bailon

Field Representative

United States Senator Barbara Boxer

312 N. Spring Street, Suite 1748

Los Angeles, CA 90012

Chief, Technological Services Branch

FEMA Region IX

Department of Homeland Security

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Southern California Edison Co. -5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (KMK)

Senior Resident Inspector (CCO1)

Branch Chief, DRP/D (TWP)

Senior Project Engineer, DRP/D (NFO)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

RidsNrrDipmIipb

W. A. Maier, RSLO (WAM)

ADAMS: WYes G No Initials: _TWP_

W Publicly Available G Non-Publicly Available G Sensitive W Non-Sensitive

R:\_SO23\2005\SO200503RP-CCO.wpd

RIV:RI:DRP/D SRI:DRP/D C:DRS/PEB C:DRS/PSB C:DRS/OB

MASitek CCOsterholtz LJSmith MPShannon ATGody

T - TWPruett T - TWPruett /RA/ /RA/ /RA/

7/13/05 7/13/05 7/8/05 7/12/05 7/12/05

C:DRS/EB C:DRP/D

JAClark TWPruett

/RA/ /RA/

7/11/05 7/15/05

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-361, 50-362

Licenses: NPF-10, NPF-15

Report No.: 05000361/2005003 and 5000362/2005003

Licensee: Southern California Edison Co. (SCE)

Facility: San Onofre Nuclear Generating Station, Units 2 and 3

Location: 5000 S. Pacific Coast Hwy.

San Clemente, California

Dates: April 8 through June 26, 2005

Inspectors: C. J. Araguas, General Engineer, NRR

T. W. Jackson, Senior Resident Inspector, Project Branch B, DRP

R. E. Lantz, Senior Emergency Preparedness Inspector

C. C. Osterholtz, Senior Resident Inspector, Project Branch D, DRP

M. A. Sitek, Resident Inspector, Project Branch D, DRP

T. F. Stetka, Senior Operations Engineer

Approved By: Troy W. Pruett, Chief, Project Branch D

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000361/2005003, 05000362/2005003; 04/08/05 - 06/26/05; San Onofre Nuclear

Generating Station, Units 2 & 3; Integrated Resident and Regional Report; Maintenance

Effectiveness and Temporary Plant Modifications

This report covered a 3-month period of inspection by three resident inspectors, two regional

office inspectors, and one headquarters inspector. The inspection identified one noncited

violation and one finding. The significance of most findings is indicated by their color (Green,

White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination

Process." Findings for which the significance determination process does not apply may be

Green or be assigned a severity level after NRC management's review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a finding for the failure to develop an adequate

plan to identify hydraulic leakage on Main Feedwater Block Valve 3HV4051.

This issue involved human performance crosscutting aspects associated with

operators failing to identify the leak on shiftly rounds. This issue was entered

into the licensees corrective action program as Action Requests 050401214 and

050401222.

The finding is determined to be greater than minor because it was associated

with the human performance attribute of the initiating events cornerstone and

affects the cornerstone objective of limiting the likelihood of those events that

upset plant stability. Furthermore, if left uncorrected, the finding would have

become a more significant safety concern in that continued hydraulic fluid

leakage from Valve 3HV4051 could result in a plant transient. Using Manual

Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the

finding was determined to have very low safety significance because the

hydraulic fluid leakage had not increased to the point where it would contribute to

both the likelihood of a reactor trip and the likelihood that mitigation equipment or

functions would not be available (Section 1R23).

Cornerstone: Mitigating Systems

the failure to include component deficiencies of a system important to safety in

the maintenance rule program. Specifically, the licensee did not incorporate

piping header failures of the Unit 2 and Unit 3 steam bypass control system into

the maintenance rule program to ensure appropriate monitoring and goal setting

activities were established. This issue was entered into the corrective action

program as AR 050200923.

ENCLOSURE

-2-

The finding was determined to be greater than minor because it affected the

equipment performance attribute of the mitigating systems cornerstone and

affected the cornerstone objective of ensuring the availability and reliability of

systems that respond to initiating events. Using Manual Chapter 0609,

Significance Determination Process, Phase 1 worksheet, the finding was

determined to have very low safety significance because the steam bypass

control system did not experience a loss of function (Section 1R12).

B. Licensee-Identified Violations

  • None.

ENCLOSURE

REPORT DETAILS

Summary of Plant Status

Unit 2 operated at approximately 99 percent reactor power until April 16, 2005, when the unit

was shutdown to repair an internal hydraulic leak on main feedwater isolation Valve 2HV4052.

The unit returned to approximately 99 percent power on April 19 and remained there for the

duration of the inspection period.

Unit 3 operated at approximately 100 percent reactor power until May 4, 2005, when the unit

was shutdown to repair cracks in the steam bypass system header piping and to repair an

external hydraulic leak from main feedwater block Valve 3HV4051. The unit returned to

approximately 100 percent reactor power on May 12 and remained there for the duration of the

inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

a. Inspection Scope

The inspectors completed a review of the licensees readiness for impending adverse

weather involving the effects of a tsunami that may be generated from an off shore

earthquake. The inspectors (1) reviewed plant procedures, the Updated Final Safety

Analysis Report, and Technical Specifications to ensure that operator actions defined in

adverse weather procedures maintained the readiness of essential systems; (2) walked

down portions of the below listed systems to ensure that adverse weather features were

sufficient to support operability, including the ability to perform safe shutdown functions;

(3) reviewed maintenance records to determine that applicable surveillance

requirements were current if an anticipated tsunami developed; and (4) reviewed plant

modifications, procedure revisions, and operator work arounds to determine if recent

facility changes challenged plant operation.

