ML051310282
ML051310282 | |
Person / Time | |
---|---|
Site: | Millstone ![]() |
Issue date: | 05/11/2005 |
From: | Paul Krohn NRC/RGN-I/DRP/PB6 |
To: | Christian D Dominion Resources Services |
Krohn P, RI/DRP/PB6/610-337-5120 | |
References | |
IR-05-002 | |
Download: ML051310282 (60) | |
See also: IR 05000336/2005002
Text
May 11, 2005
Mr. David A. Christian
Sr. Vice President and Chief Nuclear Officer
Dominion Resources
5000 Dominion Boulevard
Glenn Allen, VA 23060-6711
SUBJECT: MILLSTONE POWER STATION UNIT 2 AND UNIT 3 - NRC INTEGRATED
INSPECTION REPORT 05000336/2005002 AND 05000423/2005002
Dear Mr. Christian:
On March 31, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed inspections at
your Millstone Power Station Unit 2 & Unit 3. The enclosed integrated inspection report
documents the inspection findings, which were discussed on April 21, 2005, with
Mr. J. Alan Price and other members of your staff.
The inspections examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
This report documents four NRC-identified and two self-revealing findings of very low safety
significance (Green). Five of these findings were determined to involve violations of NRC
requirements. However, because of their very low safety significance and because they have
been entered into your corrective action program, the NRC is treating these issues as Non-cited
Violations (NCVs), in accordance with Section VI.A.1 of the NRCs Enforcement Policy.
If you contest any NCV in this report, you should provide a response within 30 days of the date
of these inspection reports, with the basis for your denial, to the Nuclear Regulatory
Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the
Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear
Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the
Millstone Power Station.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
enclosures, and your response (if any) will be available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Website at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Paul G. Krohn, Chief
Projects Branch 6
Division of Reactor Projects
Mr. D. A. Christian 2
Docket Nos.: 50-336, 50-423
Enclosure: Inspection Report 05000336/2005002 and 05000423/2005002
w/Attachment: Supplemental Information
cc w/encl:
J. A. Price, Site Vice President, Millstone Station
C. L. Funderburk, Director, Nuclear Licensing and Operations Support
D. W. Dodson, Supervisor, Station Licensing
L. M. Cuoco, Senior Counsel
C. Brinkman, Manager, Washington Nuclear Operations
J. Roy, Director of Operations, Massachusetts Municipal Wholesale Electric Company
First Selectmen, Town of Waterford
R. Rubinstein, Waterford Library
J. Markowicz, Co-Chair, NEAC
E. Woollacott, Co-Chair, NEAC
E. Wilds, Director, State of Connecticut SLO Designee
J. Buckingham, Department of Public Utility Control
G. Proios, Suffolk County Planning Department
R. Shadis, New England Coalition Staff
G. Winslow, Citizens Regulatory Commission (CRC)
S. Comley, We The People
D. Katz, Citizens Awareness Network (CAN)
R. Bassilakis, CAN
J. M. Block, Attorney, CAN
Mr. D. A. Christian 3
Distribution w/encl (VIA E-MAIL):
S. Collins, RA
J. Wiggins, DRA
S. Lee, RI OEDO
D. Roberts, NRR
V. Nerses, NRR
G. Wunder, NRR
S. Schneider, Senior Resident Inspector
E. Bartels, Resident OA
P. Krohn, RI
S. Barber, RI
T. Madden, OCA
ROPreports@nrc.gov
Region I Docket Room (with concurrences)
SISP Review Complete: ___PGK______ (Reviewers Initials)
DOCUMENT NAME: E:\Filenet\ML051310282.wpd
After declaring this document An Official Agency Record it will be released to the Public.
To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure
"E" = Copy with attachment/enclosure "N" = No copy
OFFIC RI/DRP RI/DRP RI/DRP
E
NAME SSchneider/PGK SBarber/PGK PKrohn/PGK
for for
DATE 05/06/05 05/11/05 05/11/05 05/ /05
OFFICIAL RECORD COPY
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket No.: 05000336, 05000423
Report No.: 05000336/2005002 and 05000423/2005002
Licensee: Dominion Nuclear Connecticut, Inc.
Facility: Millstone Power Station, Unit 2 and Unit 3
Location: P. O. Box 128
Waterford, CT 06385
Dates: January 1, 2005 - March 31, 2005
Inspectors: S. M. Schneider, Senior Resident Inspector, Division of Reactor Projects
(DRP)
S. R. Kennedy, Resident Inspector, DRP
K. A. Mangan, Resident Inspector, DRP
K. M. Jenison, Senior Reactor Inspector, DRP
M. X. Davis, Reactor Inspector, Division of Reactor Safety (DRS)
K. S. Kolaczyk, Senior Resident Inspector, Ginna, DRP
J. A. Krafty, Reactor Inspector, DRS
T. A. Moslak, Health Physicist, DRS
J. G. Schoppy, Senior Reactor Inspector, DRS
Accompanied by: M. L. Heath, Nuclear Safety Professional
Approved by: Paul G. Krohn, Chief
Projects Branch 6
Division of Reactor Projects
Enclosure
CONTENTS
SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iii
REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1R01 Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5
1R06 Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6
1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7
1R11 Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . 10
1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11
1R13 Maintenance Risk Assessments and Emergent Work Evaluation . . . . . . . . . . 11
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events . . . 12
1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14
1R16 Operator Work-Arounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
1R19 Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20
1R23 Temporary Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21
1EP4 Emergency Action Level and Emergency Plan (E-PLAN) Changes . . . . . . . . 23
1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24
2OS1 Access Controls to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . 24
2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27
OTHER ACTIVITIES [OA] . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28
4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29
4OA4 Cross Cutting Aspects of Findings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30
4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30
4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 32
SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2
LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3
LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-16
ii Enclosure
SUMMARY OF FINDINGS
IR 05000336/2005002, 05000423/2005002; 01/01/2005 - 03/31/2005; Millstone Power Station,
Unit 2 and Unit 3; Adverse Weather Protection, Heat Sink Performance, Post-Maintenance
Testing, Temporary Plant Modifications, Other Activities.
The report covered a 3-month period of inspection by resident inspectors and announced
inspections by regional inspectors. Five (Green) NCVs and one (Green) finding were identified.
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using
Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SDP). Findings
for which the SDP does not apply may be Green or be assigned a severity level after NRC
management review. The NRC's program for overseeing the safe operation of commercial
nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3,
dated July 2000.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Initiating Events
Unit 2
! Green. The inspectors identified a self-revealing finding for the failure to
adequately address issues related to the operation of an outdoor temporary air
compressor and associated air dryer skid during cold weather conditions. On
November 11, 2004, Dominion had identified that additional freeze protection
actions were required to ensure the availability of the compressor during cold
weather. Subsequently, the inspectors identified two occasions where actions
taken to ensure availability of the compressor were not adequate. On December
17, 2004, the inspectors identified that a heat trace for the system dryer was
deenergized. On February 1, 2005, the temporary air compressor failed causing
the B instrument air compressor to start. Following the air transient, Dominion
conducted an investigation and concluded that the cause of the temporary air
compressor failure was freezing of the pre-filter on the air dryer skid. Dominion
replaced the compressor, installed a tent around the air-dryer towers, and placed
a heating unit inside the tent.
The finding was more than minor because it affected the equipment performance
attribute of the Initiating Events cornerstone objective of limiting the likelihood of
events that upset plant stability at power. The performance issue associated
with this finding was the failure to take adequate actions to ensure that adverse
weather conditions did not affect the availability of the temporary instrument air
system. The risk of this finding was determined to be of very low safety
significance (Green), because, although the temporary air compressor system
became unavailable, the standby instrument air compressor restored instrument
air system pressure. The instrument air system pressure stabilized and
recovered such that the instrument air header pressure did not cause a reactor
trip. This finding was related to the cross-cutting area of Problem Identification
iii Enclosure
and Resolution in that Dominion failed to take adequate corrective actions to
prevent the air dryer skid from freezing.. (Section 1R01.2)
Cornerstone: Mitigating Systems
Unit 2
! Green. The inspectors identified a self-revealing non-cited violation of Technical
Specification 6.8.1a, Procedures and Programs, for the failure to adequately
implement the procedure for installing temporary ventilation through the East 480
volt vital switchgear room when normal cooling was disabled for maintenance.
The procedure establishes the required flow path in the switchgear room when
compensatory cooling measures were required. On January 12, 2005, operators
failed to perform the procedure step that opens doors to provide for an exhaust
path to allow warm air to leave the switchgear room.
The finding was greater than minor because the failure to install the
compensatory cooling system, per the procedure, caused the air flow through
the East 480 volt switchgear room to be below the minimum required to support
cooling of the 480 volt system for initiating events (transients), mitigating
systems, and barrier integrity systems. The finding was associated with the
equipment performance attribute of the initiating events and mitigating systems
cornerstones, and the containment structures, systems, and components and
barrier performance attribute of the barrier integrity cornerstone. Since more
than one cornerstone was affected, a Reactor Safety Significance Determination
Process Phase 2 analysis was performed. The analysis resulted in a finding of
very low safety significance (Green) because the improper installation of the
compensatory measures did not result in an actual loss of the supported 480 volt
AC system or electro hydraulic control functions. This finding was related to the
cross-cutting area of Human Performance in that both Engineering and
Operations personnel failed to correctly implement the procedure for
compensatory cooling. (Section 1R23)
Unit 3
! Green. The inspector identified a non-cited violation of 10 CFR Part 50,
Appendix B, Criterion XVI, Corrective Action, for Dominions failure to take
prompt and appropriate corrective actions to address a condition adverse to
quality. Specifically, Dominion did not promptly evaluate and correct a degraded
condition associated with the divider plate for all three reactor plant component
cooling water (RPCCW) heat exchangers (HXs).
The inspector determined that this issue was more than minor because it was
associated with the equipment performance attribute of the mitigating systems
cornerstone, and it potentially affected the objective to ensure the availability and
reliability of the RPCCW HXs. The finding was of very low safety significance
(Green), because the finding was a qualification deficiency confirmed not to
result in loss of a function. The issue was similarly of very low risk in the
Initiating Events cornerstone because the finding did not increase the likelihood
iv Enclosure
of a reactor trip or a loss of service water (SW) event. The finding was
associated with the cross-cutting area of problem identification and resolution
(PI&R) in that Dominions inadequate evaluation and untimely corrective actions
for a degraded condition potentially affected the RPCCW HXs. (Section 1R07.2)
! Green. The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,
Criterion XI, Test Control, for the failure to adequately implement
post-maintenance test (PMT) procedures for restoring the A emergency diesel
generator (EDG) to service following maintenance of the neutral breaker. On
March 1, 2005, Dominion conducted maintenance and doble testing of the A
EDG neutral breaker. The Maintenance Department turned the breaker over to
Operations for final post-maintenance testing and restoration. After racking in
the breaker, Operations noted that the red light on the front of the EDG neutral
breaker panel did not light as expected. Contrary to the PMT acceptance
criteria, Operations assessed that the PMT was satisfactorily completed and
exited the EDG technical specification. The oncoming shift investigated and
determined the red light was not lit because there was a problem with the neutral
breaker trip circuit. Operations declared the EDG inoperable and re-entered the
EDG technical specification.
This issue was more than minor because it was associated with the reliability of
the A EDG. The inspectors determined that the finding was of very low safety
significance (Green) because it did not involve a design or qualification
deficiency, represent an actual loss of safety function of the A EDG, or involve
seismic, flooding, or severe weather initiating events. This finding was related to
the cross-cutting area of Human Performance in that Dominion personnel signed
the PMT as satisfactory and restored the EDG neutral breaker to an operable
status although the acceptance criteria was not met. (Section 1R19.1)
! Green. The inspectors identified a non-cited violation of 10 CFR 50, Appendix B,
Criterion XVI, Corrective Action, which requires, in part, that measures be
established to assure that conditions adverse to quality are promptly identified
and corrected. From May to October 2004, Dominion failed to properly assess
and correct a degraded A Residual Heat Removal (RHR) system during an
extent of condition examination for air found in the RHR discharge piping.
Specifically, after discovering a significant amount of air in the A RHR piping
system in May 2004, Dominion vented the system but did not adequately
evaluate whether the corrective actions were effective in removing air from the
RHR heat-exchanger tubing. As a result, Dominion did not evaluate the effect of
the remaining air on the RHR and high pressure injection systems. Dominion
subsequently instituted compensatory measures to vent the suction piping after
every RHR pump run and performed a special procedure to flush the air out of
the heat exchanger.
This finding was more than minor because it affected the equipment
performance attribute and the availability, reliability, and capability objective of
the Mitigating system cornerstone. Specifically, Dominions extent of condition
evaluation did not determine that a significant volume of air remained in the A
RHR heat exchanger tubing even though air was found in several other sections
v Enclosure
of piping subsequent to their initial corrective actions. This air could have
caused the A RHR pump to become inoperable if enough air had migrated to
the suction of the RHR pump and could have adversely affected high pressure
injection pumps if air had migrated to crossover piping. This finding was
determined to be of very low safety significance (Green) since an actual loss of
RHR would not have occurred with the amount of air identified and no air
pockets were subsequently identified in crossover piping to the charging and
high pressure injection systems; the finding did not involve a design or
qualification deficiency; or involve seismic, flooding, or severe weather initiating
events. This finding was related to the cross-cutting area of Problem
Identification and Resolution in that Dominion failed to perform an adequate
extent-of-condition review to fully evaluate the effect of air that had been
introduced into the A RHR system. (Section 4OA5.2)
Cornerstone: Barrier Integrity
Unit 3
! Green. The inspectors identified a non-cited violation of Technical Specification
(TS) 3.6.4.2, Electric Hydrogen Recombiners, which requires that two
independent hydrogen recombiner systems remain Operable. On February 22,
2005, Dominion performed maintenance on the A train hydrogen monitor. On
February 23, 2005, Dominion identified that pipe fittings for the A train
hydrogen monitor had been disassembled, however, a post-maintenance test
had not been conducted to prove operability of the system. Dominion performed
a leak test on February 24, 2005, however, the test failed. Dominions
investigation determined that the leakage was from a mechanical joint that had
been worked on December 2, 2004, but that this joint had not been disturbed
during the February 22, 2005, maintenance. Additionally, Dominion determined
that following the work in December 2004 no post-maintenance leak test had
been performed to verify system operability. The inspectors identified that the
leakage would have resulted in the shutdown of the A hydrogen recombiner,
under post-accident conditions. Therefore, the train would not have been
considered operable from December 2, 2004 to March 1, 2005. Following the
identification of the failed joint, Dominion repaired the joint, leak tested the
system, and restored the A train hydrogen monitor to service.
This issue was more than minor because it was associated with the Barrier
Integrity cornerstone attribute of configuration control in that it affected
containment boundary preservation and maintaining containment design
parameters. The failure to specify adequate PMT resulted in loose mechanical
joints in the system not being detected which would have allowed an open
pathway to the atmosphere from containment during post accident conditions.
Additionally, Dominion postulated that the post accident leakage from these
joints would have caused a radiation monitor alarm which would have isolated
the A hydrogen recombiner. This violation was evaluated using an IMC 0609,
Appendix H, Containment Integrity Significance Determination Process, Phase
2 analysis, and was determined to be of very low safety significance (Green).
Specifically, the leak was not of the magnitude to recycle the containment
vi Enclosure
atmosphere in a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period, post event. This finding was related to the
cross-cutting issue of Human Performance in that Dominion failed to adequately
perform post-maintenance testing to ensure incorrect maintenance activities
were identified prior to returning the hydrogen monitor to service.
(Section 1R19.2)
B. Licensee-Identified Violations
None.
vii Enclosure
REPORT DETAILS
Summary of Plant Status
Unit 2 operated at or near 100 percent power for the duration of the inspection period.
