ML020810177

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IR 05000483/2002-007; on 01/28-02/27/2002; Union Electric Co; Callaway Plant. Augmented Inspection Report; Problem Identification and Resolution, Modifications. One Preliminary White Finding
ML020810177
Person / Time
Site: Callaway Ameren icon.png
Issue date: 03/21/2002
From: Howell A
Division of Reactor Safety IV
To: Randolph G
Union Electric Co
References
EA-02-046 IR-02-007
Download: ML020810177 (57)


See also: IR 05000483/2002007

Text

March 21, 2002

EA-02-046

Garry L. Randolph, Senior Vice

President and Chief Nuclear Officer

Union Electric Company

P.O. Box 620

Fulton, Missouri 65251

SUBJECT: NRC AUGMENTED INSPECTION TEAM (AIT) REPORT 50-483/02-07 AND

PRELIMINARY WHITE FINDING - CALLAWAY PLANT

Dear Mr. Randolph:

On February 27, 2002, the NRC completed an Augmented Inspection at your Callaway Plant.

The enclosed report documents the inspection findings which were discussed on

February 27, 2002, with you and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

Within these areas, the inspection consisted of selected examination of procedures and

representative records, observations of activities, and interviews with personnel.

The report discusses an issue that appears to have low to moderate safety significance. The

issue involved the failure, on multiple occasions, to identify and correct a risk significant

condition adverse to quality regarding the degraded condition of the condensate storage tank

diaphragm seal. Foam from the degraded seal was eventually entrained in the auxiliary

feedwater system suction piping and caused an on-demand failure of an auxiliary feedwater

pump, while plant operators reduced reactor power on December 3, 2001. The finding was

assessed using the Significance Determination Process (SDP) and was preliminarily

determined to be White. The finding has a low to moderate safety significance under the SDP

because it involved an increase in the core damage frequency of between 1E-6/year and

1E-5/year.

The failure to promptly identify and correct the degraded diaphragm seal is also an apparent

violation of Criterion XVI of Appendix B to 10 CFR Part 50 and is being considered for

escalated enforcement action in accordance with the "General Statement of Policy and

Procedure for NRC Enforcement Actions" (Enforcement Policy), NUREG-1600. The current

Enforcement Policy is included on the NRCs website at http://www.nrc.gov/what-we-

do/regulatory/enforcement.html.

Before the NRC makes a final decision on this matter, we are providing you an opportunity to

request a Regulatory Conference where you would be able to provide your perspectives on the

Union Electric Company 2

significance of the finding, the basis for your position, and whether you agree with the apparent

violation. If you choose to request a Regulatory Conference, we encourage you to submit your

evaluation and any differences with the NRC evaluation at least one week prior to the

conference in an effort to make the conference more efficient and effective. If a conference is

held, it will be open for public observation. The NRC will also issue a press release to

announce the conference.

Please contact Dr. Dale A. Powers at (817) 860-8195 within 10 days of the date of this letter to

notify the NRC of your intentions. If we have not heard from you within 10 days, we will

continue with our significance determination and enforcement decision and you will be advised

by separate correspondence of the results of our deliberations on this matter.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for the corrective action program finding at this time. In addition, please be advised that

the number and characterization of the apparent violations described in the enclosed report

may change as a result of further NRC review.

The NRC inspection also identified one additional issue that was evaluated under the risk

significance determination process as having very low safety significance (Green). The NRC

has also determined that a violation was associated with this issue. The violation is being

treated as a noncited violation (NCV), consistent with Section VI.A of the Enforcement Policy.

The NCV is described in the subject inspection report. If you contest the violation or

significance of the NCV, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional

Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive,

Suite 400, Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Callaway Plant facility.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response will be made available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Arthur T. Howell lll, Director

Division of Reactor Safety

Docket: 50-483

License: NPF-30

Union Electric Company 3

Enclosure:

NRC Inspection Report

50-483/02-07

cc w/enclosure:

Professional Nuclear Consulting, Inc.

19041 Raines Drive

Derwood, Maryland 20855

John ONeill, Esq.

Shaw, Pittman, Potts & Trowbridge

2300 N. Street, N.W.

Washington, D.C. 20037

Mark A. Reidmeyer, Regional

Regulatory Affairs Supervisor

Regulatory Affairs

AmerenUE

P.O. Box 620

Fulton, Missouri 65251

Manager - Electric Department

Missouri Public Service Commission

301 W. High

P.O. Box 360

Jefferson City, Missouri 65102

Ronald A. Kucera, Deputy Director

for Public Policy

Department of Natural Resources

205 Jefferson Street

Jefferson City, Missouri 65101

Otto L. Maynard, President and

Chief Executive Officer

Wolf Creek Nuclear Operating Corporation

P.O. Box 411

Burlington, Kansas 66839

Dan I. Bolef, President

Kay Drey, Representative

Board of Directors Coalition

for the Environment

6267 Delmar Boulevard

University City, Missouri 63130

Union Electric Company 4

Lee Fritz, Presiding Commissioner

Callaway County Courthouse

10 East Fifth Street

Fulton, Missouri 65251

J. V. Laux, Manager

Quality Assurance

AmerenUE

P.O. Box 620

Fulton, Missouri 65251

Jerry Uhlmann, Director

State Emergency Management Agency

P.O. Box 116

Jefferson City, Missouri 65101

Gary McNutt, Director

Section for Environmental Public Health

P.O. Box 570

Jefferson City, Missouri 65102-0570

John D. Blosser, Manager

Regulatory Affairs

AmerenUE

P.O. Box 620

Fulton, Missouri 65251

Union Electric Company 5

Electronic distribution from ADAMS by RIV:

Chairman Meserve (MESERVE)

Commissioner Diaz (JXD2)

Commissioner Dicus (DICUS)

Commissioner McGaffigan (EXM)

Commissioner Merrifield (JMER)

John Larkins, Executive Director, ACRS (JTL)

W. Travers, EDO (WDT)

S. Collins, D/NRR (SJC1)

J. Donohew, Project Manager (JND)

S. Newberry, Director, RES/DRAA (SFN)

M. Mayfield, Director, RES/DET (MEM2)

C. Nolan, OE (MCN)

T. Frye, NRR (TJF)

Regional Administrator (EWM)

DRP Director (KEB)

DRS Director (ATH)

DRS/STA (DAP)

G. Sanborn, (GFS)

Senior Resident Inspector (VGG)

Branch Chief, DRP/B (DNG)

Senior Project Engineer, DRP/B (RAK1)

DRP/TSS (PHH)

RITS Coordinator (NBH)

OEMAIL

Only inspection reports to the following:

Scott Morris (SAM1)

CWY Site Secretary (DVY)

Hard Copy:

Records Center, INPO

DOCUMENT NAME: R:\_CW\CW2002-07RP-TWP.WPD

RIV:DRS\SRA NRR/PM SRI RI D:ACES

  • TWPruett:nlh *JNDonohew *TLHoeg *TWJackson *GFSanborn

/RA/ TWPruett - T TWPruett - T TWPruett - E /RA/

03/08/02 03 /08 /02 03 /07/02 03/05 /02 03/13/02

D:DRP DRS/STA D:DRS

  • KEBrockman DAPowers ATHowell lll

/RA/ /RA/ /RA/

03/11/02 03/20/02 03/20/02

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

  • Previously concurred.

ENCLOSURE 1

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 50-483

License: NPF-30

Report No.: 50-483/02-07

Licensee: Union Electric Company

Facility: Callaway Plant

Location: Junction Highway CC and Highway O

Fulton, Missouri

Dates: January 28 through February 27, 2002

Inspectors: Troy W. Pruett, Senior Reactor Analyst (Team Leader)

Timothy L. Hoeg, Senior Resident Inspector

Terry W. Jackson, Resident Inspector

Jack N. Donohew, Project Manager

Approved By: Arthur T. Howell lll

Attachments: Supplemental Information

Augmented Inspection Team Charter

Sequence of Events

System Figures

SUMMARY OF FINDINGS

Callaway Plant

NRC Inspection Report 50-483/02-07

IR 05000483-02-07; on 01/28-02/27/2002; Union Electric Co; Callaway Plant. Augmented

Inspection Report; Problem Identification and Resolution, Modifications. One preliminary White

finding.

The inspection was conducted by regional inspectors and an Office of Nuclear Reactor

Regulation project manager. The inspection identified one apparent violation and one noncited

violation of NRC requirements. The significance of most findings is indicated by their color

(Green, White, Yellow, Red) using Inspection Manual Chapter 0609 Significance Determination

Process. Findings for which the significance determination process does not apply are

indicated by No Color or by the severity level of the applicable violation. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described at its

Reactor Oversight Process website at

http://www.nrc.gov/NRR/OVERSIGHT/ASSESS/index.html.

Identification and Resolution of Problems

The team determined that several opportunities were missed to promptly identify and correct a

risk significant condition adverse to quality involving the degraded condition of the condensate

storage tank diaphragm seal. Quality assurance personnel were not actively involved in

providing oversight of the event review team and root cause investigation processes. The

event review team process did not ensure that statements were obtained from all personnel

involved in the event. The corrective action program did not include guidance or expectations

on the assignment of appropriate resources to review the highest classification of significant

conditions adverse to quality. Minimal resources were initially assigned to the root cause

investigation and may have contributed to the delay in identifying the degraded diaphragm seal.

Based on interviews with the licensees staff and a review of the corrective action program

procedure, the team determined that licensed operators were only notified of equipment

deficiencies if the individual discovering the condition believed there was an immediate impact

on nuclear, plant, or personnel safety. Consequently, the potential existed for operability

decisions to be made by non-licensed personnel. The operability evaluation program did not

implement the guidance provided in NRC Generic Letter 91-18, Information to Licensees

Regarding NRC Inspection Manual Section on Resolution of Degraded and Nonconforming

Conditions.

Cornerstone: Mitigating Systems

+ TBD. Between January 1992 and January 31, 2002, several opportunities were missed

to promptly identify and correct a significant condition adverse to quality involving

foreign material in the auxiliary feedwater system and condensate storage tank. The

failure to promptly identify the degraded condition resulted in the failure of an auxiliary

feedwater pump on December 3, 2001. In addition, between January 25 and 29, 2002,

the identification of a significant condition adverse to quality involving the as-found

condition of the degraded diaphragm seal was not reported to the appropriate levels of

management. The multiple examples of missed opportunities to identify a significant

condition adverse to quality was a violation of 10 CFR Part 50, Appendix B,

2

Criterion XVI and also represented a significant human performance cross cutting issue

involving the timely recognition of degraded conditions.

The finding had greater than minor significance because there was a credible impact on

plant safety. Specifically, auxiliary feedwater Pump A failed to run when started by

operations personnel during a plant shutdown. Had a plant event occurred, the potential

existed for foam from the degraded condensate storage tank diaphragm to fail one or

more auxiliary feedwater pumps. The failure of an auxiliary feedwater pump would have

adversely affected the decay heat removal critical safety function. A Significance

Determination Process Phase 3 analysis preliminarily determined that the issue had low

to moderate safety significance (White). This finding was entered in the licensees

corrective action program as Callaway Action Request System Item CARS 200107423.

+ Green. Calculations for auxiliary feedwater pump net positive suction head did not

account for nitrogen saturated water. The failure of calculational methods to verify the

adequacy of net positive suction head requirements for the auxiliary feedwater pumps

was a violation of 10 CFR Part 50, Appendix B, Criterion III.

The failure to account for nitrogen saturated water in the net positive suction head

calculation for the AFW pumps was more than minor because there was a credible

impact on safety in that the available margin of net positive suction head was reduced

by 11 feet. Using Phase 1 of the Significance Determination Process, the issue was

determined to be of very low safety significance because adequate available net positive

suction head remained after accounting for dissolved nitrogen. Therefore, the auxiliary

feedwater pump would have remained available during an actual plant event. The

finding was entered in the licensees corrective action program as Callaway Action

Report System Item CARS 200200485.