  • June 12, 2005, Unit 2 and 3 saltwater cooling system and emergency diesel

generators

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

ENCLOSURE

-2-

1R04 Equipment Alignment

Partial System Walkdowns

a. Inspection Scope

The inspectors: (1) walked down portions of the two listed risk important systems and

reviewed plant procedures and documents to verify that critical portions of the selected

systems were correctly aligned; and (2) compared deficiencies identified during the walk

down to the licensee's corrective action program to ensure problems were being

identified and corrected.

  • On May 3, 2005, the inspectors walked down the Unit 3 Train A high pressure

safety injection system while Train B of the same system was being used to fill

safety injection Tank T-008

  • On May 9, 2005 the inspectors walked down the Units 2 and 3 control room

emergency air cleanup system while maintenance was being performed on the

Units 2 and 3 toxic gas isolation system

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

a. Inspection Scope

Quarterly Inspection

The inspectors walked down the six listed plant areas to assess the material condition of

active and passive fire protection features and their operational lineup and readiness.

The inspectors: (1) verified that transient combustibles and hot work activities were

controlled in accordance with plant procedures; (2) observed the condition of fire

detection devices to verify they remained functional; (3) observed fire suppression

systems to verify they remained functional; (4) verified that fire extinguishers and hose

stations were provided at their designated locations and that they were in a satisfactory

condition; (5) verified that passive fire protection features (electrical raceway barriers,

fire doors, fire dampers, steel fire proofing, penetration seals, and oil collection systems)

were in a satisfactory material condition; (6) verified that adequate compensatory

measures were established for degraded or inoperable fire protection features; and

(7) reviewed the corrective action program to determine if the licensee identified and

corrected fire protection problems.

ENCLOSURE

-3-

C May 18, 2005, Unit 2 Train A engineered safety feature (ESF) switchgear room

C May 18, 2005, Unit 2 Train B ESF switchgear room

C June 14, 2005, Unit 2 auxiliary feedwater (AFW) room, all accessible elevations

C June 16, 2005, Unit 3 Train A ESF switchgear room

C June 16, 2005, Unit 3 Train B ESF switchgear room

C June 17, 2005, Unit 3 AFW room, all accessible elevations

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

a. Inspection Scope

On June 21, 2005, the inspectors observed testing and training of senior reactor

operators and reactor operators to identify deficiencies and discrepancies in the training,

to assess operator performance, and to assess the evaluator's critique. The training

scenario involved a steam generator tube rupture and loss of offsite power.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

a. Inspection Scope

The inspectors reviewed the two below listed maintenance activities to: (1) verify the

appropriate handling of structure, system, and component (SSC) performance or

condition problems; (2) verify the appropriate handling of degraded SSC functional

performance; (3) evaluate the role of work practices and common cause problems; and

(4) evaluate the handling of SSC issues reviewed under the requirements of the

maintenance rule, 10 CFR 50 Appendix B, and the Technical Specifications.

  • April 8 - June 26, 2005, Units 2 and 3 inspections of 480 VAC ABB breakers

following a failure of the Unit 3 Holdup Tank Pump 3P741 480 VAC ABB breaker

ENCLOSURE

-4-

evaluation under the requirements of the maintenance rule

The inspectors completed two samples.

b. Findings

Introduction. The inspectors identified a Green noncited violation (NCV) of 10 CFR

50.65(a)(1) for the failure to include Units 2 and 3 SBCS deficiencies in the maintenance

rule program. This caused a lapse in the determination of appropriate system

monitoring and goal setting to maintain system reliability.

Description.

On February 14, 2005, the licensee identified that a small amount of air was leaking into

the Unit 3 main condenser due to a decrease in condenser vacuum. The source of the

air intrusion was determined to be a through-wall crack of approximately 14 inches in the

north piping header of the SBCS between the SBCS control valves and the Unit 3 main

condenser. The SBCS consists of two piping headers. Each header is designed to

remove heat to the main condenser at the equivalent of approximately 30 percent

reactor power. The affected portion of the SBCS was isolated, and the SBCS remained

operable with the south header still available. On February 21 the licensee inspected

the Unit 2 north SBCS header and discovered that cracks were developing at a similar

location to that observed on Unit 3. The Unit 2 north header was also isolated. The

south headers of the SBCS for both Units 2 and 3 had undergone an upgrade in 1986

and neither showed any signs of degradation.

The licensees analysis of the degraded piping concluded that a combination of weld

defects, residual stresses, and high frequency vibrations contributed to the degradation.

The repairs to the SBCS headers included upgrades to minimize vibration and residual

stresses.

The inspectors discovered that the licensee had not captured the SBCS deficiencies in

their maintenance rule program for monitoring or goal setting. The inspectors

determined that the through-wall cracking rendered the SBCS inherently unreliable in

accordance with NUMARC 93-01, Nuclear Energy Institute Industry Guideline for

Monitoring the Effectiveness of Maintenance of Nuclear Power Plants, Revision 2.

Specifically, Section 9.3.3 of NUMARC 93-01 indicated that, . . . an inherently reliable

structure, system, or component (SSC) is one that, without preventive maintenance, has

high reliability. The need to place an SSC under (a)(1) and establish goals may arise if

the inherently reliable SSC has experienced a failure. In such cases, the SSC cannot

be considered inherently reliable. The inspectors concluded that the SBCS failures

should have been tracked for monitoring and goal setting in the licensees maintenance

rule program.