Unit 3 operated at or near 100 percent power for the duration of the inspection period.
1. REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
1R01 Adverse Weather Protection (71111.01 - Two Unit 2 Samples and One Unit 3 Sample)
1. Onset of Adverse Weather Site Inspection (One Unit 2 Sample and One Unit 3 Sample)
a. Inspection Scope
The inspectors performed a review of adverse weather preparations during the onset of
a winter snowstorm on January 22, 2005, to evaluate the sites readiness for the
expected weather conditions. The inspectors reviewed Dominions
preparations/protection for the adverse weather and its impact on the protection of
safety-related systems, structures and components. The inspectors verified that
operator actions, taken in response to the adverse weather, maintained readiness of
essential systems and that adequate operator and Site Emergency Response
Organization staffing was specified. Documents reviewed during the inspection are
listed in the Attachment.
b. Findings
No findings of significance were identified.
2. System Inspection (One Unit 2 Sample)
a. Inspection Scope
The inspectors reviewed the Unit 2 temporary instrument air system for extreme
weather condition preparation. The inspection was intended to ensure that the indicated
equipment, its instrumentation, and its supporting structures were configured in
accordance with Dominion procedures and that adequate controls were in place to
ensure functionality of the system. The inspectors reviewed licensee procedures and
condition reports and walked down the system. Documents reviewed during the
inspection are listed in the Attachment.
Enclosure
2
b. Findings
Introduction. A Green self-revealing finding was identified for the failure to implement
adequate actions to ensure the availability of a temporary instrument air compressor
during cold weather conditions. This resulted in the failure of the compressor while it
was required for operation.
Description. The inspectors reviewed Dominions installation of a diesel-driven outdoor
instrument air compressor (IAC) and associated air dryer skid used to provide air to the
Unit 2 instrument air system. Unit 2 was designed with three IACs, however, a fourth
temporary IAC was installed due to reliability issues associated with these compressors
and the retirement of the C IAC. On January 30, 2005, the A instrument air
compressor failed to load and was declared inoperable. The temporary instrument air
compressor was placed in service as the lead compressor and the B instrument air
compressor was placed in standby. On February 1, 2005, the temporary air compressor
failed. The B instrument air compressor started on a low instrument air header
pressure and restored the instrument air system pressure. Dominion determined that
the prefilter for the outdoor air drying unit had frozen which had prevented the air
compressor from providing air to the instrument air system.
The inspectors review of licensee actions related to the temporary IAC found that
Dominion had several opportunities to take measures to prevent cold weather from
affecting the temporary air compressor. On November 11, 2004, an operator
questioned what actions were required for freeze protection of the temporary air
compressor and documented his concerns in CR-04-10102. Dominion addressed the
concern by applying heat wrap to the air dryer and energizing the engine heater block.
On December 17, 2004, the inspectors walked down the system and questioned the
adequacy of the installation and the freeze protection methods since, for example, the
dryer heat trace did not appear to be operating. Subsequently, Dominions investigation
identified the heat trace power supply breaker had tripped. Dominion addressed the
specific concerns but did not perform an evaluation as to the adequacy of the entire
system to operate during cold weather conditions. As a result, on February 1, 2005, the
temporary air compressor failed when the prefilter for the outdoor air drying unit froze.
The inspectors discussed the adequacy of the November 11, 2004, corrective actions
with Operations. Following the second failure of the system, Dominion replaced the
IAC, enclosed the dryer skid in a tent, and installed a heater inside the tent.
Analysis. The performance deficiency associated with this issue was that Dominion
failed to adequately address issues related to freeze protection of the outdoor temporary
air compressor, which subsequently resulted in a failure of the system when the prefilter
on the air dryer skid froze. Traditional enforcement does not apply to this issue because
there were no violations of NRC requirements, no actual safety consequences, and no
impacts on the NRCs ability to perform its regulatory function. The finding was more
than minor because it affected the equipment performance attribute of the Initiating
Events cornerstone objective of limiting the likelihood of events that upset plant stability
at power. Specifically, the failure to take measures to prevent the air compressor from
freezing increased the likelihood of a loss of instrument air event and manual scram. If
Enclosure
3
the B instrument air compressor had failed, the instrument air system pressure would
have fallen below the 80 psig limit, requiring operators to manually scram the reactor.
The inspectors determined that the finding was of very low safety significance (Green)
through performance of a Phase 1 SDP in accordance with IMC 0609, Appendix A,
"Significance Determination of Reactor Inspection Findings for At-Power Situations,"
dated December 1, 2004. Specifically, the finding did not contribute to the likelihood of
a primary or secondary system loss of coolant accident initiator, contribute to both the
likelihood of a reactor trip and the likelihood that mitigating equipment would not be
available, or increase the likelihood of a fire or internal/external flood. The instrument air
system remained operable during the duration of the transient. Therefore, the risk of
this finding was determined to be of very low safety significance (Green).
This finding was related to the cross-cutting issue of problem identification and
resolution because Dominion failed to take adequate corrective actions to prevent the
air dryer skid from freezing.
Enforcement. There were no violations of NRC regulatory requirements since the
instrument air system is not safety-related. However, the instrument air system
functions have an impact on the overall plant risk, and the inspectors determined that
Dominion was ineffective in taking corrective actions to prevent failure of the temporary
air compressor. The issues relating to this inspection were documented by the
Dominion corrective action program under CR-05-00922. (FIN 05000336/2005002-01)
1R04 Equipment Alignment (71111.04)
1. Partial System Walkdowns (71111.04Q - Three Unit 2 Samples and Three Unit 3
Samples)
a. Inspection Scope
The inspectors performed six partial system walkdowns during this inspection period.
The inspectors reviewed the documents listed in the Attachment to determine the
correct system alignment. The inspectors conducted a walkdown of each system to
verify that the critical portions of selected systems were correctly aligned in accordance
with these procedures and to identify any discrepancies that may have had an effect on
operability. The inspectors verified that equipment alignment problems that could cause
initiating events, impact mitigating system availability or function, or affect barrier
functions, were identified and resolved. The following systems were reviewed based on
their risk significance for the given plant configuration:
Unit 2
- Partial equipment alignment of the "B" train of the auxiliary feedwater (AFW)
system during maintenance on the "A" train of the AFW system,
January 25, 2005;
Enclosure
4
- Partial equipment alignment of the A motor-driven auxiliary feedwater pump
(MDAFW) during maintenance and testing on the turbine-driven auxiliary
feedwater (TDAFW) pump, February 4, 2005; and
- Partial equipment alignment of the TDAFW system during maintenance on the
"B" train of the AFW system, March 7, 2005.
Unit 3
- Partial equipment alignment of the A and B motor driven auxiliary feedwater
trains while turbine driven AFW train was out for maintenance, March 9, 2005;
- Partial equipment alignment of offsite electrical distribution system due to
Montville-Haddam Neck line out of service, March 10, 2005; and
- Partial equipment alignment of auxiliary steam system during power supply
replacement, March 21, 2005.
b. Findings
No findings of significance were identified.
2. Complete System Walkdown. (71111.04S - One Unit 2 Sample and One Unit 3
Sample)
a. Inspection Scope
Unit 2
The inspectors completed a detailed review of the alignment and condition of the Unit 2
control room air conditioning (CRAC) system. The inspectors conducted a walkdown of
the system to verify that the critical portions, such as valve positions, switches, control
room heat loads and breakers, were in accordance with procedures and any
discrepancies that may have had an effect on operability were resolved.
The inspectors also conducted a review of outstanding maintenance work orders to
verify that the deficiencies did not significantly affect the CRAC system function. The
inspectors discussed system health with the system engineer and reviewed the
condition report database to verify that equipment alignment problems were being
identified and appropriately resolved. Documents reviewed during the inspection are
listed in the Attachment.
Unit 3
The inspectors completed a detailed review of the alignment and condition of the Unit 3
post accident control room ventilation envelope. The inspectors conducted a complete
control room verification and/or walkdown of critical system functions, alignments, valve
positions, switches, and breakers, to ensure correct alignment in accordance with
procedures and to determine if any identified conditions affected operability. The
inspectors also conducted a review of outstanding maintenance work orders to verify
Enclosure
5
that existing deficiencies did not significantly affect the system operability. The
inspectors reviewed control room ventilation system health documents and related
condition reports to verify that equipment alignment, temporary modifications, operator
workarounds and other problems were being identified and appropriately resolved.
Documents reviewed during the inspection are listed in the Attachment.
b. Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05)
1. Quarterly Sample Review (71111.05Q - Six Unit 2 Samples and Six Unit 3 Samples)
a. Inspection Scope
The inspectors performed twelve walkdowns of fire protection areas during the
inspection period. The inspectors reviewed Dominion's fire protection program to
determine the required fire protection design features, fire area boundaries, and
combustible loading requirements for the selected areas. The inspectors walked down
those areas to assess Dominion's control of transient combustible material and ignition
sources. In addition, the inspectors evaluated the material condition and operational
status of fire detection and suppression capabilities, fire barriers, and any related
compensatory measures. The inspectors then compared the existing conditions of the
inspected fire protection areas to the fire protection program requirements to ensure all
program requirements were being met. Documents reviewed during the inspection are
listed in the Attachment. The fire protection areas reviewed included:
Unit 2
- West Pipe Penetration, -5' Elevation (Fire Area A-8C);
- West Electric Penetration, 14'6" Elevation (Fire Area A-8D);
- Upper 4160 Volt Switchgear Room - Turbine Building, 31'-6" Elevation (Fire Area
T-7);
- Lower 4160 Volt Switchgear Room - Turbine Building, 56'-6" Elevation (Fire Area
T-10);
- A and B Motor Driven Auxiliary Feedwater Pump Cubicle - Turbine Building,
1'-6" Elevation (Fire Area T-3); and
- Turbine Driven Auxiliary Feedwater Pump Cubicle - Turbine Building, 1'-6"
Elevation (Fire Area T-4).
Unit 3
- Instrument Rack Room - Control Building, 47'-6" Elevation - (Fire Area CB-11,
Zones A and B);
- North Floor Area - Auxiliary Building, 4'-6" Elevation - (Fire Area AB-1, Zone A);
- South Floor Area - Auxiliary Building, 4'-6" Elevation - (Fire Area AB-1, Zone B);
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- East Floor Area, 4'-6" Elevation - (Fire Area ESF-4, Zone N/A);
- Southeast Floor Area - Auxiliary Feed Pump Cubicle, 4'-6" & 24'-6" Elevation -
(Fire Area ESF-5, Zone N/A); and
- South Air Conditioning Unit Cubicle- Engineered Safety Features Building, 36'-6"
Elevation - (Fire Area ESF-11, Zone N/A).
b. Findings
No findings of significance were identified.
2. Annual Fire Drill Observation (71111.05A - One Unit 3 Sample)
a. Inspection Scope
Unit 3
The inspectors observed personnel performance during a fire brigade drill on March 16,
2005, to evaluate the readiness of station personnel to prevent and fight fires. The drill
simulated a fire on the Turbine Deck in the Unit 3 Turbine Building. The inspectors
observed the fire brigade members using protective clothing, turnout gear, and
self-contained breathing apparatus and entering the fire area in a controlled manner.
The inspectors also observed the fire fighting equipment brought to the fire scene to
evaluate whether sufficient equipment was available to effectively control and extinguish
the simulated fire. The inspectors evaluated whether the permanent plant fire hose lines
were capable of reaching the fire area and whether hose usage was adequately
simulated. The inspectors observed the fire fighting directions and communications
between fire brigade members. The inspectors verified that the pre-planned drill
scenario was followed and reviewed the post drill critique to ensure that the drill
objectives were satisfied and that any drill weaknesses were discussed.
b. Findings
No findings of significance were identified.
1R06 Flood Protection Measures (71111.06)
Internal Flooding Inspection (One Unit 3 Sample)
a. Inspection Scope
The inspectors reviewed one sample of flood protection measures for equipment in the
safety related room listed below. This review was conducted to evaluate Dominions
protection of the enclosed safety-related systems from internal flooding conditions. The
inspectors performed a walkdown of the area and reviewed the Final Safety Analysis
Report, the internal flooding evaluation and related documents. The inspectors
compared the as-found equipment and conditions to ensure they remained consistent
with those indicated in the design basis documentation, flooding mitigation documents,
Enclosure
7
and risk analysis assumptions. Documents reviewed during the inspection are listed in
the Attachment.
Unit 3
- B Residual Heat Removal (RHR) Cubicle.
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance (71111.07 - One Unit 2 Sample and Five Unit 3 Samples)
1. Annual Heat Sink Performance (71111.07A - One Unit 2 Sample and One Unit 3
Sample)
a. Inspection Scope
The inspectors reviewed two samples of safety related heat exchanger testing to identify
any degraded performance or potential for common cause problems that could increase
plant risk. The inspectors reviewed the results of inspections performed in accordance
with Dominion procedures. The inspectors reviewed the inspection results against the
acceptance criteria contained within the procedure, and verified that all acceptance
criteria had been satisfied. The inspectors also reviewed the Final Safety Analysis
Report to ensure that heat exchanger inspection results were consistent with the design
basis. The inspectors verified that adverse conditions identified by Dominion were
appropriately entered into Dominion's corrective action program. Documents reviewed
during the inspection are listed in the Attachment.
Unit 2
- A Reactor Building Closed Cooling Water System Heat Exchanger.
Unit 3
- Engineered Safety Features Building Ventilation Heat Exchanger.
b. Findings
No findings of significance were identified.
2. Biennial Heat Sink Performance (71111.07B - Four Unit 3 Samples)
a. Inspection Scope
Based on a plant specific risk assessment, resident inspector input, and the last biennial
inspection, the inspector selected the B RPCCW, B containment recirculation spray
Enclosure
8
system (RSS), B emergency diesel generator jacket water (JW), and B EDG
intercooler HXs for this biennial review. Each of these HXs transfers its heat load
directly to the SW system. The SW system was designed to supply cooling water from
Long Island Sound (the ultimate heat sink) to various heat loads to ensure a continuous
flow of cooling water to systems and components necessary for plant safety both during
normal operation and under abnormal or accident conditions.
The inspector reviewed Dominions inspection, cleaning, chemical control, and
performance monitoring methods and frequency for the selected components to ensure
alignment with Dominions response to Generic Letter 89-13, Service Water System
Problems Affecting Safety-Related Equipment. The inspector compared surveillance
test and inspection data to the established acceptance criteria to verify that the results
were acceptable and that operation was consistent with design. The inspector walked
down the selected HXs, the sodium hypochlorite system, and the SW system to assess
the material condition of these systems and components. In addition, the inspector
walked down control room instrumentation panels, viewed several SW intake inspection
videos, reviewed work order history for the selected HXs, and discussed system health
with the respective system engineers.
The inspector also reviewed a sample of condition reports (CRs) related to the selected
HXs and the SW system to ensure that Dominion was appropriately identifying,
characterizing, and correcting problems related to these essential systems and
components. Documents reviewed during the inspection are listed in the Attachment.
b. Findings
Introduction. The inspector identified a Green non-cited violation of 10 CFR Part 50,
Appendix B, Criterion XVI, Corrective Action, for Dominions failure to take prompt and
appropriate corrective actions to evaluate and correct a degraded condition associated
with the divider plate for all three RPCCW HXs.
Description. On May 20, 2003, engineering identified a bent divider plate in the B
RPCCW HX. The divider plate was deflected approximately 1/2 inch from centerline to
the outlet SW side. The divider plate separates the inlet SW flow from the outlet SW
flow and ensures that the incoming SW flow is routed to the tube side of the two-pass
RPCCW HXs. Engineering initiated CR-03-04924 that included actions to straighten the
divider plate, inspect the A and C RPCCW HXs, modify their HX inspection form to
include a divider plate inspection step, and to develop and implement a modification to
strengthen the divider plate.