TABLE OF CONTENTS

1.0 Description of Event and Chronology . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1.1 System Descriptions . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1.2 Event Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1.3 Preliminary Risk Significance of Event . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

1.4 Sequence of Events . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

2.0 Human Factors and Procedural Aspects of the Event . . . . . . . . . . . . . . . . . . . . . . . . . . 2

3.0 Root Cause of Equipment Failures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

3.1 Auxiliary Feedwater Pump A Root Cause . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

3.2 Corrective Actions Associated With Auxiliary Feedwater Pump A . . . . . . . . . . . 3

3.3 Condensate Storage Tank Diaphragm Root Cause . . . . . . . . . . . . . . . . . . . . . . 8

3.4 Corrective Actions Associated With Condensate Storage Tank Degraded Seal. 9

4.0 Contributing Causes . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

4.1 Operating Experience . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

4.2 Nitrogen Effect on Condensate Storage Tank Diaphragm Seal . . . . . . . . . . . . 13

4.3 Nitrogen Effect on Net Positive Suction Head (NPSH) . . . . . . . . . . . . . . . . . . . 14

4.4 Condensate Storage Tank Modification Corrective Actions . . . . . . . . . . . . . . . 15

4.5 Condensate Storage Tank Seal Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . 16

4.6 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

5.0 Extent of Condition Review . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

6.0 Quality Assurance Review . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

6.1 Review of the Quality Assurance Aspects of the Event . . . . . . . . . . . . . . . . . . 21

6.2 Quality Assurance Audits of Foreign Material and Operating Experience . . . . 22

7.0 Risk Significance of Event . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

8.0 Overall Adequacy of the Licensees Response . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

9.0 Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 30

ATTACHMENT 1 - Supplemental Information

ATTACHMENT 2 - Augmented Inspection Team Charter

ATTACHMENT 3 - Sequence of Events

ATTACHMENT 4 - System Figures

Figure 1 - Auxiliary Feedwater System Simplified Diagram

Figure 2 - Condensate Storage Tank Diaphragm Seal

Figure 3 - Degraded Diaphragm Seal

Figure 4 - Condensate Storage Tank Configuration

Report Details

1.0 Description of Event and Chronology

1.1 System Descriptions

Auxiliary Feedwater System

The auxiliary feedwater (AFW) system has 2 motor-driven pumps (A and B) and

1 turbine-driven pump. The pumps were normally aligned through a common suction

line to the non-safety related condensate storage tank (CST). The essential service

water system was credited as the safety-related source of make-up water to the steam

generators. The AFW pump suction automatically switched from the CST to the

essential service water system following a low level condition in the CST (See Figure 1).

Condensate Storage Tank Diaphragm

The CST diaphragm was a rigid structure that floated on the surface of the water to

minimize the oxygen content of the water in the CST. The diaphragm was

approximately 43 feet in diameter and constructed of rigid closed cell foam laminated

with fiberglass and polyester resin. A seal was attached to the diaphragm and located

between the outer periphery and the inner surface of the CST. The seal was

constructed of soft pliable polyurethane foam covered with a Teflon-coated fiberglass

fabric. The fabric reduced the frictional forces between the seal and the inside wall of

the CST when the water level fluctuated (See Figure 2).

1.2 Event Summary

On December 3, 2001, at 1:15 p.m., operations personnel commenced a reactor

shutdown to repair a leaking main generator bushing. At 10:39 p.m, the Number 4 main

turbine bearing high vibration alarm annunciated in the main control room. At

10:48 p.m., the Number 4 bearing vibration increased to 10 mils and operations

personnel manually tripped the main turbine. Operations personnel prepared to reduce

main condenser vacuum to alleviate the increasing Number 4 bearing vibration. In

anticipation of breaking main condenser vacuum, operations personnel started AFW

Pump B followed by AFW Pump A. At 10:57 p.m., the Number 4 bearing vibration

exceeded 15 mils and operations personnel broke main condenser vacuum. At

10:58 p.m., operations personnel observed reduced pressure and flow from AFW

Pump A and no flow to Steam Generators B and C. Operations personnel started the

turbine-driven AFW pump and dispatched the field supervisor and an equipment

operator to AFW Pump Room A. The field supervisor and the equipment operator

observed that AFW Pump A had no leak-off flow from the outboard pump packing. The

field supervisor left AFW Pump Room A to inspect the turbine-driven AFW pump. Upon

returning to AFW Pump Room A, the field supervisor and the equipment operator

observed that the AFW Pump A outboard pump packing housing was hot to the touch.

The field supervisor contacted the main control room and recommended that AFW

Pump A be secured. At 11:07 p.m., main control room personnel secured AFW

Pump A. Operations personnel continued to cool down the reactor coolant system and

entered Mode 3 at 11:19 p.m.

2

1.3 Preliminary Risk Significance of Event

Following the December 3, 2002, failure of AFW Pump A, the NRC completed an

evaluation of the preliminary risk significance. The analysis determined that the

conditional core damage probability (CCDP) was approximately 1.1E-6. The CCDP is

the probability of core damage over a period of time given a specific plant condition.

The CCDP analysis assumed that there was no potential for common cause failure of

the remaining two AFW pumps and that the duration associated with the failure of AFW

Pump A was less than 30 days. In response to the failure of AFW Pump A, the NRC

determined that a Special Inspection Team (SIT) would assess the causes of the event

during the week of January 28, 2002.

On January 27, 2002, the licensees root cause investigation determined that

polyurethane foam from a degraded CST floating diaphragm may have caused the

failure of AFW Pump A.

On January 28, 2002, the SIT determined that the duration of the degraded condition

could have been greater than 1 year. In addition, the SIT determined that the potential

existed for common cause failure of the AFW system or multiple AFW pumps. The

NRC completed an additional analysis of the event and determined that the new

estimated CCDP was in the range of approximately 5E-5 to 5E-4.

NRC Management Directive 8.3, NRC Incident Investigation Program, required the

consideration of the initiation of an Augmented Inspection Team (AIT) when the

estimated CCDP was greater than or equal to 1E-5. Based on the potential for a

substantial increase in risk stemming from common mode failure implications, the NRC

upgraded the SIT to an AIT on January 31, 2002.

1.4 Sequence of Events

The team developed a detailed sequence of events and organizational response

time-line. The time-line included applicable events and actions before, during, and

following the failure of AFW Pump A on December 3, 2001. The time-line was

generated from control room computer printouts, operator logs, written records, and

interviews with members of the licensees staff. The teams review satisfied the

activities associated with AIT Charter Element 1, Develop a complete description and

sequence of events related to the subject AFW pump failure (including the degraded

CST floating diaphragm), and operator actions taken in response to regain feedwater

flow. The AIT Charter is provided as Attachment 2. The detailed sequence of events is

provided as Attachment 3.

2.0 Human Factors and Procedural Aspects of the Event

a. Inspection Scope

The team reviewed operator actions associated with the failure of AFW Pump A and the

actions taken to restore feedwater flow to Steam Generators B and C. The team

interviewed operations personnel, evaluated control room logs and trend data, analyzed

3

AFW pump performance data, and reviewed control room operating procedures. The

teams review satisfied a portion of the activities associated with AIT Charter Element 5,

Identify any human factor, procedural or quality assurance deficiencies that may have

contributed to the condition.

b. Observations and Findings

No deficiencies were identified with the operator actions associated with the event or

with procedures utilized during the event.

3.0 Root Cause of Equipment Failures

3.1 Auxiliary Feedwater Pump A Root Cause

a. Inspection Scope

The team reviewed the results of the licensees investigation documented in Callaway

Action Request System Item CARS 200107423, Auxiliary Feedwater System Event

Review, to determine if the root cause was of appropriate scope including;

independence, completeness, and accuracy to identify the probable causes of the

failure of AFW Pump A. The team reviewed operations documents, corrective action

documents, maintenance records, and operating experience. The team completed a

walk down of portions of the AFW system and CST. The team also interviewed several

members of the licensees staff. The teams review satisfied a portion of the activities

associated with AIT Charter Element 2, Review the licensees root and probable cause

determination for independence, completeness, and accuracy, including the licensees

assessment of the risk associated with the condition.

b. Observations and Findings

The team determined that the licensees investigation into the failure of AFW Pump A

was of adequate scope and detail to conclude that the pump failure was due to the

entrainment of a piece of foam from the CST diaphragm seal. The foam material

entered the eye of the first stage impeller and produced a localized low pressure region.

The low pressure region caused gas to come out of solution and create voids in AFW

Pump A. The voiding led to a partially air-bound pump which was incapable of

developing the required pump discharge pressure and flow.

3.2 Corrective Actions Associated With Auxiliary Feedwater Pump A

a. Inspection Scope

The team assessed the licensees prompt and long-term corrective actions to address

the root and probable causes of the failure of AFW Pump A. The team reviewed the

licensees root cause analysis, the event review team report, the past operating and

maintenance history for AFW Pump A, surveillance test data, the results of system

walkdown inspections, vendor information, boroscopic inspections of the AFW system,

and inspections of the CST. The team assessed the adequacy of AFW system

inspections by direct observation or by viewing video footage and photographs. The

4

teams review satisfied a portion of the activities associated with AIT Charter Element 7,

Identify and assess the licensees prompt and long-term corrective actions to address

the root and probable causes of the condition.

b. Observations and Findings

The team identified several examples of an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Actions. Each of the examples involved a

missed opportunity to promptly identify and correct a significant condition adverse to

quality associated with foreign material in the AFW system and CST.

On December 3, 2001, operations personnel completed a vent-and-fill of AFW Pump A.

Air was vented from the pump casing for approximately 15 seconds. No steam was

released during the venting. Therefore, the team determined that the licensee

appropriately concluded that the failure of AFW Pump A was not due to steam binding.

On December 4, 2001, the licensee completed a walkdown of AFW Train A. The team

reviewed Procedure OSP-AL-00001, AFW Flow Paths Valve Alignment, Revision 5,

which described the proper system alignment for the AFW system. The team also

interviewed operations and engineering personnel involved with the system walkdown.

The team determined that the licensee appropriately concluded that there was no

evidence of an improper valve alignment or an obvious pathway for air-entrainment into

the AFW system.

On December 4, 2001, the licensee convened an event review team to gather

information that would aid in identifying the root cause of the failure of AFW Pump A.

The team reviewed UOTH 01-0047, Event Review Meeting Minutes: High Main Turbine

Vibration, AFAS, and No Flow on A-AFW Pump, and concluded that the report

accurately reflected the sequence of events. However, during interviews with operations

personnel, the team determined that the event review team did not obtain statements

from the two reactor operator trainees who were in the control room at the time of the

event, or the equipment operator who was the first person to monitor and vent AFW

Pump A. Furthermore, the event review team meeting minutes were not distributed to

the control room supervisor, the reactor operator trainees, or the equipment operator for

verification of information.

The team assessed the licensees review of the operational and maintenance history for

AFW Pump A. The team also reviewed the previous 2 years of test data collected with

Procedure OSP-AL-P001A, Motor Driven Aux. Feedwater Pump A In Service Test,

and the previous 2 years of maintenance activities competed on AFW Pump A. The

team determined that the licensee appropriately concluded that past operational and

maintenance activities associated with AFW Pump A did not contribute to the root

cause.

On December 4, 2001, the licensee initiated Callaway Action Request System Item

CARS 200107423, Auxiliary Feedwater System Event Review, to investigate the event.

The licensee classified the significance of Callaway Corrective Action System Item

CARS 200107423 as Level 1 and specified that a formal root cause evaluation should

be completed. The acting mechanical system engineering supervisor and a root cause

5

analyst from the corrective action group were assigned to complete the investigation.

Based on discussions with the licensees staff, the team determined, on the basis of

interviews, that the root cause analyst was not actively involved in the investigation until

mid-to-late January 2002. Based on interviews with the licensees staff and a review of

Procedure APA-ZZ-00500, Corrective Action Program, the team determined that there

were no formal requirements or expectations on the formulation of teams to review the

highest classification of significant conditions adverse to quality.

On December 5, 2001, the licensee started AFW Pump A in order to troubleshoot and

attempt to recreate the failure mechanism. The licensee determined that AFW Pump A

could not meet the minimum flow requirements of the surveillance test procedure and

that the outboard shaft seal stuffing box temperature increased abnormally. The

licensee replaced the outboard shaft seal packing, re-baselined the pump performance

criteria, and satisfactorily completed the pump surveillance test. In addition, the

licensee implemented compensatory measures to perform shiftly vents of all AFW

pumps and decreased the surveillance test interval from quarterly to monthly for each

AFW pump (In January 2002, the licensee decreased the AFW Pump A frequency to

weekly). The licensee determined that the most probable cause of the AFW Pump A

failure was air intrusion into the AFW system. Although no cause had been confirmed,

the licensee determined that the compensatory measures involving shiftly pump venting

and increased testing were sufficient to declare AFW Pump A operable.

Technical Manual M-021000061, Instruction Manual for Ingersoll Rand Centrifugal

Pumps, Revision 25, recommended opening and inspecting the pump when insufficient

pump capacity and stuffing box overheating were experienced. The technical manual

troubleshooting chart identified foreign material as a probable cause for both the

insufficient flow and stuffing box overheating, which were symptoms experienced on

December 3 and 5, 2001. In addition, the guidance in Table 5-2 of Electric Power

Research Institute TR-114612-V2, Pump Troubleshooting, was consistent with the

technical manual information. Nevertheless, as of December 5, 2001, the licensee did

not consider foreign material as a credible failure mechanism. The team determined

that the licensees lack of an evaluation of foreign material in the AFW system or CST

as a possible cause immediately following the event was an example of not promptly

identifying and correcting a significant condition adverse to quality. This missed

opportunity to promptly identify a condition adverse to quality represented an example of

a significant human performance crosscutting issue involving the timely recognition of

degraded conditions. The significance of this cross cutting issue and other examples of

the apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI, is documented in

Section 7.