ENCLOSURE

-5-

Analysis

The performance deficiency associated with this finding was the failure to recognize the

applicability of the maintenance rule for a failure of the SBCS. This finding was

associated with the mitigating systems cornerstone. The finding was determined to be

greater than minor because it affected the equipment performance attribute of the

mitigating systems cornerstone and affected the cornerstone objective of ensuring the

availability and reliability of systems that respond to initiating events. Using Manual

Chapter 0609, Significance Determination Process, Phase 1 worksheet, the finding

was determined to have very low safety significance because the SBCS did not actually

experience a loss of function.

Enforcement

10 CFR 50.65(a)(1) requires, in part, that the licensee monitor the performance or

condition of SSCs against licensee established goals, in a manner sufficient to provide

reasonable assurance that such SSCs are capable of fulfilling their intended function.

Contrary to the above, the licensee did not establish goals to provide a reasonable

assurance that the Units 2 and 3 SBCSs were capable of fulfilling their intended

function. Because the finding is of very low safety significance and has been entered

into the licensees corrective action program as AR 050200923, this violation is being

treated as an NCV consistent with Section VI.A of the Enforcement Policy: NCV

05000361;05000362/2005003-01, Failure to Properly Implement Maintenance Rule

Requirements for SBCS Header Cracks.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a. Inspection Scope

Emergent Work Control

The inspectors: (1) verified that the licensee performed actions to minimize the

probability of initiating events and maintained the functional capability of mitigating

systems and barrier integrity systems; (2) verified that emergent work-related activities

such as troubleshooting, work planning/scheduling, establishing plant conditions,

aligning equipment, tagging, temporary modifications, and equipment restoration did not

place the plant in an unacceptable configuration; and (3) reviewed the corrective action

program to determine if the licensee identified and corrected risk assessment and

emergent work control problems.

  • April 8, 2005, Unit 2 main feedwater isolation Valve 2HV4052 hydraulic fluid leak

(AR 050301752)

  • May 1, 2005, Unit 3 safety injection Tank T-008 leakage through low pressure

safety injection Loop 1A Check Valve 3MU072 (AR 050500027)

ENCLOSURE

-6-

  • May 2, 2005, Unit 3 pressurizer level error Bistable 3110BX failure

(AR 050500031)

  • May 13, 2005, Unit 2 reactor coolant Pump 3P001 speed input failure to core

protection calculator Channel B (AR 050500561)

The inspectors completed four samples.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Nonroutine Plant Evolutions (71111.14, 71153)

a. Inspection Scope

The inspectors: (1) reviewed operator logs, plant computer data, and/or strip charts for

the below listed evolutions to evaluate operator performance in coping with nonroutine

events and transients; (2) verified that the operator response was in accordance with the

response required by plant procedures and training; and (3) verified that the licensee

has identified and implemented appropriate corrective actions associated with personnel

performance problems that occurred during the nonroutine evolutions sampled.

  • On April 28, 2005, Unit 2 second point main feedwater Heater E038 steam

extraction Valve 2HV8808 closed because of level oscillations in the first and

second point feedwater heaters. Operator action was required to compensate

for the approximately 0.5 percent reactor power increase that occurred when

Valve 2HV8808 automatically closed.

  • On May 4-5, 2005, operators began reducing power on Unit 3 to Mode 3 in order

to support repairs to the hydraulic system associated with main feedwater block

Valve 3HV4051.

The inspectors completed two samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors: (1) reviewed plant status documents such as operator shift logs,

emergent work documentation, deferred modifications, and standing orders to

determine if an operability evaluation was warranted for degraded components;

ENCLOSURE

-7-

(2) referred to the Updated Final Safety Analysis Report and design basis documents to

review the technical adequacy of licensee operability evaluations; (3) evaluated

compensatory measures associated with operability evaluations; (4) determined

degraded component impact on any Technical Specifications; (5) used the Significance

Determination Process to evaluate the risk significance of degraded or inoperable

equipment; and (6) verified that the licensee has identified and implemented appropriate

corrective actions associated with degraded components.

  • April 8, 2005, AR 050400354 - Unit 3 refueling water storage tank to charging

pump suction Valve 3LV0227C relay failure

  • April 21, 2005, AR 050301800 - effect on the Unit 2 component cooling water

(CCW) system as a result of missing taper pins from CCW return isolation valve

2HV6500 from the Train B shutdown cooling heat exchanger

  • May 12, 2005, AR 050500710 - Unit 2 cask handling crane modifications not

completed before return to service

  • May 13, 2005, AR 050500795 - Unit 2 missing seismic restraints from the

Train A and B emergency diesel generator air start system piping

  • June 1, 2005, AR 050301091 - Units 2 and 3 potentially degraded offsite grid

voltage

The inspectors completed five samples.

b. Findings

No findings of significance were identified.

1R16 Operator Work-Arounds (71111.16)

a. Inspection Scope

The inspectors reviewed the one below listed operator workaround to: (1) determine if

the functional capability of the system or human reliability in responding to an initiating

event is affected; (2) evaluate the effect of the operator workaround on the operators

ability to implement abnormal or emergency operating procedures; and (3) verify that

the licensee has identified and implemented appropriate corrective actions associated

with operator workarounds.

  • May 30, 2005, Unit 3 safety injection Tank T009 Fill/Drain Valve 3HV9362 leakby

The inspectors completed one sample.