On June 9, 2003, engineering found a deflected divider plate in the C RPCCW HX and
a deflected divider plate in the A RPCCW HX on June 25, 2003. Engineering
determined that high differential pressure (d/p) across the divider plates due to tube
plugging caused the plates to bend. In addition, Engineering reviewed the May 2003
operating experience (OE) information from D.C. Cook that discussed catastrophic
failure of a component cooling water HX divider plate due to repeated divider plate
deflections (OE16319). Based on the above information, engineering proposed a
Enclosure
9
modification to stiffen the RPCCW HX divider plates through their Engineering Level of
Effort (LOE) process. Maintenance used mechanical means to straightened the divider
plate in each HX; however, engineering found the divider plate deflected again on
subsequent HX inspections (A HX on May 23, 2004; B HX on September 9, 2004
and December 1, 2004).
The inspector noted that engineering had treated each of the six instances of deflected
divider plates discovered since May 2003 in a broke-fixed manner without evaluating
the degraded condition for continued operability of the RPCCW HXs. Given the
degraded condition of the divider plates deflecting over time and potentially causing
fatigue failure of the divider plate welds, and the industry OE documenting the failure of
a similar HX under operating conditions, the inspector determined that engineering
should have promptly evaluated and documented their basis for a reasonable
expectation of operability.
Engineering designated the divider plate stiffening modification as a low priority item.
The inspector noted that Engineering extended the due date for the associated LOE
review seven times since August 2003, and in March 2004 deferred the activity out to
2005. Presently, the Engineering portion of the modification package is scheduled to be
completed by September 2005. The inspector determined that the timeliness of
Dominions corrective actions were not commensurate with the potential safety
significance of the issue. The inspector found no evidence that Dominion evaluated the
effects on operability or the significance of the degraded condition when extending the
corrective actions well beyond their first opportunity to correct.
The inspector also identified that Dominion failed to implement their corrective action
assignment (CR-03-04924/03003369-05) to revise the SW cooled HX inspection form,
although they closed out this action as complete in September 2003 (CR-05-01233).
On February 10, 2005, Engineering initiated CR-05-01281 to evaluate additional
information concerning the RPCCW HX divider plates. Subsequently, on February 25,
Engineering initiated CR-05-01767 to evaluate an elevated RPCCW HX DP (23 psid as
compared to a 20 psid design) observed by the RPCCW system engineer during two
SW pump operation during SW surveillance testing. Engineering performed an
operability determination (MP3-004-05) and concluded that the RPCCW HXs were
operable but not fully qualified. Engineerings determination was based on recent HX
inspections, a structural evaluation of the divider plate (conservatively assuming 35
psid), and a flow and heat transfer analysis (including surveillance testing trends).
Engineering also documented their evaluation of OE16319 in CR-05-01767.
Engineering determined that the RPCCW HXs would be able to remove the required
heat loads during accident events.
Analysis. The inspector considered Dominions failure to take timely and adequate
corrective actions for the degraded RPCCW HX divider plates a performance deficiency
since Dominions corrective action program should correct conditions adverse to quality
in a timely manner. Given the repeated nature of the adverse condition (deflected
divider plates) and industry OE relative to an in-service failure, the deficiency was
Enclosure
10
reasonably within Dominions ability to appropriately evaluate and correct prior to
February 2005.
The inspector determined that the issue was more than minor because it was
associated with the Mitigating Systems cornerstone attribute for equipment performance
and potentially affected the objective to ensure the availability and reliability of the
RPCCW HXs. The RPCCW system mitigates initiating events as it supplies cooling to
the residual heat removal pumps and HXs in the shutdown cooling mode. The
degraded RPCCW HX divider plates, if left uncorrected, would result in a more
significant safety concern should a divider plate fail catastrophically while in service.
The inspector determined the issue to be very low safety significance (Green) using the
Phase 1 SDP worksheet for at power situations for the Mitigating Systems cornerstone.
This was because the finding was a qualification deficiency confirmed not to result in
loss of function. The issue was similarly of very low risk in the Initiating Events
cornerstone because the finding did not increase the likelihood of a reactor trip or a loss
of SW event.
The finding was associated with the cross-cutting area of PI&R based on Dominions
inadequate evaluation and untimely corrective actions for this identified deficiency
potentially affecting the RPCCW HXs.
Enforcement. Code of Federal Regulations 10 CFR Part 50, Appendix B, Criterion
XVI, Corrective Action, requires, in part, that conditions adverse to quality are promptly
identified and corrected. Contrary to this requirement, Dominion failed to take prompt
and appropriate corrective actions to address a condition adverse to quality.
Specifically, since May 2003, Dominion failed to promptly evaluate and correct a
degraded condition associated with the divider plate for all three RPCCW HXs.
However, because of the very low safety significance and because the issue was
entered into Dominions corrective action program (CR-05-01281 & CR-05-01767), this
finding is being treated as a non-cited violation, consistent with Section VI.A of the
Enforcement Policy, issued May 1, 2000 (65FR25368). (NCV 05000423/2005002-02)
1R11 Licensed Operator Requalification Program (71111.11Q - Two Unit 2 Samples and One
Unit 3 Sample)
a. Inspection Scope
The inspectors observed two samples of Unit 2 licensed operator requalification training
on March 30, 2005, and March 31, 2005. The inspectors observed one sample of Unit 3
licensed operator requalification training on February 1, 2005. The inspectors verified
that the training evaluators adequately addressed that the applicable training objectives
had been achieved. Documents reviewed during the inspection are listed in the
Attachment.
b. Findings
No findings of significance were identified.
Enclosure
11
1R12 Maintenance Effectiveness (71111.12)
Routine Maintenance Effectiveness Inspection (71111.12Q - Two Unit 2 Samples and
Two Unit 3 Samples)
a. Inspection Scope
The inspectors reviewed four samples of Dominion's evaluation of degraded conditions,
involving safety related structures, systems and/or components (SSC) for maintenance
effectiveness during this inspection period. The inspectors reviewed licensee
implementation of the Maintenance Rule (MR), 10 CFR 50.65, and verified that the
conditions associated with the referenced CRs were appropriately evaluated against
applicable MR functional failure criteria as found in licensee scoping documents and
procedures. The inspectors also discussed these issues with the system engineers and
maintenance rule coordinators to verify that they were appropriately tracked against
each system's performance criteria and that the systems were appropriately classified in
accordance with MR implementation guidance. Documents reviewed during the
inspection are listed in the Attachment. The following conditions were reviewed:
Unit 2
- Failure of B51 Motor Control Center Air Conditioning System (CR-04-11119);
and
- Facility 2 Control Room Air Conditioning failure (CR-05-00638).
Unit 3
- Station Blackout Diesel Uninterruptible Power Supply Battery Failed Voltage
Testing (CR-05-00127); and
- Engineered Safety Features Building Ventilation Filter Clogged Due to Snow
(CR-05-00617).
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13 - Four Unit 2
Samples and Six Unit 3 Samples)
a. Inspection Scope
The inspectors reviewed ten samples of the adequacy of maintenance risk assessments
of emergent and planned activities on Unit 2 and Unit 3 during the inspection period.
The inspectors utilized the Equipment Out of Service quantitative risk assessment tool
to evaluate the risk of the plant configurations and compared the results to Dominion's
stated risk. The inspectors verified that Dominion entered appropriate risk categories
and implemented risk management actions as necessary. Documents reviewed during
Enclosure
12
the inspection are listed in the Attachment. The inspectors verified the conduct and
adequacy of scheduled maintenance risk assessments for plant conditions affected by
the following maintenance and testing activities:
Unit 2
- Work schedule for the week of January 17, 2005, including maintenance and
testing on the containment sump/shutdown cooling heat exchanger valve;
- Work schedule for the week of February 28, 2005, including maintenance on the
A circulating water bay;
- Work schedule for the week of March 7, 2005, including maintenance and
testing on emergency safeguards actuation system, reserve station service
transfer, and sequencer; and
- Work schedule for the week of March 14, 2005, including maintenance and
testing on the B high pressure safety injection pump.
Unit 3
- Work schedule for the week of January 3, 2005, including maintenance and
testing on the A circulating water pump;
- Emergent risk assessment of "A" EDG sequencer inoperability on January 21,
2005;
- Work schedule for the week of January 31, 2005, including maintenance and
testing on the A circulating water bay outage, switchyard breaker, and C
service water strainer;
- Work schedule for the week of February 28, 2005, including maintenance and
testing on the B EDG;
- Work schedule for the week of March 21, 2005, including maintenance and
testing on the supplementary leak collection and release system, quench spray
system pump, and power operated relief valves relays; and
- Work schedule of the week of March 28, 2005, including maintenance and
testing on A safety injection pump, A train ESF air conditioning, and A train
emergency diesel fuel oil pump
b. Findings
No findings of significance were identified.
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events (71111.14 -
Three Unit 2 Samples and Two Unit 3 Samples)
a. Inspection Scope
The inspectors reviewed five samples of events that demonstrated personnel
performance in coping with non-routine evolutions and transients on Unit 2 and Unit 3.
The inspectors observed operations in the control room and reviewed applicable
operating and alarm response procedures, technical specifications, plant process
Enclosure
13
computer indications, and control room shift logs to evaluate the adequacy of
Dominion's response to these events. The inspectors also verified the events were
entered into the corrective action program to resolve identified adverse conditions.
Documents reviewed during the inspection are listed in the Attachment.
Unit 2
- On January 12, 2005, the inspectors observed Dominions actions following the
identification of a defective cable insulation on one of the two offsite power
supplies to Unit 2. During unrelated maintenance, Dominion observed a partial
phase to phase ground between the A and C phases of the backup offsite
power supply to Unit 2. This fault also prevented the station blackout diesel from
supplying Unit 2 loads. Dominion entered the appropriate Technical
Specification, de-energized the cable, and completed repairs. Additionally,
Dominion took appropriate actions to minimize risk to the plant while the power
supply was unavailable.
- On January 14, 2005, Operations personnel responded to a fire in an electrical
panel in the Unit 2 turbine building. Dominion declared an Unusual Event since
the fire lasted greater than 15 minutes and was located in an area of concern for
safe shutdown (the Unit 2 turbine building). The resident inspectors responded
and Region I staffed the Incident Response Center. A special inspection team
was chartered to conduct an investigation and evaluation of this event which will
be documented in Inspection Report 05000336/2005009.
- On January 22, 2005, Operations personnel notified the inspectors regarding
their actions taken in response to an impending snowstorm. See Unit 3
discussion for details.
Unit 3
- On January 20, 2005, Operations personnel responded to the unexpected start
of the A auxiliary building filter fan and an A EDG sequencer alarm.
Operations bypassed the A EDG sequencer and entered Technical
Specification 3.3.2, Engineered Safety Features Actuation System
Instrumentation, which specifies a six hour shutdown action statement.
Instrumentation and Controls personnel commenced troubleshooting and
determined that the A EDG sequencer circuitry was not resetting an automatic
test signal. An operability determination was generated that determined the
function of the sequencer was not impacted. The EDG sequencer automatic
testing function was removed from service by placing the EDG sequencer
automatic tester switch in RESET and TS 3.3.2 was exited.
- On January 22, 2005, Operations personnel notified the inspectors of an
impending snowstorm and of the actions they had taken in preparation for the
snowstorm. These actions included notifying Site Emergency Response
Organization members to ensure each position had staffing available (two people
Enclosure
14
deep) who lived between the I-95 bridges. This ensured their ability to respond
to the plant even if the bridges were closed. On January 23, 2005, Operations
personnel notified the inspectors that they had entered Technical Specification
3.0.3, Limiting Condition For Operation, due to snow loading which affected the
inlets of both trains of emergency safeguards features (ESF) building ventilation.
Maintenance personnel were called in, the filter elements were changed out, and
the ESF ventilation was restored in approximately one hour.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15 - Four Unit 2 Samples and Six Unit 3 Samples)
a. Inspection Scope
The inspectors reviewed ten operability determinations associated with degraded or
non-conforming conditions to ensure that operability was justified and that mitigating
systems or those affecting barrier integrity remained available and no unrecognized
increase in risk had occurred. The inspectors also reviewed compensatory measures to
ensure that the compensatory measures were in place and were appropriately
controlled. The inspectors reviewed licensee performance to ensure all related TS and
Final Safety Analysis Report (FSAR) requirements were met. The inspectors reviewed
the following degraded or non-conforming conditions:
Unit 2
- Failure of the Facility 2 Control Room Air Conditioning system (CR-05-00638);
- Loss of Remote Shutdown Panel Steam Generator Pressure Indication
(CR-05-01336);
- Failure of the Pressurizer Power Operated Relief Valve acoustic monitor and tail
pipe temperature indication (CR-05-00748); and
- "B" Charging Pump/Train metallic noise (CR-05-02350).
Unit 3
- A Service Water Header Brazed Joint Leak (MP3-002-05);
- Non-Safety Related Valve Seat Material Used in a Safety Related Application
(CR-05-01213);
- A Hydrogen Recombiner Leakage (CR-05-01689);
- A Emergency Generator Loading Sequence Autotest Circuit Failed, Resulting
in Auto Start of 3HVR*FN6A (CR-05-00550)
- Station Blackout Failed Battery Surveillance (CR-05-00127); and
- Leakage Detection Systems Unidentified Leakage Sump Pump (CR-05-02751).
Enclosure
15
b. Findings
No findings of significance were identified.
1R16 Operator Work-Arounds (71111.16)
1. Selected Operator Work-arounds (One Unit 2 Sample)
a. Inspection Scope
The inspectors reviewed one risk significant operator work-around (OWA) for Unit 2
during the inspection period. The inspectors evaluated the condition to determine if
there was any effect on human reliability in responding to an initiating event or any
adverse effects on the function of mitigating systems. The work-around was also
reviewed to ensure compliance with licensee documents which administratively control
OWAs. Documents reviewed during the inspection are listed in the Attachment.
- Inoperable Automatic Steam Dump Valve Pressure Control Function
b. Findings
No findings of significance were identified.
2. Cumulative Effects of Operator Work-Arounds (One Unit 2 Sample and One Unit 3
Sample)
a. Inspection Scope
The inspectors reviewed the current listing of active OWAs for Millstone Unit 2 and Unit
3. The review was conducted to verify that Dominion procedures and practices provided
the necessary guidance to plant personnel, that the cumulative effects of the known
OWAs were addressed, and that the overall impact on the affected systems was
assessed by Dominion. The inspectors independently assessed the cumulative impact
of known OWAs to determine if they adversely affected the ability of plant operators to
implement emergency procedures, respond to plant transients, or perform normal
functions within the expectations of the established Dominion risk models. In support of
this assessment, the inspectors reviewed various condition reports regarding OWAs and
verified that OWAs were being identified, tracked, and resolved in Dominion's corrective
action program.
b. Findings
No findings of significance were identified.
Enclosure
16
1R19 Post-Maintenance Testing (71111.19 - Five Unit 2 Samples and Six Unit 3 Samples)
a. Inspection Scope
The inspectors reviewed eleven samples of PMTs during this inspection period. The
inspectors reviewed these activities to determine whether the PMT adequately
demonstrated that the safety-related function of the equipment was satisfied given the
scope of the work specified and that operability of the system was restored. In addition,
the inspectors evaluated the applicable test acceptance criteria to verify consistency
with the associated design and licensing bases, as well as Technical Specification
requirements. The inspectors also verified that conditions adverse to quality were
entered into the corrective action program for resolution. Documents reviewed during
the inspection are listed in the Attachment. The following maintenance activities and
their post maintenance tests were evaluated:
Unit 2
- "A" Train of the Auxiliary Feedwater system (M2-00-19686);
- D Instrument Air compressor (DM2-00-0363-04);
- Containment Radiation Monitor (RM-8123) (M2-04-06866);
- UAC4 Transformer Replacement (M2-03-00711); and
- "B" Charging Pump/Train Metallic Noise (M2-05-02151).