On December 6, 2001, the licensee formally initiated the investigation into the failure of

AFW Pump A. In addition, the licensee added a system engineer to the root cause

investigation. A vibrations engineer and a licensed operator were utilized on an

as-needed basis.

On December 14, 2001, the licensee contacted the pump vendor and discussed

possible causes of the failure of AFW Pump A. The pump vendor recommended that

the licensee inspect the seal water piping for a possible flow obstruction. Based on

interviews with engineering personnel, the team determined that the licensee continued

6

to believe that foreign material was an unlikely cause since the CST was assumed to be

free of foreign material and because the AFW pumps had been operated successfully.

Consequently, the licensee determined that the inspection of the seal water line could

be delayed until the next regularly scheduled maintenance interval for AFW Pump A.

The team determined that not promptly following the vendors recommendation to

inspect the seal water line for obstructions was an additional example of the significant

human performance cross cutting issue involving the timely recognition of degraded

conditions.

During the January 8, 2002, management meeting, the licensee added individuals from

regulatory affairs and engineering to the root cause investigation. In addition, the

licensee decided to bring the pump vendor and a pump contractor to the site during the

January 14, 2002, maintenance week for AFW Pump A.

Following the January 8, 2002, management meeting, the licensee narrowed the root

cause of the failure of AFW Pump A to three possibilities: (1) low net positive suction

head (NPSH), (2) nitrogen gas disassociation, or (3) foreign material. However, the

licensee continued to believe that foreign material was an unlikely cause since there

was no recent activity which would have introduced foreign material into the CST or the

AFW system. Therefore, foreign material continued to receive a low priority in the root

cause investigation. The team concluded that narrowing the potential root causes to

those listed above was appropriate. However, this conclusion could have been reached

in a more timely manner and causes not related to the event could have been eliminated

sooner. Specifically, the following information was available to the licensee following the

event:

1. Evidence of air during the vent-and-fill process for AFW Pump A suggested that

either air/gas was entrained into the pump, that gas came out of solution, or that

foreign material caused the gas to come out of solution at the eye of the

impeller.

2. System walkdowns performed after the event did not identify any source of air

intrusion.

3. The inability to re-create a failure of AFW Pump A due to air entrainment in

subsequent pump runs on December 5, 2001, demonstrated that air-entrainment

was an unlikely cause of pump failure.

4. The absence of air during shiftly venting indicated that air intrusion was unlikely.

5. Vendor and industry information suggested that foreign material was a possible

cause for the failure of AFW Pump A.

The team determined that the 35-day delay in identifying the potential root causes was

an additional example of the significant human performance cross cutting issue

involving the timely recognition of degraded conditions.

10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that measures be

established to assure that conditions adverse to quality, are promptly identified and

7

corrected. For significant conditions adverse to quality, the measures shall assure that

the causes of the condition are determined and corrective actions taken to preclude

recurrence. The identification of significant conditions adverse to quality shall be

documented and reported to appropriate levels of management.

During the week of January 15, 2002, the licensee contracted the services of the pump

vendor, Flowserve, and a pump consultant, Dominion Engineering. The consultants

were present during the testing of AFW Pump A on January 15, 2002. The licensee

also inspected the seal water cooling line on AFW Pump A and found a piece of foam

lodged in the orifice. Even though foreign material was identified in the AFW system,

the licensee continued to believe that foreign material was not a credible cause for the

failure of AFW Pump A. The team determined that the failure to promptly identify and

correct the degraded CST diaphragm seal after discovering foreign material in the seal

water cooling line was an example of an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI (APV 05000483/0207-01). In addition, this missed

opportunity to promptly identify a condition adverse to quality represented an additional

example of a significant human performance cross cutting issue involving the timely

recognition of degraded conditions.

On January 17, 2002, the licensee began ultrasonic testing of the AFW pump suction

piping to determine if nitrogen gas was coming out of solution and collecting in the

system. The team reviewed Procedure QPC-ZZ-05046, Ultrasonic Examination

Procedure for Determining Liquid Level in Pipes and Components, Revision 0, and

recorded test data obtained between January 17 and 31, 2002. The team determined

that the ultrasonic procedure was adequate, and that the licensees interpretation of the

data was appropriate. The team noted that the licensee believed that air intrusion was

the most probable cause of the AFW Pump A failure between December 4, 2001, and

January 24, 2002. Therefore, the team concluded that the initiation of ultrasonic testing

was untimely in that testing could have commenced at an earlier date to help eliminate

air or gas accumulation in the suction piping as a root cause.

On January 23, 2002, with the assistance of the consultants, the licensee eliminated low

NPSH and air intrusion as potential root causes of the failure of AFW Pump A. The

pump vendor provided a report titled, Evaluation of Auxiliary Feedwater Pump 1A Event

12/3/01, and the pump consultant provided a report titled, Auxiliary Feed Pump Event.

On January 24, 2002, the licensee increased the level of effort associated with the root

cause investigation as preparations were made to inspect the CST for foreign material.

The licensee also decided to complete the AFW system inspections during the regularly

scheduled maintenance window for each train.

On January 26, 2002, the licensee identified foreign material in the CST (See

Sections 3.3 and 3.4).

On January 30, 2002, the licensee initiated boroscopic inspections of AFW Pump B, the

turbine-driven AFW pump, AFW system suction piping, and portions of the AFW system

discharge piping. The team reviewed several work orders and found that the scope of

the inspection activities was appropriate. The following is a sample of work orders

reviewed:

8

+ W220254, Replace Rotating Element on A MDAFP

+ W682227, Suction Piping Inspection

+ W687231, A MDAFP Discharge Piping Inspection

+ W687232, B MDAFP Discharge Piping Inspection

+ W687233, TDAFP Discharge Piping Inspection

On January 31, 2002, the licensee significantly increased the team size and scope of

the root cause investigation.

The team observed portions of the boroscopic inspections and found them to be

appropriate. The licensee identified one additional piece of foam lodged in the AFW

Pump A casing vent line. No other foreign material was identified. The team

determined that the scope of the licensees inspections of the AFW system and CST

were sufficient to ensure the AFW system would perform its safety function.

3.3 Condensate Storage Tank Diaphragm Root Cause

a. Inspection Scope

The team reviewed the licensees root cause investigation documented in Callaway

Corrective Action System Item CARS 200107423, to determine if it was of appropriate

scope including; independence, completeness, and accuracy to identify the probable

causes of the failure of the CST diaphragm. The team reviewed operations documents,

corrective action documents, maintenance records, and operating experience

associated with the AFW pumps and CST. The team completed a walk down of

portions of the AFW system and CST. The team also interviewed several members of

the licensees staff. The teams review satisfied a portion of the activities associated

with the AIT Charter Element 2, Review the licensees root and probable cause

determination for independence, completeness, and accuracy, including the licensees

assessment of the risk associated with the condition.

b. Observations and Findings

On January 26 and 27, 2002, the licensee found foreign material in the CST. The

foreign material mainly consisted of pieces from the diaphragm seal assembly. The seal

materials consisted of a Teflon-coated fiberglass fabric, flexible polyurethane foam,

caulking material, and a piece of fiberglass (See Figure 2).

The team determined that the licensees investigation of the CST diaphragm seal failure

was of adequate scope and detail to conclude that the degraded Teflon-coated fabric

and inner foam material was due to constant nitrogen sparging of the CST at 5 standard

cubic feet per minute. The nitrogen bubbles from the sparging impinged on the

diaphragm seal and increased the wear on a 6-foot section of the approximately

130-foot circumference. The licensee calculated that the impact forces were on the

magnitude of 0.02-lb force on each square inch of the lower surface of the seal at a rate

of approximately 68,700 cycles per impact site over a 4.5-year period. Once the Teflon

coating failed, the same mechanism acted directly on the foam. This failure mechanism

continued to occur until sections of foam became detached and settled on the bottom of

the tank.

9

3.4 Corrective Actions Associated With Condensate Storage Tank Degraded Seal

a. Inspection Scope

The team assessed the licensees prompt and long-term corrective actions to address

the root and probable causes of the failure of the CST diaphragm seal. The team

reviewed the licensees root cause analysis, the past operating and maintenance history

for the seal, and inspections of the CST. The team assessed the adequacy of CST

inspections by direct observation or by viewing video footage and photographs. The

teams review satisfied a portion of the activities associated with AIT Charter Element 7,

Identify and assess the licensees prompt and long-term corrective actions to address

the root and probable causes of the condition.

b. Observations and Findings

The team identified an additional example of the apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI. Specifically, members of the licensees staff failed to notify

management of a significant condition adverse to quality.

On January 24, 2002, the licensee initiated efforts to inspect the CST. Initially, the

assessment consisted of using a diver to inspect the CST and diaphragm seal. During

the divers inspection, approximately 71 inches of the diaphragm seal was found

degraded (See Figure 3). The diver removed a 25-inch section of foam hanging from

the diaphragm. The diver also found various pieces of foam, Teflon-coated fabric,

caulking, and two rubber pads in the CST sump. The foam found in the CST sump

included a section measuring 12 x 3 x 8 inches, a section measuring 2 x 3 x 8 inches,

and approximately 10 smaller pieces of foam under 1 cubic inch in total volume. No

foam was located outside the sump; however, some caulking and two additional rubber

pads were recovered from the CST floor.

The team reviewed Work Orders W202393, CST Seal Inspection, and W686916,

Camera and Diver Inspection of CST. The diver was given instructions to enter the

CST and assess the integrity of the diaphragm seal cover and the attachment of the

seal to the diaphragm. In the process of communicating the integrity of the diaphragm

seal cover, the licensees staff incorrectly understood that the seal cover had a single

tear at the damaged area and did not have any missing pieces. The fabric found in the

CST sump was incorrectly assumed to have been left in the CST during construction of

the floating diaphragm. This misunderstanding led senior licensee management to

believe the diaphragm seal would not present any impact on plant safety once the

repairs outlined in Work Order W686916 were performed.

On January 30, 2002, following a viewing of video footage with the team, senior licensee

management contacted the diver and questioned the as-found condition of the seal.

Senior licensee management was informed that the Teflon fabric did not have a single

tear, but was missing pieces and had jagged edges.

Even though foam was found in the AFW Pump A seal water line, as well as the CST,

the licensees operability evaluation included in Callaway Corrective Action System Item

CARS 200200489, Complete an Operability Evaluation on the CST Due to the

10

Existence of the Foam Pieces, did not document activities to determine the potential for

foreign material to have been retained in other sections of the AFW system. The team

interviewed senior licensee management to determine what activities were completed by

the licensee following the discovery of foreign material in the CST. Based on the

interviews, the team determined the following:

+ Before entering the CST, senior management had implemented compensatory

measures to declare the CST inoperable and align the AFW suction source to

the essential service water system if significant foreign material was identified.

+ During the morning of January 27, 2002, the licensee had evaluated the effect

on the AFW system from foreign material in the CST. Even though the extent of

the diaphragm seal degradation was not yet known, senior management

concluded that the effect of foreign material on the AFW system was low due to

the number of hours the AFW pumps had operated, the visual clarity of water in

the CST, and the lack of debris on the floor of the CST.

+ During the evening of January 27, 2002, the licensee removed the foreign

material from the CST. Senior management was informed that the material had

been removed and that the CST was clean.

+ During the morning of January 28, 2002, the licensee believed that the removed

material had been in the CST for an extended period of time. Senior

management determined that the Teflon material was not an operability concern

(at this time senior management had been incorrectly informed on several

occasions that the Teflon material had a single tear). In addition, senior

management believed that the foam was not an operability concern based on the

run times for each of the AFW pumps.

+ During the evening of January 28, 2002, senior management questioned

engineering personnel about the Teflon fabric. Senior management was

incorrectly informed that the area where the foam was missing was intact (i.e.,

single tear in material). Senior management determined that the Teflon material

had probably been in the CST since construction.

+ During the afternoon of January 29, 2002, the licensee discussed the results of

inspection activities with the team. The licensee indicated that no inspections of

the AFW system were planned for the near term. The team subsequently

determined that the licensee had planned to inspect small diameter piping

associated with the AFW pumps during the next regularly scheduled planned

maintenance period for each AFW pump train.

