ML031220563

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IR 05000327-03-003 and IR 05000328-03-003 on 04/05/03 for Sequoyah Nuclear Power Plant
ML031220563
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 05/02/2003
From: Cahill S
Reactor Projects Region 2 Branch 6
To: Scalice J
Tennessee Valley Authority
References
IR-03-003
Download: ML031220563 (30)


See also: IR 05000328/2003003

Text

May 2, 2003

Tennessee Valley Authority

ATTN: Mr.J. A. Scalice

Chief Nuclear Officer and

Executive Vice President

6A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

SUBJECT: SEQUOYAH NUCLEAR POWER PLANT - NRC INTEGRATED INSPECTION

REPORT 50-327/03-03 AND 50-328/03-03

Dear Mr. Scalice:

On April 5, 2003, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

the Sequoyah Nuclear Power Plant, Units 1 and 2. The enclosed report presents the results of

the integrated inspection which were discussed on April 9, 2003, with Mr. Rick Purcell and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the inspectors identified one issue of very low safety

significance (Green). This issue was determined to involve a violation of NRC requirements.

However, because of its very low safety significance and because it has been entered into your

corrective action program, the NRC is treating this issue as a non-cited violation, in accordance

with Section VI.A.1 of the NRCs Enforcement Policy. If you contest this non-cited violation, you

should provide a response with the basis for your denial, within 30 days of the date of this

inspection report to the Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001, with copies to the Regional Administrator, Region II; the Director,

Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-

0001; and the NRC Resident Inspector at the Sequoyah facility.

TVA 2

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) components of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/ADAMS.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Stephen J. Cahill, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Docket Nos.: 50-327, 50-328

License Nos.: DPR-77, DPR-79

Enclosure: NRC Inspection Report 50-327/03-03, 50-328/03-03

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

TVA 3

cc w/encl: County Executive

Karl W. Singer Hamilton County Courthouse

Senior Vice President Chattanooga, TN 37402-2801

Nuclear Operations

Tennessee Valley Authority Ann Harris

Electronic Mail Distribution 341 Swing Loop

Rockwood, TN 37854

James E. Maddox, Acting Vice President

Engineering and Technical Services John D. White, Jr., Director

Tennessee Valley Authority Tennessee Emergency Management

Electronic Mail Distribution Agency

Electronic Mail Distribution

Richard T. Purcell

Site Vice President Distribution w/encl: (See page 4)

Sequoyah Nuclear Plant

Electronic Mail Distribution

General Counsel

Tennessee Valley Authority

Electronic Mail Distribution

Robert J. Adney, General Manager

Nuclear Assurance

Tennessee Valley Authority

Electronic Mail Distribution

Mark J. Burzynski, Manager

Nuclear Licensing

Tennessee Valley Authority

Electronic Mail Distribution

Pedro Salas, Manager

Licensing and Industry Affairs

Sequoyah Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

D. L. Koehl, Plant Manager

Sequoyah Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

Lawrence E. Nanney, Director

TN Dept. of Environment & Conservation

Division of Radiological Health

Electronic Mail Distribution

TVA 4

Distribution w/encl:

M. Marshall, NRR

L. Slack, RII EICS

RIDSNRRDIPMLIPB

PUBLIC

OFFICE DRP/RII DRP/RII DRP/RII DRP/RII DRSP/RII DRP/RII

SIGNATURE TCK TCK for RC TCK for SF RT

NAME TKolb:aws RCarrion SFreeman RTelson SVias

DATE 05/02/2003 05/02/2003 05/02/2003 05/02/2003 05/02/2003

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

PUBLIC DOCUMENT YES NO

OFFICIAL RECORD COPY DOCUMENT NAME: C:\ORPCheckout\FileNET\ML031220563.wpd

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-327, 50-328

License Nos: DPR-77, DPR-79

Report No: 50-327/03-03, 50-328/03-03

Licensee: Tennessee Valley Authority (TVA)

Facility: Sequoyah Nuclear Plant, Units 1 & 2

Location: Sequoyah Access Road

Soddy-Daisy, TN 37379

Dates: January 5, 2003 - April 5, 2003

Inspectors: S. Freeman, Senior Resident Inspector

R. Telson, Resident Inspector

R. Carrion, Senior Project Engineer (Section 1R06)

S. Vias, Senior Reactor Inspector (Section 40A5)

Approved by: S. Cahill, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000327-03-03, IR 05000328-03-03, Tennessee Valley Authority, 1/5/2003 - 4/5/2003

Sequoyah Nuclear Power Plant, Units 1 & 2, Operability Evaluations.

The report covered a three-month period of inspection by resident inspectors and an

announced inspection by two regional based inspectors. The significance of most findings is

indicated by their color (Green, White, Yellow, Red) using IMC 0609, "Significance

Determination Process" (SDP). Findings for which the SDP does not apply may be Green or be

assigned a severity level after NRC management review. The NRCs program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG 1649,

Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector-Identified and Self-Revealing Findings

Cornerstone: Barrier Integrity

  • Green. Inadequate technical guidance was identified because the associated

procedure did not contain the necessary steps to ensure that multiple breaches

of the shield building would be adequately controlled.