Unit 3
- Auxiliary feed pump cubicle ventilation intake filter replacement (M3-05-010226);
- A EDG Sequencer (M3-05-04081);
- BYS*CHGR7 Battery Charger Leakage Test (M3-01-09552);
- ACUS2A ESF Air Conditioning Maintenance (M3-04-15984);
- A EDG Neutral Breaker Preventive Maintenance (M3-02-16737); and
- Hydrogen Recombiner (M3-05-04144)
b. Findings
Unit 2
No findings of significance were identified.
Unit 3
1. A Emergency Diesel Generator Neutral Breaker
Introduction. The inspectors identified a green NCV of Appendix B, Criterion XI, Test
Control, for the failure to adequately implement PMT procedures for restoring the A
EDG to service following maintenance of the neutral breaker.
Enclosure
17
Description. On March 1, 2005, Dominion conducted maintenance and doble testing of
the A EDG neutral breaker. After Operations racked down the breaker, the
electricians removed the breaker from its cubicle. The Maintenance Department
conducted planned maintenance on the breaker and then performed doble testing.
After completing doble testing, the Maintenance Department returned the breaker to its
cubicle in the seismic position (racked out), and turned the breaker over to Operations
for final post-maintenance testing and restoration.
Operations racked in the breaker in accordance with OP 3370A, Electrical Breaker
Procedure. After the breaker was racked in, Operations noted that the red light on front
of the EDG neutral breaker panel did not light as expected. Operations confirmed that
the breaker closed electrically and assessed that the close and trip fuses were not
blown. Additionally, the plant equipment operator stated that the red flag properly
indicated the breaker was closed. Satisfied the breaker was closed, Operations
returned the EDG to operable status and exited the EDG technical specification. The
oncoming shift investigated and determined the red light was not lit because there was a
problem with the neutral breaker trip circuit. An auxiliary circuit contact did not make up
properly when the breaker was racked in. Operations declared the EDG inoperable and
re-entered the EDG technical specification.
The inspectors reviewed the work order and determined Operations did not adequately
implement the post-maintenance test procedure. The post-maintenance test directed by
the work order was to cycle the breaker in accordance with MP-20-WP-GDL40,
Attachment 4. Specifically, MP-20-WP-GDL40, paragraph 2.3.6, stated in part, Direct
performance of PMT as described in Work Order/PMT Plan, to include the following, as
appropriate: PMT results reviewed against the acceptance criteria. Attachment 4
stated that acceptance criteria for electrical breakers included verifying local/remote
indications function properly, and correctly indicate component position/status. Despite
this acceptance criteria, Dominion signed the PMT as satisfactory and restored the EDG
neutral breaker to an operable status although the acceptance criteria was not met.
Specifically, the neutral breaker trip circuitry indication did not indicate as expected.
This resulted in restoration of the A EDG with the neutral breaker trip circuitry
Additionally, the inspectors noted a deficiency in OP 3370A, Electrical Breaker
Procedure, which was used for racking and testing electrical breakers. Although
Operations used this procedure to implement the PMT requirements, the procedure
lacked steps to ensure that all indications were properly checked for the racking of
breakers.
Analysis. The performance deficiency was Dominions failure to adequately implement
testing procedures for restoring the A EDG to service following maintenance and doble
testing of the neutral breaker. Dominion returned the EDG to an operable status
although the position indication for the neutral breaker did not indicate in accordance
with the acceptance criteria. This resulted in restoration of the EDG with the neutral
breaker inoperable. This issue was more than minor because it was associated with the
reliability of the A EDG. On phase-to-ground faults initiating in the emergency system,
Enclosure
18
the generator neutral breaker trips first to attempt to isolate the fault while continuing to
supply vital loads powered from the emergency bus. Thus, during an event requiring
emergency diesel generator operation with the neutral breaker inoperable, a ground on
the emergency bus or diesel could cause the diesel to trip prematurely. The inspectors
determined that the finding was of very low safety significance (Green) through
performance of a Phase 1 SDP in accordance with IMC 0609, Appendix A, "Significance
Determination of Reactor Inspection Findings for At-Power Situations." Specifically, this
finding did not involve a design or qualification deficiency, represent an actual loss of
safety function of the A EDG, or involve seismic, flooding, or severe weather initiating
events.
Enforcement. Code of Federal Regulations 10 CFR Part 50, Appendix B, Criterion XI,
Test Control, states in part, A test program shall be established to assure that all
testing required to demonstrate that structures, systems, and components will perform
satisfactorily in service is identified and performed in accordance with written test
procedures which incorporate the requirements and acceptance limits contained in
applicable design documents. Contrary to this requirement, on March 1, 2005,
Dominion failed to implement testing procedures for returning the A EDG neutral
breaker to an operable status following completion of electrical breaker maintenance.
This violation has been determined to have a very low safety significance and is in
Dominion's corrective action program as CR-05-03569. Therefore, this violation is being
treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy
2. Hydrogen Recombiner
Introduction. A non-cited violation of TS 3.4.6.2, Electric Hydrogen Recombiners, was
identified for the failure to perform post maintenance tests of the hydrogen recombiner
following intrusive testing on the piping system which disturbed piping joints.
Subsequent testing found leakage from the system which would have affected
operability of the A hydrogen recombiner during a design basis event.
Description. On December 2, 2004, Dominion performed maintenance on the A
hydrogen recombiner which included disassembly and reassembly of mechanical joints.
Following the maintenance, the associated TSs were exited and the system was
returned to service without performing a post maintenance leak test. Subsequently, on
February 22, 2005, Dominion performed maintenance on the A hydrogen monitor.
Following the maintenance, the system was returned to service and the TS action
statement was exited without performing the required post-maintenance test. Dominion
then determined that pipe fittings for the A hydrogen monitor had been disassembled
and, therefore, a PMT was required to show the joints were reassembled correctly.
Since this test was required to assure operability of the system, Dominion declared the
hydrogen monitor inoperable and re-entered the associated TS. The A hydrogen
recombiner was also declared inoperable in order to support the test boundaries for the
Enclosure
19
The inspectors observed that a leak tightness surveillance test was conducted to verify
the integrity of the disturbed joints for the hydrogen monitor. The test results found that
there was an approximately 11,000 standard cubic centimeter per minute (SCCM) leak
on the system. This exceeded the 2000 sccm limit established in the surveillance.
Dominion investigation found that the leak was not on a mechanical joint disturbed
during the February 22, 2005, maintenance. A review of previous maintenance activities
determined that work performed on December 2, 2004, disturbed the joint that had
failed and the leaking joints remained unidentified until a post-maintenance test was
conducted on February 23, 2005.
The inspectors determined that the leak would impact both the integrity of containment
and operability of the A hydrogen recombiner. When the hydrogen recombiner would
be placed in service following a design basis event, the air inside containment would
have had an open path to atmosphere through the hydrogen recombiner room and
ventilation train via the loose mechanical joints. As a result, radiation levels inside the
A hydrogen recombiner room would increase and cause the ventilation radiation
monitor to alarm which would shut down the hydrogen recombiner. Operators following
their alarm response procedure would then isolate the recombiner which would stop the
leak.
Analysis. The performance deficiency associated with this issue was that Dominion
failed to adequately perform post-maintenance testing to ensure incorrect maintenance
activities were identified prior to declaring the A hydrogen recombiner system
Operable, exiting TS, and returning the system to service. Traditional enforcement does
not apply to this issue because there were no actual safety consequences, impacts on
the NRCs ability to perform its regulatory function, or willful aspects to the violation.
This issue was more than minor because it is associated with the Barrier Integrity
cornerstone of configuration control for containment boundary preservation and
ensuring containment design parameters are maintained. The failure to specify
adequate PMT resulted in loose mechanical joints in the system not being detected
which would have allowed an open pathway to atmosphere from containment.
Additionally, Dominion postulated that the post accident leakage from these joints would
have caused a radiation monitor alarm which would have isolated the A hydrogen
recombiner during an event. This condition existed from December 2, 2004, through
March 1, 2005.
The inspectors performed a Phase 1 SDP in accordance with Inspection Manual
Chapter (IMC) 0609, Appendix A, "Significance Determination of Reactor Inspection
Findings for At-Power Situations" which required that an Appendix H, Containment
Integrity Significance Determination Process of IMC 0609 be used because there was a
direct path from containment to atmosphere. The Appendix H analysis for large dry and
sub-atmospheric containment types determined that, since the leak was of a small
enough magnitude (11,000 SCCM), the entire containment atmosphere would not leak
to the environment over a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period. Therefore, the risk of this finding was
determined to be of very low safety significance (Green).
Enclosure
20
Enforcement. Technical Specification 3.6.4.2, Electric Hydrogen Recombiners,
requires that two independent hydrogen recombiner systems remain Operable.
Contrary to this, on December 2, 2004, Dominion exited the associated TS action
statement with an inoperable system. As a result, Dominion did not comply with the
required TS action statement which states restore the inoperable system to Operable
status within 30 days or be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, an action
required on January 1, 2005. Dominion continued in this condition until March 1, 2005,
when the system was repaired, tested, and restored to an Operable status. This
violation has been determined to be of very low safety significance and was entered into
Dominion's corrective action program (CR-05-01713 and CR-05-03896). Therefore, this
violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC
Enforcement Policy. (NCV 05000423/2005002-04).
1R22 Surveillance Testing (71111.22 - Five Unit 2 Samples and Five Unit 3 Samples)
a. Inspection Scope
The inspectors reviewed ten samples of surveillance activities to determine whether the
testing adequately demonstrated the equipments' operational readiness and its ability to
perform its intended safety-related function. The inspectors attended pre-job briefs,
verified that selected prerequisites and precautions were met and that the tests were
performed in accordance with the procedural steps. Additionally, the inspectors
evaluated the applicable test acceptance criteria to verify consistency with associated
design basis, licensing bases and Technical Specification requirements, and to ensure
that the applicable acceptance criteria were satisfied. The inspectors also verified that
conditions adverse to quality were entered into the corrective action program for
resolution. Documents reviewed during the inspection are listed in the Attachment. The
following surveillance activities were evaluated:
Unit 2
- B Containment Spray (CS) Pumps IST (SP-2606B);
- AFW/Fire System Cross Connects 2-Fire-94A/B/C Testing (SP-2605R).
Unit 3
- Steam Generator Water Level Channel Calibration Channel 3 (SP-3444A01);
- Sweep of Train A RHR to Refueling Water Storage Tank (SP-3610A.3);
- A Quench Spray Pump Operational Readiness Test (SP-3609.1);
- B RPCCW Operational Test IST (SP-3630A.5); and
- RHR A Pump Operational Readiness Test IST (SP-3610A.1).
b. Findings
Enclosure
21
No findings of significance were identified.
1R23 Temporary Plant Modifications (71111.23 - One Unit 2 Sample and One Unit 3 Sample)
a. Inspection Scope
The inspectors reviewed two samples of temporary modifications to verify that the
temporary modifications did not affect the safety function of important safety systems.
The inspectors reviewed the temporary modifications and their associated 10 CFR 50.59
screening against the FSAR and Technical Specifications to ensure the modifications
did not affect system operability or availability. Documents reviewed during the
inspection are listed in the Attachment.
Unit 2
- Installation and operation of compensatory cooling to East 480 Volt Switchgear
(OP-2315D)
Unit 3
- B Circulating Water Pump Proceduralized Temporary Modification (OP-3225A).
b. Findings
Unit 2
Introduction. A green self-revealing NCV of TS 6.8.1, Procedures and Programs, was
identified for the failure to correctly install temporary cooling to the East 480 volt
switchgear room. Dominion failed to perform all required steps in the procedure
resulting in insufficient cooling to the room.
Description. On January 12, 2005, Dominion installed temporary cooling to the East 480
volt switchgear room. The safety-related cooler in the East 480 volt switchgear room
was removed from service to perform preventive maintenance. Compensatory cooling
measures to the switchgear room were installed per Operating Procedure (OP) 2315D -
"Vital Electric Switchgear Room Cooling". The temporary cooling system consisted of
two Appendix R air blowers and a ventilation lineup which including positioning room
doors and securing fans external to the room. The procedure was completed and the
vital switchgear cooling system was removed from service. Subsequent to the
installation of the equipment, the system engineer walked down the compensatory
measures installation and found that door 203-31-008 was closed. This door was
required to be open per the procedure to provide a discharge path for the compensatory
fans. The engineer reported the discrepancy to the control room. The switchgear was
declared inoperable until the door was opened and the complete lineup verified.
Enclosure
22
The inspectors noted that prior to this failure Dominion had taken numerous corrective
actions to ensure proper implementation of the compensatory cooling. Non-cited
Violation 05000336/2003010-03 discussed a similar violation related to the installation of
this equipment and subsequent corrective actions. More recently, Dominion required
that the system engineer review the procedure with the Operating crew to ensure the
system was properly installed to address confusion with the use of the procedure. In
this case, the engineer discussed the procedure with the implementing operations crew
over the phone. Procedure step 4.9.9.c states: "Open the following doors: Door
203-31-007, 203-31-008, 105-36-112. As required, station security guards and fire
watches". The discussion between the Operations crew and the engineer determined
that operation of these doors was "as required" and, therefore, only door 203-45-003
was opened. The inspectors determined that all the doors were required to be opened
and the statement "as required" only applied to the stationing of security guards and fire
watches. Dominion's corrective actions include a revision to the procedure to remove all
"as required statements.
Analysis. The performance deficiency associated with this issue was that Dominion
failed to implement procedures to correctly install temporary cooling to the East 480 volt
switchgear. The finding was more than minor because, if left uncorrected, one division
of the 480 volt vital AC system (480VACS) may not be available to respond to design
basis events due to increasing room temperatures exceeding the switchgear design
temperature limits and subsequent failure of the switchgear In addition, the equipment
performance attribute of the mitigating systems cornerstone and the objective of
ensuring the availability of systems that respond to initiating events to prevent
undesirable circumstances was affected, since the 480VACS provided vital power to a
number of safety-related systems designed to mitigate design basis events. The finding
also affected the containment structures, systems, and components and barrier
performance attribute of the barrier integrity cornerstone and the objective of providing
reasonable assurance that physical design barriers protect the public from radionuclide
releases caused by accidents or events, because hydrogen recombiners and
containment air recirculation fans are also powered from the 480VACS. Finally, the
finding impacted the equipment performance attribute of the initiating events
cornerstone objective of limiting the likelihood of those events that upset plant stability
since temperature sensitive electro hydraulic control (EHC) equipment was located in
this room. The failure of this equipment would result in a turbine trip. Traditional
enforcement did not apply to this issue because there were no actual safety
consequences, impacts on the NRC's ability to perform its regulatory function, or willful
aspects to the violation.
Manual Chapter 0609, Appendix A , was used to determine the risk associated with this
finding. Phase 1 of the Appendix requires that a Phase 2 analysis be performed
because three cornerstones were affected. The entry into the tables associated with the
Phase 2 analysis assumed that the 480VACS is inoperable. However, this finding
concerned the support room cooling system for the 480VACS, therefore, an evaluation
of the impact on this system due to the degraded cooling system was performed. Since
the actual room temperature did not exceed 104 degrees Fahrenheit, it was reasonable
Enclosure
23
to conclude that although the compensatory measures for the 480VACS room cooling
system were not properly implemented, the 480VACS remained operable. This
evaluation also applied to the EHC equipment located in this room. Since both trains of
the 480VACS and the EHC equipment remained operable, there was no entry condition
for evaluating this in the Phase 2 Tables. Therefore, the safety significance of this issue
is very low (Green).