+ On January 30, 2002, the team viewed the video footage of the CST and

degraded diaphragm seal with the plant manager. The team determined that the

plant manager had not viewed the footage involving the degraded diaphragm

seal. After viewing the video footage, the team and the plant manager

questioned the validity of the information obtained from the licensees staff

regarding the as-found condition of the diaphragm seal. The plant manager then

re-interviewed the diver and determined that the Teflon material did not have a

11

single tear, but had jagged edges and was missing multiple pieces. Based on

the information obtained from the diver, senior licensee management determined

that the appropriate action would be to shutdown the plant and complete

additional inspections of the CST and AFW system.

The team determined that the incorrect information provided by the licensees staff to

senior management delayed the initiation of the extent of condition review associated

with the discovery of foreign material in the CST. Once initiated, the extent of condition

review was thorough and provided assurances that the AFW system did not contain any

further foreign material. The team determined that the failure of the licensees staff to

correctly report a significant condition adverse to quality to the appropriate levels of

management in a timely manner was an additional example of the apparent violation of

10 CFR Part 50, Appendix B, Criterion XVI.

4.0 Contributing Causes

4.1 Operating Experience

a. Inspection Scope

The team reviewed industry operating experience information related to tank

diaphragms to determine if the licensee applied the data appropriately. The review

consisted of interviewing licensee personnel, searching operating experience

databases, reviewing corrective action documents, reviewing the licensees responses

to operating experience information, and verifying licensee actions taken in response to

applicable operating experience. The teams review satisfied the activities associated

with AIT Charter Element 6, Identify and assess the licensees evaluation of applicable

industry operating experience.

b. Observations and Findings

Information Notice 91-82

On December 18, 1991, the NRC issued Information Notice (IN) 91-82, Problems with

Diaphragms in Safety Related Tanks. NRC IN 91-82 reminded licensees that

diaphragms in safety related tanks had finite service lives and could cause various

safety hazards if they fail. On January 21, 1992, the licensee initiated Callaway Action

Tracking System Item CATS 31040, Generate PM for Regular Inspection of CST

Cover, to ensure a maintenance activity to periodically inspect the CST diaphragm seal

was generated. On February 10, 1992, the licensee issued a response to

NRC IN 91-82 which specified that the licensee had experienced some problems with

rubber diaphragm type tank seals and had initiated programs to inspect tank internals

for degradation of diaphragms.

On September 15, 1999, the licensee initiated Callaway Corrective Action System Item

CARS 199901955, PM to Inspect CST Internal Cover Not Generated, in response to

an NRC resident inspector question regarding the condition of the CST diaphragm seal.

The licensee identified that Callaway Action Tracking System Item CATS 31040 had

been closed without performing an inspection of the diaphragm seal. The team

12

determined that the closure of Callaway Action Tracking System Item CATS 31040

without having completed an inspection may have contributed to the delay in identifying

the degraded condition of the CST diaphragm seal and was an additional example of

the apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI.

The licensee contacted the seal vendor and was informed that the only expected

degradation of the diaphragm seal would be wear of the outer Teflon skin covering the

foam seal as it rubbed against the tank wall when level fluctuated. The licensee realized

an inspection should be performed and initiated Generic Work Request G631231125,

Periodic Inspections of CST Diaphragm Seal, to perform periodic seal inspections.

After further review, the licensee determined that a specific inspection activity was more

appropriate than a generic inspection activity and initiated Work Order W201820,

Inspect CST Floating Cover, to inspect the seal in the Spring of 2000. At that time, the

CST seal had not been inspected since its final closeout inspection in 1982. The team

determined that the seal inspection activity per Work Order W201820 was rescheduled

twice (Spring and Summer of 2000) before being performed in October 2000. The

licensees basis for deferring the inspections was to allow enough time for completion of

the seal inspection work. The team determined that the licensees basis for delaying the

inspection did not fully consider the potential consequences of a degraded seal and was

an additional example of the apparent violation of 10 CFR Part 50, Appendix B,

Criterion XVI. In addition, this missed opportunity to promptly identify a condition

adverse to quality represented an additional example of a significant human

performance cross cutting issue involving the recognition of degraded conditions.

On October 17, 2000, the licensee performed a topside visual inspection of the CST

diaphragm seal. The licensee did not thoroughly inspect the outer seal fabric which the

vendor had stated one year earlier was vulnerable to wear failure. The team determined

that the scope of the licensees inspection was inadequate to determine that the

diaphragm seal was intact and was an additional example of the apparent violation of

10 CFR Part 50, Appendix B, Criterion XVI. In addition, this missed opportunity to

promptly identify a condition adverse to quality represented an additional example of a

significant human performance cross cutting issue involving the recognition of degraded

conditions.

The team also determined that the licensee had initiated Preventive Maintenance

Item P663567, Inspect CST Cover, to inspect the topside of the diaphragm seal on a

10-year periodicity. Preventive Maintenance Item P663567 did not include instructions

to inspect the bottom side of the seal assembly. Therefore, future inspections may not

have identified the degradation.

Significant Operating Experience Report 97-01

The team reviewed the licensees response to Significant Operating Experience

Report 97-01, Potential Loss of High Pressure Injection and Charging Capability From

Gas Intrusion. No deficiencies were identified.

13

4.2 Nitrogen Effect on Condensate Storage Tank Diaphragm Seal

a. Inspection Scope

The team reviewed the modifications to the CST that added and later modified a

nitrogen sparging system to control dissolved oxygen. The team reviewed two

modification packages; (1) Request for Resolution 04991, Revision A, Permanent N2

for the Condensate Storage Tank, dated May 4, 1988, to replace the temporary tubing

in CST by permanent connections; and (2) Restricted Modification Package 88-2016,

Revision A, dated November 20, 1992, to install the permanent nitrogen sparger system

in the CST. The documentation for the modification to add the temporary nitrogen

tubing to the CST in 1986 was not available.

b. Observations and Findings

The licensees evaluation of the modifications did not consider the effect of nitrogen on

the CST floating diaphragm. Specifically, the location of the nitrogen piping and how the

nitrogen would diffuse from the sparger and affect the floating diaphragm or the

AFW pump available NPSH was not considered. The licensee concluded, without

documentation, that the release of small quantities of nitrogen gas were insignificant,

not regulated by any state or federal agency, and that no unreviewed environmental

question existed.

There were no drawings of the temporary tubing or the permanent piping in the CST in

the documentation provided by the licensee. There was also no documentation of any

calculations performed to determine, based on the sparger design, the flow rate needed

to saturate the tank water with nitrogen or the effect of nitrogen on the diaphragm seal.

4.3 Nitrogen Effect on Net Positive Suction Head (NPSH)

a. Inspection Scope

The team reviewed Calculation AL-10, Determine the Available NPSH for the Auxiliary

Feedwater Pumps, dated July 21, 1977, as revised in 1980; Calculation AL-13, A

System Model of the AFW System, dated September 14, 1995; and Calculation AL-24,

Determine the Effect of Dissolved Nitrogen on Available NPSH for the Auxiliary

Feedwater Pumps, dated February 6, 2002, to determine if there was adequate NPSH

for AFW Pump A.

b. Findings and Observations

The team identified a violation of 10 CFR Part 50, Appendix B, Criterion III, Design

Control, which involved the failure account for the effect of nitrogen on AFW pump

NPSH.

Calculation AL-10 was completed for the CST and AFW system before the CST was

modified to add a nitrogen sparging system to control dissolved oxygen. Prior to 1988,

the amount of oxygen in the CST water was controlled by recirculating water to the main

condenser hotwell. However, the licensee determined that this method of removing

14

oxygen from the CST resulted in water temperatures during the summer months that

could exceed the design temperature of the AFW system suction piping. To prevent the

high temperature water, the licensee installed modifications to the CST to add a nitrogen

sparging system.

The team determined that the evaluations for the modifications did not address the

affect of the nitrogen saturated water on the pump tolerable volume fraction and the

available NPSH for the AFW pumps. The tolerable volume fraction of gases is a

measure of the quantity of free gases which can be passed by the pump without the gas

volume affecting pump performance (i.e., reducing pump performance to the point of

gas binding the pump). The NPSH required for a pump with a lower tolerable gas

volume fraction will be smaller than the NPSH required for a pump with a higher

tolerable gas volume fraction. NPSH is the minimum suction head required for a pump

to operate. The team determined that the tolerable volume fraction for AFW Pump A

was approximately 5 percent. The licensee determined that the expected volume of free

nitrogen, based on the reduction of pressure from the CST to the pump impeller eye,

was less than 5 percent.

On January 25, 2002, the licensee initiated Callaway Corrective Action System Item

CARS 200200485, Evaluate the Potential Effects of Dissolved Nitrogen on the Auxiliary

Feedwater System, following the identification that nitrogen had not been accounted for

in AFW pump NPSH calculations.

On February 6, 2002, the licensee completed Calculation AL-24 to address the effect of

nitrogen on the available NPSH for the AFW pumps. Calculation AL-24 was reviewed

by the team to determine if the assumptions were conservative and the calculated

available NPSH was correct. The equations used by the licensee were from the

following papers: (1) Daniel W. Wood, et. al., Proceedings of the 15th International

Pump Users Symposium, Application Guidelines for Pumping Liquids that have a Large

Dissolved Gas Content, pages 91 through 98, dated March 1998, (2) Mao J. Tsai,

Chemical Engineering, Accounting for Dissolved Gases in Pump Design, dated July

26, 1982; and (3) C. C. Chen, Chemical Engineering, Optimal System Design Requires

the Right Vapor Pressure. Heres How to Calculate It, pages 106 through 112, dated

October 1983.

Calculation AL-10, specified that the available NPSH for AFW Pump A was 28 feet,

assuming the CST water level was at the suction of the AFW system. The available

NPSH for AFW Pump A at the CST to essential service water system swap-over level

was 35 feet. Calculation AL-10 did not account for dissolved nitrogen because the CST

was not modified with a nitrogen sparger until 1988.

Calculation AL-24 included the effect of nitrogen saturated water, and assumed a

minimum temperature of 50oF, a 5 percent tolerable volume fraction of gas, and the

CST to essential service water system swap-over elevation. The team reviewed

Calculation AL-24 and determined that the reduction in available NPSH for AFW

Pump A, due to the effect of the dissolved nitrogen in the CST, was approximately

11 feet.

15

10 CFR Part 50, Criterion III, Design Control, required, in part, that the licensee

implement design control measures for verifying or checking the adequacy of the design

by the use of calculation methods. The team concluded that the licensees identification

that calculational methods failed to verify the adequacy of NPSH requirements for the

AFW pumps was a violation of 10 CFR Part 50, Appendix B, Criterion III

(05000483/0207-02). The team determined that the failure to account for nitrogen

saturated water in the NPSH calculation for the AFW pumps was more than minor

because there was a credible impact on safety in that the available margin of NPSH was

reduced by 11 feet. Using Phase 1 of the Significance Determination Process, the team

determined that the issue was of very low safety significance (Green) in that adequate

available NPSH remained after accounting for the affect of dissolved nitrogen.

Therefore, the availability of AFW pumps was not effected by the reduction in available

NPSH margin.

4.4 Condensate Storage Tank Modification Corrective Actions

a. Inspection Scope

The team reviewed Request for Resolution 21798, Revision D, Evaluate Permanent

Removal of TAP01 Floating Cover, dated February 1, 2002, to ensure the licensee

appropriately considered any negative consequences associated with the modification.

b. Observations and Findings

The team determined that members of the licensees staff believed that the non-safety

related CST did not have a function important to safety. The equipment qualification

impact review section of the licensing impact review form required that an individual

determine if the activity involved any safety-related structure, system, or component.

The individual was not required to state if the non-safety related structure, system, or

component had a safety function or if it was important to safety. The team noted that

there was a probabilistic risk assessment (PRA) review section on the licensing impact

review form which questioned if there was a potentially PRA-significant change to a

plant system.

The team noted that if the originator of the licensing impact review form did not

understand the safety function of the non-safety component, the answer to the question

about a potential PRA-significant change to a plant system may be incorrect. In this

case, the reviewer did not consider the change PRA-significant. The review was

subsequently re-evaluated by the PRA group. The team determined that the PRA staff

appropriately determined that the modification to remove the diaphragm seal was not

risk significant.

The team interviewed several members of the licensees staff and was informed that

evaluations associated with non-safety related equipment did not receive the same level

of rigor as evaluations associated with safety-related equipment. The team determined

from these interviews that this lack of rigor existed even in those instances in which the

non-safety component had a function which was important to safety.

16

The licensee also determined that not properly acknowledging the relationship between

the non-safety related CST and the safety-related AFW pumps led to non-conservative

decisions that may have contributed to December 3, 2001, event. The licensee planned

to address these concerns by bringing a heightened awareness to the plant organization

through group discussions or training.