This inspector-identified finding was determined to be a non-cited violation of

(NCV) Technical Specification 6.8.1.a. It was more than minor, because if left

uncorrected it could result in the actual shield building breached area exceeding

the margin of operability for the emergency gas treatment system. The finding

also affected the configuration control attribute of the containment barrier. The

finding is of very low safety significance because the actual margin was not

exceeded. It was also considered to constitute a deficiency in the cross-cutting

element of Problem Identification and Resolution (Section 1R15 and 40A2).

B. Licensee Identified Violations

None

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near 100 percent rated thermal power until March 17, 2003 when it was

shut down for a scheduled refueling and steam generator replacement outage.

Unit 2 began the inspection period shutdown for repair of the Number 3 reactor coolant pump

motor. The motor was repaired and the unit returned to 100 percent power on January 8, 2003.

The unit operated at or near 100 percent rated thermal power until March 10, 2003, when it

tripped automatically due to problems with a heater drain tank level control valve and a hotwell

pump. The problems were repaired and the Unit returned to 100 percent power on March 18,

2003. Unit 2 was manually shutdown on March 24, 2003, due to a hydrogen leak on the main

generator. The leak was repaired on March 30, 2003 and the unit was returned to 100 percent

power.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity,

Emergency Preparedness

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors observed the licensee responsed to a tornado watch on March 19, 2003.

The inspectors reviewed licensee Procedure AOP-N.02, Tornado Watch/Warning,

Revision 11, for its effectiveness to limit the risk of tornado-related initiating events and

to adequately protect mitigating systems from the effects of a tornado. In addition, the

inspectors verified the securing of large outside cranes in accordance with guidance in

Topical Report 24370-TR-C-002, Rigging and Heavy Load Handling.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

The inspectors conducted partial walkdowns of the following three systems to verify the

availability of redundant or diverse systems and components and that defense-in-depth

was maintained during periods when safety equipment was inoperable. The inspectors

reviewed applicable operating procedures, walked down critical system components,

and reviewed identified problems to ensure they were entered into the corrective action

program. Documents reviewed are listed in the attachment.

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Water Pump 1A-A

  • A-Train electric board room chiller during unavailability of B-train electric board

room chiller

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors conducted a tour of eight areas to assess the material condition,

operational status, and lineup of fire protection systems, equipment, and features. The

inspectors assessed control of transient combustibles and ignition sources, and verified

fire protection equipment was available for use. Documents reviewed are listed in the

attachment. The areas toured are listed below.

  • Essential Raw Cooling Water Building
  • Turbine Building Elev. 662
  • Auxiliary building Elev. 714 (temporary containment access pathway)

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

a. Inspection Scope

The inspectors reviewed selected risk-important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

and external flooding events. The inspectors reviewed flood analysis and design

documents including UFSAR Sections 2.3 and 2.4, including Appendix 2.4A, Flood

Protection Plan, and Design Criteria Document SQN-DC-V-12.1, Sequoyah Nuclear

Plant - Flood Protection Provisions, for licensee commitments. The inspectors also

reviewed licensee instructions for cross-tying systems in the event of severe flooding

and evaluated the availability of a selected Unit 1 spool piece identified in the

instructions and on Drawing 1,2-47W845-2, Flow Diagram - Essential Raw Cooling

Water System. The inspectors reviewed selected risk-important external flood

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protection barriers to evaluate the inadequacy at protecting risk-important equipment.

The inspectors performed a walkdown of risk-significant areas, susceptible systems,

and equipment to verify that the respective floor drain system, including room sump

pumps, was operable, including:

  • Essential Raw Cooling Water (ERCW) pump house elevations 704' and 720'
  • 161-kV cable tunnel

The inspectors reviewed the following plant procedures for coping with flooding events

to verify that the actions were consistent with the plants design basis assumptions:

  • AOP-N.04, Revision 5, Break of Downstream Dam

The inspectors also reviewed the licensees corrective action documents with respect to

flood-related items identified in Problem Evaluation Reports (PERs) written in 2002 to

verify the adequacy of the corrective actions:

  • PER 02-003277-000, AOP-N.04, Break of Downstream Dam, was revised to add

steps to makeup to the forebay using ERCW to maintain the required level.

  • PER 02-005674-000, AOP-N.03, Flooding, was revised to re-align the sluice

gates not previously included in the procedure to satisfy the requirements of

Design Criteria SQN-DC-V-12.1, Flood Protection Provisions.

The inspectors also reviewed completed preventive maintenance procedures for

monthly checks for standing water in manholes/handholes for September and

December 2002 and related PER 03-000418-000.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

a. Inspection Scope

The inspectors observed simulator training on February 19, 2003. The scenario

involved a leak on the Residual Heat Removal (RHR) system during mid-loop

operations. The leak was within the capability of the charging system. This placed the

simulated unit in the abnormal operating procedure for RHR malfunctions.