This finding was related to the Human Performance cross cutting area because of the
failure of Engineering and Operations to correctly implement the procedure for
compensatory cooling.
Enforcement. Technical Specification 6.8.1 requires, in part, that written procedures
shall be established and implemented as recommended in Appendix "A" of Regulatory
Guide 1.33. Contrary to this requirement, on January 12, 2005, Dominion failed to
correctly establish temporary cooling with the correct flow path in accordance with
procedure OP-2315D which affected safety-related equipment in the East 480 volt
switchgear room. However, the failure to establish the correct ventilation path was
determined to be of very low safety significance and has been addressed in Dominion's
Corrective Action Program (CR-05-00370). Therefore, this violation is being treated as
an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.
Unit 3
No findings of significance were identified.
Cornerstone: Emergency Preparedness [EP]
1EP4 Emergency Action Level and Emergency Plan (E-PLAN) Changes (IP 71114.04 -
1 Sample)
a. Inspection Scope
During the period of January 11, 2005, through March 31, 2005, the NRC has received
and acknowledged the changes made to Millstones E-Plan in accordance with 10 CFR
50.54(q), which Dominion Nuclear had determined resulted in no decrease in
effectiveness to the Plan and which have concluded to continue to meet the
requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR 50. The inspector
conducted a sampling review of the Plan changes which could potentially result in a
decrease in effectiveness. This review does not constitute an approval of the changes
and, as such, the changes are subject to future NRC inspection. The inspection was
conducted in accordance with NRC Inspection Procedure 71114, Attachment 4, and the
applicable requirements in 10 CFR 50.54(q) were used as reference criteria.
b. Findings
Enclosure
24
No findings of significance were identified.
1EP6 Drill Evaluation (71114.06 - One Unit 2 Sample and One Unit 3 Sample)
a. Inspection Scope
The inspectors observed one sample of the conduct of Unit 2 licensed operator
simulator training on January 24, 2005. The inspectors evaluated the Operations crew
activities related to evaluating the scenario related to a loss of off site power, during a
reduced inventory plant configuration, and making proper classification determinations.
Additionally, the inspectors assessed the ability of Dominions evaluators to adequately
address operator performance deficiencies identified during the exercise. Documents
reviewed during the inspection are listed in the Attachment.
The inspectors observed one sample of the conduct of a Unit 3 licensed operator
simulator training on February 1, 2005, including assessment of Emergency Planning for
performance indicator submittals. The inspectors observed the Operations crew
performance at the simulator and emergency response organization performance at the
site emergency operations center and technical support center. The inspectors verified
that the classification, notification, and protective action recommendations were
accurate and timely. Additionally, the inspectors assessed the ability of Dominions
evaluators to adequately address operator performance deficiencies identified during
the exercise. Documents reviewed during the inspection are listed in the Attachment.
b. Findings
No findings of significance were identified.
2. RADIATION SAFETY
Cornerstone: Occupational Radiation Safety [OS]
2OS1 Access Controls to Radiologically Significant Areas (71121.01)
a. Inspection Scope (Eleven Samples)
During the period February 28, 2005, through March 3, 2005, the inspector conducted
the following activities to verify that Dominion was properly implementing physical,
administrative, and engineering controls for access to locked high radiation areas, and
other radiologically controlled areas, and that workers were adhering to these controls
when working in these areas. Implementation of these controls was reviewed against
the criteria contained in 10 CFR 20, Technical Specifications, and Dominions
procedures. This inspection activity represents completion of eleven (11) samples
relative to this inspection area.
Enclosure
25
Plant Walkdown and Radiation Work Permits (RWP) Reviews
- The inspector identified areas in Units 2 and 3 where radiologically significant
work was being performed. These areas included the Unit 2 spent fuel pool,
where diving operations were being conducted to repair fuel transfer system
components, and the Unit 3 containment building, where entries were being
made for steam generator blow-down system valve realignments and component
inspections. The Unit 3 containment entry involved personnel entering a
potentially very high radiation area (VHRA), the moveable in-core detector
(MIDS) area. The inspector reviewed RWPs associated with these activities,
RWP Nos. 74 and 90/91, respectively, and the radiation survey maps of the work
areas to determine if the radiological controls were acceptable. Additionally, the
inspector reviewed the procedural controls implemented for personnel entry into
a potential VHRA in the Unit 3 containment.
- The inspector toured accessible radiologically controlled areas in Units 2 and 3,
and with the assistance of a radiation protection technician, performed
independent radiation surveys of selected areas to confirm the accuracy of
survey data and the adequacy of postings.
- In reviewing various RWPs, the inspector reviewed electronic dosimeter
dose/dose rate alarm setpoints to determine if the setpoints were consistent with
the survey indications and plant policy. The inspector verified that the workers
were knowledgeable of the actions to be taken when the electronic dosimeter
alarms or malfunctions for tasks being conducted under selected RWPs. Work
activities reviewed included Unit 2 spent fuel pool diving operations (RWP 74),
Unit 3 steam generator blowdown system valve realignment (RWP 90), and
Unit 3 in-containment inspections of the MIDS (RWP 91).
- The inspector reviewed the RWPs and associated instrumentation and
engineering controls for potential airborne radioactivity areas. Through review of
relevant condition reports and supporting documentation, the inspector reviewed
the dose assessment methodology and corrective actions for airborne incidents
that occurred during 2004, resulting in an internal dose in excess of 50 mrem.
- The inspector reviewed the physical and procedural controls for highly
activated/contaminated materials stored in the Unit 2 and 3 spent fuel pools.
Problem Identification and Resolution
- The inspector reviewed elements of Dominions Corrective Action Program
related to controlling access to radiologically significant areas, completed since
the last inspection of this area, to determine if problems were being entered into
the program for resolution. Details of this review are contained in Section 4OA2
of this report.
Enclosure
26
Jobs-In-Progress Review
- The inspector observed aspects of various maintenance activities being
performed during the inspection period to verify that radiological controls, such
as required pre-job surveys, area postings, job coverage, and pre-job RWP
briefings were conducted; personnel dosimetry was properly worn; and that
workers were knowledgeable of work area radiological conditions. The inspector
attended the pre-job RWP briefings and observed selected aspects of Unit 2
spent fuel pool diving operations and a Unit 3 containment entry.
High Risk Significant, High Dose Rate High Radiation Area and VHRA Controls
- The inspector discussed with Radiation Protection Supervision the adequacy of
physical and procedural controls for performing work in potential VHRAs.
Specific VHRA controls were reviewed for ongoing work performed in the MIDS
area in the Unit 3 containment building (during power operations) and diving
operations performed in the Unit 2 spent fuel pool. Safety measures reviewed
included use of remote dosimetry, multi-badging, pre-job removal of radioactive
sources, confirmatory surveys, video cameras, management authorizations, and
key controls.
- Keys to Unit 2 and 3 locked high radiation areas (LHRA) and VHRAs were
inventoried and accessible LHRAs were verified to be properly secured and
posted during plant tours.
- The inspector discussed with the project lead and cognizant radiation protection
staff the radiological controls to be implemented for replacement and storage of
the Unit 2 reactor head during the upcoming spring 2005 refueling outage.
Radworker and Radiation Protection Technician Performance
- The inspector evaluated radiation worker and radiation protection technician
performance by observing various jobs-in-progress, reviewing daily log entries,
attending pre-job RWP briefings, and attending outage challenge board and
daily departmental meetings.
- The inspector reviewed condition reports related to radiation protection
technician and radiation worker errors to determine if an observable pattern
traceable to a similar cause was evident.
b. Findings
No findings of significance were identified.
Enclosure
27
2OS2 ALARA Planning and Controls (71121.02)
a. Inspection Scope (Four Samples)
During the period February 28, 2005, through March 3, 2005, the inspector conducted
the following activities to verify that Dominion was properly implementing operational,
engineering, and administrative controls to maintain personnel exposure
as-low-as-is-reasonably-achievable (ALARA) for activities performed in 2004 and in
preparing for the upcoming Unit 2 refueling outage. Implementation of these controls
was reviewed against the criteria contained in 10 CFR 20, applicable industry standards,
and Dominions procedures. The inspection represents completion of four samples
relative to this inspection area.
Radiological Work Planning
- The inspector reviewed pertinent information regarding cumulative exposure
history, current exposure trends, and ongoing activities to assess current
performance and the challenges for the upcoming Unit 2 refueling outage.
- The inspector reviewed the projected Unit 2 (spring 2005) refueling outage work
schedule and the associated work activity exposure estimates. Scheduled work
reviewed included reactor head replacement, permanent cavity pit seal
installation, Alloy 600 mitigation activities, and primary systems equipment
changeouts.
- The inspector evaluated the departmental interfaces between radiation
protection, operations, maintenance crafts, and engineering to identify missing
ALARA program elements and interface problems. The evaluation was
accomplished by interviewing the ALARA Coordinator and Radiation Protection
Manager, reviewing station ALARA Council meeting minutes, attending the
Unit 2 Outage Schedule Review meeting, and attending Unit 2 Outage Project
Challenge Board meetings. Challenge Board meetings attended included
primary systems equipment changeout and Alloy 600 mitigation activities.
- The inspector reviewed the assumptions and basis for the annual site collective
exposure projections for site power operations and for the Unit 2 and Unit 3
refueling outages, scheduled later this year. Additionally, the inspector reviewed
the 2005-2006 Station Exposure Reduction Plan.
b. Findings
No findings of significance were identified.
Enclosure
28
4. OTHER ACTIVITIES [OA]
4OA2 Identification and Resolution of Problems (71152)
1. Daily Review of Problem Identification and Resolution
a. Inspection Scope
As required by Inspection Procedure 71152, "Identification and Resolution of Problems",
and in order to help identify repetitive equipment failures or specific human performance
issues for followup, the inspectors performed a daily screening of items entered into
Dominion's corrective action program. This review was accomplished by reviewing
summary lists of each condition report, attending screening meetings, and accessing
Dominion's computerized condition report database.
b. Findings
No findings of significance were identified.
2. Annual Sample Review (One Unit 3 Sample)
Unit 3
a. Inspection Scope
The inspectors completed one Unit 3 sample by selecting condition report CR-04-01569,
EDG exhaust temperature spread, for a detailed review. The deficiency report was
associated with exhaust temperatures on the B EDG and a technical evaluation
M3-EV-04-002, EDG Exhaust Temperature Spread performed by Dominion. The
specific CR and CR history were reviewed to ensure that the full extent of the issue was
identified, appropriate evaluations were performed, and appropriate corrective actions
were specified and prioritized. The inspectors also evaluated the reports against the
requirements of Dominions corrective action program.
b. Findings
No findings of significance were identified.
3. Access Control to Radiologically Significant Areas (71121.01)
a. Inspection Scope
The inspector reviewed ten (10) Condition Reports, recent ALARA Council Meeting
minutes, and Nuclear Quality Assessment field observation reports to evaluate the
threshold for identifying, evaluating, and resolving occupational radiation safety
Enclosure
29
problems. This review included a check of possible repetitive issues such as radiation
worker and radiation protection technician errors.
The review was conducted against the criteria contained in 10 CFR 20, Technical
Specifications, and Dominions procedures.
b. Findings
No findings of significance were identified.
4. Cross-References to PI&R Findings Documented Elsewhere
Section 1R01 describes a failure to take adequate actions to prevent the air dryer skid
from freezing following identification of an inadequate freeze protection system. The
inspectors determined that the Dominion extent of condition review was not adequate to
ensure Dominion assessed and corrected the degraded condition in a timely manner.
Section 1R07.2 describes a failure to promptly identify and take actions to address a
condition adverse to quality concerning a degraded condition associated with all three
RPCCW HXs.
Section 4OA5.2 describes a failure to take effective corrective actions to identify air
entrapped in the residual heat removal heat exchanger. The inspectors determined that
the extent-of-condition review was not adequate to ensure Dominion assessed and
corrected the degraded condition in a timely manner.
4OA3 Event Followup (71153)
1. Unit 2 Unusual Event Declared Due To Fire
a. Inspection Scope
On January 14, 2005, Operations personnel responded to a fire in an electrical panel in
the Unit 2 turbine building. Dominion declared an Unusual Event since the fire lasted
greater than 15 minutes and was located in an area of concern for safe shutdown (the
Unit 2 turbine building). The resident inspectors responded and Region 1 staffed the
Incident Response Center. A special inspection team was chartered to conduct an
investigation and evaluation of this event which will be documented in NRC Inspection
Report 05000336/2005009.
b. Findings
Refer to Special Inspection Report Number 05000336/2005009.
Enclosure
30
2. (Closed) Licensee Event Report (LER) 0500423/2004-002-00, Inoperable Motor Driven
Auxiliary Feedwater (MDAFW) Pump Resulting From A Degraded Service Water
System Brazed Joint
The inspectors interviewed Dominion personnel and reviewed this LER with its
associated condition reports to verify that the root cause and corrective actions related
to the event described in the LER was adequate. No findings were identified during the
inspectors review. This LER is closed.
4OA4 Cross Cutting Aspects of Findings
Cross-Reference to Human Performance and PI&R Findings Documented Elsewhere
Section 1R19.1 describes a failure to implement testing procedures for returning the A
EDG to an operable status following completion of electrical breaker maintenance. The
finding was related to the cross cutting area of human performance in that Dominion
signed a PMT as satisfactory and restored the EDG neutral breaker to an operable
status although the acceptance criteria was not met. .
Section 1R19.2 describes a failure to implement testing procedures for maintenance
performed on the A hydrogen recombiner and which would have made the hydrogen
recombiner inoperable during an actual event. This finding was related to the cross-
cutting issue of Human Performance in that Dominion failed to adequately perform
post-maintenance testing to ensure incorrect maintenance activities were identified prior
to returning the hydrogen monitor to service.
Section 1R23 describes a failure to implement compensatory cooling measures as
required by procedure when normal cooling to the East 480VACS was not available.
This finding was related to the cross-cutting area of Human Performance in that both
Engineering and Operations personnel failed to correctly implement the procedure for
East 480 volt swithcgear room compensatory cooling.
Section 4OA5.2 describes a failure to properly assess and correct degraded conditions
in the A RHR discharge piping. This finding was related to the cross cutting area of
Problem Identification and Resolution in that Dominion failed to perform an adequate
extent-of-condition review to fully evaluate the effect of air that had been introduced into
the A RHR system.
4OA5 Other Activities
1. (Closed) URI 05000336/2004007-01, Adequacy of the Enclosure Building Filtration
System (EBFS) Operability Determination And The Potential Risk Significance Of Any
Degradation in EBFS Function
This URI was opened to assess the impact of a steam and debris laden atmosphere on
the post accident operation of the EBFS. Based on Dominion Engineering Technical
Enclosure
31
Evaluation M2-EV-04-0024, Evaluation of Pressure Entering the EBFS Region, the
inspectors determined that there was no operability impact on the EBFS. This URI is
closed.
2. (Closed) URI 05000423/2004008-01, Air Entrainment of Residual Heat Removal System
This URI was opened to assess the impact of additional air found in the A residual
heat removal system heat exchanger. The inspectors reviewed the operability
determinations and Technical Evaluations associated with the degraded condition of the
RHR system to ensure that operability was justified and that mitigating systems or those
affecting barrier integrity remained available and no unrecognized increase in risk had
occurred. The inspectors also reviewed compensatory measures to ensure that the
compensatory measures were in place and were appropriately controlled. The
inspectors reviewed licensee performance to ensure all related TS and FSAR
requirements were met. Documents reviewed are listed in the Attachment.
Introduction. A green non-cited violation of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, was identified for failure to determine the extent of condition of air
found in the RHR discharge piping. Specifically, after discovering and subsequently
venting a significant amount of air in the A RHR system in May 2004, Dominion did not
adequately investigate to determine if air remained in the RHR heat exchanger tubing.