4.5 Condensate Storage Tank Seal Maintenance

a. Inspection Scope

The team reviewed design information associated with the expected service life of the

diaphragm seal and the frequency of maintenance and inspection activities.

b. Observations and Findings

The team determined that not all of the original design specifications for the diaphragm

seal were readily available to the licensee during its investigation of the failure of the

diaphragm seal. CST Design Specification 10466-M-109 (Q), Section 5.27.4.3,

referenced a negotiated seal life guarantee and warranty period but did not provide any

actual life expectancy. The licensee was not able to produce any documentation

regarding the seal life or warranty information referenced in the design specifications.

The team determined that the lack of information may have contributed to a decrease in

the sensitivity for the need to complete periodic inspection and maintenance activities on

the diaphragm seal.

4.6 Operability Evaluations

a. Inspection Scope

The team reviewed three operability evaluations associated with the CST and AFW

system to determine the adequacy of the licensees review of degraded but operable

conditions. The team also compared Generic Letter 91-18, Revision 1, Information to

Licensees Regarding NRC Inspection Manual Section on Resolution of Degraded and

Nonconforming Conditions, to the licensees implementing procedures for operability

evaluations. The teams review satisfied a portion of the activities associated with AIT

Charter Element 3, Assess the timeliness and effectiveness of the licensees evaluation

of potential AFW common cause failure stemming from the degraded condensate

storage tank floating diaphragm.

b. Observations and Findings

The team identified several weaknesses associated with the licensees corrective action

and operability evaluation programs.

Procedure APA-ZZ-00500, Corrective Action Program, Section 3.1.1, specified that all

personnel are responsible for the immediate notification of the shift supervisor upon

discovery of a condition that they believe to have an immediate impact on nuclear,

plant, or personnel safety. Section 5.3.1.2 specified that if the condition discovered is

believed to have an immediate impact on operability, reportability, plant or personnel

17

safety, then the originator is to immediately notify the shift supervisor. The team

interviewed personnel assigned to the corrective action group and determined that

equipment deficiencies did not require the notification of the shift supervisor if the

individual believed that equipment operability was not immediately affected. The team

also interviewed the assistant operations superintendent and determined that his

expectations were for personnel to notify the shift supervisor of any equipment

deficiency. The team determined that the guidance and expectations regarding the

notification of the shift supervisor of equipment deficiencies were not consistently

implemented. In addition, the team determined that the opportunity for licensed

personnel to assess operability for degraded equipment conditions may not occur if the

originator (possibly non-licensed individual) believed that an operability concern did not

exist. The team determined that the failure to notify the shift supervisor of deficiencies

associated with plant equipment could have a credible impact on safety. For example,

the shift supervisor was not notified of the significant condition adverse to quality

described in Callaway Corrective Action System Item CARS 200200264, Foreign

Material Found in the AL System and Callaway Corrective Action System Item

CARS 200200485, Evaluate the Potential Effects of Dissolved Nitrogen on the Auxiliary

Feedwater System. The safety significance associated with foreign material in the

AFW system and CST is described in Section 7.

Procedure APA-ZZ-00500, Attachment 7, OPER Disposition, provided guidance for

completing operability evaluations. The guidance consisted of eight steps which

involved:

+ reviewing documentation to understand the issue, assuring the correct individual

was assigned to review the issue,

+ investigating the issue,

+ assigning actions to other individuals if necessary,

+ preparing a response,

+ entering correct information,

+ attaching supporting information, and

+ closing the OPER action.

The team determined that there were no references in Attachment 7 to Generic

Letter 91-18. Consequently, the licensees operability evaluation program did not

provide the following:

+ Guidance to aid the reviewer in determining when a safety evaluation was

required to be considered.

+ A requirement for a licensed operator to be notified when an operability

evaluation was being or had been performed.

18

+ Guidance on the amount of time required to complete an operability evaluation.

+ Guidance on the required level of review of an operability evaluation.

+ Guidance for the completion of safety evaluations associated with compensatory

measures.

+ Guidance for the periodic reviews of open operability evaluations.

The team determined that the failure to have an adequate program for processing

operability evaluations could have a credible impact on safety. For example, the

operability evaluations for Callaway Corrective Action System Item CARS 200200264,

Foreign Material Found in the AL System; Callaway Corrective Action System Item

CARS 200200485, Evaluate the Potential Effects of Dissolved Nitrogen on the Auxiliary

Feedwater System; and Callaway Corrective Action System Item CARS 200200489,

Complete an Operability Evaluation on the CST Due to the Existence of the Foam

Pieces did not provide an adequate basis for continued operability of the AFW system

and the CST. The safety significance associated with these operability evaluations is

described in Section 7.

Callaway Corrective Action System Item CARS 200200264, Foreign Material Found in

the AL System, dated January 15, 2002, involved the discovery of foam in the AFW

Pump A seal water cooling line. The shift supervisor was not notified of this significant

condition adverse to quality. Callaway Corrective Action System Item CARS 200200264

was assigned a Significance Level of 3 (no onsite review committee evaluation

required). The assigner (acting system engineering mechanical supervisor) assigned

the operability evaluation to himself. The operability evaluation had a required

completion date of February 16, 2002, and was completed on January 17, 2002. The

required completion date was well beyond the allowed outage time associated with the

AFW and CST Technical Specifications, which were 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> and 7 days, respectively.

No peer or supervisory review of the finished operability evaluation was completed.

Operations personnel were not provided the opportunity to review the completed

operability evaluation. The team determined that the operability evaluation did not

adequately assess the extent of condition. Specifically, no assessment of the source of

the foreign material or where additional foreign material could be located was

performed. This failure to adequately assess the presence of foreign material in the

AFW system is documented in Section 3.2 as an example of an apparent violation of

10 CFR Part 50, Appendix B, Criterion XVI.

Callaway Corrective Action System Item CARS 200200485, Evaluate the Potential

Effects of Dissolved Nitrogen on the Auxiliary Feedwater System, dated January 25,

2002, involved the identification by the licensee that the effect of dissolved nitrogen on

the AFW system had not been considered. The shift supervisor was not notified of this

significant condition adverse to quality. Callaway Corrective Action System Item

CARS 200200485 was assigned a Significance Level of 3 (no onsite review committee

evaluation required). The operability evaluation had a required completion date of

February 16, 2002, and was not completed before the plant shutdown on

January 31, 2002. The required completion date was well beyond the allowed outage

time associated with the AFW and CST Technical Specifications, which were 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

and 7 days, respectively. The team determined that the response to the operability

19

evaluation was untimely in that the plant continued to operate beyond the allowed

outage time associated with the AFW system without an assessment of the potential

safety significance of the impact dissolved nitrogen had on the CST and AFW system.

The failure to account for the affect of nitrogen on available NPSH is documented in

Section 4.3 as a noncited violation of 10 CFR Part 50, Appendix B, Criterion III.

Callaway Corrective Action System Item CARS 200200489, Complete an Operability

Evaluation on the CST Due to the Existence of the Foam Pieces, dated January 27,

2002, involved the discovery of foam in the CST. The shift supervisor was notified of

the condition. Callaway Corrective Action System Item CARS 200200489 was assigned

a Significance Level of 2 (onsite review committee evaluation of the root cause

required). The operability evaluation had a required due date of January 27, 2002, and

was completed as required. The licensee determined that the AFW system was

operable because: (1) the material identified in the tank was fragile and not able to clog

an AFW pump orifice, (2) an insufficient flow velocity existed in the CST to cause the

identified material to enter the AFW system, (3) the isolation of secondary plant systems

returning to the CST (minimize recirculation of the CST contents), and (4) successful

completion of AFW pump testing. The team determined that inadequate information

provided by the licensees staff to senior management delayed the initiation of the extent

of condition review associated with the discovery of foreign material in the CST. Once

initiated, the extent of condition review was thorough and provided assurances that the

AFW system did not contain any foreign material. The failure to communicate

information regarding significant conditions adverse to quality is documented in

Section 3.2 as an example of an apparent violation of 10 CFR Part 50, Appendix B,

Criterion XVI.

Corrective Actions

The licensee planed to institute a series of programmatic and procedural enhancements

to improve weaknesses in the operability evaluation program. These enhancements

included:

+ Adding an operability evaluation form to the Callaway Corrective Action System

Item procedure.

+ Attaching completed operability evaluation forms to the associated Callaway

Corrective Action System Item.

+ Requiring operability evaluation forms to specify compensatory actions.

+ Requiring a review of operability evaluations.

+ Supplementing operability evaluation guidance with information from Generic

Letter 91-18.

+ Requiring shift supervisor approval for completed operability evaluations.

+ Tracking operability evaluations with their associated Callaway Corrective Action

System Item.

20

+ Adding criteria for timely completion of operability evaluations.

+ Implementing timely root cause evaluations for Significance Level 1 and 2

events.

5.0 Extent of Condition Review

a. Inspection Scope

The team reviewed documentation to determine to what extent the degraded CST

diaphragm seal may have had on other systems, structures, or components. The

review included visual inspections of the degraded seal and examination of the foreign

material removed from the CST and AFW Pump A. The teams review satisfied the

activities associated with the AIT Charter Element 4, Determine to what extent the

degraded CST floating diaphragm could potentially impact plant equipment. In addition

to the AFW system, this review should assess the potential impact on any other

components and systems, which may be affected.

b. Observations and Findings

The licensee had seven tanks with diaphragm seal devices. Six of those tanks used a

rubber seal assembly and the CST used the rigid diaphragm seal designed by

Conservaflote. The six tanks designed with rubber type diaphragm seals have had

periodic inspections performed in the past and were not expected to fail before signs of

degradation were identified by the licensee. The most risk significant tank (reactor

makeup water tank) had been inspected on a 5-year periodicity and the diaphragm was

replaced in 1998. The team determined that the same or similar condition did not exist

in other tanks at the facility.

The licensee performed laboratory analysis of the foam in order to determine the

potential effect on the steam generators. The analysis concluded that the foam was of a

polyurethane type where degradation (melting) commenced at 428-F and significant

degradation occurred at 513-F. As a result of the analysis and the temperature

environment in the steam generators at the time of the event, the licensee determined

that any foam entering the steam generators would have quickly degraded and become

diluted in the steam generator inventory. The team determined that there were no

apparent effects from the foam on the steam generator internals or instrumentation.

6.0 Quality Assurance Review

6.1 Review of the Quality Assurance Aspects of the Event

a. Inspection Scope

The team interviewed personnel to determine the extent of quality assurance (QA)

personnel involvement in the resolution of the failure of AFW Pump A. The teams

review satisfied the QA activities portion of Charter Element 5, Identify any human

21

factor, procedural or quality assurance deficiencies that may have contributed to the condition.

b. Observations and Findings

The team interviewed the QA manager and determined that QA did not participate in the

event response team meeting for the December 3, 2001, event. In addition, the team

determined that the licensee did not notify QA when event response team meetings

were conducted. Consequently, QA was not provided the opportunity to oversee the

process.

The team also determined that no one from QA was specifically assigned to oversee the

resolution of the root cause analysis and that QA personnel provided limited oversight of

the investigation into the failure of AFW Pump A. Specifically, QAs involvement was

limited to the following: (1) The Callaway Corrective Action System Item was reviewed

as part of the daily screening of corrective action program documents. (2) In early

December 2001, a print-out of the AFW flow control valve response and NRC

Bulletin 88-04, Potential Safety-Related Pump Loss, was provided to the corrective

action group facilitator assigned to assist in the development of the root cause (the

facilitator was not directly involved in the investigation of the failure of AFW Pump A until

mid-to-late January 2002). Bulletin 88-04 involved minimum flow line issues associated

with safety-related pumps and was not related to the failure of AFW Pump A. (3) A

review of the evaluation for returning AFW Pump A to an operable status was

completed. (4) Assessment activities associated with the entry into the CST were

completed.

6.2 Quality Assurance Audits of Foreign Material and Operating Experience

The licensee did not specifically perform audits of the foreign material and operating

experience programs. Instead, the licensee audited the foreign material and operating

experience aspects of whatever audits and assessments were completed. The licensee

provided copies of audits that contained the key words foreign material or operating

experience. The team did not identify any abnormal trends in the foreign material or

operating experience programs.

7.0 Risk Significance of Event

a. Inspection Scope

The team reviewed the licensees risk analysis associated with the failure of AFW

Pump A. The issue was determined to be more than minor because the on-demand

failure of AFW Pump A had an actual impact on plant safety. In addition, the degraded

condition of the diaphragm seal could have affected the availability of the AFW system.