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The inspectors observed crew performance to ensure the following criteria were

satisfied: appropriate communications; ability to take timely and proper actions;

prioritizing, interpreting, and verifying alarms; correct use and implementation of

procedures, including the alarm response procedures; timely control board operation

and manipulation, including high-risk operator actions; oversight and direction provided

by the shift manager, including the ability to identify and implement appropriate

Technical Specification (TS) actions; and group dynamics involved in crew performance.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed six activities to verify that the appropriate risk assessments

were performed prior to removing equipment for work. When emergent work was

performed, the inspectors verified that the risk for the work was assessed and required

equipment was protected. The inspectors referenced Procedure SPP-7.1, Work

Control Process, Revision 4, and Instruction, 0-TI-DSM-000-007.1, Equipment to Plant

Risk Matrix, Revision 7, during these inspection activities.

for check valve testing

  • Loss of Unit 2 Refueling Water Storage Tank (RWST) Instrumentation

in-service testing

  • Operational Defense-in-Depth Assessment for Week of March 21, 2003

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-Routine Plant Evolutions

a. Inspection Scope

The inspectors reviewed operating crew performance and plant indications associated

with the automatic reactor trip and loss of secondary heat sink that occurred on

March 10, 2003, while Unit 2 was operating at 100 percent power. The review evaluated

what occurred and how operators responded to the event. The inspectors reviewed

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plant operating logs, plant computer information, associated PERs, and conducted

discussions with operations and engineering personnel. The inspectors also reviewed

plant procedures, to determine whether the operators response was in accordance with

those procedures.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed seven selected functional evaluations and related documents

to verify that the licensee had adequately assessed TS operability. In addition, the

inspectors reviewed applicable documents to verify that the system or component was

capable of performing required functions and any required compensatory actions were

properly implemented. The inspectors reviewed the functional evaluations against the

requirements of licensee Procedure SPP-10.6, Engineering Evaluations for Operability

Determination. Additional documents reviewed are listed in the attachment.

  • PER 03-000564-000, Rag found under EDG 1A2 engine lube oil strainer
  • PER 03-000290-000, Inability to reach Mode 5 in 30-hour limit required by TS
  • PER 03-000830-000, Damage to EDG 1B-B battery due to momentary short

during testing

  • PER 03-000835-000, EDG 1B-B Stator Winding Polarization Index below IEEE

Standard 43

  • Breach Permit VBP-2002-0071, Core Drill 4 inch diameter scaffold holes in Unit

1 Shield Building

  • PER 03-001354-000, EDG 2A1 Pillow Block Bearing Alignment
  • PER 03-003216-000, High temperature conductor feeding electric board room

chiller B-B

b. Findings

Introduction: In reviewing the operability evaluation and associated aspects of a four-

inch diameter hole drilled in the dome of the Unit 1 Shield Building for the steam

generator replacement outage, the inspectors identified a green NCV for failure to

provide complete instructions governing shield building breaches.

Description: The licensee opened the four-inch diameter shield building breach to allow

workers to pass scaffold material through the dome rather than carry it up the ladder in

the annulus. The licensee further indicated that the breach area had been analyzed and

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was less than the area that would affect the operability of the Emergency Gas

Treatment System (EGTS) and annulus vacuum systems. The inspectors reviewed the

breach permit for the hole; V.P.-2002-0071; the associated operability evaluation; and

Calculation 65NQL041296, Determine Maximum Breach Area Between Auxiliary

Building Secondary Containment Envelope, Outside, and The Shield Building. The

inspectors noted that the area of the shield building breach was 12.57 square inches

and that the calculation allowed 14 square inches before affecting the operability of the

EGTS System, a margin of less than two square inches.

On February 15, 2003, the licensee initiated Problem Evaluation Report (PER) 03-

001577-000, which identified that two other shield building breaches had not been

documented on Vent Boundary Tracking Sheets. Because this indicated the possibility

of three simultaneous breaches of the shield building, the inspectors reviewed the

tracking sheets, Procedure, 0-TI-SXX-000-016.0, Breaching The Shield Building,

Auxiliary Building Secondary Containment Envelope (ABSCE), or Control Room

Boundaries, Revision 15, and interviewed personnel associated with installation of the

breaches. The inspectors determined that the work documents which installed the

breaches adequately controlled the work such that the amount of shield building area

open at any one time was less than 14 square inches. However, the inspectors

subsequently identified that this control was only successful in this case because all

three breaches were controlled by the same organization, (i.e. the Steam Generator

Replacement Project).

Procedure 0-TI-SXX-000-016.0 controlled breaches via appendices, one for each area,

with instructions for anyone using the procedure to go directly to the applicable

appendix. The inspectors determined that, even though a general precaution specified

a vent boundary log, there were no specific instructions in the appendix for shield

building breaches (Appendix D) that required breaches to be logged or required that the

breached area be added to the log when a permit was approved. Without these

instructions the inspectors concluded that specific breaches could be missed and not

logged as happened with the two breaches in PER 03-001577-000.

Analysis: The inspectors determined that this finding affected only the radiological

barrier function of the containment. If left uncorrected it could result in the actual

breached area exceeding the margin of operablility for the EGTS system, a more

significant safety concern. The finding also affected the configuration control attribute of

the containment barrier. This makes it more than minor. However, because the actual

margin was not exceeded, there was no degradation to the radiological barrier function

of the containment. Therefore, the inspectors considered the finding to be of very low

safety significance (Green).

The inspectors also determined that there was a Problem Identification and Resolution

(PI&R) aspect to this finding. PER 03-001577-000 identified that two shield building

breaches had not been tracked. However, the PER did not identify the lack of specific

instructions nor consider that the undocumented breaches had the potential to allow

enough of the shield building to be breached to exceed the margin of operability for the

EGTS system. The inspectors therefore considered this finding to indicate a potential

problem identification deficiency and have noted it in Section 4OA2.

7

Enforcement: TS 6.8.1.a, requires that activities affecting quality be prescribed and

accomplished using instructions, procedures, or drawings In Accordance With (IAW)

Regulatory Guide 1.33, Revision 2, February 1978. RG 1.33 requires procedures for

performing maintenance that can affect the performance of safety-related equipment.