Description. Following the Spring 2004 refueling outage, NRC inspectors questioned
why Dominion had found air in the RHR discharge piping. The inspectors determined
that the build-up of air in the "A" RHR train occurred when Dominion secured the "A"
RHR pump during the reactor coolant system sweep and vent evolution during the
Spring outage. Additionally, contrary to procedure requirements, Dominion had decided
not to vent the A RHR train while coming out of the outage. This issue was dis-
positioned as an NCV in Inspection Report 05000423/2004007.
Dominion performed a root cause evaluation to determine the cause of the air intrusion
and to recommend actions to prevent recurrence. One of the corrective actions that
was recommended by the root cause team was to add an RHR suction piping vent valve
to the monthly venting surveillance of the system. The root cause evaluation was
completed in August 2004 and concluded that there was no air remaining in the RHR
system. Subsequently, additional air was found in July 2004 and again in October 2004
during RHR system venting (CR-04-09306) following quarterly RHR pump runs.
The inspectors questioned Dominion as to the source of this additional air discovered in
July and again in October 2004. Dominion suspected that the source of air was the A
RHR heat exchanger and determined that this amount of additional air did not impact
A RHR pump operability. However, during the subsequent November vent and valve
lineup of the "A" train of the RHR system, air was again vented from the suction piping
of the "A" RHR pump. Operations determined that this amount of air was excessive,
declared the "A" RHR train inoperable, and entered the appropriate limiting condition of
operation. Dominion instituted a troubleshooting plan consisting of running the A RHR
Enclosure
32
pump several times to strip the air out of the system, performing ultrasonic tests to
identify voids, and running full recirculation flow through the "A" RHR heat exchanger.
Based on this troubleshooting effort, Dominion confirmed that the source of air was the
"A" RHR heat exchanger and was part of the original volume of air first identified in the
A RHR system following the Spring outage. When the "A" RHR pump was run on
recirculation, air was swept out of the "A" RHR heat exchanger and relocated to a
horizontal run of pipe at the "A" RHR pump suction. Dominion determined that it would
take running the A RHR pump approximately 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> to build up enough air to make
the RHR pump inoperable. According to Dominion, the mission time of the RHR pump
for a design basis loss of coolant accident (LOCA) is 30 minutes. Dominion evaluated
whether the air in the A RHR heat exchanger would adversely affect any emergency
core cooling system (ECCS) pumps and wrote an operability determination (OD) to
support continued operability of the A RHR system. Operations then declared the A
RHR train operable and exited the associated technical specification.
Analysis. The performance deficiency was the failure to take prompt corrective actions
to determine the extent of condition of air that was introduced into the A RHR system
during the Spring 2004 outage. Dominions extent-of-condition review did not determine
that a significant volume of air remained in the RHR heat exchanger after finding and
venting air in the A RHR system during subsequent venting evolutions conducted in
July and October of 2004. Specifically, Dominion did not recognize the need to expand
and accelerate their extent of condition corrective actions following the identification that
air remained in the A RHR system in July and subsequently again in October of 2004.
This finding was more than minor because it affected the equipment performance
attribute and the availability, reliability, and capability objective of this mitigating system.
However, subsequent analysis determined that for a large break LOCA, the air would be
swept into the core without affecting the RHR pump, and for small break LOCAs, the air
would not have affected the operability of the RHR pump within its required mission
time, and for all accidents the air would not have migrated to a section of crossover
piping that could affect other ECCS equipment. Therefore, this finding, assessed in
accordance with NRC Manual Chapter 0609, Appendix A, Attachment 1, Significance
Determination Process for Reactor Inspection Findings for At-Power Situations, was
determined to be of very low safety significance (Green) because it did not involve a
design or qualification deficiency, represent an actual loss of safety function, or involve
seismic, flooding, or severe weather initiating events.
This finding was related to the cross-cutting issue of problem identification and
resolution because Dominion failed to perform an adequate extent of condition review to
fully evaluate the effect of air that was introduced into the A RHR system.
Enforcement. Code of Federal Regulations 10 CFR Part 50 Appendix B, Criterion XVI,
Corrective Action, requires, in part, that measures shall be established to assure that
conditions adverse to quality are promptly identified and corrected. Contrary to this
requirement, from May to October 2004, Dominion failed to properly assess and correct
degradation of the A RHR system caused by air introduction during the Spring 2004
Enclosure
33
refueling outage. Because subsequent evaluation of the air void determined that the
system retained operability, the issue was determined to be of very low safety
significance and has been addressed by Dominions CAP (CR 04-10129), this violation
is being treated as an NCV, consistent with Section VI.A of the NRC Enforcement
Policy. (NCV 05000423/2005002-06)
4OA6 Meetings, Including Exit
Heat Sink Performance Exit Meeting Summary
On February 11, the inspector presented the inspection results to members of Dominion
management led by Mr. Alan Price. Dominion management stated that none of the
information reviewed by the inspector was considered proprietary. The inspector also
discussed Dominions associated operability determination and OE evaluation during a
conference call on March 21, 2005.
Occupational Radiation Safety Exit Meeting Summary
On March 3, 2005, the inspector presented the inspection results to Mr. Skip Jordan,
and other members of the Dominion staff, who acknowledged the findings.
Integrated Report Exit Meeting Summary
On April 21, 2005, the resident inspectors presented the overall inspection results to
Mr. J. Alan Price and other members of his staff who acknowledged the findings. The
inspectors confirmed that proprietary information was not provided or examined during
the inspection.
ATTACHMENT: SUPPLEMENTAL INFORMATION
Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
A. Airas, System Engineer
S. Alligood, Radiation Protection Technician
T. Armagno, Supervisor, Health Physics
B. Bartron, Licensing
B. Bowen, Radiation Protection Technician
P. Calandra, ALARA Coordinator
W. Collins, Radiation Protection Technician
D. DelCore, Shift Supervisor, Health Physics, Unit 2
E. Dundon, System Engineer
I. Haas, Acting Supervisor Exposure Control
A. Johnson, Supervisor, Radiation Protection Support, (Technical)
A. Jordan, Director, Nuclear Engineering
J. Joszick, Radiation Protection Technician
B. Kaufman, (Acting) Manager, Nuclear Quality Assurance
R. King, ALARA Coordinator
E. Laine, Manager, Radiological Protection & Chemistry
J. Langan, Site Engineering Manager
L. Loomis, System Engineer
F. Mueller, System Engineer
F. Perkins, System Engineer
A. Price, Site Vice President - Millstone
D. Regan, Supervisor, Radiation Protection Support (ALARA)
S. Sarver, Director, Nuclear Station Operations & Maintenance
S. Scace, Director, Nuclear Station Safety and Licensing
W. Spahn, Site Engineering Supervisor
M. Wood, Health Physicist
M. Wynn, Health Physicist
NRC personnel
M. X. Davis, Reactor Inspector, Division of Reactor Safety (DRS)
M. L. Heath, Nuclear Safety Professional
K. M. Jenison, Senior Reactor Inspector, Division of Reactor Projects (DRP)
S. R. Kennedy, Resident Inspector, DRP
K. S. Kolaczyk, Senior Resident Inspector, Ginna, DRP
J. A. Krafty, Reactor Inspector, DRS
K. A. Mangan, Resident Inspector, DRP
T. A. Moslak, Health Physicist, DRS
S. M. Schneider, Senior Resident Inspector, DRP
J. G. Schoppy, Senior Reactor Inspector, DRS
Attachment
A-2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
05000336/2005002-01 FIN Failure to adequately address
concerns related to freeze protection
of an outdoor temporary instrument
air compressor (1R01.2)05000423/2005002-02 NCV Failure to promptly evaluate and
correct a degraded condition
associated with the divider plate for
all three RPCCW HXs
(Section 1R07.2)05000423/2005002-03 NCV Failure to adequately implement
testing procedures for restoring the
A EDG to service (1R19.1)05000423/2005002-04 NCV Failure to adequately perform
post-maintenance testing on
hydrogen recombiner (1R19.2)05000336/2005002-05 NCV Failure to implement procedures to
correctly install temporary cooling to
the East 480 volt switchgear (1R23)05000423/2005002-06 NCV Failure to take prompt corrective
actions to determine the extent of
condition of air trapped in the RHR
suction and discharge piping
(4OA5.2)
Closed
05000423/2004-002-00 LER Inoperable Motor-Driven Auxiliary
Feedwater Pump Resulting From A
Degraded Service Water System
Brazed Joint (4OA3.2)05000336/2004007-01 URI Adequacy of the Enclosure Building
Filtration System Operability
Determination And The Potential
Risk Significance Of Any
Degradation in EBFS Function
(4OA5.1)05000423/2004008-01 URI Air Entrainment of Residual Heat
Removal System (4OA5.2)
Attachment
A-3
Discussed
None
LIST OF DOCUMENTS REVIEWED
Section 1R01: Adverse Weather Protection
CR-05-00633, Organization Response to Weekend Snowstorm
CR-05-00922, Temporary Air Compressor Dryer Prefilters High DP and Lowering Air Pressure
TS 3.0.3, Limiting Condition For Operation
C OP 2006, Revision 001-02, Storm and Other Hazardous Phenomena (Preparation and
Recovery)
Section 1R04: Equipment Alignment
Major Equipment Schedule
Electrical On-Line Diagrams
OPS Form 2610C-002, Revision 019-05, Auxiliary Feedwater System Lineup Verification
OP-3314F, Unit 2 Control Building HVC HVK Valve Lineup
OP-2322, Revision 025-02, Auxiliary Feedwater System
OP-2315A, Revision 014-03, Control Room Air Conditioning System
SP-2610C, Revision 012-08, AFW System Lineup Valve Operability and Operational Readiness
Tests
SP-3670.1, Revision 010-10, Control Room Surveillances
SP-3670.2, Revision 010-06, Technical Specification Related PEO Rounds (Mode 1 to 4)
SP-3670.1-002, Revision 010-03, SP-3670.1 Surveillance Form
SP-3670.2-002, Revision 013-05, SP-3670.2 Surveillance Form
SP-2669A-002, Revision 034, Unit 2 Aux Building Rounds
SP-2610CO, Revision 000-00, Auxiliary Feedwater Flow-Path Lineup Verification
SP-2609B, Revision 016-01, EBFS and Control Room Ventilation Operability Test, Facility 2
SP-3622.4-002, Revision 005-02, Auxiliary Feedwater System Lineup (MDAFW Train B)
SP-3622.4-001, Revision 005-02, Auxiliary Feedwater System Lineup (MDAFW Train A)
SP-3622.4, Revision 005-02, Auxiliary Feedwater System Lineup Verification
PI&D 25203-26005, Sheet 3 of 4, Revision 46, Condensate Storage and Auxiliary Feedwater
P&ID 25203-26027, Sheet 3 of 4, Revision 28, Control Room Air Conditioning System
DCM 05-5A, Revision 010, MP2 Control Room, Heating, Cooling & Ventilation Requirements
Calculations
DCM Form 5-1A, Revision 05, Control Room HVAC Regain, Pressure Drop and Flowrate
FSAR, Table 9.9-11, Revision 21, Control Room Air Conditioning System
EOP 2541, Appendix 43, Revision 000, Operating Control Room Emergency Air Intakes
Millstone Nuclear Power Station Unit 2 Technical Specifications 4.7.1.2.a
Millstone Nuclear Power Station Unit 2 Technical Specifications 3/4 3-33, Table 3.3-11
Millstone Nuclear Power Station Unit 2 (MNPS-2) Final Safety Analysis Report (FSAR)
CR-05-00638, The Facility 2 Control Room Air Conditioning System is not Maintaining Control
Room Temp. And it Appears that the Compressor is Tripped
Attachment
A-4
CR-04-01743, The A Vital Chiller (X169A) Tripped During its Surveillance Run Via SP-2604T
CR-04-11217, The Facility 1 Control Room Air Conditioning System is not Maintaining Control
Room Temp. And it Appears that the Compressor is Tripped
CR-05-00769, The Vital Chillers (X169A/B) Require a Maintenance Rule (a)(1) Evaluation due
to Repetitive Failures
CR-05-02072, Discovered Montville-Haddam Neck 364 Line Out of Service Which is the Same
as Millstone-Montville 371 Line Out
CR-05-02873, MP2 Control Room HVAC System Calculation Changes
Drawing 25203-32023, Sheet 55, Revision 6, Control Room A/C Air Cool Condenser MF36A
Drawing 25203-32023, Sheet 53, Revision 8, Control Room A/C System Refrig. Compressor
MF22A
Maintenance Rule (a)(1) Evaluation, Revision 0, Control Room Air Conditioning System (2315A)
COP 200.8, Revision 002-01, Response to ISO New England/Convex Emergencies & Alerts
Unit 3 Final Safety Analysis Report
EM-135B&C, Auxiliary Steam System
Section 1R05: Fire Protection
SP-3641B.2, Revision 013-00, Functional Check of the Fire Protection Halon System
SP-3641D.5-001, Revision 008-4, Fire Damper Operability Verification
CR-04-02019, Incorrect reference in MP3 Fire Protection Evaluation Report
CR-04-02202, Audit 04-04 Hourly Fire Watch for MP3 impairment #23534-01-H exceeded 25%
CR-04-02762, Fire Protection: Tank inspections not performed as required by procedure
CR-04-07072, During fire protection inspection, identified slight difference in component name
between label and procedure
CR-04-07377, Fire protection cleaned up small oil spill
CR-04-07430, During NRC fire protection inspection, apparent inconsistency between fire
shutdown action matrix and EOP direction
CR-04-08275, Excessive leakage from fire protection water system
CR-04-08399, Review of OE-18887 unanalyzed condition related to fire protection cable
separation
S&W Drawing No. 12179 Piping and Instrument Diagram Fire Protection
Millstone Unit 3 Fire Protection Evaluation Report, Revision 17
Millstone Unit 3 Updated Final Safety Analysis Report
Millstone Unit 3 Licensed Operator Training Manual
Millstone Unit 3 Technical Requirements Manual
FPI 50-001, Revision 010-00, Fire Brigade Drill Assessment Data Sheet
Millstone Unit 2 Individual Plant Examination for External Events
Millstone Unit 2 Fire Hazards Analysis
Millstone Unit 2 Fire Hazard Analysis Boundary Drawing Area Figures
Unit 3 Fire Hazards Analysis
Attachment
A-5
Section 1R06: Flood Protection Measures
Millstone Unit 3 PSD Civil/Mechanical Design Calculation No. P) 1194, ESF Bldg Flood
Study: Maximum Flood Height in the ESF Bldg due to a Pipe Break
Calculation No. 12179-P)-1194, Revision 2, Change No. 1, ESF Building Flood Study:
Maximum Flood Height in the ESF Building due to a Pipe Break
Calculation No. 12179-P)-1194, Revision 2, Change No. 2, ESF Building Flood Study:
Maximum Flood Height in the ESF Building due to a Pipe Break
Calculation No. 12179-P)-1194, Revision 2, Change No. 3, ESF Building Flood Study:
Maximum Flood Height in the ESF Building due to a Pipe Break
Calculation No. P)-1038, Revision 0, Change No. 1, Fuel Bldg. Flood Study: Determination of
Maximum Height of Water in Fuel Bldg. Due to Pipe Crack
Section 1R07: Heat Sink Performance
MP-2701J-096, Revision 007, Service Water Cooled Heat Exchangers Subject to GL-89-13
M2-EV-99-0103, Revision 03, MP2 Service Water System Operability for Increase in Ultimate
Heat Sink Temperature to 77 Degrees F.