The team completed an NRC Manual Chapter 0609, Significance Determination

Process, Phase 1 analysis of the failure of AFW Pump A. The SDP Phase 1 screening

process required that an SDP Phase 2 analysis be performed because the finding

represented an actual loss of a train of the AFW system. The team also completed an

SDP Phase 3 analysis in addition to the Phase 2 analysis to obtain a better

understanding of the increase in core damage frequency (CDF) stemming from the

identified performance issues. The CDF is the expected frequency of a core damage

22

event. The teams review satisfied the risk assessment activities associated with AIT

Charter Element 2, Review the licensees root and probable cause determination for

independence, completeness, and accuracy, including the licensees assessment of the

risk associated with the condition, and a portion of Charter Element 3, Assess the

timeliness and effectiveness of the licensees evaluation of potential AFW common

cause failure stemming from the degraded condensate storage tank floating

diaphragm.

b. Observations and Findings

Potential Impact of Safety Functions

A failure of the AFW system had a significant impact on the decay heat removal safety

function. The AFW system was the third most risk important system for the Callaway

Plant.

Potential for Common Cause Failure of the AFW System

The team inspected the condition of the diaphragm seal once it had been removed from

the CST to determine the extent of the condition of the degraded seal. The team also

interviewed various members of the licensees staff to evaluate the effect the degraded

seal could have on systems supplied by the CST.

The team determined that the degradation of the seal was limited to a 71-inch

circumferential section of the diaphragm. The degraded portion of the diaphragm seal

was located above the single suction source of the AFW system (See Figure 4). The

following table provides a listing of the missing foam portions of the seal.

Degraded Diaphragm Seal Inventory

Amount (length/height/width) Location

2 inch x 3 inch x 8 inch CST Sump

11.5 inch x 3 inch x 8 inch Removed by diver to complete seal

repair

12 inch x 3 inch x 8 inch CST Sump

20.5 inch x 3 inch x 8 inch Total amount of unaccounted foam.

25 inch x 3 inch x 8 inch Hanging from diaphragm and

removed by diver.

The team determined that the amount of unaccounted foam could have been one or

more pieces totaling 20.5 x 3 x 8 inches of material. The foam could have entered the

suction of the AFW system as a single piece of foreign material or as multiple pieces of

foreign material. The team determined that the proximity of the degraded seal location

to the suction of the AFW system increased the likelihood that a piece of foam could

23

enter the AFW system. The team also determined that the length and configuration of

the foam could affect the operation of the AFW system following an event.

The licensees lower bound risk analysis of the degraded diaphragm seal assumed

there was no potential for common cause failure of the AFW system or multiple AFW

pumps because the AFW pump would have recovered without operator action. The

licensees upper bound risk analysis of the degraded diaphragm seal assumed that the

two pieces of foam located in the CST sump, plus one additional piece of foam, could

affect the AFW pumps for a period of 1.8 months. After 1.8 months, only one piece of

foam was assumed to exist. Specifically:

+ The licensee determined that the 25-inch long section of foam removed by the

diver could not have fallen into the CST before January 25, 2002. Specifically,

the section of removed foam was attached to a 6-foot section of foam and the

diver was unable to pull the foam away from the masonite board or tear the

foam. Additionally, the licensee believed that the clearances between the CST

wall and the floating diaphragm were sufficient to prevent the foam from being

pinched off.

+ The licensee determined that the two pieces of foam found in the sump would

not have entered the AFW suction piping once the specific gravity exceeded

1.03. The specific gravity of the foam attached to the diaphragm was

approximately 1.0. The specific gravity of the water saturated foam in the CST

sump was approximately 1.31. The depth of the CST sump was approximately 3

feet. The licensee determined that a linear velocity of approximately 1.5 feet per

second would be required to lift water saturated foam from the bottom of the

CST. The actual linear flow velocity across the CST sump was determined to be

less than 1 foot per second. The licensee chemically analyzed the foam in the

CST sump and determined that the material had undergone hydrolytic

decomposition, indicating that the foam had been in the sump for an extended

duration. The chemical analysis was supported by the recognition that biological

materials had permeated the entire volume of the foam.

+ The licensee evaluated the effect of a single 20.5 inch long piece of foam on the

AFW system. The licensee determined that the elasticity of the foam would have

prevented it from obstructing the suction piping at the CST vortex breaker or the

manual suction isolation valve. The licensee also determined that a single piece

of foam would not have torn into multiple pieces as the foam traveled from the

CST to the suction of an AFW pump.

The team determined that there was a wide variance in the possible effects foam could

have on AFW system performance. Consequently, the team determined that there was

an increased likelihood for common cause failure of the AFW system due to foam from

the degraded diaphragm seal. Specifically: (1) multiple pieces of foam could have

become dislodged from the diaphragm seal. The multiple pieces could have affected

one or more AFW pumps following a demand signal. (2) A single piece of foam could

have separated into multiple pieces as it traversed the AFW suction piping and affected

one or more AFW pumps.

24

Recovery of AFW Pump A

The licensee hypothesized that the foam was extruded through the pump impeller and

that the pump would have self-recovered within a few additional minutes had operations

personnel not secured the pump. The licensee indicated that the pump was recovering

and eventually would have delivered design flow for the following reasons:

+ AFW Pump A motor current was increasing during the event.

+ AFW Pump A pump was vented for approximately 15 seconds allowing gas to

escape. No steam was present during the venting.

+ AFW Pump A was started successfully following the pump vent.

The licensee determined that the pump motor amperage increase during the event

indicated that AFW Pump A was recovering. The team determined that the motor

current increase from 42 to 46 amps, during the 10 minutes the pump operated, did not

support a conclusion that the pump would have recovered without operator intervention.

The team noted that the current increase could have been the result of the rise in

temperature on the outboard stuffing box which may have increased the frictional forces

on the shaft rotor due to the contact with the dry stuffing box packing material.

Moreover, trend data indicated that there was no corresponding increase in pump

discharge pressure or flow.

The team also noted that as a result of operating the pump in a partially air-bound

condition, the pump experienced some minor hydraulic degradation, which required the

licensee to establish new baseline pump characteristics to satisfactorily complete the

required surveillance tests (following the event, AFW Pump A could not attain the

required minimum flow). This information further indicated to the team the significance

of the air-binding event and the potential that the pump may not have been able to

self-recover. In addition, had operations personnel not de-energized the pump, the

potential existed for additional degradation of AFW Pump A.

The team determined that the successful venting and starting of the pump indicated that

the potential existed for operations personnel to recover a failed AFW pump. Two

independent flow paths existed for supplying water to the outboard packing housing.

Even though the seal water cooling line was obstructed with foam, the normal leakage

along the pump shaft should have been sufficient to provide lubricating flow to the

outboard packing housing. The team determined that the licensees human error

probability calculation for recovery of an AFW pump was appropriate. The analysis

considered the available time to diagnose the condition and take actions to restore the

pump. The team also determined that operations personnel possessed the requisite

skills to successfully complete a pump vent. Therefore, the team determined that the

licensee had appropriately determined that the potential for successful recovery of a

failed AFW pump was 0.95.

25

Review of Licensees Risk Calculations

The licensees preliminary lower bound risk analysis assumed that; (1) only one pump

would be affected (no potential for common cause failure), (2) the affected pump would

self-recover, (3) the likelihood that a piece of foam large enough to affect the system

would enter the AFW suction piping was 0.5, and the likelihood that an operator would

fail the pump as part of a recovery action was 2.9E-3. Based on these assumptions, the

licensee determined that the increase in core damage frequency (CDF), excluding

external events and flooding, was approximately 8E-7/year for a 100 percent capacity

factor and 6.8E-7/year for an 85 percent capacity factor. The team determined that the

85 percent capacity factor represented the actual at-power operating history of the

facility. In addition, the team determined that for the 15 percent shutdown interval, the

licensee did not credit the use of the AFW system while the residual heat removal

system was operating with the plant in Modes 4, 5, and 6.

The licensees upper bound case assumed a potential for common cause failure existed

for the first 1.8 months and only a single piece of foam for the remaining 10.2 months.

The licensee based the 1.8 month interval on their determination that the two pieces of

foam found in the CST would have entered the sump within 1.8 months. In addition, the

licensee assumed that the human error probability for recovery of a failed AFW Pump

was approximately 0.05. The licensees upper bound result of the increase in CDF,

excluding external events and flooding, was 5.53E-6/year for a 100 percent capacity

factor and 4.7E-6/year for an 85 percent capacity factor.

The licensees average test and maintenance Probabilistic Safety Assessment (PSA)

model used a loss of offsite power (LOOP) initiating event frequency of 3.9E-2/year

(Electric Power Research Institute TR 110398). The licensees next PSA model update

planned to use a revised LOOP frequency of 2.2E-2/year. The revised LOOP frequency

used the values in EPRI 1000158 (2.8E-2) minus the contribution from coastal LOOP

events and shut-down LOOP events. In addition, the licensee completed a Bayesian

update to reflect plant specific values associated with a LOOP event. Specifically, the

licensee has not had a LOOP event during the previous 17 years of plant operation.

The Bayesian update further reduced the LOOP frequency to 2.2E-2/year. The new

LOOP frequency reduced the baseline average test and maintenance CDF from

2.45E-5/year to 1.59E-5/year.

NRC Phase 2 Risk Assessment

The team completed a preliminary significance determination using the SDP Phase 2

process described in NRC Manual Chapter 0609, Significance Determination Process.

Two analyses were completed. The first analysis assumed that AFW Pump A was

unavailable for 1 year without any credit for recovery actions. The second analysis

assumed that all three AFW pumps were unavailable for 1 year without credit for

recovery actions. Table 2, Initiators and System Dependency for Callaway Nuclear

Generating Station, Unit 1, of the Callaway Plant Phase 2 site specific notebook

required that all initiating event scenarios except a loss of service water and a large

break loss of coolant accident be evaluated for findings affecting a motor driven AFW

26

pump and that all initiating event scenarios except a large break loss of coolant accident

be evaluated for findings affecting the turbine driven AFW pump.

The team analyzed 28 sequences using the site specific notebook and determined that

the dominate initiating event scenarios for a failure of AFW Pump A were transients

without the power conversion system and loss of offsite power. This case produced a

preliminary significance determination of substantial (Yellow).

The team analyzed 45 sequences using the site specific notebook and determined that

the dominate initiating event scenarios for a failure of all AFW Pumps were transients

with and without the power conversion system, loss of offsite power, and loss of a vital

dc bus. This case produced a preliminary significance determination of high (Red).

The team determined that an SDP Phase 3 analysis should be performed because the

results of the Phase 2 analysis may have been overly conservative. Specifically,

mitigation credit was not applied for recovery of a failed AFW pump, all AFW pumps

were assumed to fail in order to account for a potential common cause failure mode,

and the site specific notebook had not accounted for changes in the licensees PSA

model.

NRC Phase 3 Risk Assessment

The team requested that the licensee use their PSA model to calculate the change in

CDF for several combinations of AFW pump failures due to common cause with various

recovery probabilities. The duration for all the combinations was 1 year because no

information was provided which suggested that the diaphragm seal was degraded for an

interval of less than 1 year. The first variable involved adjusting the likelihood that a

piece of foam from the diaphragm entered the suction of the AFW system to 0.25, 0.5,

and 1.0. The second variable involved adjusting the recovery probability of a failed

AFW pump to 0.05, 0.20, and 1.0. The third variable accounted for a change in the

licensees capacity factor from 100 to 85 percent. The team determined that the 85

percent capacity factor represented the actual at-power operating history of the facility.

The lower bound results assumed the duration was 1 year, a potential common cause

failure of the remaining two AFW pumps, the likelihood that a piece of foam from the

diaphragm entered the suction of the AFW system was 0.25, the recovery probability of

a failed AFW pump was 0.05, and the capacity factor was 85 percent. The increase in

CDF, excluding external events and flooding, was approximately 2.1E-6/year.

The upper bound results assumed the duration was 1 year, a potential common cause

failure of the remaining two AFW pumps, the likelihood that a piece of foam from the

diaphragm entered the suction of the AFW system was 1.0, the recovery probability of a

failed AFW pump was 0.2, and the capacity factor was 100 percent. The increase in

CDF, excluding external events and flooding, was approximately 1.1E-5/year.

The teams final determination of the safety significance of the degraded CST

diaphragm seal was based on the following assumptions:

27

(1) An 85 percent capacity factor. In addition, the team determined that for the 15

percent shutdown interval, the licensee did not credit the use of the AFW system

while the residual heat removal system was operating with the plant in shutdown

Modes 4, 5, and 6.

(2) The revised LOOP frequency of 2.2E-2/year.

(3) A potential for common cause failure of the remaining two AFW pumps. The use

of the nominal fail-to-run probability associated with the remaining AFW pumps

was considered inappropriate in that there was an increased likelihood that foam

could affect an AFW pump. Therefore, the team, increased the failure

probability of the remaining motor-driven pump from 4.2E-3 to 0.1 and the

turbine-driven pump from 2.4E-3 to 0.1.