Contrary to this, Procedure 0-TI-SXX-000-016.0, which was designated quality related

and controlled work on the safety-related containment barrier, did not contain the

instruction steps necessary to ensure that multiple breaches of the shield building would

be adequately controlled. This is a violation of TS 6.8.1.a. Because it is of very low

safety significance and has been entered into the licensees corrective action program

as PER 03-003612-000, this violation is being treated as an NCV, consistent with

Section VI.A of the NRC enforcement policy: NCV 50-327/03-03-01, Inadequate

Instructions for Controlling Shield Building Breaches.

1R16 Operator Workarounds

a. Inspection Scope

The inspectors reviewed operator actions to manually start and load the security diesel

generator while its auto start feature was out of service to determine whether the

functional capability of the diesel was affected. The inspectors specifically considered

whether the workaround affected the operators ability to implement abnormal or

emergency operating procedures. Documents reviewed are listed in the attachment.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the five post-maintenance tests listed below to verify that

procedures and test activities ensured system operability and functional capability. The

inspectors reviewed the licensees test procedure to verify that the procedure

adequately tested the safety function(s) that may have been affected by the

maintenance activity, that the acceptance criteria in the procedure were consistent with

information in the applicable licensing-basis and/or design-basis documents, and that

the procedure had been properly reviewed and approved. The inspectors also

witnessed the test or reviewed the test data, to verify that test results adequately

demonstrated restoration of the affected safety function(s). Additional documents

reviewed are listed in the attachment.

  • WO 03-000284-000, Transfer switch 0-XSW-201-DA for the Security BU DG

failed to properly transfer during testing

  • 1-PI-EFT-082-002.B, Diesel Generator 1B-B Two (2) Year Electrical Inspection,

Revision 4

8

  • 0-SI-EBT-082-238.2, Diesel Generator Battery Quarterly Operability, Revision 8
  • WO 03-001019-000, Electric Board Room Chiller Package B-B, Repair leaks,

Recharge, and Retest

  • WO 03-002725-000 Repair 1-PSV-068-0340A0, Unit 1 pressurizer power

operated relief valve

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities

a. Inspection Scope

The inspectors reviewed the outage safety plan and contingency plans for the Unit 1

refueling and steam generator replacement outage to confirm that the licensee had

appropriately considered risk, industry experience, and previous site-specific problems

in developing and implementing a plan that assured maintenance of defense-in-depth.

Between March 17, 2003 and April 5, 2003, the inspectors observed portions of the

shutdown and cooldown processes to verify compliance with TS cooldown restrictions

and monitored licensee controls over the outage activities listed below. Documents

reviewed during the inspection are listed in the attachment.

  • Licensee configuration management, including daily outage reports, to evaluate

defense-in-depth commensurate with the outage safety plan and compliance

with the applicable TS when taking equipment out of service.

  • Licensee implementation of clearance activities to ensure equipment was

appropriately configured to safely support the work or testing.

  • Installation and configuration of reactor coolant instruments to provide accurate

indication and an accounting for instrument error.

  • Controls over the status and configuration of electrical systems and switchyard to

ensure that TS and outage safety plan requirements were met.

generators, when relied upon, were a viable means of backup cooling.

  • Controls to ensure that outage work was not impacting the ability to operate the

spent fuel pool cooling system during and after core offload.

alternative means for inventory addition, and controls to prevent inventory loss.

  • Reactivity controls to verify compliance with TS and that activities which could

affect reactivity were reviewed for proper control within the outage risk plan.

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  • Containment closure for control of containment penetrations in accordance with

refueling TS, to ensure that containment closure could be achieved during

selected configurations, and to verify maintenance of secondary containment in

accordance with TS.

  • Defueling activities for compliance with TS and to verify proper tracking of fuel

assemblies from the core to the spent fuel pool.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed surveillance tests and/or reviewed test data of six risk-

significant structures, systems and components (SSC) conducted using the surveillance

instructions, listed below, to assess, as appropriate, whether the SSCs met TS

operability requirements, the Updated Final Safety Analysis Report (UFSAR) and

licensee procedure requirements, and to determine if the testing effectively

demonstrated that the SSCs were operationally ready and capable of performing their

intended safety functions.

  • 1-SI-SXP-062-201.B, Centrifugal Charging Pump 1B-B Performance Test,

Revision 7*

  • SI-90.8, Reactor Trip Instrumentation Monthly Functional Test (SSPS),

Revision 25 (Unit 1 Train B)

Performance Test, Revision 13*

  • 0-SI-OPS-082-007.W, AC Electrical Power Source Operability Verification,

Revision 6

  • 1-SI-OPS-000-002.0, Shift Log, Revision 65
  • 1-SI-OPS-082-024.A, 1A-A DG 24 Hour Run and Load Rejection Test,

Revision 9

  • This procedure included inservice testing requirements.

b. Findings

No findings of significance were identified.

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1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the temporary modification described in Temporary Alteration

Control Form (TACF) 2-02-0018-063, Unit 2 refueling water storage tank heaters, to

verify that the design was adequate, the modification was properly installed, the

modification did not affect system operability, drawings and procedures were

appropriately updated, and post-modification testing was satisfactorily performed.