ENCLOSURE

-8-

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors selected the five below listed postmaintenance test activities of risk

significant systems or components. For each item, the inspectors: (1) reviewed the

applicable licensing basis and/or design-basis documents to determine the safety

functions; (2) evaluated the safety functions that may have been affected by the

maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested

the safety function that may have been affected. The inspectors either witnessed or

reviewed test data to verify that acceptance criteria were met, plant impacts were

evaluated, test equipment was calibrated, procedures were followed, jumpers were

properly controlled, the test data results were complete and accurate, the test

equipment was removed, the system was properly re-aligned, and deficiencies during

testing were documented. The inspectors also reviewed the corrective action program

to determine if the licensee identified and corrected problems related to

postmaintenance testing.

2G003 governor upgrade

  • April 13, 2005, WAR 2-0500287 - Unit 2 AFW Pump 2P141 planned

maintenance

  • April 16, 2005, WAR 2-0500339 - Unit 2 Train B CCW Pump 2P026 discharge

check Valve 2MU102 replacement

  • April 18, 2005, WAR 2-D3H4052 - Unit 2 main feedwater isolation

Valve 2HV4052 hydraulic fluid leak repair

  • April 20, 2005, MO 04111321000 - Unit 2 AFW Pump 2P504 packing

adjustments

The inspectors completed five samples.

b. Findings

No findings of significance were identified.

ENCLOSURE

-9-

1R20 Refueling and Outage Activities (71111.20)

a. Inspection Scope

For the listed outage, the inspectors reviewed the following risk significant outage

activities to verify defense in depth commensurate with the outage risk control plan and

compliance with the Technical Specifications: (1) the risk control plan;

(2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical

power; (5) decay heat removal; (6) reactivity control; (7) containment closure; (8) heatup

and coldown activities; and (9) licensee identification and implementation of appropriate

corrective actions associated with outage activities.

  • May 4, 2005, Unit 3 planned outage to repair cracks in the steam bypass header

piping and to repair an external hydraulic leak from main feedwater block Valve

3HV4051

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and Technical Specifications to ensure that the six below listed

surveillance activities demonstrated that the SSCs tested were capable of performing

their intended safety functions. The inspectors either witnessed or reviewed test data to

verify that the following significant surveillance test attributes were adequate:

(1) preconditioning; (2) evaluation of testing impact on the plant; (3) acceptance criteria;

(4) test equipment; (5) procedures; (6) jumper/lifted lead controls; (7) test data;

(8) testing frequency and method demonstrated Technical Specification operability;

(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME

Code requirements; (12) updating of performance indicator data; (13) engineering

evaluations, root causes, and bases for returning tested SSCs not meeting the test

acceptance criteria were correct; (14) reference setting data; and (15) annunciators and

alarms setpoints. The inspectors also verified that the licensee identified and

implemented any needed corrective actions associated with the surveillance testing.

  • April 12, 2005, Unit 2 safety injection Tank 2T-009 surveillance per

Procedure SO123-III-1.1.23, Units 2 and 3 Chemical Control of Primary Plant

and Related Systems, Revision 43

ENCLOSURE

-10-

  • May 5-6, 2005, Unit 3 pressurizer spray Valves 3PV100A and 3PV100B

performance tests per Procedure SO23-I-6.300, Air Operated Valve Diagnostic

Testing, Revision 7

  • May 13, 2005, Unit 3 CCW Pump 3P026 inservice test per Procedure SO23-3-

3.60.3, Component Cooling Water and Seismic Makeup Pump Test, Revision 5

  • May 26, 2005, Unit 2 AFW Pump 2P140 inservice test per Procedure SO23-3-

3.60.6, Auxiliary Feedwater Pump and Valve Testing, Revision 10

  • June 1, 2005, Unit 3 AFW Pump 3P504 inservice test per Procedure SO23-3-

3.60.6, Auxiliary Feedwater Pump and Valve Testing, Revision 10

  • June 16, 2005, Units 2 and 3 sound powered phone system check per

Procedure SO23-6-31, Communication System Operation, Revision 4

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, plant drawings,

procedure requirements, and Technical Specifications to ensure that the one listed

temporary modification was properly implemented. The inspectors: (1) verified that the

modification did not have an effect on system operability and availability; (2) verified that

the installation was consistent with the modification documents; (3) ensured that the

post-installation test results were satisfactory and that the impact of the temporary

modification on permanently installed SSCs were supported by the test; (4) verified that

the modifications were identified on control room drawings and that appropriate

identification tags were placed on the affected drawings; and (5) verified that appropriate

safety evaluations were completed. The inspectors verified that the licensee identified

and implemented any needed corrective actions associated with the temporary

modification.

  • April 20, 2005, Unit 3 main feedwater block Valve 3HV4051 to Steam

Generator E089 Fermanite repair

The inspectors completed one sample.

ENCLOSURE

-11-

b. Findings

Introduction. The inspectors identified a Green finding for the failure to develop an

adequate monitoring plan to identify a hydraulic fluid leak on main feedwater block

Valve 3HV4051.

Description. On January 20, 2005, the licensee identified that Unit 3 main feedwater

block Valve 3HV4051 had an approximate one drop per second hydraulic fluid leak. On

January 27 the licensee successfully stopped the leak by installing a Furmanite rig

around a leaking fitting on the hydraulic supply piping to the valve.