NRC Generic Letter 89-13 dated July 18, 1989, Service Water System Problems Affecting
Safety-Related Equipment
M2-04-10878, A RBCCW Heat Exchanger Inspection
89-13 Program and Design Basis Documents
Millstone Unit 3 Generic Letter 89-13 Responses and Updates, January 1990 - February 2001
EN 31084, Revision 006-02, Operating Strategy For Service Water System At Millstone Unit 3
M3-EV-02-0031, Technical Evaluation for Service Water Heat Exchanger Monitoring Millstone
Unit 3, dated 3/4/04
EPRI NP-7552, Heat Exchanger Performance Monitoring Guidelines, December 1991
EPRI TR-107397, Service Water Heat Exchanger Testing Guidelines, March 1998
Corrective Action Documents
PIR 3-93-056 03-05653 04-03673 04-09608
AR 97000674 03-05942 04-04036 04-10667
01-10079 03-06070 04-06364 04-10672
02-03287 03-06080 04-06977 05-01227*
03-04802 03-08587 04-05227 05-01233*
03-04924 03-08729 04-06364 05-01278*
03-05524 03-08819 04-08539 05-01281*
03-05528 03-09039 04-08578 05-01767*
03-05615 03-09241 04-09331
- Initiated in response to inspector concerns.
Attachment
A-6
Engineering Evaluations and Calculations
DCR M3-97045, Revision 1, RSS Pump Restriction Orifices to Prevent Suction Line Flashing
DCR M3-00029, Revision 0, Operation with the MP3 Ultimate Heat Sink Temperature below the
Design Basis Low Temperature of 330F
CALC No.03-059, Revision 0, Analysis of the Emergency Diesel Generator Jacket Water
Cooler Thermal Performance Test Results
CALC No.03-060, Revision 0, Emergency Diesel Generator Intercooler Water Cooler Proto-HX
Benchmark and Analysis of the Thermal Performance Test Results
Calculation No. 90-069-1130 M3, Revision 0, Millstone Unit 3 - Service Water System -
Summary of Westinghouse Heat Exchanger Calculations
Calculation No. 90-069-01065M3, Revision 1, MP3 SW System - Service Water System - NRC
Generic Letter 89-13, Item No. IV, Design Basis Summary Report
Operability Determination MP3-004-05, Revision 0
EDG Testing and Inspections
SP 3646A.2, Emergency Diesel Generator B Operability Tests, dated 12/21/04
PD04266.02, Record of Eddy Current Inspection of Emergency Diesel Generator - B Air Cooler
3EDS-1B and Water jacket Cooler 3EDS-2B, May 1999
Service Water Cooled Heat Exchangers Inspection Form (EN31084 Attachment 2) for 3GS-
E1B & E2B; dated 10/26/04
SP 3626.13, CCI and EGS Train B Heat Exchanger Fouling Determination, dated 1/31/05
SP 3626.13, CCI and EGS Train B Heat Exchanger Fouling Determination, dated 2/7/05
Miscellaneous
Risk-Informed Inspection Notebook for Millstone Nuclear Power Plant, Unit 3, Revision 1
Millstone Unit 3 Individual Plant Examination for Severe Accident Vulnerabilities (NUSCO 171)
S & W DWG. No. 12179-EM-133D, Piping & Instrumentation Diagram Service Water
Intake Structure Information Book
System Operability Determination Notebook (MP3-065-01, MP3-072-04, MP3-079-04)
Request for Engineering LOE Support, dated 12/8/04
Millstone Power Station Unit 3 2003 Annual Environmental Protection Plan Operating Report
Intercooler Water Cooler Heat Exchanger Specification Sheet, dated 7/28/75
Jacket Water Cooler Heat Exchanger Specification Sheet, dated 7/28/75
Containment Recirculation Coolers Tubular Heat Exchanger Data, dated 2/10/74
D.C. Cook Nuclear Power Plant, Units 1 and 2 NRC Special Inspection Report 50-315/03-08;
50-316/03-08, dated 7/3/03
Operating Experience
NRC Information Notice 94-59: Accelerated Dealloying of Cast Aluminum-Bronze Valves
Caused by Microbiologically Induced Corrosion, dated 8/17/94
NRC Information Notice 96-36: Degradation of Cooling Water Systems Due to Icing, dated
6/12/96
Attachment
A-7
NRC Information Notice 98-02: Nuclear Power Plant Cold Weather Problems and Protective
Measures, dated 1/21/98
Millstone Unit 3 Response to NRC IN 94-59, NRC IN 96-36, and NRC IN 98-02
NUREG-1275, Vol. 3 - Operating Experience Feedback Report - Service Water System
Failures and Degradations
Ice Blockage of Water Intakes, NUREG/CR-0548
Generic Service Water System Risk-Based Inspection Guide, NUREG/CR-5865 EGG-2674
NRC Generic Letter 96-06, Supplement 1: Assurance of Equipment Operability and
Containment Integrity During Design-Basis Accident Conditions, dated 11/13/97
Millstone Unit 3 Generic Letter 96-06 Responses and Updates, May 1998 - December 2000
Procedures
AOP 3560, Revision 007, Loss of Service Water
AOP 3569, Revision 015-02, Severe Weather Conditions
OP 3326, Revision 021-15, Service Water System
OP 3306, Revision 008-03, Containment Recirculation Spray System
OP 3330A, Revision 015-08, Reactor Plant Component Cooling Water
OP 3353.WTC, Revision 1, Chlorine Panel Annunciator Response
OP 3353.MBIB, Revision 002-06, Chlorination System Trouble
OP 3353.MBIC, Revision 005-04, RPCCW HX SW FLOW HI/LO
OP 3353.MBIC, Revision 005-04, CTMT RECIRC CLR SW FLOW HI/LO
OP 3353.MBIC, Revision 005-04, DG B COOLER SW FLOW HI
OP 3353.MBIC, Revision 005-04, DG B COOLER SW FLOW LO
OP 3353.MBIC, Revision 005-04, Service WTR PP Strainer DIFF Pres HI
OP 3353.MBIC, Revision 005-04, Service WTR Pump DIS Pres LO
OP 3353.MBIC, Revision 005-04, RPCCW HX OUT TEMP HI/LO
OP 3353.MBID, Revision 002-04, CTMT RECIRC Spray System
OP 3353.MBID, Revision 002-04, Service Water System
Op 3346A, Revision 021-02, Emergency Diesel Generator
SP 3626.13, Revision 019-04, Service Water Heat Exchangers Fouling Determination
SP 3626.14, Revision 001-01, RSS Heat Exchanger SW Supply Piping Flush
RPCCW Testing and Inspections
Service Water Cooled Heat Exchangers Inspection Form (EN31084 Attachment 2) for
3CCP*E1A; dated 2/6/02, 4/29/02, 6/25/03, 5/24/04
Service Water Cooled Heat Exchangers Inspection Form (EN31084 Attachment 2) for
3CCP*E1B; dated 9/3/02, 11/25/02, 5/14/03, 9/8/03, 9/20/04
Service Water Cooled Heat Exchangers Inspection Form (EN31084 Attachment 2) for
3CCP*E1C; dated 7/27/01, 7/2/02, 6/9/03
Longview Inspection damaged Tube/Condition Report for RPCCW E1-B, dated 9/28/01
PD04573, Record of Eddy Current Inspection of RPCCW Heat Exchanger 3CCP-E1B,
September 2003
Attachment
A-8
RSS Testing and Inspections
Service Water Cooled Heat Exchangers Inspection Form (EN31084 Attachment 2) for
3RSS*E1B; dated 12/15/04
Service Water Cooled Heat Exchangers Inspection Form (EN31084 Attachment 2) for
3RSS*E1D; dated 12/16/04
SP 3626.14, RSS Train B Heat Exchangers SW Supply Piping Flush, dated 12/15/04 &
12/17/04
SW Testing and Inspections
SP-3626.3, 3SWP*MOV71B, TPCCW HX SW Supply, Stroke Test; dated 12/20/04
SP-3626.3, 3SWP*MOV50A and MOV50B, CCP HXs Train A and Train B SW Supply, Stroke
Test; dated 4/24/04
SP-3626.3, 3SWP*MOV54B and MOV54D, RSS Coolers B and D SW Supply, Stroke Test;
dated 12/15/04
SP-3626.3, 3SWP*AOV39B, EDG B Service Water HX Outlet, Stroke Test; dated 10/26/04
SP-3626.4, Service Water Pump 3SWP*P1A Operational Readiness Test, dated 11/09/04
SP-3626.5, Service Water Pump 3SWP*P1B Operational Readiness Test, dated 12/23/04
SP-3626.6, Service Water Pump 3SWP*P1C Operational Readiness Test, dated 11/10/04
SP-3626.7, Service Water Pump 3SWP*P1D Operational Readiness Test, dated 12/20/04
SP-3626.6, Service Water Pump 3SWP*P1C Operational Readiness Test, dated 11/10/04
SP 3626.13, Service Water Heat Exchangers Fouling Determination, dated 1/29/05, 2/6/05
System Health Reports and Trending Data
B EDG Service Water Flow and Differential Temperature, 09/28/04 - 01/18/05
B EDG Lube Oil & Jacket Water Temperatures, 09/28/04 - 01/18/05
B EDG JW and Intercooler, B RSS, and B RPCCW HX Flow & D/P Trending, 1/7/02 - 1/10/05
Emergency Diesel Generator and EDG Fuel Oil System Health Report (Third Quarter 2004)
Service Water System Health Report (Third Quarter 2004)
Containment Recirculation Spray System Health Report (Third Quarter 2004)
Reactor Plant Component Cooling Water System Health Report (Third Quarter 2004)
Work Orders
M30106969 M30206235 M30307754 M30416542
M30202096 M30206237 M30308193 M39803648
M30202098 M30206239 M30310919 M39804420
M30206009 M30206241 M30407936 M39804423
M30206010 M30206243 M30413782
M30206233 M30307593 M30414020
Attachment
A-9
Section 1R11: Licensed Operator Requalification Program
2R16 Outage Modification Lesson Plan
2R16 Shutdown Cooling on Containment Spray SPROC Lesson Plan
LORTSE11, Revision 5, Change 3, Unit 3 Simulator Exam Overview
Emergency Action Level Tables
Section 1R12: Maintenance Effectiveness
CR-05-00638, The Facility 2 Control Room Air Conditioning System is not Maintaining Control
Room Temp. And it Appears that the Compressor is Tripped
CR-04-01743, The A Vital Chiller (X169A) Tripped During its Surveillance Run Via SP-2604T
CR-04-11217, The Facility 1 Control Room Air Conditioning System is not Maintaining Control
Room Temp. And it Appears that the Compressor is Tripped
CR-05-00769, The Vital Chillers (X169A/B) Require a Maintenance Rule (a)(1) Evaluation due
to Repetitive Failures
CR-04-10911, MCC B51 Air Conditioning Unit A/C-3 Making High Pitched Whistle
CR-04-1119, MCC B51 Enclosure Air Conditioner Not Working
CR-03-06001, A/C-3 (MCC B51 AC Unit) TRS not Resolved in a Timely Manner
CR-04-08032, AC-4 not Operating Properly
CR-04-02083, Air bubbles Noted in B51 Enclosure Cooler Sight Glass
CR-04-00969, B61 Enclosure Cooling Unit A/C-4, Operating with Bubbles in the Liquid Line
Sightglass
CR-03-00634, The Air Conditioner for MCC B61 was not Maintaining Temperature
CR-05-00127, SBO Diesel UPS Battery #1 Failed Voltage Testing
CR-05-00617, Received HI DP on HVQ*PDIS47, HVQ*FLT3 Closed due to Snow; Required
Entry into TS 3.0.3 to Restore
SP-M2-ME-018, Vital MCC Coolers
MP-24-MR-FAP710, Revision 000, Maintenance Rule Functional Failure Evaluation
MP-24-MR-FAP710, Revision 000-02, Maintenance Rule Functional Failures and Evaluations
IM-034060-1, Revision 0, March 1998, Installation, Operation & Maintenance Manual for Air-
conditioning Unit EEI P/N: 394
DCM Form 5-1A, Revision 05, Auxiliary Building - MCC B51, B61 Enclosures - Vital Cooling
System
Maintenance Rule Functional Failure Evaluation dated January 27, 2005
Drawing 25203-32023, Sheet 55, Revision 6, Control Room A/C Air Cool Condenser MF36A
Drawing 25203-32023, Sheet 53, Revision 8, Control Room A/C System Refrig. Compressor
MF22A
Maintenance Rule (a)(1) Evaluation, Revision 0, Control Room Air Conditioning System (2315A)
Maintenance Rule Scoping Table, Vital SWGR Emergency Cooling
Unit 3 Control Room Logs
Section 1R13: Maintenance Risk Assessments and Emergent Work Evaluation
MP-13-PRA-FAP01.1, Revision 000, Performing Risk Reviews
MP-20-OM-FAP02.1, Revision 001-02, Shutdown Risk Management
Attachment
A-10
MP-20-WM-FAP02.1, Revision 009-00, Conduct of On-Line Maintenance
NUMARC 93-01, Revision 2, NEI Industry Guideline for Monitoring the Effectiveness of
Maintenance at Nuclear Power Plants
Millstone Nuclear Power Station Unit 3 Technical Specifications L.C.O 3.3.2 (Table 3.3-3)
Millstone Nuclear Power Station Unit 3 (MNPS-3) Final Safety Analysis Report (FSAR)
CR-05-00550, Unplanned LCO Entry (3.3.2) due to 3HVR*FN6A starting Unexpectedly,
followed by MB2B 2-4A Sequencer A Trouble
CR-04-09890, 3SIH*PIA oil leakage will exceed the oil reservoir capacity within the SIH pump
design mission run time
Major Equipment Schedule
Equipment Out of Service Quantitative Risk Assessment Tool
Unit 2 Control Room Logs
Unit 3 Control Room Logs
Section 1R14: Personnel Performance During Non-Routine Plant Evolutions and Events
Technical Specification 3.0.3, Limiting Condition for Operation
C OP 200.6, Revision 001-02, Storms and Other Hazardous Phenomena (Preparation and
Recovery)
CR-05-00633, Organization Response to Weekend Snowstorm
CR-05-00399, Unusual Event Declared Due to Fire
Incident Report Forms
Unit 2 Control Room Logs
Unit 3 Control Room Logs
DNAP-2000, Troubleshooting Sheet
Equipment Out of Service Risk Tool
RP-5, Revision 004-00, Operability Determinations
RECO MP3-001-05, A EDG Autotest Circuit Failed, Resulting in Auto Start of 3HVR*FN6A
ISO-New England, Master/Local Control Center Procedure No. 2, Abnormal Conditions Alert
TS 3.3.2, Engineered Safety Features Actuation System Instrumentation
Trouble Shooting Plan, A Diesel Sequencer is Displaying a Failure Code and Needs to be
Troubleshot to Determine Operability
OP-3250.46A, Revision 006-01, Diesel Sequencer Bypass Procedure
SP-3448E31, Revision 006-02, Train A - diesel Sequencer Actuation Logic Test
Section 1R15: Operability Evaluations
MP2-003-05, On second sound cut of pulsation dampener surveillance SP2664, a rattling noise
was detected by accelerometers from the B charging pump pulsation dampener
MP3-002-05, Service water brazed joint leak in drain line for A train
CR-05-01960, TE-107 Spiking at C03F
CR-05-01959, TE-106 Operation is Erratic
CR-05-01336, Alternate Plant Configuration was Established by Isolating Steam to #2 Steam
Generator Pressure Instrument Loop
CR-05-02655, Backup Measurement Method Required for TI-106
CR-05-00748, TI-106 PORV Discharge Temp Appears to be Drifting High
Attachment
A-11
CR-05-02359, Acoustic Valve Monitor for RC-404 Reading 15%
CR-05-00127, SBO Diesel UPS Battery #1 Failed Voltage Testing
CR-05-02751, Unplanned LCO entry TS Section 3.4.6.1, Leakage Detection Systems, Action
Statement B
CR-05-02350, Impact of LER 2004-002-00, Inoperable EDG
CR-05-01213, 3CDS*CTV38A T-Ring (Seat) Requires Upgrade to Safety Related Per DCM03
(MEPL) Procedure
CR-05-01689, Retest for Hydrogen Monitor Maintenance Needs Resolution
CR-05-00550, Unplanned LCO Entry (3.3.2) due to 3HVR*FN6A Starting Unexpectedly,
Followed by MB2B 2-4A Sequencer A Trouble
RECO MP3-001-05, A EGLS Autotest Circuit Failed, resulting in Auto Start of 3HVR*FN6A
RECO/OD MP3-003-05, During a Review of the bill of materials for 3CDS*CTV38A-B,
3CDS*CTV39A-B, 3CDS*CTV91A-B, and 3SWP*ADV39A-B, it was discovered that the
T-ring (valve seat) had been improperly evaluated by previous MEPL determinations as
being non-safety related (NSR)
RP-5, Revision 004-00, Operability Determinations
OD MP3-001-05, Revision 1, Autotest Circuit Failed, Resulting in Auto Start of 3HVR*FN6A
Millstone Unit 3 Risk Informed Inspection Notebook - Brookhaven
IC-3471A01, Revision 002, Station Blackout Diesel Uninterruptable Power Supply Testing
AMP-24-MR-GDL700, Revision 003, Attachment 3, Availability Assessment for Emergent
Conditions
Unit 3 Technical Specifications Section 3.4.6.1, Leakage Detection Systems
TS 3.3.2, Engineered Safety Features Actuation System
Unit 3 Control Room Logs
Section 1R16: Operator Work-Arounds
Unit 2 and 3 Operator Workaround Management Summaries dated 3/11/05
MP-14-OPS-GDL600, Revision 001, Plant Status and Configuration Control
MP-14-OPS-GDL400, Revision 002, Operations Administrative Procedures
Section 1R19: Post-Maintenance Testing
AWO M2-00-19686, "A" Auxiliary Feedwater (AFW) Pump
AWO M2-05-00565, NT
AWO M2-00-12762, Removal/Re-Install Elbow in TDAFW PMP Suction Line
M2-02009, Replacement of Non Vital Transformer
M3-02-06072, 18 Month Battery Charger Load Test
M3-03-13876, A EDG Sequence Troubleshooting Plan
AWO M3-05-010226, Auxiliary Feed Pump Cubicle Vents
M3-03-05461, Train A Hydrogen Recombiner Instrumentation
M3-05-04144, Replace Leaking Tubing and Fittings per C MP 721A
OP-3314D, Revision 010-12, ESF Building Ventilation and Air Conditioning
CR-05-00617, Received Hi Dip on HVQ*PDIS47, HUQ*FLT3 Clogged due to Snow, Required
Entry into TS 3.0.3 to Restore
CR-03-00712, M&TE QA-3000-17G (AEMC Corp Clamp-on Model MN-115) Was Lost
Attachment
A-12
CR-05-03569, PMT Requirements of OP3370A not Consistent with Those in MP-20-GDL40
CR-05-01713, A Hydrogen Recombiner Failed the Leak Tightness Verification
CR-05-01689, Retest for Hydrogen Monitor Maintenance Needs Resolution
CR-05-03896, A Hydrogen Recombiner may have been Inoperable for Greater than the Tech
Spec Allowed Outage Time
SP-2610AO-001, Revision 000-00, "A" AFW Pump and Recirc Check Valve IST, Facility 1
MP-20-WP-GDL40, Revision 03, "Pre and Post Maintenance Testing"
MP-20-WP-GDL40, Revision 002-01, Pre and Post Maintenance Testing C PT 1405,
Revision 000, 4.16KV and 6.9KV Motor and Surge Capacitor
DM2-02-0237-03, Replacement Containment Air Radiation Monitor, RM-8123
DM2-00-0363-04, Instrument Air Compressor F3C Replacement, Electrical and I&C Changes
Unit 3 Control Room Logs
DWG EM115A, rev 33, Quench Spray and Hydrogen Recombiner
SP-2664, Charging Pump Pulsation Dampner
SP-3448E31, EDG Sequencer Actuation Logic Test
SP-3646A.1, EDG Operability Test
SP-2402M, Function Test of AFW Ignition
SPROC 6T503-2-01, Mag-Amp Regulating Transformers
NRC IEN 85-91, Load Sequencers for EDG
M3-02-16737, A EDG Neutral Grounding Breaker Preventive Maintenance and Doble Testing
CR-05-01888, 15G-14U-2N, A EDG Ground Neutral Breaker, Red Closed Light on Breaker
Cabinet Not Lit.