Documents reviewed are listed in the attachment.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

a. Inspection Scope

The inspectors sampled licensee submittals for the PIs listed below for the period

January 1, 2002, through December 31, 2002. To determine the accuracy of the PI

data reported for that period, guidance contained in NEI 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 2, was used to verify the basis for reporting

each indicator.

Cornerstone: Initiating Events

  • Unplanned Scrams per 7000 Critical Hours
  • Scrams With Loss of Normal Heat Removal

The inspectors reviewed selected LERs and portions of the operator logs to verify that

the licensee had accurately identified the number of scrams and unplanned power

changes greater than 20 percent that occurred during the previous four quarters for both

units. The inspectors also reviewed the accuracy of the number of critical hours

reported and the licensees basis for crediting normal heat removal capability for each of

the reported scrams.

b. Findings

No findings of significance were identified.

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4OA2 Identification and Resolution of Problems

Section 1R15 describes a finding for a procedure that did not contain the instructions

necessary to ensure that multiple breaches of the shield building would be adequately

controlled. The licensee had written PER 03-001577-000 and identified that two shield

building breaches had not been tracked. However, the PER did not identify the lack of

specific instructions nor consider that the undocumented breaches had the potential to

allow enough of the Shield building to be breached to exceed the margin of operability

for the EGTS system. The inspectors therefore considered this finding to indicate a

potential problem identification deficiency.

4OA3 Event Follow-up

.1 Frozen RWST Level Instrumentation (NOED 03-6-001)

On January 24, 2003, Unit 2 RWST wide range level transmitters 2-LT-63-50 and 2-LT-

63-52 failed when the impulse lines froze due to a failure of the strip heaters within the

transmitter enclosures. This resulted in the licensee entering TS 3.0.3. The licensee

requested and was granted discretion from enforcement of TS 3.3.2.9.a, which required

three of four channels to be operable. The NRC granted a one-time 48-hour reduction

in the required minimum number of operable channels from three to two to permit the

licensee to repair the transmitters without shutting down the unit.

The licensee agreed to the following compensatory measures during the period the

NOED was in effect: (1) establishment of temporary heat for all RWST wide level

transmitters for both units, (2) the establishment of a fire watch to monitor the additional

temporary heat, (3) briefing of licensed operators on the situation and review of

procedural operation for manual Emergency Core Cooling System (ECCS) switch over

from the RWST to the containment sump, (4) suspension of all work involving the

RWST channels for both units, and (5) increased Unit 1 RWST level monitoring

frequency from every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> to every 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

The inspectors reviewed the cause and compensatory measures to ensure they

matched the licensees oral assertions and were consistent with NRC policy and

guidance. Pending evaluation of the root cause of the problem leading to the request

for enforcement discretion, and any associated enforcement, this issue is identified as

URI 50-328/03-03-02 Frozen RWST Instrumentation (NOED 03-6-001). Documents

reviewed are listed in the attachment.

.2 Containment Purge Valve Leakage (NOED 03-2-004)

On February 27, 2003, Unit 2 containment penetration X-6 purge valves 2-FCV-30-50

and 2FCV-30-51 failed a local leak rate test due to a broken key on the stem of the

inboard valve. The as-found leakage of 29.6 scfm exceeded the TS 3.6.1.9 acceptance

limit of 11.25 scfm (0.05La). The licensee requested and was granted discretion from

enforcement of TS 3.6.1.9 Action b, which required the inoperable valves to be restored

within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The NRC granted an additional 144 hours0.00167 days <br />0.04 hours <br />2.380952e-4 weeks <br />5.4792e-5 months <br /> for the licensee to identify

the source of leakage, repair or replace the valve(s), and to perform verification testing

without shutting down the unit.

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The licensee agreed to the following compensatory measures during the period the

NOED was in effect: (1) one valve in Penetration X-6 would be closed and deactivated

at all times with leak rate monitoring during the maintenance activity, (2) if overall

containment leakage increased to 0.06La the shutdown actions of TS 3.6.1.9.b would be

implemented, (3) the scheduled testing of Diesel Generator 2A-A would be postponed to

outside the NOED repair activity and no component would be removed from service that

would cause the ORAM-Sentinel risk significance to go above the Green level, (4)

containment purge operations would not be allowed for the duration of the valve

maintenance, and (5) the activity of the reactor coolant would be monitored to provide

early detection of an adverse trend.

The inspectors reviewed the cause and compensatory measures to ensure they

matched the licensees oral assertions and were consistent with NRC policy and

guidance. Pending evaluation of the root cause of the problem leading to the request

for enforcement discretion and any associated enforcement, this issue is identified as

URI 50-328/03-03-03 Containment Purge Valve Leakage. Documents reviewed are

listed in the attachment.

.3 Unit 2 Manual Reactor Trip With Loss of Normal Heat Sink

On March 10, 2003, following a Unit 2 manual reactor trip due to the loss of condensate

pressure and one main feed water pump, the inspectors evaluated plant status,

mitigating actions, and the licensees classification of the event, to enable the NRC to

determine an appropriate NRC response. Balance-of-plant problems following the trip

resulted in the operators breaking vacuum and closing main steam isolation valves,

which resulted in a loss of the normal heat sink. The event was reported to the NRC as

event notification39652 and documented in the licensee corrective action program

as PER 03-002313-000. Evaluation of personnel performance is addressed in Section

1R14.