On April 20 the inspectors walked down portions of the Unit 3 main feedwater system in

order to evaluate the condition of the Furmanite rig that had been installed on

Valve 3HV4051. The inspectors observed that the Furmanite rig was leaking hydraulic

fluid at the rate of approximately ten drops per minute. Furthermore, the inspectors

observed that the leak collection system revealed enough hydraulic fluid to demonstrate

that the leak had been active for more than one operations shift. Specifically, the catch

basin was full of hydraulic fluid and the tygon tubing that was leading into the 55 gallon

drum had an approximate eight inch section that was full of hydraulic fluid. The

inspectors informed the Unit 3 control room supervisor of the degraded condition of

Valve 3HV4051 and the licensee reinjected additional Furmanite the following day to

stop the leak.

Valve 3HV4051 serves as a backup to main feedwater isolation Valve 3HV4052, but it is

not currently credited in the Updated Final Safety Analysis Report as a containment

isolation valve. The hydraulic system of Valve 3HV4051 serves to keep the valve open

against high pressure nitrogen and its subsequent loss would result in the valve closing.

The closing of the valve would likely result in the loss of main feedwater and a reactor

trip.

The inspectors interviewed operations personnel that were on shift the three days prior

to the Furmanite rig leaking on April 20, 2005. The interviews consisted of three field

operators that performed rounds on Valve 3HV4051 and their shift manager. The

inspectors determined that all three operators and the shift manager had a different

understanding of the status of the valve and were either provided incomplete or no

instructions on how to monitor the status of the Furmanite rig on the valve. The

inspectors determined that a monitoring plan had not been established despite the

licensees assessment that the Furmanite rig was susceptible to leakage. The licensee

indicated that operators were expected to monitor the condition of the valve as part of

their normal shifty rounds, which included checking equipment for fluid leakage as

described in Procedure OSM-5, Operator Rounds. The licensee subsequently

developed a monitoring plan to ensure that Valve 3HV4051 would be inspected twice

per shift. The value of the monitoring plan was demonstrated when a three to four drop

per minute leak through the Furmainte rig was identified by the licensee on May 2. The

licensee elected not to reinject the valve, but instead permanently repaired it during a

planned shutdown on May 4.

ENCLOSURE

-12-

Analysis. The performance deficiency associated with this finding was the failure to

develop an adequate monitoring plan to identify a hydraulic fluid leak from Valve

3HV4051. This finding was associated with the initiating events cornerstone. The

finding was determined to be greater than minor because it was associated with the

human performance attribute of the initiating events cornerstone and affects the

cornerstone objective of limiting the likelihood of those events that upset plant stability.

Furthermore, if left uncorrected, the finding would have become a more significant

safety concern in that it continued hydraulic fluid leakage on Valve 3HV4051 could result

in a plant transient. Using Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheet, the finding was determined to have very low safety significance

because the hydraulic fluid leak had not increased to the point where it contributed to

both the likelihood of a reactor trip and the likelihood that mitigation equipment or

functions were not available. This issue involved personnel human performance

crosscutting aspects associated with the failure to identify the hydraulic leak during

operator rounds.

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because Valve 3HV4051

is not subject to the requirements of 10 CFR Part 50, Appendix B. While

Valve 3HV4051 serves as a backup to a containment isolation valve, it is not currently

credited in the Updated Final Safety Analysis Report as a containment isolation valve.

This finding had been entered into the licensees corrective action program as AR

050401214 and AR 050401222. This finding is identified as FIN 05000362/2005003-02,

Failure to Identify Hydraulic Leak on Main Feedwater Block Valve 3HV4051.

Cornerstone: Emergency Preparedness

1EP1 Exercise Evaluation (71114.01)

a. Inspection Scope

The inspectors reviewed the objectives and scenario for the 2005 Biennial Emergency

Preparedness Exercise to determine if the exercise would acceptably test major

elements of the emergency plan. The scenario included a loss of electrical power to all

of the main control room alarms, a seized reactor coolant pump, a main steam line

break into the primary containment, and a helicopter crash into the main switchyard

which resulted in a loss of offsite power. The scenario continued with a station blackout

due to failures of the emergency diesel generators, and a steam generator tube rupture

and fuel cladding failure, resulting in an ongoing radioactive steam release to the

environment. The licensee activated all of their emergency facilities to demonstrate

their capability to implement the emergency plan.

The inspectors evaluated exercise performance by focusing on the risk-significant

activities of classification, notification, protective action recommendations, and

assessment of offsite dose consequences in the simulator control room and the

following emergency response facilities:

ENCLOSURE

-13-

  • Operations Support Center
  • Emergency Operations Facility

The inspectors also assessed personnel recognition of abnormal plant conditions, the

transfer of emergency responsibilities between facilities, communications, protection of

emergency workers, emergency repair capabilities, and the overall implementation of

the emergency plan to verify compliance with the requirements of 10 CFR 50.47(b),

10 CFR 50.54(q), and Appendix E to 10 CFR Part 50.

The inspectors attended the post-exercise critiques in each of the above emergency

response facilities to evaluate the initial licensee self-assessment of exercise

performance. The inspectors also attended the formal presentation of critique items to

plant management. The inspectors also reviewed emergency facility logs, emergency

notification forms, dose assessment records, and emergency news center press

releases to assess license performance during the exercise.