(4) The duration of 1 year. No information was provided which suggested that the

diaphragm seal was degraded for an interval of less than 1 year.

(5) The likelihood of 0.50 that a piece of foam which separates from the diaphragm

enters the AFW system. Two pieces of foam totaling 14 inches in length were

identified in the CST sump. This provided information to suggest that some of

the foam material would not enter the AFW suction piping.

(6) The potential for successful recovery of a failed AFW pump of 0.95. The NRC

analysts determined that the licensees human error probability calculation for

recovery of an AFW pump was appropriate. The steam generator dryout time

for a loss of all feedwater was approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. Adequate time existed to

diagnose the event and take actions to restore at least 1 AFW pump. The team

determined that operations personnel possessed the requisite skills and

knowledge to successfully complete a pump vent. In addition, there were no

environmental or human factor issues which could have affected the ability of

operations personnel to vent and fill an AFW pump.

Given the above assumptions, the team determined that the increase in CDF, excluding

external events and flooding, was approximately 4.3E-6/year. The initiating events with

the greatest contribution to core damage involved a loss of offsite power, loss of service

water, and loss of dc power. For the loss of offsite power initiating events, the dominant

sequences involved a failure to recover ac power within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, a failure of both

emergency diesel generators, and a failure of the turbine driven AFW pump. For the

loss of service water initiating event, the dominant sequences involved a failure to

recover service water and a failure of the turbine driven AFW pump. For the loss of dc

power initiating event, the dominant sequences involved a failure of the turbine driven

AFW pump, the motor driven AFW pumps, charging pumps, and residual heat removal

pumps.

Consideration of External Events and Flooding

The licensee did not have a PSA model which integrated internal, external, and flooding

events. The contribution from seismic events was negligible because the licensee had

28

adequately resolved the vulnerabilities identified during the completion of their seismic

margins analysis. The CDF associated with fire events was approximately 8.9E-6/year.

The CDF associated with flooding events was approximately 6E-6/year.

The AFW system was the third most risk important system for the Callaway Plant

internal PSA model. The team reviewed the licensees Individual Examination of

External Events document and determined that the AFW system supported the decay

heat removal critical safety function in each of the licensees external event analyses.

The team noted that the percent increase in CDF for the internal events PSA model

(4.3E-6/1.59E-5) was approximately 27 percent. Because of the importance of the AFW

system for both the internal and external event models, the team qualitatively

determined that there was some modest increase in risk associated with the

consideration of external events. The team determined that the increase due to external

events would not likely be sufficient for the performance deficiency to be characterized

as having substantial safety significance (Yellow).

Large Early Release Frequency

The team determined that the contribution from the failure of the AFW system had a

negligible impact on the large early release frequency. The team reviewed the dominate

large early release frequency sequences affected by failures of the AFW system and

determined that the increase was less than 1E-7/year. The dominate sequences

involved a steam generator tube rupture with a failure to isolate the affected steam

generator and a failure to establish either main feedwater or auxiliary feedwater flow.

Uncertainty

The mean values for the licensees original internal events PSA model, which included

flooding, was 1.95E-5. The 95th percentile of the PSA model was 4.16E-5 and the

5th percentile of the PSA model was 8.51E-6. Given the relatively narrow range between

the 5th and 95th percentiles, the team determined that it was appropriate to use the point

estimates derived from the PSA model quantifications without an additional adjustment

to account for uncertainty.

Conclusions

The team determined that the preliminary safety significance of the degradation of the

CST diaphragm seal was low to moderate (White). Specifically, the estimated increase

in CDF was greater than or equal to 4.3E-6/year and less than 1E-5/year, assuming an

85 percent capacity factor, the revised LOOP frequency, an increased likelihood that a

common cause failure could occur, a 1-year duration for the condition, the likelihood that

a piece of foam which separates from the diaphragm enters the AFW system at least

50 percent of the time, and the potential for the affected AFW pumps to be recovered at

least 95 percent of the time.

29

8.0 Overall Adequacy of the Licensees Response

a. Inspection Scope

The team assessed the observations and findings identified during the inspection in

order to complete an assessment of the overall adequacy of the effectiveness of the

licensees corrective actions in response to the failure of AFW Pump A. The teams

review satisfied AIT Charter Element 8, Review the overall adequacy of the licensees

response to the failure of the AFW pump.

b. Observations and Findings

The team determined that the licensee missed several opportunities to promptly identify

and correct a risk significant condition involving the degraded condition of the CST

diaphragm seal. The team also determined that the multiple failures of the licensee to

identify the degraded CST diaphragm seal was a significant human performance cross

cutting issue involving the recognition of degraded conditions.

Quality assurance personnel were not actively involved in providing oversight of the

event review team and root cause investigation process. The event review team

process did not ensure that statements were obtained from all personnel involved in the

event. The corrective action program did not include guidance or expectations on the

assignment of appropriate resources to review the highest classification of significant

conditions adverse to quality. Minimal resources were assigned to the root cause

investigation and may have contributed to the delay in identifying the degraded CST

diaphragm seal. Based on interviews with the licensees staff and a review of Procedure

APA-ZZ-00500, Corrective Action Program, the team determined that licensed

operators were only notified of equipment deficiencies if the individual discovering the

condition believed there was an immediate impact on nuclear, plant, or personnel safety.

Consequently, the potential existed for operability decisions to be made by non-licensed

personnel. The operability evaluation program did not implement the guidance provided

in NRC Generic Letter 91-18.

9.0 Exit Meeting Summary

On February 27, 2002, the team presented the inspection results to Mr. G. Randolph

and other members of his staff at a public exit meeting held at the Callaway Plant.

ATTACHMENT 1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

R. Affolter, Vice President Nuclear

J. Blosser, Manager, Regulatory Affairs

S. Bond, Supervisor, Design Engineering

K. Connelly, Engineer, Regulatory Affairs

J. Laux, Manager, Quality Assurance

J. McGraw, Superintendent, Nuclear Engineering

T. Moser, Superintendent, System Engineering

G. Randolph, Senior Vice President and Chief Nuclear Officer

M. Reidmeyer, Supervisor, Regional Regulatory Affairs

M. Taylor, Manager, Nuclear Engineering

M. Waltz, Engineer, Regulatory Affairs

R. Wink, System Engineer

W. Witt, Plant Manager

NRC

L. Ellershaw, Senior Reactor Inspector

M. Franovich, Reactor Analyst

I. Jung, Reactor Analyst

P. Wilson, Senior Reactor Analyst

Y. Huang, Mechanical Engineer

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000483/0207-01 APV Failure to promptly identify and correct a significant

condition adverse to quality.

Opened and Closed

050-00483/0207-02 NCV Failure to verify calculational methods.

2

DOCUMENTS REVIEWED

The following documents were selected and reviewed by the inspectors to accomplish the

objectives and scope of the inspection and to support any findings:

Audit and Assessment Reports

Assessment Report AP01-005 and SA-QA-001, Access Adequacy and Implementation of the

Optimized Audit Process, July 2, 2001

Audit Report AP00-008, Fourth Quarter 2000 Quality Assurance Audit Report,

January 11, 2001

Audit Report AP01-001, First Period 2001 Quality Assurance Report, June 26, 2001

Audit Report AP01-002, Second Period 2001 Quality Assurance Audit Report,

October 2, 2001

Audit Report AP01-006, Quality Assurance Audit of the Training, Qualification, and

Performance of Nuclear Division Personnel, February 2, 2002

Audit Report AP98-017, Quality Assurance Audit of Callaway Cycle 10 Reload Design and

Safety Analysis, February 1, 2002

Surveillance Report SP98-001, Self Assessment of the FSAR Review Effort, Callaway Plant,

February 1, 2002

Surveillance Report SP98-016, A Safety Injection Outage, February 1, 2002

Surveillance Report SP99-023, Spent Fuel Pool (SFP) Re-rack Modification, CMP97-1016,

February 2, 2002

Surveillance Report SP99-013, Spent Fuel Pool Rerack Modification, February 2, 2002

Calculations

Calculation AL-10, Determine the Available NPSH for the Auxiliary Feedwater Pumps,

July 21, 1977

Calculation AL-13, A System Model of the AFW System, September 14, 1995

Calculation AL-24, Determine the Effect of Dissolved Nitrogen on Available NPSH for the

Auxiliary Feedwater Pumps, February 6, 2002

3

Corrective Action Program Documents

CARS 199901955, PM to Inspect CST Internal Cover Not Generated

CARS 200001900, B MDAFP Run Stopped Due to Lack of Discharge Flow Indication

CARS 200107423, Auxiliary Feedwater System Event Review

CARS 200200264, Foreign Material Found in AL System

CARS 200200485, Evaluate the Potential Effects of Dissolved Nitrogen on the Auxiliary

Feedwater System, January 25, 2002

CARS 200200489, Complete an Operability Evaluation on the CST Due to the Existence of

the Foam Pieces

CARS 200200669, Flow Rate on the B MDAFP Miniflow Line was Lower Than Expected

CATS 31040, Generate PM for Regular Inspection of CST Cover

Maintenance Documents

Generic Work Request G631231125, Periodic Inspections of CST Diaphragm Seal

Preventive Maintenance Item P663567, Inspect CST Cover

W201820, Inspect CST Floating Cover

W220254, Replace Rotating Element on A MDAFP

W682227, Suction Piping Inspection

W686916, Camera and Diver Inspection of CST

W687231, A MDAFP Discharge Piping Inspection

W687232, B MDAFP Discharge Piping Inspection

W687233, TDAFP Discharge Piping Inspection

W202393, CST Seal Inspection

Miscellaneous Documents

C. C. Chen, Utwin Engineers and Constructors, Inc., Chemical Engineering, Optimal System

Design Requires the Right Vapor Pressure. Heres How to Calculate It, pages 106 through

112, October 1983

4

Chemir/Polytech Laboratory Report, Job 39979, January 28, 2002

CST System Flow Diagram, M-01AP01, Revision E

CST Inspection Document, System Release Exception Form Item Number AP-015,

July 15, 1982

Conservatek Design Drawing, 43-D2, Revision 1

CST Design Specification No. 10466-M-109(Q)

Daniel W. Wood, et. al., Proceedings of the 15th International Pump Users Symposium,

Application Guidelines for Pumping Liquids that have a Large Dissolved Gas Content, pages

91 through 98

Dominion Engineering, Auxiliary Feed Pump Event, January 25, 2002

EPRI TR-114612-V2, Pump Troubleshooting, April 2000

INPO SOER 97-01, Potential Loss of High Pressure Injection and Charging Capability From

Gas Intrusion

Mao J. Tsai, Techon International, Inc., Chemical Engineering, Accounting for Dissolved

Gases in Pump Design, July 26, 1982

Report UOTH 01-0047, Event Review Meeting Minutes: High Main Turbine Vibration, AFAS,

and No Flow on A-AFW Pump, December 4, 2001

Technical Manual M-021000061, Instruction Manual for Ingersoll Rand Centrifugal Pumps,

Revision 25

UOTE 92-048, Callaway Response to NRC Generic Letter 91-82, February 10, 1992

Watson Tomlinson, Evaluation of Auxiliary Feedwater Pump 1A Event 12/3/01,

January 21, 2002

Modification Documents

Request For Resolution 21798, Revision D, Evaluate Permanent Removal of TAP01 Floating

Cover, February 1, 2002

Request For Resolution 04991, Permanent N2 for the Condensate Storage Tank, Revision A,

May 4, 1988

Restricted Modification Package 88-2016, Revision A, November 20, 1992

Procedures

Procedure APA-ZZ-00500, Corrective Action Program, Revision 31

5

Procedure OSP-AL-P001A, Motor Driven Aux. Feedwater Pump A In Service Test,

Revision 27

Procedure OSP-AL-00001, AFW Flow Paths Valve Alignment, Revision 5

Procedure OSP-AL-V001A, Train A Auxiliary Feedwater Valve Operability, Revision 25

Procedure OSP AL-00002, AFW to Steam Generators Flow Path Verification, Revision 3

Procedure OSP-AL-V0002, Auxiliary Feedwater Valve Operability Test, Revision 12

Procedure OSP-AL-V0003, Auxiliary Feedwater Pump Discharge Check Valve Closure Test,

Revision 2

Procedure QPC-ZZ-05046, Ultrasonic Examination Procedure for Determining Liquid Level in

Pipes and Components, Revision 0

Procedure OSP-ZZ-00001, Technical Specification Logs, Revision 37, December 2-5, 2001

Procedure OTG-ZZ-00004, Power Operation, Revision 35

Procedure OTN-AE-00001, Feedwater System Operation, Revision 23

Procedure OTN-AL-00001, Auxiliary Feedwater System Operation, Revision 7

LIST OF ACRONYMS USED

AIT Augmented Inspection Team

AFW Auxiliary Feedwater

CARS Callaway Action Request System

CATS Callaway Action Tracking System

CCDP Conditional Core Damage Probability

CDF Core Damage Frequency

CFR Code of Federal Regulations

CST Condensate Storage Tank

IN Information Notice

LOOP Loss of Offsite Power

NPSH Net Positive Suction Head

PRA Probabilistic Risk Assessment

PSA Probabilistic Safety Assessment

QA Quality Assurance

SDP Significance Determination Process

SIT Special Inspection Team

ATTACHMENT 2

AUGMENTED INSPECTION TEAM CHARTER

January 31, 2002

MEMORANDUM TO: Troy Pruett

Senior Reactor Analyst

FROM: Ellis W. Merschoff

Regional Administrator /RA/ BY TPGwynn

SUBJECT: CHARTER FOR THE AUGMENTED INSPECTION TEAM AT THE

CALLAWAY PLANT

In response to recently developed information stemming from the continuing evaluation of the

impact of the Train A motor-driven auxiliary feedwater (AFW) pump failing to deliver required

flow to the steam generators during a controlled reactor plant shutdown performed on

December 3, 2001, the ongoing special inspection at the Callaway Plant is being upgraded to

an augmented inspection team (AIT). You are hereby designated as the AIT leader.