OP 3370A, Revision 013-07, Electrical Breaker Maintenance
Section 1R22: Surveillance Testing
SP-2606B, Revision 013-01 Containment Spray Pump Operability and Inservice Testing
SP-2604D, Revision 011-00, LPSI Pump Tests
SP-3444A01, Revision 006-02, Steam Generator Water Level Channel Calibration
SP-3444A01-003R, Revision 000-01, Steam Generator Water Level Channel 3 Calibration -
Rack Instrumentation Data Sheet
SP-3609.1, Revision 009-03, Quench Spray Pump 3QSS*P3A Operational Readiness Test
SP-3610A.3-001, Revision 005, RHR System Venting & Valve Lineup-Train A
SP-3610A.3-002, Revision 006, RHR System Valve Lineup Verification Train A and Common
SP-2609F-004, Revision 001-01, Control Room Ventilation System Filter Testing Efficiency,
Facility 2
SP-2609F-002, Revision 011-01, Control Room Ventilation System Filter Testing, Flow and
D/P, Facility 2
SP-3630A.5, Revision 008-005, Reactor Plant Component Cooling Water Pump 3CCP*P1B
Operational Readiness Test
SP-3630A.5-002, Revision 006-04, Reactor Plant Component Cooling Water Pump 3CCP*P1B
Operational Test
Attachment
A-13
SP-3626.7-001, Revision 013-04, Service Water Pump 35SWP*PID Operational Readiness
Test
SP-3646A.1, Revision 015-07, Emergency Diesel Generator A Operability Test
SP-2619A-001, Channel Check of Radiation Monitoring Systems
SP-2730B, Main Steam Safety Valve Testing (IPTE)
SP-2605R, 2-Fire-34/94A/94B/94C Stroke Time Test IST
SP-3610A.1, Residual Heat Removal Pump 3RHS*P1A Operational Readiness Test
SPROC OPS04-2-04, Revision 000-01, Sweep of A Train RHR to RWST
Surveillance Form SP-3609.1-001, Revision 011-01, Quench Spray Pump 3QSS*P3A
Operational Readiness Test
Surveillance Form SP-3610A.1-001, Revision 010-02, 3RHS*P1A Operational Readiness Test
in Mode 1, 2, 3, or 4 (when aligned for injection)
MP-UT-5, Revision 000-03, UT Examination Straight Bean Measurements
CR-04-03611, TDAFW Pump Control Valve Failed Stroke Time Test
CR-04-03491, Failed Operations Surveillance on 3CCP*V060
CR-04-03348, Diesel Surveillance Step Could Not Be Performed
CR-04-09799, Failed Surveillance SP-31029 Channel 4T
CR-04-10217, Incorrect Revision of Procedure Form Used to Complete Surveillance
CR-04-10814, Surveillance SP-3604C.7 Requires Addition of 2 Valves for Non Operating Boric
Acid Pump
CR-05-00281, CCP OP Test Surveillance Requires Additional Steps to Establish Minimum Flow
While Shifting Pumps
CR-05-02888, QSS Pump Surveillance Procedures Need to be Revised to be Consistent with
RHR and SIH Surveillance Procedures regarding the Auto-Start of 3HVQ*ACUS1A/B
PI&D 25203-26015, Revision 28, Low Pressure Safety Injection System
TS 3/4.6.2, Containment Quench Spray System
TS 3.5.2, ECCS SubsystemsTarg greater than or equal to 350EF.
FSAR Chapter 6.2, Containment Systems
FSAR Chapter 9.2, Service Water System
OPS Form 3609.1-1, IST Pump Test Plan
Millstone Nuclear Power Station Unit 2 Technical Specifications 3.5.2.a, 4.0.5, and 4.5.2.d
Millstone Nuclear Power Station Unit 2 Technical Specifications 3.3.2.1 and 4.6.2.1.1.b
Millstone Nuclear Power Station Unit 2 (MNPS-2) Final Safety Analysis Report (FSAR),
Sections 6.3 and 6.4.
SV-138, (Excerpted) Hydroset Analysis - Dresser Safety Valve Report
MP-05-DC-REF02, Verification Determination and Standards
M3-EV-98-0183, MSSV Set Pressure Test Validation
Dresser Letter dated 2/14/2005, Certificate of Compliance
MTDI 4.02, MTE Calibration
Calibration Verification of Hydroset 1566-2, dated 2/9/2000
MTE-HEI-004, Heise Pressure Gauge
10CFR Part 21, Notification 1566 Hydroset Constant dated August 3, 1990
WC-10, Revision 005-01, Temporary Modifications
WC-10-006, Revision 000, Equipment Used For Testing and Maintenance Design Configuration
Review
Attachment
A-14
Section 1R23: Temporary Plant Modifications
CR-05-01595, Negative Trend Identified Regarding Compensatory Cooling of Vital Electrical
Equipment Rooms
CR-05-00360, During the Implementation of Comp Cooling for the East 480V Switchgear Room
(OP-2315D), Door 203-31-008 (#229) was Improperly Left Closed
CR-05-00370, Follow Up Details for CR-05-00360 Related to Performance of OP-2315D
Compensatory Cooling Section for East 480 Volt Switchgear Room
CR-05-00922, Temporary Air Compressor Dryer Prefilters High DP and Lowering Air Pressure
CR-04-10102, Freeze Protection not Apparent on Temporary Air Compressor Dryer Assy.
OP-2332B, Revision 019-08, Instrument Air System
OP-2315D, Revision 012-03, Vital Electrical Switchgear Room Cooling Systems
OP-3225A, Revision 022-01, Circulating Water
Unit 2 Shift Orders
MP3 Shift Turnover Report
WC-10, Revision 005-02, Temporary Modification
MP-14-OPS-GDL200, Revision 009, Attachment 2, MP2 Shift Turnover Report (Sheet 6 of 10)
Section 1EP4: Emergency Action Level (EAL) and Emergency Plan (E-Plan) Changes
Millstone Emergency Plan and Implementing Procedures
Section 1EP6: Drill Evaluation
NEI 99-01, Revision 4, Permanently Defueled Station IC/EALs
Simulator Exercise Guide Approval Sheet, Operational Exercise #3, Loss of All AC Power
During Shutdown Conditions, Abnormal Events During RIO, Fuel Handling Accident
MP-26-EPA-REF02, Revision 005, Millstone Unit 2 Emergency Action Level (EAL) Technical
Basis Document
Emergency Action Level Tables
LORTSE11, Revision 5, Change 3, Unit 3 Simulator Exam Overview
DNAP-2605, Revision 0, Emergency Preparedness Performance Indicators
MP-26-EPA-GDL01, Revision 002, Attachment 1, Drill and Exercise Performance Indicator
Evaluation Form
Millstone Emergency Plan, Revision 30, December 2003, Page I-2 of 8
Section 2OS1: Access Control to Radiologically Significant Areas
Procedures
RPM 1.3.8, Revision 8, Criteria for Dosimetry Issue
RPM 1.4.1, Revision 7, ALARA Reviews and Reports
RPM 1.4.2, Revision 2, ALARA Engineering Controls
RPM 1.4.4, Revision 2, Temporary Shielding
RPM 1.5.2, Revision 4, High Radiation Area Key Control
RPM 1.5.5, Revision 4, Guidelines for Performance of Radiological Surveys
Attachment
A-15
RPM 1.5.6, Revision 3, Survey Documentation and Disposition
RPM 2.1.1, Revision 5, Issuance and Control of RWPs
RPM 2.1.2, Revision 2, ALARA Interface with the RWP Process
RPM 2.2.8, Revision 2, Underwater Radiological Surveys
RPM 2.4.1, Revision 3, Posting of Radiological Control Areas
RPM 2.5.1, Revision 1, Health Physics Requirements for Diving Operations
RPM 2.5.2, Revision 2, Guidelines for Spent Fuel Pool & Flooded Reactor Cavity Work
RPM 2.5.7, Revision 0, SAIC Underwater Personnel Dosimetry Operation
RPM 2.5.8, Revision 2, Staytime Tracking & Multi-badging for Special Work
RPM 5.2.2, Revision 10, Basic Radiation Worker Responsibilities
RPM 5.2.3, Revision 3, ALARA Program and Policy
RPM-GDL-008, Revision 0, Electronic Dosimeter Alarm Setpoints
MP-02-NO-GDL110, Revision 0, oversight by Nuclear Specialists
EN 31013, Revision 2, Spent Fuel Pool Operations
Nuclear Oversight Field Observations (QCFOB):
05-006, 04-04204-036,04-034, 04-031
Condition Reports:
05-01236, 05-01614, 05-01631, 04-11038, 04-11230, 04-11288, 04-09849, 04-10328,
04-09176, 04-07577
ALARA Council Meeting Notes:
Meetings conducted on: 02/08/2005, 02/16/2005
Section 4OA3: Event Followup
CR-05-00399, Unusual Event Declared Due to Fire
Incident Report Forms
Section 4OA5: Other Activities
NUREG/CR-2792, An Assessment of Residual Heat Removal and Containment Spray Pump
Performance Under Air and Debris Ingesting Conditions
PI&D 12179-EM-112A, Revision 42, Low Pressure Safety Injection
SP-3610A.3, Revision 005-03, RHR System Vent and Valve Lineup Verification
MP3-EV-04-0021, Revision 1, Assessment for as Accumulations in the RHR A Train Piping as
Documented in CR-04-05384, CR-04-05822, and CR-04-06615
M3-EV-04-0021, Revision 2, Assessment for Gas Accumulations in the RHR A Train Piping as
Documented in CR-04-05384, CR-04-05822, CR-04-0-06615, CR-04-6697 and
CR-04-10129
CR-05-00835, Small Amount of Air Found at 3SIL*V875 Following Run on Miniflow
Recirculation
Attachment
A-16
MP3-080-04, Revision 0, Operability Determination for CR-04-10129
MP3-080-04, Revision 1, Operability Determination for CR-04-10129
LIST OF ACRONYMS
AC alternating current
ALARA as low as reasonably achievable
CFR Code of Federal Regulations
CR condition report
CRAC control room air condition
DRP Division of Reactor Projects
DRS Division of Reactor Safety
EBFS enclosure building filtration system
EAL emergency action level
ECCS emergency core cooling system
EDG emergency diesel generator
EHC electro hydraulic control
ESF emergency safeguards features
FSAR Final Safety Analysis Report
HX heat exchanger
IAC instrument air compressor
IMC Inspection Manual Chapter
IST in-service testing
JW jacket water
LCO limiting condition of operations
LER Licensee Event Report
LHRA locked high radiation area
LOCA loss of coolant accident
LOE level of effort
LPSI low pressure safety injection
MCC motor control center
MDAFWP motor-driven auxiliary feedwater pump
MIDS moveable-in core detector
MR Maintenance Rule
NCV non-cited violation
NRC Nuclear Regulatory Commission
OE operating experience
OP operating procedure
OWA operator workaround
PI&R problem identification and resolution
PM planned maintenance
Attachment
A-17
PMT post maintenance testing
RPCCW reactor plant component cooling water
RSS recirculation spray system
RWP radiation work permits
SCCM standard cubic centimeter per minute
SSC structures, systems and components
SDP significance determination process
TDAFW turbine-driven auxiliary feedwater
TS technical specification
480VACS 480 volt vital AC system
VHRA very high radiation area
Attachment