.4 (Closed) Licensee Event Report (LER) 50-328/2002-003-00, Automatic Reactor Trip

Resulting from a Generator Stator Cooling Water High Temperature Caused by a Raw

Cooling Water Valve Failure.

The LER was reviewed by the inspectors and no findings of significance were identified.

The licensee documented the event and failed equipment in PERs 02-006086-000, 02-

006114-000, and 01-005036-000. This event did not constitute a violation of NRC

requirements. This LER is closed.

The licensee included additional information in this LER regarding the delayed insertion

of Rod Control Cluster Assembly (RCCA) L-11 during the trip. This item has been

previously reviewed by the NRC and is the subject of unresolved item (URI) 50-327,

328/02-02-05, Corrective Actions Related to the Apparent Failure of RCCA L-11 to

Properly Insert.

.5 (Closed) LER 50-327/2002-002-00, Automatic Reactor Trip Resulting From a Failure of

a Breaker Causing an Undervoltage Condition on Two Reactor Coolant Pumps and

Failure to Perform a Technical Specification Required Action

13

The LER was reviewed by the inspectors and no findings of significance were identified.

The licensee documented the event and failed equipment in PER 02-008460-000.

In addition to the event described in this report, the licensee identified that offsite power

to both units was affected by the loss of Start Bus 2B. With one source of offsite power

unavailable to Unit 1, TS 3.8.1.1 required that the remaining source be demonstrated

operable within one hour. The licensee determined that this was not done but later

demonstrated that the proper offsite sources were operable. This licensee identified

violation was previously discussed in Inspection Report 50-327,328/02-04 (Section

4OA7). The inspectors review did not identify any new findings. The licensee

documented the problem in PER 02-008493-000. This LER is closed.

.6 (Closed) LER 50-328/2002-004-00, Reactor Trip Resulting From The Loss of a Reactor

Coolant Pump

The LER was reviewed by the inspectors and no findings of significance were identified.

The licensee documented the event failed equipment in PERs 02-015494 and-000 03-

000190-000. This event did not constitute a violation of NRC requirements. This LER is

closed.

4OA5 Other Activities

.1 NRC Temporary Instruction (TI) 2515/150, Reactor Pressure Vessel Head and Vessel

Head Penetration Nozzles (NRC Bulletin 2002-02)

a. Inspection Scope

The inspectors reviewed the Unit 1 bare metal visual examination and susceptibility

calculations performed by the licensee in response to the NRC Order EA-03-009 on

interim inspection requirements for reactor pressure vessel heads dated February 11,

2003. The inspection guidelines were provided in TI 2515/150. Additional documents

are listed in the attachment.

b. Findings and Observations

No findings of significance were identified. Per the documentation requirements of TI

2515/150, the following attributes were observed:

Verification that visual examination was performed by qualified and knowledgeable

personnel

Two teams of three individuals performed the examination of the Unit 1 reactor head.

One team worked the day shift and one team worked the night shift. One individual on

each shift was a licensee Level III Non-Destructive Examination (NDE) qualified to

perform VT-2 inspections. The inspectors reviewed the qualification records and

verified that these individuals were certified as Level III VT-2 inspectors.

14

The other members of each team were vendor employees that operated the remote

video camera equipment. These individuals had performed the same examination on

Unit 2 in the fall of 2002. The inspectors interviewed all of the individuals and noted they

were knowledgeable of the criteria to determine leakage.

Verification that visual examination was performed in accordance with demonstrated

procedures

The inspectors reviewed Procedure N-VT-17, Visual Examination for Leakage of

Pressurized Water Reactor (PWR) Head Penetrations, Revision 2. The inspectors

observed that the examination was done using this procedure. The inspectors verified

by direct observation and in discussions with examination personnel that the approved

acceptance criteria for head leakage were applied in accordance with the procedures.

Verification that the licensee was able to identify, disposition, and resolve deficiencies

The licensees examination plan included a VT-2 examination using a remote crawler

with attached video cameras in the front and rear. In addition, the examination used the

resolution level of a VT-1. The licensee recorded all examinations of the nozzles. Any

suspected leakage observed by the visual examination was noted and reviewed by

materials engineers. The inspectors verified that the examination results for each

nozzle were individually documented.

Verification that the licensee was capable of identifying the Primary Water Stress

Corrosion Cracking (PWSCC) phenomenon described in the bulletin

The inspectors visually observed the Unit 1 reactor head during the licensees

examination; observed the licensee conduct the examination; discussed the examination

with the licensee examiners prior to, during, and following the examination; and verified

the qualifications of the licensee examination personnel. The inspectors concluded that

the licensees visual examination was adequate to identify potential leakage resulting

from PWSCC cracking of reactor head penetrations.

Evaluate condition of the reactor vessel head (debris, insulation, dirt, boron from other

sources, physical layout, viewing obstructions)

The inspectors viewed the condition of the Unit 1 reactor vessel head via remote video

and performed a direct observation of the peripheral portions of the head. There was

some debris around several nozzles (metal shavings, nails, other construction type

debris). Most of the debris was removed with compressed air. Those nozzles where

the debris could not be removed were reviewed by engineering. At four locations the

licensee used a wedge to support the insulation shroud to allow room for the crawler to

reach the upper portions of the head. The inspectors concluded that this was only a

minimal obstruction and that the annulus area of nozzles near the wedge could be

viewed from the entire circumference. The inspectors observed no other significant

items that prevented a thorough visual examination.