A. Basis

On December 3, 2001, the licensee manually started the motor-driven AFW pumps

prior to breaking condenser vacuum in anticipation of losing the operating main

feedwater pump during a controlled plant shutdown. After the main feedwater pump

tripped on low vacuum, as expected, the operators noticed the Train A motor-driven

AFW pump was not delivering the required flow to the steam generators. The licensee

manually stopped the A Train AFW pump and started the turbine-driven AFW pump to

provide necessary cooling flow to the steam generators. The initial risk assessment for

this condition indicated an estimated conditional core damage probability (CCDP) of

1.1E-6. As a result of this risk assessment, a Special Inspection Team was initiated in

accordance with NRC Management Directive 8.3, "NRC Incident Investigation Program."

The special inspection started onsite inspection activities at the Callaway Plant on

January 28, 2002.

On January 27, 2002, the licensee's investigation revealed that polyurethane foam from

a degraded condensate storage tank (CST) floating diaphragm may have caused the

pump failure. The revised risk assessment, which takes into account the potential

common cause impact on the AFW pumps, indicates a preliminary estimated CCDP in

the range of about 5E-5 to 5E-4. Management Directive 8.3 requires the consideration

of the initiation of an AIT when the estimated CCDP is greater than or equal to 1E-5.

On the basis of a potential for a substantial increase in risk stemming from common

mode failure implications, the ongoing special inspection is being upgraded to an AIT,

consistent with the guidance in Management Directive 8.3.

2

An AIT will be dispatched to better understand the cause of the AFW pump failure, the

extent of impact on the remaining AFW pumps, and operator actions leading up to and

including the event. The team is also tasked with gaining a better understanding of the

licensees common mode failure analysis as related to their root cause(s). The team

should build on the work already accomplished by the Special Inspection Team.

B. Scope

Specifically, the team is expected to perform data gathering and fact-finding in order to

address the following:

1. Develop a complete description and sequence of events related to the subject

AFW pump failure (including the degraded CST floating diaphragm), and

operator actions taken in response to regain feedwater flow.

2. Review the licensee's root and probable cause determination for independence,

completeness, and accuracy, including the licensee's assessment of the risk

associated with the condition.

3. Assess the timeliness and effectiveness of the licensee's evaluation of potential

AFW pump common cause failure stemming from the degraded condensate

storage tank floating diaphragm.

4. Determine to what extent the degraded CST floating diaphragm could potentially

impact plant equipment. In addition to the AFW system, this review should

assess the potential impact on any other components and systems, which may

be affected.

5. Identify any human factor, procedural or quality assurance deficiencies that may

have contributed to the condition.

6. Identify and assess the licensee's evaluation of applicable industry operating

experience.

7. Identify and assess the licensees prompt and long-term corrective actions to

address the root and probable causes of the condition.

8. Review the overall adequacy of the licensees response to the failure of the AFW

pump.

C. Guidance

This memorandum designates you as the AIT leader. Your duties will be as described

in Inspection Procedure 93800, "Augmented Inspection Team." The team composition

has been discussed with you directly. During performance of the augmented inspection,

designated team members are separated from their normal duties and report directly to

you. The team is to emphasize fact-finding in its review of the circumstances

3

surrounding the event, and it is not the responsibility of the team to examine the

regulatory process. Safety concerns identified that are not directly related to the event

should be reported to the Region IV office for appropriate action.

The team will report to the site, conduct an entrance meeting, and begin inspection on

Thursday, January 31, 2002. Tentatively, the inspection should be completed by close

of business February 2, 2002, with a report documenting the results of the inspection,

including findings and conclusions, issued within 30 days of the public exit meeting.

While the team is on site, you will provide daily status briefings to Region IV

management.

This Charter may be modified should the team develop significant new information that

warrants review. Should you have any questions concerning this Charter, contact Art

Howell III, Director, Division of Reactor Safety at (817) 860-8180.

ATTACHMENT 3

SEQUENCE OF EVENTS

Date and Time Event

July 1982 Plant personnel performed the final CST closeout inspection.

June 20, 1983 Startup Field Report AP-004A initiated to address oxygen

specifications for water from the CST.

July 11, 1983 SWR AP015 installed flanged connections to the CST lower manway

and added a suction and discharge line inside the tank. The

discharge line extended across the tank. CST drawings were not

updated.

January 2, 1985 Temporary Modification 85-M-001 documented CST manway

connections, but the internal tank piping configuration was not

updated.

June 6, 1985 Drawing M-22AP01 was revised to show manway connections;

however, internal tank pipe configuration was not recognized.

September 16, 1991 A modification is requested to sparge nitrogen. The impact of

sparging nitrogen into the CST was not evaluated.

December 18, 1991 NRC issues Information Notice 91-82, Problems With Diaphragms in

Safety-Related Tanks.

January 21, 1992 Corrective Action Tracking System CATS 31040 was generated to

develop a periodic inspection activity of the CST.

February 10, 1992 The licensee issued a response to Information Notice 91-82

(UOTE 92-048) stating that action was initiated to inspect the tank

internals for degradation.

February 1, 1999 Particulate matter was found in CST sampling equipment. Work

Order 197670 was initiated to clean and inspect the inside of the CST

during Refueling Outage 10.

September 15, 1999 Upon questioning by the NRC resident inspector, the licensee

reviewed its records and determined CATS 31040 was closed without

the task being accomplished. CARS 199901955 was initiated.

September 16, 1999 Generic Work Request G631231125 was initiated to inspect the CST

floating diaphragm.

2

Date and Time Event

December 1, 1999 Work Order W201820 replaces Generic Work Request G631231125.

CST floating diaphragm inspection was planned for the Spring

of 2000.

January 27, 2000 Work Order W202393 supercedes Work Order W197670.

October 17, 2000 The licensee performed an limited scope visual inspection of the CST

floating diaphragm and found no degradation.

November 14, 2000 The licensee established a preventive maintenance program to

inspect the CST floating diaphragm every 10 years.

March 31, 2001 Work Order W202393 is deferred from Refueling Outage 10.

December 3, 2001 Operations personnel commenced a reactor shutdown to Mode 3 in

at 1:15 p.m. order to repair a leaking main generator bushing.

December 3, 2001 Operations personnel received high vibration alarms on main turbine

at 10:39 p.m. Bearing Number 4. Vibration levels are recorded as 8.72 mils and

increasing.

December 3, 2001 Operations personnel manually trip the main turbine in response to

at 10:48 p.m. high vibration.

December 3, 2001 Operations personnel manually started AFW Pump B in anticipation of

at 10:56 p.m. breaking main condenser vacuum.

December 3, 2001 Operations personnel manually started AFW Pump A.

at 10:56 p.m.

December 3, 2001 Operations personnel broke main condenser vacuum in response to

at 10:57 p.m. main turbine bearing vibration levels exceeding 15 mils.

December 3, 2001 AFW Pump A ceased to provide flow to Steam Generators B and C.

at 10:58 p.m. Operations personnel started the turbine-driven AFW pump and

dispatched the field supervisor and an equipment operator to AFW

Pump Room A.

December 3, 2001 The field supervisor and an equipment operator observed no leak-off

at 11:01 p.m. flow from the outboard packing gland on AFW Pump A. The field

supervisor left AFW Pump Room A and inspected the turbine-driven

AFW pump.

3

Date and Time Event

December 3, 2001 The field supervisor returned to AFW Pump Room A. The outboard

at 11:05 p.m. packing gland was hot to the touch.

December 3, 2001 The field supervisor recommended that AFW Pump A be secured.

at 11:07 p.m. Control room personnel secured AFW Pump A.

December 3, 2001 The reactor entered Mode 3.

at 11:19 p.m.

December 3, 2001 Operations personnel vented AFW Pump A and observed 15 seconds

at 11:47 p.m. of air (not steam).

December 4, 2001 The licensee convened an event review team to investigate AFW

at 1:30 a.m. Pump A failure.

December 4, 2001 The licensee initiated CARS 200107423, assigned a root-cause

analyst to the event, and classified the event as Significance Level 1.

December 4, 2001 The licensee verified proper system alignment for AFW Pump A.

December 4, 2001 The licensee evaluated Significant Operating Experience

Report 97-01 for potential gas binding of AFW Pump A.

December 4, 2001 The licensee reviewed past operating and maintenance activities for

AFW Pump A.

December 4, 2001 AFW Pump A was started with operations and engineering personnel

present. Normal packing leak-off was observed, but the outboard

packing gland reached a temperature of 190oF after 4 minutes of

operation. The pump was secured, the outboard packing was

replaced, and the licensee re-baselined the inservice testing

performance criteria.

December 5, 2001 AFW Pump A was declared operable. The formal root cause team

was developed with personnel from system engineering and the

corrective action group.

December 6, 2001 The licensee formally initiated the root cause investigation for the

failure of AFW Pump A.

4

Date and Time Event

December 14, 2001 The licensee held a teleconference with the pump vendor to discuss

the pump malfunction. The vendor suggested that an inspection of

the seal water cooling line to the inboard and outboard packing

housing be completed.

January 8, 2002 The licensee conducted a meeting to discuss AFW performance

issues. A member from regulatory affairs, engineering, and two

contractors were added to the root cause team.

January 9, 2002 The licensee narrowed the cause of the event to three possibilities:

(1) low NPSH (2) nitrogen gas disassociation, and (3) foreign material.

Foreign material was not considered a credible failure mechanism.

January 11, 2002 The licensee completed ultrasonic testing of the AFW suction lines.

No significant air or gas accumulation was identified.

January 15, 2002 The licensee performed a surveillance test of AFW Pump A while the

Dominion Engineering and Flowserve representatives were on site.

The licensee found foam material in the orifice of the AFW Pump A

seal water cooling line.

January 17, 2002 The licensee initiated daily ultrasonic testing of the AFW suction lines.

January 23, 2002 The licensee concluded that inadequate NPSH and nitrogen

disassociation were not the causes of air-binding in AFW Pump A.

January 24, 2002 The licensee initiated an inspection of the CST floating diaphragm.

The team size associated with the root cause was expanded to

accommodate the CST inspection.

January 26, 2002 The licensee retrieved approximately 14 inches of foam from the

diaphragm seal from the CST sump. The diver also removed

approximately 25 inches of foam that was hanging from a 6 foot

damaged section of the diaphragm seal. Approximately 20.5 inches

of foam from the 71 inch damaged section was missing.

January 28, 2002 The NRC special inspection team arrived on site.

January 30, 2002 The licensee inspected the small bore piping, first and last stage

impellers, and part of the suction piping for AFW Pump B.

5

Date and Time Event

January 31, 2002 The licensee performed a reactor shutdown to Mode 4 to inspect the

AFW system. The NRC upgraded to an augmented inspection team

(AIT). The licensee increased the scope of the root cause

investigation.

February 1, 2002 The licensee began draining the CST. The licensee initiated foreign

material inspections for the AFW system.

February 2, 2002 The licensee inspected the CST floating diaphragm. The licensee

commenced removal of the CST floating diaphragm and replacement

of the rotating assembly on AFW Pump A.

February 5, 2002 Inspections on the AFW system were completed.

February 6, 2002 The CST is restored. AIT completes onsite inspection activity.

ATTACHMENT 4

SYSTEM FIGURES

Figure 1

Auxiliary Feedwater System

Simplified Diagram

Figure 2

Condensate Storage Tank

Diaphragm Seal

Figure 3

Degraded Diaphragm Seal

Figure 4

Condensate Storage Tank Configuration