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspectors reviewed the San Onofre Emergency Plan, Revisions 18 and 19,

submitted in November 2004 and April 2005 respectively. Revision 18 deleted two

Unit 1 emergency response positions and assigned their functions to Units 2 and 3

emergency response personnel, updated emergency action levels associated with

security events, and added the position of Emergency Operations Facility Security

Director to the licensees emergency response organization. Revision 19 removed two

Unit 1 radiation monitors from listed emergency plan equipment, consistent with License

Amendment 163 to Unit 1 Technical Specifications.

The inspectors reviewed the emergency plan implementing Procedure SO123 VIII-1,

Recognition and Classification of Emergencies, Revisions 22 and 23, submitted in

November 2004 and April 2005 respectively. Revision 22 removed two security related

emergency action levels and added six additional emergency action level initiating

conditions associated with security events, consistent with the safeguards contingency

plan and the security order from the Commission that implemented Nuclear Energy

Institute 03-12, "Template for the Security Plan, Training and Qualification Plan,

Safeguards Contingency Plan, [and Independent Spent Fuel Storage Installation

Security Program]." The revision also removed reference to the Unit 1 Fuel Storage

Building and associated radiation monitors from the emergency action levels due to

ENCLOSURE

-14-

removal of all fuel from the building. Revision 23 made changes to equipment

references to be consistent with Revision 19 of the Emergency Plan.

The revisions were compared to the previous revisions, to the criteria of NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, and to the requirements

of 10 CFR 50.47(b) to determine if the licensee adequately implemented the emergency

plan change process described in 10 CFR 50.54(q).

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a. Inspection Scope

For the below listed simulator-based training evolution contributing to Drill/Exercise

Performance and Emergency Response Organization Performance Indicators, the

inspectors: (1) observed the training evolution to identify any weaknesses and

deficiencies in classification, notification, and protective action requirements

development activities; (2) compared the identified weaknesses and deficiencies against

licensee identified findings to determine whether the licensee is properly identifying

failures; and (3) determined whether licensee performance is in accordance with the

guidance of the NEI 99-02, Reulatory Assessment Indicator Guidelines, acceptance

criteria.

  • June 21, 2005, Unit 2 simulator, seismic event followed by a loss of coolant

accident

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

a. Inspection Scope

The inspectors sampled submittals for the performance indicators listed below for the

period July 1 through December 31, 2004. The definitions and guidance of Nuclear

ENCLOSURE

-15-

Engineering Institute 99-02, Regulatory Assessment Indicator Guideline, were used to

verify the licensees basis for reporting each data element in order to verify the accuracy

of performance indicator data reported during the assessment period.

  • Drill and Exercise Performance
  • Emergency Response Organization Participation
  • Alert and Notification System Reliability

The inspectors reviewed a 100 percent sample of drill and exercise scenarios, licensed

operator simulator training sessions, notification forms, and attendance and critique

records associated with training sessions, drills, and exercises conducted during the

verification period. The inspectors reviewed the qualification, training, and drill

participation records for a sample of 10 emergency responders. The inspectors

reviewed alert and notification system maintenance records and procedures, and a

100 percent sample of siren test results. The inspectors also interviewed licensee

personnel that were responsible for collecting and evaluating the performance indicator

data.

The inspectors completed three samples.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Daily Reviews

In order to help identify repetitive equipment failures or specific human performance

issues for followup, the inspectors performed a daily screening of items entered into the

licensees corrective action program. This review was accomplished by reviewing daily

action request (AR) summary reports and attending AR review meetings.

.2 Annual Sample Review

The inspectors selected AR 050200369 for more in depth review to verify that licensee

personnel had taken corrective actions commensurate with the significance of the issue.

The AR was written to address a service advisory from Engine Systems Incorporated to

alert licensees that fuel injectors used in emergency diesel generators should be pop

tested if the injector had been stored for more than one year. The AR was reviewed to

ensure that the full extent of the issues were identified, an appropriate evaluation was

performed, and appropriate corrective actions were specified and prioritized. The

inspectors evaluated the licensees actions against the requirements of the licensees

corrective action program as delineated in Procedure SO123-XV-50, Corrective Action

ENCLOSURE

-16-

Process, Revision 4. The inspectors determined that AR 050200369 was closed

without any corrective actions identified or documented in appropriate AR assignments.

The licensee subsequently reopened AR 050200369 in order to update the appropriate

emergency diesel generator procedures.

.3 Semiannual Review

a. Inspection Scope

The inspectors performed a semiannual review of licensee internal documents, reports,

audits, and PIs to identify trends that might indicate the existence of more significant

safety issues. The inspectors reviewed the following:

  • ARs generated during the previous six months
  • station performance reports
  • weekly production performance reviews
  • corrective maintenance backlog
  • quality assurance audit executive summaries
  • system health reports
  • performance indicators

b. Findings and Observations

No findings of significance were identified. However, during the review the inspectors

noted the following trends where performance deficiencies have recurred:

  • On several occasions the inspectors have identified plant deficiencies that were

not identified as operator workarounds per licensee program requirements

(ARs 050400215, 050201018, 050600134). Through interviews and periodic

program reviews, the inspectors determined that on shift operators have little

ownership in the operator workaround program. The licensees philosophy that

the operator workaround program is only a management tool and not a tool for

shift operators may be a contributing factor to this deficiency.

  • The inspectors noted at the end of the inspection period that Unit 2 safety

injection Tank 8 had developed a small leak of approximately 0.5 gallons

per hour through safety injection system check valves. Although minor, check

valve leakage in the safety injection system has been a chronic problem

(ARs 050500027, 030400450; also see IR 05000361;362/2003003

Section 1R13). The licensee indicated that an effort to benchmark other utilities

to better identify effective corrective actions would be performed.