15

Evaluate ability for small boron deposits, as described in the bulletin, to be identified and

characterized

The inspectors observed that the reactor head was generally free of any deposits that

would have hindered the visual examination. The licensee observed evidence of boric

acid leakage around Nozzle 3, performed follow-up NDE on this nozzle, and found no

evidence of a leak path. In addition, the licensee characterized six nozzles on the

periphery of the head (Nozzles 53, 64, 65, 72, 73, and 78) as indeterminate due to

either heavy debris or boron deposits. They performed NDE on five of these nozzles

with no indication of a leak path. The licensee did not perform any extra testing on

Nozzle 78, but determined from isotopic analysis that the boron deposits on this nozzle

as well as those on Nozzle 3 came from external leakage on a previous cycle.

Determine extent of material deficiencies (associated with the concerns identified in the

bulletin) which were identified that required repair

The licensee found boron deposits around Nozzle 3 and boron deposits on six nozzles

around the periphery of the head. The licensee performed NDE on these nozzles to

clarify whether or not the deposits were from inside the head. All NDE results were

negative. Additional inspection per Technical Instruction 2515/150 will be performed for

Unit 1 in the next inspection period. This will include a more in-depth review of the

identified indications in the nozzles and if Reactor Coolant System (RCS) pressure

boundary leakage existed. Technical Instruction 2515/150 will remain open pending

completion of the inspection objectives.

Determine any significant items that could impede effective examinations

Other than those minor examples mentioned above, the inspectors observed no

examples of significant items that could impede the visual examination process.

Determine the basis for the temperatures used in the susceptibility ranking calculation

The licensee used 547°F as the head temperature in the calculation. This was based

on the reactor vessel inlet temperature, T-cold, described in the UFSAR, and test data.

In January, 1981, the licensee placed five thermocouples on the Unit 1 head to test

bypass flow modifications and to confirm the existence of enhanced flow in the head.

The test data showed the head temperature to match T-cold. The inspectors reviewed

the UFSAR and the test data. The test data showed that the lowest T-cold measured

was generally higher than the highest head temperature. In cases where the head

temperature exceeded T-cold, the difference was 3°F or less. Based on this data and

the UFSAR T-cold of 544.8°F, the inspectors determined the calculation was

conservative. The inspectors also checked Unit 2, which was operating at full power

and confirmed that T-cold temperature was less than 547°F.

16

.2 Steam Generator Replacement (SGR) Inspection Overview

This inspection report documents completion of inspections required by Inspection

Procedure (IP) 50001, Steam Generator Replacement Inspection, some of which were

completed in accordance with baseline inspection procedures. The table below

identifies and correlates specific IP 50001 inspection requirements examined during this

inspection period with the corresponding sections of this report.

IP 50001 Section of

Section Inspection Scope This Report

02.02.d.2. Controls and plans to minimize any adverse impact on the 1R4, 1R20,

operating unit and common systems 4OA5.4

02.03.e.1. Establishment of operating conditions including defueling, 1R20

RCS draindown, system isolation and safety tagging

02.03.e.2. Implementation of radiation protection controls 4OA5.3

02.03.e.4. Installation, use, and removal of temporary services 1R20,

4OA5.3

.3 SGR Operating Conditions, Radiation Protection Controls, and Temporary Services

a. Inspection Scope

As required by IP 50001 Section 02.03.e, throughout this inspection period, the

inspectors routinely inspected the following activities as they occurred:

  • Establishment of operating conditions including defueling, RCS draindown, and

system isolation and safety tagging/blocking.

  • Implementation of radiation protection controls.
  • Installation, use, and removal of temporary services directly related to steam

generator replacement activities.

b. Findings

No findings of significance were identified.

17

.4 SGR Controls to Minimize Adverse Impact on Operating Unit

a. Inspection Scope

As required by IP 50001 Section 02.02.d.2, the inspectors reviewed plans and

periodically monitored licensee controls to minimize any adverse impact on the

operating unit and common systems. Specific areas reviewed included:

  • Modifications to the ABSCE

b. Findings

No findings of significance were identified.

4OA6 Meetings, including Exit

.1 Exit Meeting Summary

On April 9, 2003, the resident inspectors presented the inspection results to Mr. Rick

Purcell and other members of his staff, who acknowledged the findings. The inspectors

confirmed that proprietary information was not provided nor examined during the

inspection.

.2 Annual Assessment Meeting Summary

Subsequent to the end of this inspection period, on April 10, 2003, the NRCs Chief of

Reactor Projects Branch 6 and the Senior Resident Inspector assigned to the

Sequoyah Nuclear Plant met with the Tennessee Valley Authority (TVA) to discuss the

NRCs Reactor Oversight Process (ROP) and the Sequoyah annual assessment of

safety performance for the period of January 1, 2002 - December 31, 2002. The major

topics addressed were: the NRCs assessment program, the results of the Sequoyah

assessment, and NRC security activities. Attendees included Sequoyah site

management, members of site staff, and corporate management.

This meeting was open to the public. The presentation material used for the discussion

is available from the NRCs document system (ADAMS) as accession number

ML031130023. ADAMS is accessible from the NRC Web site at

http://www/nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel:

J. Bajraszewski, Licensing Engineer

T. Carson, Maintenance Manager

H. Cothran, Steam Generator Manager

D. Clift, Acting Maintenance and Modifications Manager

E. Freeman, Operations Manager

J. Gates, Business & Work Performance Manager

C. Kent, Radcon/Chemistry Manager

D. Koehl, Plant Manager

M. Lorek, Assistant Plant Manager

D. Lundy, Site Engineering Manager

R. Purcell, Site Vice President

R. Rogers, Design Manager

P. Salas, Licensing and Industry Affairs Manager

J. Smith, Site Licensing Supervisor

K. Stephens, Security Manager

NRC personnel:

S. Cahill, Chief, Reactor Projects Branch 6

R. Bernard, Region II, Senior Reactor Analyst

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-328/2003-003-02 URI Frozen RWST Instrumentation

(Section 4OA3.1).

50-328/2003-003-03 URI Containment Purge Valve Leakage

(Section 4OA3.2).

Opened and Closed

50-327/2003-003-01 NCV Inadequate Instructions for

Controlling Shield Building Breaches

(Section 1R15 and 4OA2).

Attachment

2

Closed

50-328/2002-003-00 LER Automatic Reactor Trip Resulting

from a Generator Stator Cooling

Water High Temperature Caused by

a Raw Cooling Water Valve Failure

(Section 4OA3.4).

50-327/2002-002-00 LER Automatic Reactor Trip Resulting

From a Failure of a Breaker Causing

an Undervoltage Condition on Two

Reactor Coolant Pumps and Failure

to Perform a Technical Specification

Required Action (Section 4OA3.5).

50-328/2002-004-00 LER Reactor Trip Resulting From the

Loss of a Reactor Coolant Pump

(Section 4OA3.6).

Discussed

50-327, 328/02-02-05 URI Corrective Actions Related to the

Apparent Failure of RCCA L-11 to

Properly Insert (Section 4OA3.4).

LIST OF DOCUMENTS REVIEWED

1R04 Equipment Alignment

1,2-47W803-2, Flow Diagram, Auxiliary Feedwater, Revision 55

1R05 Fire Protection

0-PI-FPU-410-701.Q, Inspection of Fire Doors, Revision 1

0-SI-FPU-410-703.0, Inspection of FPR Required Fire Doors, Revision 2

0-SI-FPU-013-600.0, Fire Detection Panel 0-L-600 Test, Revision 0

0-SI-FPU-013-601.0, Fire Detection Panel 0-L-601 Test, Revision 0

0-SI-EFT-039-237.0, Diesel Generator Building CO2 Fire Protection System (System

39), Revision 16

Transient Combustible Evaluation 2003-0001, Reactor Building Annulus

Fire Protection Impairment Permit FOR 2003A0074, Sprinklers and detection coverage

out of service for U2 Heating and Ventilation Room - Unprotected Security Guard House

FOR 2003A0072, Sprinkler suppression and Detection Out of Service in U2 Heating and

Ventilation Room - Covered Walkway

1R15 Operability Evaluations

0-SI-EBT-082-238.2, Diesel Generator Battery Quarterly Operability, Revision 8

1R16 Operator Work-Arounds

ODM-3.7, Operations Directive Manual - Operator Work-Around Program

WO 03-000284-000, Transfer switch 0-XSW-201-DA for the Security BU Diesel

Generator failed to properly transfer back to normal during 0-PI-OPS-000-677.0 -

Investigate and Repair

1R19 Post-Maintenance Testing

0-PI-OPS-000-677.0, Operability Performance of Security Backup Diesel Generator,

Revision 14

WO 03-000030-000, Electric Board Room Chiller Pkg. B-B Maintenance

2

1R20 Refueling and Other Outage Activities

Outage and Site Scheduling Directive Manual (O&SSDM) 4.0 - Operational Defense-in-

depth Assessment

March 21, 2003, Operational Defense-in-depth Assessment

Tagout 1-TO-2003-0001 per 0-GO-7 section 5.2[8] and 1-SI-OPS-068-001.0

1-SI-OPS-088-006.0, Containment Building Ventilation Isolation (18 Month/100 Hours/7

Days), Revision 12

1-PI-OPS-068-673.D, Daily Requirements for Reduced Inventory/Midloop Operation

0-GO-13, Reactor Coolant System Drain and Fill Operations

0-PI-IXX-068.001.0, Daily Requirements for Reduced Inventory/Midloop

SPP-5.8, Special Nuclear Material Control (fuel assembly transfer forms)

AOP-M.04, Refueling Malfunctions

0-SI-OPS-000-187.0, Containment Inspection

1R23 Temporary Plant Modifications

Drawings 1,2-45N746-2, Revision 5, 1,2-45N799-6, Revision 6, 45N776, Revision 3

UFSAR Section 6.3, Emergency Core Cooling System,

Unit 2 Technical Specification (TS) 3/4.5.5, SQN-2-SI-OPS-002.0, SQN-63-D053-EPM-

MDE-041593

4OA3 Event Follow-up

Frozen RWST Level Instrumentation

January 28, 2003, TVA NOED Request

January 30, 2003, NRC NOED (03-6-001)

Local Leak Rate Test failure on Unit 2 Containment Purge Exhaust Valves

March 4, 2003, TVA NOED Request

March 6, 2003, NRC NOED (03-2-004)

3

4OA5 Other Activities

Temporary Instruction 2515/150

Startup Test SU-8.5.1 - Units 1 & 2, Data Sheet 9, dated January 12, 13, 14, 17, 23, 30,

and 31, 1981