  • The inspectors noted that hydraulic leaks in main feedwater block valves and

main feedwater isolation valves have occurred three times within the last

six months (ARs 050500705, 050101113, and 041201554). The licensee was in

the process of evaluating the deficiencies for possible equipment aging issues

ENCLOSURE

-17-

and generic weaknesses at the end of the inspection period.

  • The inspectors have previously identified multiple instances where ARs have

been closed with no corrective action taken or they did not identify or correct

deficiencies with interdepartmental communication and coordination that

contributed to complications in the resolution of problems (see IR 05000361;

362/2003003 Section 4OA2.1). The licensee initiated a task force to implement

more effective corrective actions to improve AR documentation and

interdepartmental communications (ARs 050500741 and 050500737,

respectively).

4OA3 Event Followup (71153)

(Closed) Licensee Event Report (LER) 05000361/2005002-00, Missing Taper Pins on

CCW Valve Cause Technical Specification Required Shutdown

On February 14, 2005, the licensee manually shut down Unit 2 in response to a failure

of the component cooling water outlet isolation Valve 2HV6500 to the Train B shutdown

cooling heat exchanger. The licensee discovered that 2HV6500 had been rendered

inoperable because the two taper pins that held the valve disc to its stem were both

missing. The licensee was issued a noncited violation for this failure (see

IR 05000361;362/2005002, Section 1R13.1). This Licensee Event Report is closed.

4OA4 Crosscutting Aspects of Findings

Cross-References to Human Performance Findings Documented Elsewhere

Section 1R23 describes a finding where operations personnel failed to identify a

hydraulic fluid leak from main feedwater block Valve 3HV4051.

4OA5 Other Activities

Temporary Instruction (TI) 2515/163: Operational Readiness of Offsite Power

The inspectors collected data pursuant to TI 2515/163, "Operational Readiness of

Offsite Power." The inspectors reviewed the licensee's procedures related to General

Design Criteria 17, "Electric Power Systems;" 10 CFR 50.63, "Loss of All Alternating

Current Power;" 10 CFR 50.65(a)(4), "Requirements for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants;" and the Technical Specifications for the offsite

power system. The data was provided to the Office of Nuclear Reactor Regulation for

further review. Documents reviewed for this TI are listed in the attachment.

ENCLOSURE

-18-

4OA6 Meetings, Including Exit

On April 15, 2005, the senior emergency preparedness inspector discussed the

inspection findings with Mr. D. Nunn, Vice President, and other members of the

licensee's staff. The inspector verified that no proprietary information was provided

during the inspection.

On June 24, 2005, the resident inspectors presented the inspection results to

Dr. R. Waldo and others who acknowledged the findings. The inspectors confirmed that

proprietary information was not provided or examined during the inspection.

ATTACHMENT: SUPPLEMENTAL INFORMATION

ENCLOSURE

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

C. Anderson, Manager, Site Emergency Preparedness

B. Ashbrook, Manager, Emergency Planning

D. Breig, Station Manager

D. Cleavenger, Project Analyst, Offsite Emergency Planning

B. Culverhouse, Manager, Offsite Emergency Planning

B. Katz, Vice President, Nuclear Oversight and Regulatory Affairs

R. Garcia, Technical Specialist, Offsite Emergency Planning

S. Giannell, Technical Specialist, Emergency Planning

M. Love, Manager, Maintenance

J. Madigan, Manager, Health Physics

C. McAndrews, Manager, Nuclear Oversight and Assessment

M. McBrearty, Technical Specialist, Nuclear Regulatory Affairs

D. Nunn, Vice President, Engineering and Technical Services

N. Quigley, Manager, Mechanical/Nuclear Maintenance Engineering

D. Richards, Project Manager, Emergency Planning

A. Scherer, Manager, Nuclear Regulatory Affairs

J. Scott, Technical Specialist, Emergency Planning

M. Short, Manager, Systems Engineering

T. Vogt, Manager, Operations

R. Waldo, Vice President, Nuclear Generation

D. Wilcockson, Manager, Plant Operations

T. Yackle, Manager, Design Engineering

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000361; NCV Failure to Properly Implement Maintenance Rule

05000362/2005003-01 Requirements for SBCS Header Cracks (Section 1R12)05000362/2005003-02 FIN Failure to Identify Hydraulic Leak on Main Feedwater

Block Valve 3HV4051 (Section 1R23)

Closed

05000361/2005-002-00 LER Missing Taper Pins on CCW Valve Cause Technical

Specification Required Shutdown (Section 4OA3)

A-1 ATTACHMENT

Discussed

None

LIST OF DOCUMENTS REVIEWED

In addition to the documents called out in the inspection report, the following documents were

selected and reviewed by the inspectors to accomplish the objectives and scope of the

inspection and to support any findings:

Section 1R01: Adverse Weather Protection

Procedures

Abnormal Operating Instruction SO23-13-3, Earthquake, Revision 8

Abnormal Operating Instruction SO23-13.8, Severe Weather, Revision 8, Attachment 4, Post

Severe Weather/Tsunami Inspections, and Attachment 5, Tsunami Warning

ARs

050600633

050600890

Section 1R04: Equipment Alignment

Procedures

SO23-3-2.7.1, SIT Fill/Loop Recirculation Using a HPSI Pump, Revision 12

SO23-3-2.27, Control Room Isolation and Emergency Ventilation System, Revision 15

Section 1R12: Maintenance Implementation

ARs

050100972

050200923

Section 1R15: Operability Evaluations

Procedures

SO123-209-1-M505, Single Failure Proof Trolley Project, Revision 0

A-2 ATTACHMENT

SONGS Priority 2 Reading 2-2526, Switchyard Voltage

California ISO Procedure OPE-508, Electrical System Emergency, Revision 4.1

Western Electricity Coordinating Council Reliability Criteria dated December 2004

ARs

050401269

030600403

Section 1R16: Operator Workarounds

SO123-XX-6, Operator Work Around Program, Revision 3

Section 1R19: Postmaintenance Testing

Procedures

SO23-II-11.156, Diesel Generator G002/G003 Electric Governor Test and Calibration,

Revision 2.

SO23-II-11.152, Diesel Generator Governor and Overspeed Trip Adjustment, Revision 1

SO23-3-3.60.6, Auxiliary Feedwater Pump and Valve Testing, Revision 10

SO23-3-3.31.3, Component Cooling Water Valve Testing - Offline, Revision 10

SO23-3-3.31.6, Main and Auxiliary Feedwater Valve Testing - Offline or Long Interval,

Revision 6

SO23-3-3.30, Inservice Valve Testing Program, Revision 16

AR

050301752

Section 1R20: Refueling and Outage Activities

Procedures

SO23-5-1.4, Plant Shutdown to Hot Standby, Revision 11

SO23-V-8.15, Boric Acid Leak Inspection, Revision 0

SO23-5-1.3.1, Plant Startup from Hot Standby to Minimum Load, Revision 23

Section 1EP1: Exercise Evaluation

A-3 ATTACHMENT

Procedures

SO123-VIII-10, Emergency Coordinator Duties, Revision 21

SO123-VIII-10.1, Station Emergency Director Duties, Revision 16

SO123-VIII-10.2, Corporate Emergency Director Duties, Revision 12

SO123-VIII-10.3, Protective Action Recommendations, Revision 9

SO123-VIII-30, Units 2/3 Operations Leader Duties, Revision 10

SO123-VIII-30.1, Emergency Planning Coordinator Duties, Revision 20

SO123-VIII-30.3, OSC Operations Coordinator Duties, Revision 5

SO123-VIII-40.100, Dose Assessment, Revision 12

SO123-VIII-50, TSC Technical Leader Duties, Revision 12

SO123-VIII-50.2, EOF Technical Leader Duties, Revision 5

SO123-VIII-80, Emergency Group Leader Duties, Revision 12

SO123-XVIII-10.5, Facilities Management, Revision 4, TCN 4-2

Exercise and Drill Critiques: April 28, 2004; May 5, 2005; June 23, 2004; June 30, 2004;

March 9, 2005

Exercise Press Releases

Edison Declares "Alert" at San Onofre Nuclear Plant; "Site Area Emergency" Declared

at San Onofre; Four Fatally Injured Aboard U.S. Coast Guard Helicopter That Crashed

at San Onofre; Evaluations Underway at San Onofre Generating Station; Edison

Declares "General Emergency" at San Onofre Nuclear Plant; Field Monitoring Teams

Taking Radiation Readings; Radioactive Material Release from San Onofre Nuclear

Generating Station Continues

Section 4OA1: Performance Indicator Verification

SO123-VIII-0.401, Emergency Preparedness Performance Indicators, Revision 0

SSSPG-SO123-G-8, Offsite Emergency Planning Alert Notification System Performance

Indicators, Revision 1

SO123-XXI-1.11.3, Emergency Plan Training Program Description, Revision 13

A-4 ATTACHMENT

SO123-XVIII-10.1, Siren - Community Alert Siren System - Biweekly Silent Test,

Revision 5, TCN 5-1

SO123-XVIII-10.3, Siren - Community Alert Siren System - Quarterly Growl Test, Revision 6

SO 23-XV-24, Quarterly NRC Performance Indicator Process, Revision 1

Section 4OA2: Identification and Resolution of Problems

Procedures

SO23-I-8.76, Emergency Diesel Generator Overhaul, Revision 4

SO23-I-8.61, Emergency Diesel Generator Power Pack Replacement, Revision 0

SO23-I-8.62, Emergency Diesel Generator Fuel Injector Replacement, Revision 0

SO23-I-8.74, Emergency Diesel Generator and Components Overhaul, Revision 7

Maintenance Orders

01110787000

01121258000

ARs

020300958

Section 4OA5: Other

Procedures

SO23-13-4, "Operation During Major System Disturbances," Revision 6

SO123-0-A7, "Notification and Reporting of Significant Events," Revision 2

SO123-XX-10, "Maintenance Rule Risk Management Program Implementation," Revision 1

SO123-XX-5, "Work Authorizations," Revision 13

SO23-12-8, "Station Blackout," Revision 18

GCC Operating Procedure OP-013: SONGS Voltage

SO23-12-11 ISS 2, "EOI Supporting Attachments," Revision 2

SO23-14-8, "Station Blackout Bases and Deviations Justification," Revision 6

A-5 ATTACHMENT

ARs

050501735

050600016

LIST OF ACRONYMS

AFW auxiliary feedwater

AR action request

CFR Code of Federal Regulations

CCW component cooling water

ESF engineered safety feature

NCV noncited violation

SBCS steam bypass control system

SSC structure, system, and component

A-6 ATTACHMENT